LER 97-007-01:on 971017,entry Into TS 3.0.3 Occurred to Allow Completion of Surveillance Testing of One Channel of Rbm.Caused by Failure of Components in LPRM Output to Rbm. Submitted TS Change Request to Extend LCO Action StatementML18026A493 |
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Susquehanna |
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Issue date: |
03/30/1998 |
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From: |
Ellis S PENNSYLVANIA POWER & LIGHT CO. |
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Shared Package |
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ML17159A235 |
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References |
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LER-97-007, LER-97-7, NUDOCS 9804090017 |
Download: ML18026A493 (6) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18026A4931998-03-30030 March 1998 LER 97-007-01:on 971017,entry Into TS 3.0.3 Occurred to Allow Completion of Surveillance Testing of One Channel of Rbm.Caused by Failure of Components in LPRM Output to Rbm. Submitted TS Change Request to Extend LCO Action Statement ML18026A4891997-11-17017 November 1997 LER 97-007-00:on 971017,TS 3.0.3 Entry Voluntarily Made. Caused by Inadequate Post Maint Testing Following Earlier Work Associated W/Components.Failed Components Repaired, Replaced & Testing Completed ML18026A5961996-01-0202 January 1996 LER 95-013-00:on 951119,thermally Induced Pressure Locking of HPCI Valve Occurred Under Bonnet Pressure of 3,000-7,000 Psig.Damaged HPCI Injection Valve repaired.W/960102 Ltr ML18017A0461995-07-0707 July 1995 LER 95-008-00:on 950609,shift Average Licensed Core Thermal Power Was Exceeded.Caused by Failed Instrumentation Drift. Repaired & Recalibrated Subject Instrumentation ML18026A4261993-06-0909 June 1993 LER 90-007-01:on 900705,primary Power Supply to RPS a Power Distribution Panel Lost When One Electrical Protection Assembly (EPA) Breaker Tripped.Epa Logic Cards Reviewed & RPS Power Supply Will Be redesigned.W/930609 Ltr ML18026A4231992-11-17017 November 1992 LER 92-016-00:on 920416,discovered That Existing Analysis for Two Spent Fuel Storage Pools Did Not Reflect Current Fuel Design & Plant Operation.Caused by Failure to Modify FSAR Analysis.Fsar Will Be revised.W/921117 Ltr ML18017A0391991-07-26026 July 1991 LER 91-010-00:on 910628,RWCU Isolated on Two Occassions Due to Actuations of Steam Leak Detection Instrumentation. Caused by Design Deficiency & Elevated Ambient Penetration Room Temps.Temp Modules replaced.W/910726 Ltr ML17227A2311991-07-23023 July 1991 LER 91-009-00:on 910624,RWCU Steam Leak Detection Instrumentation Discovered to Be Inadvertently Actuated During Routine Functional Testing.Caused by Adequate Verbal Communication.Technicians briefed.W/910723 Ltr ML18026A5251991-07-0505 July 1991 LER 91-006-00:on 910608,unplanned Actuations of ESF Occurred.Caused by Unexpected Trip of Primary Power Supply EPA Breaker Losing Power.Breakers Reset & Full Power Operation Continued uninterupted.W/910705 Ltr ML20011F7881990-03-0202 March 1990 LER 90-005-00:on 900203,station Alert Declared When Reactor Coolant Temp Exceeded 200 F Due to Temporary Loss of Normal Method Dhr.Caused by Short Circuit to Ground in Bus Distribution Panel.Circuit Breakers replaced.W/900302 Ltr ML20005F3401990-01-0404 January 1990 LER 89-010-01:on 890920,determined That Estimated Leakage for Main Steam Line Containment Penetrations a & B Exceeded Tech Spec Limit During Local Leak Rate Testing.Cause Not Determined.Msiv Poppet Seats & Discs lapped.W/900104 Ltr ML18040A9121988-09-23023 September 1988 LER 88-018-00:on 880824,discovered That RWCU Pump Room Ambient Temp Sensor Not Installed Per Design.Caused by Lack of Installation Detail on Design Documents for Steam Leak Detection Sys.Tech Spec Change submitted.W/880923 Ltr ML19310G9421986-04-21021 April 1986 LER 86-005-00:on 860321 Differential Pressure Condition Detected,Causing Supply Dampers to Oscillate.Caused by Open Plenum Door & Exhaust Damper Linkage Binding.Linkage Reworked & lubricated.W/860421 Ltr ML20024E8021983-08-19019 August 1983 LER 83-107/01P-0:on 830819,during Maint,Emergency Svc Water Loop Discharge a to Spray Pond Valve Would Travel Only in Closed Direction.Cause Unstated.Mechanical Stops Loosened, Permitting Valve to Be Opened to Proper Position ML20024E6311983-08-0404 August 1983 Updated LER 83-093/01X-1:on 830711,31-day Functional Test of Containment Radiation Monitor a Not Performed for 830612-0711.Caused by Lack of Timely Chemistry Mgt Review of surveillance.W/830804 Ltr ML20024D9141983-07-26026 July 1983 Updated LER 83-035/03X-1:on 830228,during 4 H RCS Unidentified Leakage Test,Pump B of Drywell Sump a Continued to Operate for 4 H W/O Change in Sump Level.Caused by Clogged Pump Impeller.Pump cleaned.W/830726 Ltr ML20024E1601983-07-25025 July 1983 LER 83-098/03L-0:on 830625,position of Valve Indeterminate Due to Dual Status Indication for Suppression pool-to- Drywell Vacuum Breaker.Caused by Insufficient Limit Switch Plunger Position.Limit Switches adjusted.W/830725 Ltr ML20024D9911983-07-22022 July 1983 LER 83-096/03L-0:on 830624,RCIC Leak Detection B Power Failure Alarm Received.Undervoltage Trip Caused by Loss of Startup Transformer.Inverter Manually reset.W/830722 Ltr ML20024C2381983-06-29029 June 1983 LER 83-088/03L-0:on 830530,RCIC Pump Discharge Valve Would Not Open.Caused by Gap Between Breaker Male & Female Stab Clips.Female Clips Reworked to Allow Proper Contact. W/830629 Ltr ML20024C1001983-06-24024 June 1983 LER 83-085/03L-0:on 830525,containment Isolation Valve for Containment Atmosphere Control Sample Line Failed to Close. Cause Not Stated.Maint Personnel Verified Switch Positioning & Reconnected circuitry.W/830624 Ltr ML20024C1141983-06-24024 June 1983 LER 83-087/03L-0:on 830527,A Containment H2/02 Analyzers Found to Have Erratic Readings.Caused by Pressure Control Valve & Sample Pump Degradation to Point Where Proper Flow Not Maintained.Failed Components replaced.W/830624 Ltr ML20024C2451983-06-24024 June 1983 LER 83-086/03L-0:on 830525,reactor Bldg Door Opened While Maint Performed on Turbine Bldg Side of Air Lock to Reactor Bldg.Caused by Personnel Error.Individual W/Radio Communication Will Be posted.W/830624 Ltr ML20024C2461983-06-23023 June 1983 LER 83-084/03L-0:on 830524,during Surveillance Testing, Control Room Emergency Outside Air Supply Sys Fan Tripped. Caused by Out of Tolerance of Time Delay Relay for Heater Differential Temp.Relay reset.W/830623 Ltr ML20024A8401983-06-21021 June 1983 LER 83-082/01T-0:on 830607,main Turbine Trip on High Reactor Pressure Vessel Level Bypassed to Clear Interlock.After Outage,Bypass Discovered Still Installed.Caused by Lack of Clear Requirement for Bypass review.W/830621 Ltr ML20024A5331983-05-27027 May 1983 LER 83-067/01T-0:on 830516,reactor Mode Switch Placed in Startup Position & Half Scram Developed.Caused by Improper Functioning of Reactor Mode Switch Contacts.Switch Replaced. W/830527 Ltr ML20024A3421983-05-27027 May 1983 LER 83-070/01T-0:on 830517,flow Rates Required to Maintain Positive Pressure in Control Structure Appeared to Exceed Tech Spec Limits.Flow Limit Inadvertently Omitted from Procedure.Procedure corrected.W/830527 Ltr ML20024A3301983-05-27027 May 1983 LER 83-075/01T-0:on 830515,found Chlorine Detectors on Control Room Emergency Outside Air Supply May Prevent Operation in Pressurization Mode Following Loss of Power. Emergency Operation Procedures revised.W/830527 Ltr ML20024A3951983-05-26026 May 1983 LER 83-071/03L-0:on 830426,overvoltage Setting on One RPS Alternate Electrical Protection Assembly Found Greater than Tech Spec Limit.Caused by Instrument Drift.Overvoltage Setting Calibr within limits.W/830526 Ltr ML20023D5121983-05-11011 May 1983 LER 83-063/03L-0:on 830411,main Steam Line Drain Valve Leakage Exceeded Tech Spec Limit.Cause Not Stated.Seal Ring Replaced,Outboard Valve Lapped & Valves Reassembled ML20023B8381983-04-29029 April 1983 LER 83-057/01P-0:confirms 830428 Telcon Re Incident Concerning Bypass Leakage Calculations for Feedwater Following DBA LOCA ML20028D6871983-01-10010 January 1983 LER 83-001/01P-0:confirms 830107 Telcon Re Failure to Comply W/Action Statement Requiring Grab Samples of Offgas Sys After Declaring One Train of Hydrogen Monitor Inoperable. Caused by Inadequate Shift Turnover in Chemistry Dept ML20028D3141983-01-0707 January 1983 LER 82-072/03L-0:on 821210,while Performing Surveillance, One Control Rod Would Not Indicate at One Position.Possibly Caused by Intermittent Fault on Circuit Board.Printed Circuit Board Reinstalled ML20028D2871983-01-0606 January 1983 LER 82-069/03L-0:on 821207,during Startup Testing,Hpci Sys Declared Operable Prior to Closing Out Open Equipment Release Form.Caused by Work Program Design Weakness.Present Work Practice Modified ML20028D2601983-01-0505 January 1983 LER 82-061/01T-0:on 821228,during Startup Testing,While Performing Loss of Offsite Power Test,Emergency Svc Water Pumps B & D Failed to Start.Loop B Failure Caused by Loose Relay Terminal Wiring.Loop D Caused by Contact Adjustment ML20028D2671983-01-0505 January 1983 LER 82-062/01T-0:on 821222,during Loss of Offsite Power Startup Test,Standby Gas Treatment Sys Did Not Operate as Designed When False High Radiation Signal Received from Discharge Monitor.Caused by Monitor Failing High ML20028B7201982-11-24024 November 1982 LER 82-045/03L-0:on 821025,essential Svc Water Pump Failed to Start.Cause Could Not Be Determined or Reproduced.Svc Pump Tested 5 Times W/O Recurrence of Failure ML20028B5821982-11-19019 November 1982 Revised LER 82-026/01T-1:on 820717,review Revealed Certain Cables Discussed in Deficiency Rept 80-00-28 Not Flexed or Grounded Prior to Fuel Load.Caused by Failure to Maintain Control Over Fddr KRI-607 During Turnover of Const ML20028B0301982-11-18018 November 1982 LER 82-042/01T-0:on 821117,personnel Failed to Take Grab Samples When RHR Svc Water Sys Radiation Monitor Was Inoperable ML20028B4351982-11-18018 November 1982 LER 82-043/01T-0:on 821117,determined That Failure of Single Component Could Defeat Overload Detection & Protection Devices for Containment Penetration Carrying Power Cables for Reactor Recirculation Pumps.Cause Not Stated ML20028A9541982-11-16016 November 1982 LER 82-040/03L-0:on 821018,deluge Sys in CREOASS Initiated. Caused by Maint Personnel Bumping Fire Sys thermo-switch on Charcoal Beds.Charcoal Changed Out & Preventive Maint Procedures Modified to Valve Out Deluge Sys During Maint ML20028B0461982-11-12012 November 1982 Revised LER 82-003/01T-2:on 820811,during Initial Fuel Loading,Sprinkler Sys Did Not Exist in Area Designated by Tech Specs & Fire Protection Review Rept.Caused by Discrepancies in as-built Conditions.Mods Initiated ML20028A3341982-11-0303 November 1982 LER 82-034/03L-0:on 821011,during Startup Testing,Creoass Train a Declared Inoperable When Outside Air Damper Failed to Close.Caused by Inadequate Lubrication of Actuator Stem. Stem Lubricated & Damper Returned to Svc ML20027D0591982-10-19019 October 1982 LER 82-027/03L-0:on 820920,two Drywell/Suppression Chamber Vacuum Breakers Gave False Position Indications During Stroking.Caused by Loose Couplings Connecting Limit Switch to Vacuum Relief Valve Shaft.Set Screw Replaced ML17139B0311982-09-13013 September 1982 LER 82-013/03L-0:on 820814,radiation Monitor Found Inoperable.Caused by Faulty Gm Tube & Signal Conditioner (Sensor Converter).Tube & Signal Conditioner Replaced & Monitor Returned to Svc ML20027B0571982-09-0808 September 1982 LER 82-007/01T-1:on 820825,updated Secondary Containment Vol Calculation Had Not Replaced Preliminary Analysis Utilized to Obtain Values in Fsar.Vol Based on Preliminary Calculation Which Did Not Account for Floors & Equipment ML20027A9581982-09-0303 September 1982 LER 82-005/01T-1:on 820820,during Preoperational Testing, Control Room Emergency Outside Air Supply Sys Did Not Automatically Start on Isolation Signal.Caused by Unauthorized Personnel Changing Flow Controller Switch ML17139A9071982-08-0202 August 1982 LER 82-001/01T-0:on 820718,unacceptable Linear Indications Found by Radiograph of A-11 Weld.Cause Not Determined.Welds Repaired Per Approved Repair Program 1998-03-30
[Table view] Category:RO)
MONTHYEARML18026A4931998-03-30030 March 1998 LER 97-007-01:on 971017,entry Into TS 3.0.3 Occurred to Allow Completion of Surveillance Testing of One Channel of Rbm.Caused by Failure of Components in LPRM Output to Rbm. Submitted TS Change Request to Extend LCO Action Statement ML18026A4891997-11-17017 November 1997 LER 97-007-00:on 971017,TS 3.0.3 Entry Voluntarily Made. Caused by Inadequate Post Maint Testing Following Earlier Work Associated W/Components.Failed Components Repaired, Replaced & Testing Completed ML18026A5961996-01-0202 January 1996 LER 95-013-00:on 951119,thermally Induced Pressure Locking of HPCI Valve Occurred Under Bonnet Pressure of 3,000-7,000 Psig.Damaged HPCI Injection Valve repaired.W/960102 Ltr ML18017A0461995-07-0707 July 1995 LER 95-008-00:on 950609,shift Average Licensed Core Thermal Power Was Exceeded.Caused by Failed Instrumentation Drift. Repaired & Recalibrated Subject Instrumentation ML18026A4261993-06-0909 June 1993 LER 90-007-01:on 900705,primary Power Supply to RPS a Power Distribution Panel Lost When One Electrical Protection Assembly (EPA) Breaker Tripped.Epa Logic Cards Reviewed & RPS Power Supply Will Be redesigned.W/930609 Ltr ML18026A4231992-11-17017 November 1992 LER 92-016-00:on 920416,discovered That Existing Analysis for Two Spent Fuel Storage Pools Did Not Reflect Current Fuel Design & Plant Operation.Caused by Failure to Modify FSAR Analysis.Fsar Will Be revised.W/921117 Ltr ML18017A0391991-07-26026 July 1991 LER 91-010-00:on 910628,RWCU Isolated on Two Occassions Due to Actuations of Steam Leak Detection Instrumentation. Caused by Design Deficiency & Elevated Ambient Penetration Room Temps.Temp Modules replaced.W/910726 Ltr ML17227A2311991-07-23023 July 1991 LER 91-009-00:on 910624,RWCU Steam Leak Detection Instrumentation Discovered to Be Inadvertently Actuated During Routine Functional Testing.Caused by Adequate Verbal Communication.Technicians briefed.W/910723 Ltr ML18026A5251991-07-0505 July 1991 LER 91-006-00:on 910608,unplanned Actuations of ESF Occurred.Caused by Unexpected Trip of Primary Power Supply EPA Breaker Losing Power.Breakers Reset & Full Power Operation Continued uninterupted.W/910705 Ltr ML20011F7881990-03-0202 March 1990 LER 90-005-00:on 900203,station Alert Declared When Reactor Coolant Temp Exceeded 200 F Due to Temporary Loss of Normal Method Dhr.Caused by Short Circuit to Ground in Bus Distribution Panel.Circuit Breakers replaced.W/900302 Ltr ML20005F3401990-01-0404 January 1990 LER 89-010-01:on 890920,determined That Estimated Leakage for Main Steam Line Containment Penetrations a & B Exceeded Tech Spec Limit During Local Leak Rate Testing.Cause Not Determined.Msiv Poppet Seats & Discs lapped.W/900104 Ltr ML18040A9121988-09-23023 September 1988 LER 88-018-00:on 880824,discovered That RWCU Pump Room Ambient Temp Sensor Not Installed Per Design.Caused by Lack of Installation Detail on Design Documents for Steam Leak Detection Sys.Tech Spec Change submitted.W/880923 Ltr ML19310G9421986-04-21021 April 1986 LER 86-005-00:on 860321 Differential Pressure Condition Detected,Causing Supply Dampers to Oscillate.Caused by Open Plenum Door & Exhaust Damper Linkage Binding.Linkage Reworked & lubricated.W/860421 Ltr ML20024E8021983-08-19019 August 1983 LER 83-107/01P-0:on 830819,during Maint,Emergency Svc Water Loop Discharge a to Spray Pond Valve Would Travel Only in Closed Direction.Cause Unstated.Mechanical Stops Loosened, Permitting Valve to Be Opened to Proper Position ML20024E6311983-08-0404 August 1983 Updated LER 83-093/01X-1:on 830711,31-day Functional Test of Containment Radiation Monitor a Not Performed for 830612-0711.Caused by Lack of Timely Chemistry Mgt Review of surveillance.W/830804 Ltr ML20024D9141983-07-26026 July 1983 Updated LER 83-035/03X-1:on 830228,during 4 H RCS Unidentified Leakage Test,Pump B of Drywell Sump a Continued to Operate for 4 H W/O Change in Sump Level.Caused by Clogged Pump Impeller.Pump cleaned.W/830726 Ltr ML20024E1601983-07-25025 July 1983 LER 83-098/03L-0:on 830625,position of Valve Indeterminate Due to Dual Status Indication for Suppression pool-to- Drywell Vacuum Breaker.Caused by Insufficient Limit Switch Plunger Position.Limit Switches adjusted.W/830725 Ltr ML20024D9911983-07-22022 July 1983 LER 83-096/03L-0:on 830624,RCIC Leak Detection B Power Failure Alarm Received.Undervoltage Trip Caused by Loss of Startup Transformer.Inverter Manually reset.W/830722 Ltr ML20024C2381983-06-29029 June 1983 LER 83-088/03L-0:on 830530,RCIC Pump Discharge Valve Would Not Open.Caused by Gap Between Breaker Male & Female Stab Clips.Female Clips Reworked to Allow Proper Contact. W/830629 Ltr ML20024C1001983-06-24024 June 1983 LER 83-085/03L-0:on 830525,containment Isolation Valve for Containment Atmosphere Control Sample Line Failed to Close. Cause Not Stated.Maint Personnel Verified Switch Positioning & Reconnected circuitry.W/830624 Ltr ML20024C1141983-06-24024 June 1983 LER 83-087/03L-0:on 830527,A Containment H2/02 Analyzers Found to Have Erratic Readings.Caused by Pressure Control Valve & Sample Pump Degradation to Point Where Proper Flow Not Maintained.Failed Components replaced.W/830624 Ltr ML20024C2451983-06-24024 June 1983 LER 83-086/03L-0:on 830525,reactor Bldg Door Opened While Maint Performed on Turbine Bldg Side of Air Lock to Reactor Bldg.Caused by Personnel Error.Individual W/Radio Communication Will Be posted.W/830624 Ltr ML20024C2461983-06-23023 June 1983 LER 83-084/03L-0:on 830524,during Surveillance Testing, Control Room Emergency Outside Air Supply Sys Fan Tripped. Caused by Out of Tolerance of Time Delay Relay for Heater Differential Temp.Relay reset.W/830623 Ltr ML20024A8401983-06-21021 June 1983 LER 83-082/01T-0:on 830607,main Turbine Trip on High Reactor Pressure Vessel Level Bypassed to Clear Interlock.After Outage,Bypass Discovered Still Installed.Caused by Lack of Clear Requirement for Bypass review.W/830621 Ltr ML20024A5331983-05-27027 May 1983 LER 83-067/01T-0:on 830516,reactor Mode Switch Placed in Startup Position & Half Scram Developed.Caused by Improper Functioning of Reactor Mode Switch Contacts.Switch Replaced. W/830527 Ltr ML20024A3421983-05-27027 May 1983 LER 83-070/01T-0:on 830517,flow Rates Required to Maintain Positive Pressure in Control Structure Appeared to Exceed Tech Spec Limits.Flow Limit Inadvertently Omitted from Procedure.Procedure corrected.W/830527 Ltr ML20024A3301983-05-27027 May 1983 LER 83-075/01T-0:on 830515,found Chlorine Detectors on Control Room Emergency Outside Air Supply May Prevent Operation in Pressurization Mode Following Loss of Power. Emergency Operation Procedures revised.W/830527 Ltr ML20024A3951983-05-26026 May 1983 LER 83-071/03L-0:on 830426,overvoltage Setting on One RPS Alternate Electrical Protection Assembly Found Greater than Tech Spec Limit.Caused by Instrument Drift.Overvoltage Setting Calibr within limits.W/830526 Ltr ML20023D5121983-05-11011 May 1983 LER 83-063/03L-0:on 830411,main Steam Line Drain Valve Leakage Exceeded Tech Spec Limit.Cause Not Stated.Seal Ring Replaced,Outboard Valve Lapped & Valves Reassembled ML20023B8381983-04-29029 April 1983 LER 83-057/01P-0:confirms 830428 Telcon Re Incident Concerning Bypass Leakage Calculations for Feedwater Following DBA LOCA ML20028D6871983-01-10010 January 1983 LER 83-001/01P-0:confirms 830107 Telcon Re Failure to Comply W/Action Statement Requiring Grab Samples of Offgas Sys After Declaring One Train of Hydrogen Monitor Inoperable. Caused by Inadequate Shift Turnover in Chemistry Dept ML20028D3141983-01-0707 January 1983 LER 82-072/03L-0:on 821210,while Performing Surveillance, One Control Rod Would Not Indicate at One Position.Possibly Caused by Intermittent Fault on Circuit Board.Printed Circuit Board Reinstalled ML20028D2871983-01-0606 January 1983 LER 82-069/03L-0:on 821207,during Startup Testing,Hpci Sys Declared Operable Prior to Closing Out Open Equipment Release Form.Caused by Work Program Design Weakness.Present Work Practice Modified ML20028D2601983-01-0505 January 1983 LER 82-061/01T-0:on 821228,during Startup Testing,While Performing Loss of Offsite Power Test,Emergency Svc Water Pumps B & D Failed to Start.Loop B Failure Caused by Loose Relay Terminal Wiring.Loop D Caused by Contact Adjustment ML20028D2671983-01-0505 January 1983 LER 82-062/01T-0:on 821222,during Loss of Offsite Power Startup Test,Standby Gas Treatment Sys Did Not Operate as Designed When False High Radiation Signal Received from Discharge Monitor.Caused by Monitor Failing High ML20028B7201982-11-24024 November 1982 LER 82-045/03L-0:on 821025,essential Svc Water Pump Failed to Start.Cause Could Not Be Determined or Reproduced.Svc Pump Tested 5 Times W/O Recurrence of Failure ML20028B5821982-11-19019 November 1982 Revised LER 82-026/01T-1:on 820717,review Revealed Certain Cables Discussed in Deficiency Rept 80-00-28 Not Flexed or Grounded Prior to Fuel Load.Caused by Failure to Maintain Control Over Fddr KRI-607 During Turnover of Const ML20028B0301982-11-18018 November 1982 LER 82-042/01T-0:on 821117,personnel Failed to Take Grab Samples When RHR Svc Water Sys Radiation Monitor Was Inoperable ML20028B4351982-11-18018 November 1982 LER 82-043/01T-0:on 821117,determined That Failure of Single Component Could Defeat Overload Detection & Protection Devices for Containment Penetration Carrying Power Cables for Reactor Recirculation Pumps.Cause Not Stated ML20028A9541982-11-16016 November 1982 LER 82-040/03L-0:on 821018,deluge Sys in CREOASS Initiated. Caused by Maint Personnel Bumping Fire Sys thermo-switch on Charcoal Beds.Charcoal Changed Out & Preventive Maint Procedures Modified to Valve Out Deluge Sys During Maint ML20028B0461982-11-12012 November 1982 Revised LER 82-003/01T-2:on 820811,during Initial Fuel Loading,Sprinkler Sys Did Not Exist in Area Designated by Tech Specs & Fire Protection Review Rept.Caused by Discrepancies in as-built Conditions.Mods Initiated ML20028A3341982-11-0303 November 1982 LER 82-034/03L-0:on 821011,during Startup Testing,Creoass Train a Declared Inoperable When Outside Air Damper Failed to Close.Caused by Inadequate Lubrication of Actuator Stem. Stem Lubricated & Damper Returned to Svc ML20027D0591982-10-19019 October 1982 LER 82-027/03L-0:on 820920,two Drywell/Suppression Chamber Vacuum Breakers Gave False Position Indications During Stroking.Caused by Loose Couplings Connecting Limit Switch to Vacuum Relief Valve Shaft.Set Screw Replaced ML17139B0311982-09-13013 September 1982 LER 82-013/03L-0:on 820814,radiation Monitor Found Inoperable.Caused by Faulty Gm Tube & Signal Conditioner (Sensor Converter).Tube & Signal Conditioner Replaced & Monitor Returned to Svc ML20027B0571982-09-0808 September 1982 LER 82-007/01T-1:on 820825,updated Secondary Containment Vol Calculation Had Not Replaced Preliminary Analysis Utilized to Obtain Values in Fsar.Vol Based on Preliminary Calculation Which Did Not Account for Floors & Equipment ML20027A9581982-09-0303 September 1982 LER 82-005/01T-1:on 820820,during Preoperational Testing, Control Room Emergency Outside Air Supply Sys Did Not Automatically Start on Isolation Signal.Caused by Unauthorized Personnel Changing Flow Controller Switch ML17139A9071982-08-0202 August 1982 LER 82-001/01T-0:on 820718,unacceptable Linear Indications Found by Radiograph of A-11 Weld.Cause Not Determined.Welds Repaired Per Approved Repair Program 1998-03-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML17146B1741999-08-0303 August 1999 GL 96-06 Risk Assessment for Sses. ML20206D3331999-04-27027 April 1999 SER of Individual Plant Examination of External Events Submittal on Susquehanna Steam Electric Station,Units 1 & 2. Staff Notes That Licensee IPEEE Complete with Regard to Info Requested by Suppl 4 to GL 88-20 ML20195B2381999-03-31031 March 1999 Redacted Version for 10CFR2.790 Request for Decommissioning Status Rept for Sses,Units 1 & 2 ML17164A8451998-10-31031 October 1998 SSES Unit 1 Tenth Refueling & Insp Outage ISI Outage Summary Rept. ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20217Q4891998-04-21021 April 1998 Rev 1 to Draft LDCN 2482, FSAR Chapter 13.4 & FSAR Chapter 17.2 Changes to Support ITS Implementation ML18026A4931998-03-30030 March 1998 LER 97-007-01:on 971017,entry Into TS 3.0.3 Occurred to Allow Completion of Surveillance Testing of One Channel of Rbm.Caused by Failure of Components in LPRM Output to Rbm. Submitted TS Change Request to Extend LCO Action Statement ML18026A5401998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Susquehanna Steam Electric Station.W/980313 Ltr ML18026A4891997-11-17017 November 1997 LER 97-007-00:on 971017,TS 3.0.3 Entry Voluntarily Made. Caused by Inadequate Post Maint Testing Following Earlier Work Associated W/Components.Failed Components Repaired, Replaced & Testing Completed ML18017A2921997-10-28028 October 1997 1997 Nrc/Fema Observed Exercise. ML17158C1861997-06-0505 June 1997 Proceedings of Intl Topical Meeting on Advanced Reactors Safety Vol II, on 970601-05 ML20140A9661997-05-29029 May 1997 Part 21 Rept Re Ksv Emergency Diesel Generator Power Piston Failure.Caused by Jacket Water in Combustion Chamber. Recommends That Users Verify That Crown Thickness at Valve Cutout Be 100 Minimum ML18026A4781997-03-28028 March 1997 Rev 1 to Application of Anfb to ATRIUM-10 for Susquehanna Reloads. ML20137G6261997-03-25025 March 1997 Svcs Part 21 Rept Re Emergency Generators Installed at Zion Station Which Developed Significant Drop in Crankcase Lube Oil Level.Caused by Crack in Liner Wall,Allowing Jacket Water to Enter Chamber ML20155F7661996-07-25025 July 1996 Partially Deleted Job Number 739619-96, Investigation of E Diesel Breaker Misalignment ML20155F7491996-07-24024 July 1996 Independent Safety Evaluation Svcs Project Rept 3-96, Investigation of E Diesel Generator In-Operability Event ML20117G4641996-05-14014 May 1996 Part 21 Rept Re Cooper Bessemer Reciprocating Products,Div of Cooper Cameron Corp,Issued Ltr to Define Utils/Plants Containing Similar Equipment as Supplied on Cooper Bessemer Ksv & Enterprise Dsr EDGs ML18026A5961996-01-0202 January 1996 LER 95-013-00:on 951119,thermally Induced Pressure Locking of HPCI Valve Occurred Under Bonnet Pressure of 3,000-7,000 Psig.Damaged HPCI Injection Valve repaired.W/960102 Ltr ML18017A0511995-11-30030 November 1995 Monthly Operating Repts for Nov 1995 for SSES Units 1 & 2. W/951215 Ltr ML20092H7641995-08-31031 August 1995 Monthly Operating Repts for Aug 1995 for Susquehanna Ses ML17158A8771995-08-15015 August 1995 Exercise Manual. ML17158A8061995-07-14014 July 1995 Books 1 & 2 of ISI Outage Summary Rept SSES Unit 1 8th Refuel Outage. ML18017A0461995-07-0707 July 1995 LER 95-008-00:on 950609,shift Average Licensed Core Thermal Power Was Exceeded.Caused by Failed Instrumentation Drift. Repaired & Recalibrated Subject Instrumentation ML17164A6631995-04-11011 April 1995 Impact of Extending T-10 AOT from 3 to 7 Days. ML17164A5871995-01-31031 January 1995 Monthly Operating Repts for Jan 1995 for Susquehanna Ses ML18026A5351994-10-31031 October 1994 SSES Unit 1 & 2 MSIV Leakage Alternate Treatment Method Seismic Evaluation. W/One Oversize Drawing ML17158A4821994-08-23023 August 1994 ISI Outage Summary Rept Unit 2 6th Refueling Outage, Books 1 & 2 of 2 ML17158A2391994-04-0505 April 1994 Books 1 & 2 of SSES Unit 1 Seventh Refueling & Insp Outage ISI Outage Summary Rept. ML18017A2701993-12-31031 December 1993 PP&L Annual Rept 1993. ML17158A2651993-12-31031 December 1993 Allegheny Electric Cooperative,Inc Annual Rept 1993. ML17158A1631993-12-0909 December 1993 Remote Indication of Spent Fuel Pool Level & Temperature. ML18026A4281993-08-16016 August 1993 PP&L Response to NRC Concerns Re Loss of Spent Fuel Pool Cooling Following Loca,Sses,Units 1 & 2. ML18026A4261993-06-0909 June 1993 LER 90-007-01:on 900705,primary Power Supply to RPS a Power Distribution Panel Lost When One Electrical Protection Assembly (EPA) Breaker Tripped.Epa Logic Cards Reviewed & RPS Power Supply Will Be redesigned.W/930609 Ltr ML17157C2441993-02-28028 February 1993 Monthly Operating Rept for Feb 1993 for Susquehanna Steam Electric Station,Units 1 & 2 ML18017A2031993-02-0101 February 1993 Books 1 & 2 of Unit 2 Fifth Refueling & Insp Outage,Isi Outage Summary Rept. ML20044C2741993-01-31031 January 1993 Corrected Monthly Operating Rept for Jan 1993 for Susquehanna Steam Electric Station,Unit 2,consisting of Info on Unit Shutdowns & Power Reductions ML17157C3691992-12-31031 December 1992 PP&L Annual Rept 1992. ML20056C3941992-12-31031 December 1992 Allegheny Electric Cooperative,Inc Annual Rept 1992 ML18017A0421992-12-14014 December 1992 Suppl to 921127 Part 21 Rept Re High Air Concentration in Reactor Bldg Making Area Uninhabitable for Retrieving Air Filters,Per NUREG-0737,Item II.F.1.Util Current Position Re Fuel Pool Cooling Issues Contrary to Reg Guide 1.3 ML18026A2481992-11-27027 November 1992 Part 21 Rept Re Substantial Safety Hazard in Design of Facility for Loss of Normal Spent Fuel Pool Cooling ML18026A4231992-11-17017 November 1992 LER 92-016-00:on 920416,discovered That Existing Analysis for Two Spent Fuel Storage Pools Did Not Reflect Current Fuel Design & Plant Operation.Caused by Failure to Modify FSAR Analysis.Fsar Will Be revised.W/921117 Ltr ML17157C1421992-10-21021 October 1992 Engineering Assessment of Fuel Pool Cooling Piping EDR-G20020. ML17157C1411992-08-31031 August 1992 Loss of Fuel Pool Cooling Event Evaluation. ML17157C1401992-08-31031 August 1992 Review of Fuel Pool Cooling During Postulated Off-Normal & Accident Events SSES Units 1 & 2. ML20082C4941992-08-14014 August 1992 Evaluation of Unit 1 & Unit 2 Derating of Power Cables in Raceways Wrapped W/Thermo-Lag Matl ML17157C1381992-07-27027 July 1992 Safety Consequences of Boiling Spent Fuel Pool at Susquehanna Steam Electric Station. ML17157B9331992-07-24024 July 1992 Sixth Refueling & Insp Outage Inservice Insp Outage Summary Rept, Books 1 & 2 ML20097D4681991-12-31031 December 1991 Pennsylvania Power & Light Company,1991 Annual Rept ML18017A0391991-07-26026 July 1991 LER 91-010-00:on 910628,RWCU Isolated on Two Occassions Due to Actuations of Steam Leak Detection Instrumentation. Caused by Design Deficiency & Elevated Ambient Penetration Room Temps.Temp Modules replaced.W/910726 Ltr 1999-09-30
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NRC FORM 366 UCLEAR REGULATORY COMMISSION PPROVED SY OMB NO. 31504104 (4'&SI EXPIRES 04I30IBS BVRDEN PER RESPONSE TO COMPLY WITH THIS MAN(IATORY INFORMATION COLLECTION REOUESTJ 60.0 HRS.
LESSONS LEARNED ARE INCORPORATED INTO THE LXCENSEE EV1KT REPORT (LER) REPORTED ucENslJJG pRocess AND FED BACK TO INDUSTRY. FORwARD COMMENTS REGARDiNG BURDEN ESTIMA'lE TO THE INFORMATION AND RECORDS MANAG'EMENT BRANCH (T.S F331. U.S. NUCLEAR (See reverse for required number of REGULATORY COMMISSION, WASHINGTON. DC 2055$ 400I, AND digits/characters for each block) 'To THE PAPERWORK REDUCTION PRO~CT I3 I SDOIDAIi OFFICE OF MANAG/M6NTAND BUDGET, WASHING1ON, DC 20503.
FAcrtJTT JJAMa I i) ooclttT Jrv M atri QI Fnoa ar Susquehanna Steam Electric Station - Unit 2 05000388 1OF5 HJ Entry Into Technical Specification 3.0,3 - Rod Block Monitor Operability Testing R ER (6) REPORT DATE (71 THER FACILITIES INVOLVED (81 MOJttrt OAT ac QvfittrAL ~ Jttvlsrorr Morrtrr OAT TEAJt JJAM 6 JAJMIIUI NVMtN 98'ACAJTT 05000 10 17 97 97 007 01 03 30 JACLJTT JJAME 05000 EPO T IS SUBMITTED PUR SUANT TO THE REQUIREM TS OF 10CFR 6: (Checitone Or more) (11)
MODE (9) 20.2201 (01 ZoiZ 0 la) v 50.73(a1( Iti) 50.73(a)(2)(viii)
POWER 20,2203(a)(l) 20.2203(a)(3) (I) 50.73ta) (2) Oi) 50.73(a) t2) (Jt)
LEVEL (10) 100 20.2203(a) (21(r) 20. ZO (aII Iln) 0. 3(a1( Itrrrl 73. 1 20,2203(a) (2)(li) 20.2203(a) (4) 50.73(a)(21(iv) OTHER O. a) m 0.36lc)(1) ta)(2)(v) poetry In Abstra ct btlow orln NRC Form 366A 20.2203(a)(2] liv) 6(cll I 50.73(a)( ](vrrl o UC S E CDNTAC 0 HLs L 12)
JJAMK TRKFJJOJra JJVMFOt tlC4A Arto crrrJJJ Stephen J. Ellis - Nuclear Licensing Engineer 717/542-3537 COMPlETE ONE UN OR COMPONENT FAILURE DESCRIBED IN HIS REPORT(13)
CAUS i coMF0 Jrttrr MAJJUFAcrvrrot STsttM coMFoirotT SVPPLEIVIENTAL T ECTED (14) EXPECTED MONTH DA SUBMISSION YES X NO DATE (15)
(If yes, comp)cte EXPECTED SUBMISSION DATE).
ABSTRACT (Limit 1O 1400 SPaCeS. I.e.. aPPIOJCmately 15 Srn()lmPaCeo tyPeVvrrtten linea) (16)
On October 17, 1997, at 0920 hours0.0106 days <br />0.256 hours <br />0.00152 weeks <br />3.5006e-4 months <br />, with Unit 2 in Condition 1 (power Operation) at 10(W Power, a Technical Specification 3.0.3 entry was votuntan1y made. In accordance with the guidance of NUREG 1022, a Technical Specification 3.0.3 entry requires an LER to be submitted within 30 days of the event. The entry was made to allow completion of surveillance testing of one channel of the Rod Block Monitor (RBM), after considering the other available options. There is no provision provided in current Technical Speciticatlons to allow operability testing without entry into Technical Specification 3.0.3. The Technical Specification 3.1.4.3 ACTION statement had been entered to perform sulveit)ance testing of one channel of the RBM. Unexpected results had been obtained during the testing.
Investigation of these results determined that 11 LpRMs were not providing an output to the RBM. The testing resumed prior to the expiration of Technical Specification 3.1A.3 ACTION allowable time limit, but would not be completed before the limit expired.
Operations management votuntarily entered Technical Spe:ification 3.0.3, and did not take the ACTIONS described in Technical Specification 3.1A.3.a, that is placing the inoperable channel of the RBM tn the trip condition. In reconsidering this event, PPLL has recognized that the ACTION of Technical Specification 3.1.4.3.a should have been taken to avoid a condition that could be construed as an entry into Technical Specification 3.0.3 made for operational, convenience. The cause of the LPRM failures has been traced to inadequate post maintenance testing following earlier work associated with these components.. The failed components were repairedlreplaced, testing was completed and the RBM returned to operabte status. The safety significance of this event was minor, and the health and welfare of the public was not compromised. The technical aspect of this event will be reviewed with the work group a review of associated work plans and procedures witt be performed, and appropriate changes implemented. Administratively. 'nd guidance dealing with voluntary Technical Specification 3.0.3 entry and guidance dealing with actions to be taken once Technical Specification 3.0.3 has been entered, will be provided, These changes wilt be communicated to appropriate personnel.
NRC FOAM 366 (495)
~'Huu LD LNWQ LL DC$ uv ~v ~~ ta=v urr)~ I ~ IP4 NRC FORM 366A U,S. NUCLEAR REGULATORY COMlVIISSIOil (4.9$ ) +~
XJCENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACIL)TY NAME (1) DOCKET LER NUMBER (6) PAGE (3) 05000 tnlMMl Susquehanna Steam Electric Station - Unit 2 388 97 007 01 2 OF TEXT llfmore spece rc requ red, vse eddhionel copies of HRC Form 366AJ (17)
EVENT DESCRIPTION On October 17, 1997, at 0920 hours0.0106 days <br />0.256 hours <br />0.00152 weeks <br />3.5006e-4 months <br />, with Unit 2 in Condition 1(Power Operation) at100% power, a Technical Specification 3,0.3 entry was voluntarily made.
On October 16, 1997, at 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br /> Technical Specifications I.imiting Condition for Operation (LCO)
'.1.4.3 ACTION a and 3.3.6 ACTION 60 were entered to perform required surveillances for the Rod Block Monitor (RBM) (EIIS Code: I). The RBM must be removed from service to perform these surveillances. The ACTION of the most limiting Technical Specification states:
"With one RBM channel inoperative, restore the inoperative channel to OPERABLE status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and verify that the reactor is not operating on a LIMITINGCONTROL ROD PATTERN; otherwise, place the inoperable rod block monitor channel in the tripped condition within the next hour."
A few hours into the testing, unexpected results were observed and testing was halted to investigate
., these results. Since the RBM remained inoperable, the LCO ACTION remained in effect The 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> time period expired prior to restarting the surveillance testing. One hour remained before the.
Technical Specificatio'ns ACTION requires that the RBM channel be placed into the tripped condition.
Prior to the expiration of the one hour period, testing was restarted. Since testing had begun, the
, decision was made to voluntarily enter Technical Specification 3.0.3, considering that the completion of the surveillance testing would allow this channel of the RBM to be restored to service. Technical Specification 3.0.3 was entered at 0920 hours0.0106 days <br />0.256 hours <br />0.00152 weeks <br />3.5006e-4 months <br /> on October 17, 1997 and exited at 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br /> on October 17, 1997.
It was determined that the RBM was actually operating as designed, A number of the Local Power Monitors(LPRM) (EIIS Code: I) had a zero volt output to the RBM. The RBM correctly 'ange identified a zero input condition from an LPRM(s) and automatically eliminated it from the averaging circuit. As long as the RBM had more than the required minimum number of 'good'PRM inputs, it continued to function normally.
CAUSE OF EVENT The cause of the unexpected results of the RBM surveillance has been traced to the failure of components in the LPRM output to the RBM. When these components failed, their output to the RBM went to zero volts. 11 LPRMs were identified to have this condition. LPRM output to the Average Power Range Monitor (APRM) (EIIS Code: I), the Oscillation Power Range Monitor (OPRM)
. (EIIS Code:I), and to the plant computer were normal. It has been determined that the cause of the failed components stems from a power supply failure in June of 1997. The power supply had been replaced and outputs to the APRM and computer were checked, but not the outputs to the RBM. The post maintenance testing following the power supply replacement was not adequate, and is considered a root cause of the event.
NRC FORM 366A (4-()5)
tNJQ l4 4 o oQ
~ ~ h NRc.roRM 3eeA U.S. NUCLEAR REGULATORY COMMISSION l I4-'QS)
XZCENSEE EVENT REPORT (LEE)
TEXT CONTINUATION FACILITY NAME I1) DOCKET LER NUMBER le) PACE I3)
YEAN IhL 05000 NLlM46R HUM46R Susquehanna Steam Electric Station - Unit 2 388 97 007 .01 3 OF 5 TEXT /Ifmore speceis reqv/red. use edu'one/ copies of NRC Farm 866AJ {17)
Technical Specification 3.0.3 was voluntarily erltered when the inoperable channel of RBM was not in the tripped condition following the expiration of allowable time limit of Technical Specification 3.1A.3 ACTION (a). In order to perform the operability testing, the RBM can not be in the tripped condition.
The root cause of the Technical Specification 3,0.3 entry is an administrative omission in the current Technical Specifications. Improved Technical Specifications contain provisions to perform operability testing on inoperable equipment without entry, into a shutdown action statement. The decision to
'nter Technical Specification 3.0.3 is discvssed in greater detail below.
REPORTABILITY/ANALYSIS This Licensee Event Report is being made per 10 CFR 60.73(a)(2)(i)(B), in that NUREG 1022 requires the reporting of any entiy into Technical Specification LCO 3.0.3.
Technical SpecTiication 3.0.3 was entered to allow completion of surveillance testing of one channel of the RBM. As previously noted, one channel of the RBM was removed from service to perform
.surveillance testing. During that testing, unexpected results were obtained. The time to evaluate these results and then complete the testing was going to exceed the time allowed by Technical Specifications. Since completion of the svrveillance testing wovld allow the RBM to be restored to operable status, the decision was made to resume testing and a Technical Specification 3.0.3 entry
, was made when Technical Specification 3,1.4.3 ACTION (a) expired. This decision was made after considering the following alternatives:
- 1. Suspend testing of the RBM. Place the affected channel of the RBM in the tripped condition to satisfy the LCO ACTION. Enter 3.0.3 and activate the RBM channel to allow testing to resume.
- 2. Reduce power to 30% of Rated Thermal Power. The RBM is not required to be operable, and LCO 3.1.4.3.a does not apply.
- 3. Allow testing of the RBM to continue. This wovld mean that compliance with the LCO ACTION would not be maintained. As a result, entry into Technical Specification 3.0.3.
At the time this event occurred, option 1 and 2 were viewed by Operations as presenting an increased risk to nuclear safety. Option 3, the option chosen, was considered to be the least challenging to Operations, and to be within our authority as a licensee. Option 2 challenged the operator to manipulate reactor power, while option 1 required the surveillance work to be halted, delaying the restoration of the RBM, and vltimately resulting in a Technical Specification 3.0,3 entry anyway. Therefore, from strictly a safety perspective, Operations felt that Option 3 was the best option.
The above rationale was reconsidered in response to questions raised by the NRC concerning the appropriateness of entering Technical Specification 3.0.3. A review of the bases for Technical NRC FORM 366A I4 Qa)
HLJV LD, LOAD LC ~ QO NRC FORM 366A U.S. NUCLEAR REGULATORY CCMMISSIOI6 (4-96)
LICENSEE EVENT REPORT (LER)
~
TEXT CONTINUATION FACiL)TYNAME {l) DOCKET LER NUMBER (6) PAGE i3)
I N 05000 NLWOel NVMIBl Susquehanna Steam Electric Station - Unit 2 388 97 007 01 4 OF 5 TEXT Iifmore spece is rerruired,'lse eddic'ooel copies of HRC Form 36'O'AI (17)
Specification 3.0.3 states in part; "The purpose of this specification is to delineate the time limits for placing the unit in a safe shvtdown CONDITION when plant operation cannot be maintained within the limits for safe operation defined by the Limited Conditions for Operation and its ACTIbN requirements. It is not intended to be used as an operational convenience which permits (routine) voluntary removal of redvndant systems or components from service in lieu of other alternatives that would not result in redundant systems or components being inoperable." ln this case, we could have placed the subject RBM channel in the trip condition to meet the ACTION Statement. The requirement and prerequisite of the surveillance could have been re-established at which point Technical Specification 3.0.3 could have been entered to allow the testing. If a sitvation similar to this were to occur in the future, taking the Technical Specification ACTION as described would be
'roper course of action,'roperly balancing compliance and risk issues.. Additional guidance will be provided to shiff supervision as an aid in dealing with voluntary entry into Technical Specification LCO 3.0.3. This guidance will deal with removal of redundant equipment from service and with failure to meet LCO ACTION requirements.
Once entered, Technical Specification 3,0.3 requires action to be taken'to place the affected unit in STARTUP and HOT SHUTDOWN stating in part, within one hour action shall be taken to place the
'units in a OPERATIONAL'ONDITIONin which the specification does not apply by placing it, as
'pplicable in:
at least STARTUP within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> at least HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />...,"
Technical Specification LCO 3.0.3 was entered at 0920 hours0.0106 days <br />0.256 hours <br />0.00152 weeks <br />3.5006e-4 months <br />. The LCO was cleared at 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br />.
This was four hours and fifty minutes into the LCO, leaving two hours and ten minvtes for the vnit to
'~, be in STARTUP had any further problems been encountered. No power reductions were made during this time period. Throughout this period, shift supervision maintained oversight on the activities associated with Clearing the RBM problems, and had reasonable assurance that the LCO would be cleared before the allowed time to be in STARTUP expired. There was no procedvral guidance on specific actions that should have been taken, specific to a time frame, to ensure compliance with the ACTION time limits, PP&L believes it is important that we have very clear expectations associated with actions we intend to take once Technical Specification 3.0.3 is entered.
At no time during this event was the ability of the plant to safely shutdown or the health and welfare of the public compromised. The significance of this event from a safety standpoint was minor. The other channel of the RBM was available throughovt this period to provide rod block protection, as well as the APRMs to provide core protection in the event of a power transient.
In accordance with NUREG 1022, Supplement 1, the required submission date of this report was determined to be November 17, 1997.
Nile FORM 366A i4.95)
NRCiFORM 366A U,S. NUCLEAR REGULATORY COMMISSION (4.OG)
LICENSEE EVENT REPORT (LEE)
TEXT CONTINUATION FACILlTYNAME (1) DOCKET LER NUMBER (6) PAGE (3)
H 05000 'LIM6ER ~ani Susquehanna Steam Electric Station - Unit 2 388 97 007 - 01 5 OF 5 TEXT (llmora spacais required, usa additional copies of NRC Form 366AI (17)
CORRECTIVE ACTIONS r
Improved Technical Specif)cations addresses this type situation by providing allowance for operability testing without entering a shutdown action statement LCO. PP&L's Improved Technical Specification submittal is in review by the commission.
I A Technical SpecTiication change request to the current Technical Specifications has been submitted to the NRC to extend the LCO ACTION statement allowable time for one RBM channel inoperable from 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to seven days. Improved Technical Specrf(cations also reflects the lengthened ACTION time limits.
The failed components identified in the LPRMs were repaired/replaced.
The following actions are scheduled to be completed:
, A review of the technical aspects of the event with the involved maintenance work group stressing the importance of comprehensive post maintenance testing.
~ A review of work plans and procedures associated with the LPRMs, APRMs, and RBMs to determine and implement satisfactory methods of ensuring that all outputs from the LPRMs are sufficiently tested following work activities.
~ Evaluate resultslconclusions of above review for generic applicability to other systems.
~ Provide dear procedural guidance dealing with voluntary entry into Technical Specification LCO 3.0.3.
~ Provide clear procedural guidance dealing with actions to be taken by shift supervision once Technical Specification LCO 3.0.3 has been entered.
Communicate these changes to the appropriate personnel via training.
ADDITIONALINFORMATION Past similar events: None Entries into Technical Specification 3.0.3 have been reported on numerous occasions, although none of the previous reports were a result of a similar condition.
Failed Component: None LER written for Technical Specification 3.0.3 entry, the failed components were not the reason for submitting this report.
NRC FORM 3GGA (4.()5)
Hub La lusts La'ia us ~v ~~ taco urr ice. rl f 0+tC R4fd r ~ oo George J. Kuczynski PAL urces, Inc.
General Meagerusquehanna Two North Ninth Street Allentown, PA 181 01-1179 Susquehanna Steam Electric Station P.O. Box 487, 8e vlcc, PA 18803 Tet.717542.3120 Fax 717442.1949 November 17, 1997 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Station P1-137 Washington, DC 20555 SUSQUEHANNA STEAM ELECTRIC STATION LICENSEE EVENT REPORT 50-388/97-007-00 PLA - 4804 FILE R41-2 Docket No. 50-388 License No. NPF-22 Attached is Licensee Event Report 5%88/97-007-00. This event is being reported pursuant to the guidance of NUREG 1022, per 10CFR50.73(a)(2)(i)(B), for an entry into Technical Specification 3.0.3. The Technical Specification 3.0.3 entry was made voluntarily to allow completion of operability testing of one channel of the Rod Block Monitor. The operability testing was completed in a timely manner, the Rod Block Monitor was restored to operable status, and the Limiting Condition for Operation was cleared.
~
G. J. uczynski
~ ~
General Manager - Susquehanna SES Attachment Mr. H. J. Miller cc: Mr. Kenneth M. Jenison Regional Administrator Sr. Resident Inspector U. S. Nuclear Regulatory Commission U. S. Nuclear Regulatory Commission 475 Allendale Road P.O. Box 35 King of Prussia, PA 19406 Berwick, PA 18803-0035