Information Notice 2007-06, Potential Common Cause Vulnerabilities in Essential Service Water Systems: Difference between revisions

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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES


NUCLEAR REGULATORY COMMISSION
===NUCLEAR REGULATORY COMMISSION===
OFFICE OF NUCLEAR REACTOR REGULATION


OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555-0001


WASHINGTON, D.C. 20555-0001 February 9, 2007 NRC INFORMATION NOTICE 2007-06:                 POTENTIAL COMMON CAUSE
===February 9, 2007===
NRC INFORMATION NOTICE 2007-06: POTENTIAL COMMON CAUSE


VULNERABILITIES IN ESSENTIAL SERVICE
VULNERABILITIES IN ESSENTIAL SERVICE


WATER SYSTEMS
===WATER SYSTEMS===


==ADDRESSEES==
==ADDRESSEES==
Line 40: Line 42:
manner that precludes the development of potential common cause failure vulnerabilities due to
manner that precludes the development of potential common cause failure vulnerabilities due to


piping or heat exchanger degradation. It is expected that recipients will review the information
piping or heat exchanger degradation. It is expected that recipients will review the information


for applicability to their facilities and consider actions, as appropriate, to avoid similar problems.
for applicability to their facilities and consider actions, as appropriate, to avoid similar problems.
Line 51: Line 53:
There have been two events at foreign operating reactors in which external corrosion of piping
There have been two events at foreign operating reactors in which external corrosion of piping


located in vaults has caused a catastrophic loss of one train of the ESW system. These two
located in vaults has caused a catastrophic loss of one train of the ESW system. These two


events also had common cause failure aspects that were identified as part of the extent-of- condition reviews. The first foreign event occurred at a pressurized-water reactor (PWR)
events also had common cause failure aspects that were identified as part of the extent-of- condition reviews. The first foreign event occurred at a pressurized-water reactor (PWR)
designed by Westinghouse, that began commercial operation in 1988. On August 25, 2004, while operating at 100 percent power, an ESW system manhole pipe broke circumferentially
designed by Westinghouse, that began commercial operation in 1988. On August 25, 2004, while operating at 100 percent power, an ESW system manhole pipe broke circumferentially


prompting a plant shutdown from the total loss of the B train of the ESW system. The event
prompting a plant shutdown from the total loss of the B train of the ESW system. The event


was of great concern for plant safety because it could have led to a common cause failure in a
was of great concern for plant safety because it could have led to a common cause failure in a


system that is the ultimate heat sink for most safety loads. The ESW pipes are buried and use
system that is the ultimate heat sink for most safety loads. The ESW pipes are buried and use


manholes at certain intervals to allow for inspection and maintenance. The ESW piping is a
manholes at certain intervals to allow for inspection and maintenance. The ESW piping is a


BONNA design that uses a steel pipe lined with cement on both sides to prevent corrosion.
BONNA design that uses a steel pipe lined with cement on both sides to prevent corrosion.
Line 68: Line 70:
The manhole filled with surface water and corroded the exposed carbon steel manhole piping
The manhole filled with surface water and corroded the exposed carbon steel manhole piping


neck. The break resulted from external corrosion due to improper installation of external
neck. The break resulted from external corrosion due to improper installation of external


cement pipe coating. The licensee extent-of-condition review found corrosion at two other
cement pipe coating. The licensee extent-of-condition review found corrosion at two other


ESW manhole necks that also required significant repair.
ESW manhole necks that also required significant repair.
Line 76: Line 78:
The second foreign event occurred at a PWR, designed by Framatome, that began commercial
The second foreign event occurred at a PWR, designed by Framatome, that began commercial


operation in 1988. On December 11, 1998, while operating at 75 percent power, an ESW pipe
operation in 1988. On December 11, 1998, while operating at 75 percent power, an ESW pipe


ruptured and flooded the piping gallery with sea water. Since the B train of the ESW system
ruptured and flooded the piping gallery with sea water. Since the B train of the ESW system


was lost, the operators shutdown the plant. The pipe is composed of prestressed, inner and
was lost, the operators shutdown the plant. The pipe is composed of prestressed, inner and


outer concrete pipes with embedded strings and steel pipe. A visual inspection of the failed
outer concrete pipes with embedded strings and steel pipe. A visual inspection of the failed


pipe revealed a 3.3 foot long by 2.8 inches wide through-wall rupture. The prestressed wire
pipe revealed a 3.3 foot long by 2.8 inches wide through-wall rupture. The prestressed wire


and steel cylinder were found to be severely corroded. The pipe is located in an underground
and steel cylinder were found to be severely corroded. The pipe is located in an underground


gallery that has very humid conditions. The licensee determined that condensation got inside a
gallery that has very humid conditions. The licensee determined that condensation got inside a


small crack on the surface of the pipe causing corrosion of the steel wire. The licensee extent- of-condition review identified 16 other pipe spools that were also replaced.
small crack on the surface of the pipe causing corrosion of the steel wire. The licensee extent- of-condition review identified 16 other pipe spools that were also replaced.


There also have been two events at domestic operating reactor plants that experienced
There also have been two events at domestic operating reactor plants that experienced
Line 96: Line 98:
significant internal degradation of critical ESW components that had the potential for common
significant internal degradation of critical ESW components that had the potential for common


cause failures. On June 27, 2005, at the South Texas Project, Unit 2, a three gallons/hour
cause failures. On June 27, 2005, at the South Texas Project, Unit 2, a three gallons/hour


through-wall leak was identified in Train 2A, essential cooling water (ECW) system piping
through-wall leak was identified in Train 2A, essential cooling water (ECW) system piping


flange. The pipe is 30 inches in diameter, composed of an aluminum-bronze, and is located
flange. The pipe is 30 inches in diameter, composed of an aluminum-bronze, and is located


immediately downstream of an ECW return throttle (butterfly) valve. Subsequent licensee
immediately downstream of an ECW return throttle (butterfly) valve. Subsequent licensee


investigation found cavitation pitting, circumferential pipe cracking, and pipe-to-end flange weld
investigation found cavitation pitting, circumferential pipe cracking, and pipe-to-end flange weld


separation in the pipe. On August 15, 2005, as part of their extent-of-condition review, the
separation in the pipe. On August 15, 2005, as part of their extent-of-condition review, the


licensee inspected Train 2B of the ECW system and determined that a similar downstream
licensee inspected Train 2B of the ECW system and determined that a similar downstream


flange had an approximately 30 inches-long by three inches-wide segment of the aluminum- bronze pipe that broke free. Train 2B of the ECW system was declared inoperable for the
flange had an approximately 30 inches-long by three inches-wide segment of the aluminum- bronze pipe that broke free. Train 2B of the ECW system was declared inoperable for the


same reasons as ECW Train 2A and was reported to the NRC as a common-cause
same reasons as ECW Train 2A and was reported to the NRC as a common-cause
Line 116: Line 118:
inoperability of independent trains (Licensee Event Report No. 499/2005004, Agencywide
inoperability of independent trains (Licensee Event Report No. 499/2005004, Agencywide


Documents Access and Management System (ADAMS) Accession No. ML052630031). The
Documents Access and Management System (ADAMS) Accession No. ML052630031). The


licensee determined the cause of the damage was cavitation impingement from the heavily
licensee determined the cause of the damage was cavitation impingement from the heavily


throttled butterfly valve. The root cause was the failure to incorporate requisite inspection
throttled butterfly valve. The root cause was the failure to incorporate requisite inspection


activities for ECW piping into station programs.
activities for ECW piping into station programs.
Line 132: Line 134:
Licensee inspections identified significant damage to the endbell due to microbiologically
Licensee inspections identified significant damage to the endbell due to microbiologically


induced corrosion (MIC). The licensee maintenance rule evaluation determined that the poor
induced corrosion (MIC). The licensee maintenance rule evaluation determined that the poor


condition of the endbells from pitting caused by MIC was known for nearly ten years, but timely
condition of the endbells from pitting caused by MIC was known for nearly ten years, but timely


and effective corrective actions were not taken. Also, on April 22, 2005, a through-wall service
and effective corrective actions were not taken. Also, on April 22, 2005, a through-wall service


water (SW) leak occurred on the G-02 EDG heat exchanger alternate SW supply line due to
water (SW) leak occurred on the G-02 EDG heat exchanger alternate SW supply line due to
Line 145: Line 147:
The ESW system (or its equivalent) for U. S. commercial reactor plants is the assured, safety- related means of transferring sensible and decay heat from the reactor coolant system to the
The ESW system (or its equivalent) for U. S. commercial reactor plants is the assured, safety- related means of transferring sensible and decay heat from the reactor coolant system to the


ultimate heat sink. The ESW system is also relied upon for other critical safety functions, such
ultimate heat sink. The ESW system is also relied upon for other critical safety functions, such


as providing cooling water for most of the essential, safety-related equipment used for
as providing cooling water for most of the essential, safety-related equipment used for
Line 153: Line 155:
pool cooling, and for dissipating sensible and reactor decay heat during shutdown conditions. Also, on PWRs, the safety related auxiliary feedwater systems typically rely on the ESW system
pool cooling, and for dissipating sensible and reactor decay heat during shutdown conditions. Also, on PWRs, the safety related auxiliary feedwater systems typically rely on the ESW system


as an emergency makeup water source for feeding the steam generators. Plant-specific
as an emergency makeup water source for feeding the steam generators. Plant-specific


probabilistic risk assessments (PRAs) have shown that the loss of the ESW system may be a
probabilistic risk assessments (PRAs) have shown that the loss of the ESW system may be a
Line 164: Line 166:
vicinity of weld neck flanges that had been installed to allow personnel access for inspecting the
vicinity of weld neck flanges that had been installed to allow personnel access for inspecting the


inside ESW system piping surfaces. The unprotected weld neck joints were subject to
inside ESW system piping surfaces. The unprotected weld neck joints were subject to


corrosion. All of these areas were also subject to routine wetting of the unprotected exterior
corrosion. All of these areas were also subject to routine wetting of the unprotected exterior


surface of weld neck areas. In addition, NRC staff concluded that a fundamental shortcoming
surface of weld neck areas. In addition, NRC staff concluded that a fundamental shortcoming


associated with the first foreign event was the utilitys failure to adequately trend and take
associated with the first foreign event was the utilitys failure to adequately trend and take


appropriate corrective action for a known degraded condition. Domestic operating reactor
appropriate corrective action for a known degraded condition. Domestic operating reactor


plants are subject to Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B,
plants are subject to Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B,
Line 181: Line 183:
The second foreign event also involved the failure to protect the exterior piping surface of the
The second foreign event also involved the failure to protect the exterior piping surface of the


ESW system. One of the lessons learned was to implement an inspection program that
ESW system. One of the lessons learned was to implement an inspection program that


inspects for both internal and external corrosion. The licensee also painted the outside of the
inspects for both internal and external corrosion. The licensee also painted the outside of the


ESW pipes to minimize the potential for corrosion.
ESW pipes to minimize the potential for corrosion.
Line 189: Line 191:
Domestically, a potentially similar problem was noted during an NRC inspection at the Point
Domestically, a potentially similar problem was noted during an NRC inspection at the Point


Beach facility. Like the first foreign event, the licensee for Point Beach did not take appropriate
Beach facility. Like the first foreign event, the licensee for Point Beach did not take appropriate


corrective action to resolve a known degraded condition until MIC resulted in an actual failure.
corrective action to resolve a known degraded condition until MIC resulted in an actual failure.
Line 203: Line 205:
However, domestic ESW systems typically include piping sections that are buried and not
However, domestic ESW systems typically include piping sections that are buried and not


readily accessible for inspection. Buried sections of piping can be subject to periodic wetting
readily accessible for inspection. Buried sections of piping can be subject to periodic wetting


from storms or local flooding conditions. Exterior protective coatings may also not be fully intact
from storms or local flooding conditions. Exterior protective coatings may also not be fully intact


due to improper installation, age degradation, or maintenance practices. It is also possible for
due to improper installation, age degradation, or maintenance practices. It is also possible for


some ESW piping sections to be located in vaults or pipe chases that are subject to periodic
some ESW piping sections to be located in vaults or pipe chases that are subject to periodic
Line 213: Line 215:
flooding and/or high humidity that can closely mimic the foreign events. Also, at South Texas Project Unit 2, ESW system degradation led to a through-wall leak that
flooding and/or high humidity that can closely mimic the foreign events. Also, at South Texas Project Unit 2, ESW system degradation led to a through-wall leak that


ultimately became an actual common cause failure vulnerability. Similar cavitation damage was
ultimately became an actual common cause failure vulnerability. Similar cavitation damage was


found in two trains of the ESW system at Unit 2. Proper application of the recommendations of
found in two trains of the ESW system at Unit 2. Proper application of the recommendations of


NRC Generic Letter (GL) 89-13, Service Water System Problems Affecting Safety-Related
NRC Generic Letter (GL) 89-13, Service Water System Problems Affecting Safety-Related
Line 226: Line 228:
NRC GL 89-13, Service Water System Problems Affecting Safety-Related Equipment, dated
NRC GL 89-13, Service Water System Problems Affecting Safety-Related Equipment, dated


July 18, 1989, requested specific licensee actions to resolve SW system problems. In
July 18, 1989, requested specific licensee actions to resolve SW system problems. In


particular, this GL recommended that licensees ensure by a routine inspection and
particular, this GL recommended that licensees ensure by a routine inspection and
Line 235: Line 237:


NRC GL 90-05, Guidance for Performing Temporary Non-Code Repair of ASME Code Class 1,
NRC GL 90-05, Guidance for Performing Temporary Non-Code Repair of ASME Code Class 1,
2, and 3 Piping, dated June 15, 1990, provides guidance for Code Class 3 piping. Two specific
2, and 3 Piping, dated June 15, 1990, provides guidance for Code Class 3 piping. Two specific


flaw evaluation approaches, as discussed in Enclosure 1 to the GL, should be considered, namely, the "through-wall flaw" and the "wall thinning" approaches.
flaw evaluation approaches, as discussed in Enclosure 1 to the GL, should be considered, namely, the "through-wall flaw" and the "wall thinning" approaches.
Line 263: Line 265:


==CONTACT==
==CONTACT==
This information notice requires no specific action or written response. Please direct any
This information notice requires no specific action or written response. Please direct any


questions about this matter to the technical contacts listed below.
questions about this matter to the technical contacts listed below.


/TQuay for MCase/
/TQuay for MCase/
                                      Michael J. Case, Director


===Michael J. Case, Director===
Division of Policy and Rulemaking
Division of Policy and Rulemaking


Office of Nuclear Reactor Regulation
===Office of Nuclear Reactor Regulation===
 
Technical Contacts: Richard A. Laura, NRR/DIRS
Technical Contacts:   Richard A. Laura, NRR/DIRS


301-415-1837 E-mail: ral1@nrc.gov
301-415-1837 E-mail: ral1@nrc.gov
Line 285: Line 286:


==CONTACT==
==CONTACT==
This information notice requires no specific action or written response. Please direct any
This information notice requires no specific action or written response. Please direct any


questions about this matter to the technical contacts listed below.
questions about this matter to the technical contacts listed below.


/TQuay for MCase/
/TQuay for MCase/
                                          Michael J. Case, Director


===Michael J. Case, Director===
Division of Policy and Rulemaking
Division of Policy and Rulemaking


Office of Nuclear Reactor Regulation
===Office of Nuclear Reactor Regulation===
 
Technical Contacts: Richard A. Laura, NRR/DIRS
Technical Contacts:   Richard A. Laura, NRR/DIRS


301-415-1837 E-mail: ral1@nrc.gov
301-415-1837 E-mail: ral1@nrc.gov
Line 306: Line 306:
Note: NRC generic communications may be found on the NRC public web site, http://www.nrc.gov under Electronic Reading Room/Document Collections.
Note: NRC generic communications may be found on the NRC public web site, http://www.nrc.gov under Electronic Reading Room/Document Collections.


ADAMS Accession Number: ML062840608 OFFICE     DIRS:IOEB       Tech.Editor       BC:DSS:SBPB         TL:DIRS:IOEB     PGCB:DPR
ADAMS Accession Number: ML062840608 OFFICE
 
DIRS:IOEB
 
Tech.Editor
 
BC:DSS:SBPB
 
TL:DIRS:IOEB
 
PGCB:DPR
 
NAME
 
RLaura
 
CBladey
 
JSegala
 
MKing
 
CHawes CMH
 
DATE
 
10/18/2006
10/18/2006
10/23/2006
02/01/2007
10/27/2006 OFFICE
 
PGCB:DPR
 
IP
 
BC:ADRA:DPR
 
D:DPR
 
NAME
 
QNguyen
 
JDunnLee


NAME        RLaura          CBladey            JSegala            MKing            CHawes CMH
CJackson


DATE        10/18/2006      10/18/2006        10/23/2006          02/01/2007      10/27/2006 OFFICE      PGCB:DPR        IP                BC:ADRA:DPR        D:DPR
MJCase


NAME        QNguyen          JDunnLee          CJackson            MJCase
DATE


DATE        02/02/2007         01/22/2007       02/082007         02/09/2007 OFFICIAL RECORD COPY}}
02/02/2007
    01/22/2007
    02/082007
02/09/2007 OFFICIAL RECORD COPY}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 05:56, 15 January 2025

Potential Common Cause Vulnerabilities in Essential Service Water Systems
ML062840608
Person / Time
Site: Point Beach, South Texas  NextEra Energy icon.png
Issue date: 02/09/2007
From: Michael Case
NRC/NRR/ADRA/DPR
To:
Richard Laura, NRR/DIRS/IOEB
References
IN-07-006
Download: ML062840608 (6)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555-0001

February 9, 2007

NRC INFORMATION NOTICE 2007-06: POTENTIAL COMMON CAUSE

VULNERABILITIES IN ESSENTIAL SERVICE

WATER SYSTEMS

ADDRESSEES

All holders of operating licensees for nuclear power reactors, except those who have

permanently ceased operations and have certified that fuel has been permanently removed

from the reactor vessel.

PURPOSE

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to alert

addressees of the importance of maintaining essential service water (ESW) systems in a

manner that precludes the development of potential common cause failure vulnerabilities due to

piping or heat exchanger degradation. It is expected that recipients will review the information

for applicability to their facilities and consider actions, as appropriate, to avoid similar problems.

However, suggestions contained in this IN are not NRC requirements; therefore, no specific

action or written response is required.

DESCRIPTION OF CIRCUMSTANCES

There have been two events at foreign operating reactors in which external corrosion of piping

located in vaults has caused a catastrophic loss of one train of the ESW system. These two

events also had common cause failure aspects that were identified as part of the extent-of- condition reviews. The first foreign event occurred at a pressurized-water reactor (PWR)

designed by Westinghouse, that began commercial operation in 1988. On August 25, 2004, while operating at 100 percent power, an ESW system manhole pipe broke circumferentially

prompting a plant shutdown from the total loss of the B train of the ESW system. The event

was of great concern for plant safety because it could have led to a common cause failure in a

system that is the ultimate heat sink for most safety loads. The ESW pipes are buried and use

manholes at certain intervals to allow for inspection and maintenance. The ESW piping is a

BONNA design that uses a steel pipe lined with cement on both sides to prevent corrosion.

The manhole filled with surface water and corroded the exposed carbon steel manhole piping

neck. The break resulted from external corrosion due to improper installation of external

cement pipe coating. The licensee extent-of-condition review found corrosion at two other

ESW manhole necks that also required significant repair.

The second foreign event occurred at a PWR, designed by Framatome, that began commercial

operation in 1988. On December 11, 1998, while operating at 75 percent power, an ESW pipe

ruptured and flooded the piping gallery with sea water. Since the B train of the ESW system

was lost, the operators shutdown the plant. The pipe is composed of prestressed, inner and

outer concrete pipes with embedded strings and steel pipe. A visual inspection of the failed

pipe revealed a 3.3 foot long by 2.8 inches wide through-wall rupture. The prestressed wire

and steel cylinder were found to be severely corroded. The pipe is located in an underground

gallery that has very humid conditions. The licensee determined that condensation got inside a

small crack on the surface of the pipe causing corrosion of the steel wire. The licensee extent- of-condition review identified 16 other pipe spools that were also replaced.

There also have been two events at domestic operating reactor plants that experienced

significant internal degradation of critical ESW components that had the potential for common

cause failures. On June 27, 2005, at the South Texas Project, Unit 2, a three gallons/hour

through-wall leak was identified in Train 2A, essential cooling water (ECW) system piping

flange. The pipe is 30 inches in diameter, composed of an aluminum-bronze, and is located

immediately downstream of an ECW return throttle (butterfly) valve. Subsequent licensee

investigation found cavitation pitting, circumferential pipe cracking, and pipe-to-end flange weld

separation in the pipe. On August 15, 2005, as part of their extent-of-condition review, the

licensee inspected Train 2B of the ECW system and determined that a similar downstream

flange had an approximately 30 inches-long by three inches-wide segment of the aluminum- bronze pipe that broke free. Train 2B of the ECW system was declared inoperable for the

same reasons as ECW Train 2A and was reported to the NRC as a common-cause

inoperability of independent trains (Licensee Event Report No. 499/2005004, Agencywide

Documents Access and Management System (ADAMS) Accession No. ML052630031). The

licensee determined the cause of the damage was cavitation impingement from the heavily

throttled butterfly valve. The root cause was the failure to incorporate requisite inspection

activities for ECW piping into station programs.

On March 20, 2005, at Point Beach Nuclear Plant, Unit 1, the G-01 emergency diesel generator

(EDG) became inoperable due to a through-wall leak in the endbell of the EDG cooling system

heat exchanger (Inspection Report 50-266/2005-010, ADAMS Accession No. ML053000237).

Licensee inspections identified significant damage to the endbell due to microbiologically

induced corrosion (MIC). The licensee maintenance rule evaluation determined that the poor

condition of the endbells from pitting caused by MIC was known for nearly ten years, but timely

and effective corrective actions were not taken. Also, on April 22, 2005, a through-wall service

water (SW) leak occurred on the G-02 EDG heat exchanger alternate SW supply line due to

MIC.

BACKGROUND

The ESW system (or its equivalent) for U. S. commercial reactor plants is the assured, safety- related means of transferring sensible and decay heat from the reactor coolant system to the

ultimate heat sink. The ESW system is also relied upon for other critical safety functions, such

as providing cooling water for most of the essential, safety-related equipment used for

mitigating plant accident and transient conditions, reactor coolant pump seal cooling, spent fuel

pool cooling, and for dissipating sensible and reactor decay heat during shutdown conditions. Also, on PWRs, the safety related auxiliary feedwater systems typically rely on the ESW system

as an emergency makeup water source for feeding the steam generators. Plant-specific

probabilistic risk assessments (PRAs) have shown that the loss of the ESW system may be a

significant contributor to the potential for a core damage accident.

DISCUSSION

The first foreign event involved the failure to properly protect the exterior piping surfaces in the

vicinity of weld neck flanges that had been installed to allow personnel access for inspecting the

inside ESW system piping surfaces. The unprotected weld neck joints were subject to

corrosion. All of these areas were also subject to routine wetting of the unprotected exterior

surface of weld neck areas. In addition, NRC staff concluded that a fundamental shortcoming

associated with the first foreign event was the utilitys failure to adequately trend and take

appropriate corrective action for a known degraded condition. Domestic operating reactor

plants are subject to Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B,

Criterion XVI, Corrective Action, which requires that prompt and effective corrective actions be

taken to address significant conditions adverse to quality.

The second foreign event also involved the failure to protect the exterior piping surface of the

ESW system. One of the lessons learned was to implement an inspection program that

inspects for both internal and external corrosion. The licensee also painted the outside of the

ESW pipes to minimize the potential for corrosion.

Domestically, a potentially similar problem was noted during an NRC inspection at the Point

Beach facility. Like the first foreign event, the licensee for Point Beach did not take appropriate

corrective action to resolve a known degraded condition until MIC resulted in an actual failure.

Also, like the first foreign event, MIC attack of the EDG endbells represented a common cause

failure mechanism that could render all of the EDGs inoperable if not properly monitored and

resolved.

ESW systems for U. S. nuclear power plants are generally unique from one plant to another.

However, domestic ESW systems typically include piping sections that are buried and not

readily accessible for inspection. Buried sections of piping can be subject to periodic wetting

from storms or local flooding conditions. Exterior protective coatings may also not be fully intact

due to improper installation, age degradation, or maintenance practices. It is also possible for

some ESW piping sections to be located in vaults or pipe chases that are subject to periodic

flooding and/or high humidity that can closely mimic the foreign events. Also, at South Texas Project Unit 2, ESW system degradation led to a through-wall leak that

ultimately became an actual common cause failure vulnerability. Similar cavitation damage was

found in two trains of the ESW system at Unit 2. Proper application of the recommendations of

NRC Generic Letter (GL) 89-13, Service Water System Problems Affecting Safety-Related

Equipment, and 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, likely would

have prevented this event.

RELEVANT GENERIC COMMUNICATIONS

NRC GL 89-13, Service Water System Problems Affecting Safety-Related Equipment, dated

July 18, 1989, requested specific licensee actions to resolve SW system problems. In

particular, this GL recommended that licensees ensure by a routine inspection and

maintenance program for open-cycle SW system piping and components that corrosion, erosion protective coating failure, silting, and biofouling cannot degrade the performance of

safety related systems supplied by service water.

NRC GL 90-05, Guidance for Performing Temporary Non-Code Repair of ASME Code Class 1,

2, and 3 Piping, dated June 15, 1990, provides guidance for Code Class 3 piping. Two specific

flaw evaluation approaches, as discussed in Enclosure 1 to the GL, should be considered, namely, the "through-wall flaw" and the "wall thinning" approaches.

NRC IN 92-49, Recent Loss Or Severe Degradation Of Service Water Systems, dated July 2,

1992, alerted licensees to several service water related events, including one event that

resulted in the loss of the ultimate heat sink for a short period of time.

NRC IN 94-79, Microbiologically Influenced Corrosion Of Emergency Diesel Generator Service

Water Piping, dated November 23, 1994, alerted licensees that stagnant or intermittent-flow

conditions, as in the case of emergency diesel service water supply headers, are conducive to

the growth of microorganisms that can accelerate corrosion rates.

NUREG-1275, Volume 3, "Operating Experience Feedback Report - Service Water System

Failures and Degradations in Light Water Reactors," (November 1988) summarizes and

discusses SW system events from 1980 to early 1987.

NUREG-1461, "Regulatory Analysis for the Resolution of Generic Issue 153: Loss of Essential

Service Water in LWRs, (August 1993) provides a review of industry experience and plant- specific PRAs and insights related to ESW system vulnerabilities.

CONTACT

This information notice requires no specific action or written response. Please direct any

questions about this matter to the technical contacts listed below.

/TQuay for MCase/

Michael J. Case, Director

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Technical Contacts: Richard A. Laura, NRR/DIRS

301-415-1837 E-mail: ral1@nrc.gov

James E. Tatum, NRR/DSS

301-415-2805 E-mail: jet1@nrc.gov

Note: NRC generic communications may be found on the NRC public web site, http://www.nrc.gov under Electronic Reading Room/Document Collections.

CONTACT

This information notice requires no specific action or written response. Please direct any

questions about this matter to the technical contacts listed below.

/TQuay for MCase/

Michael J. Case, Director

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Technical Contacts: Richard A. Laura, NRR/DIRS

301-415-1837 E-mail: ral1@nrc.gov

James E. Tatum, NRR/DSS

301-415-2805 E-mail: jet1@nrc.gov

Note: NRC generic communications may be found on the NRC public web site, http://www.nrc.gov under Electronic Reading Room/Document Collections.

ADAMS Accession Number: ML062840608 OFFICE

DIRS:IOEB

Tech.Editor

BC:DSS:SBPB

TL:DIRS:IOEB

PGCB:DPR

NAME

RLaura

CBladey

JSegala

MKing

CHawes CMH

DATE

10/18/2006

10/18/2006

10/23/2006

02/01/2007

10/27/2006 OFFICE

PGCB:DPR

IP

BC:ADRA:DPR

D:DPR

NAME

QNguyen

JDunnLee

CJackson

MJCase

DATE

02/02/2007

01/22/2007

02/082007

02/09/2007 OFFICIAL RECORD COPY