|
|
(2 intermediate revisions by the same user not shown) |
Line 3: |
Line 3: |
| | issue date = 12/31/1995 | | | issue date = 12/31/1995 |
| | title = LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr | | | title = LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr |
| | author name = GRABO B A, LEVINE J M | | | author name = Grabo B, Levine J |
| | author affiliation = ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR | | | author affiliation = ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR |
| | addressee name = | | | addressee name = |
Line 16: |
Line 16: |
|
| |
|
| =Text= | | =Text= |
| {{#Wiki_filter:~CATEGORY j.REGULATO Y INFORMATION DISTRIBUTION STEM (RIDS)ACCESSION NBR:9601160059 DOC.DATE: 95/12/31 NOTARIZED: | | {{#Wiki_filter:~ |
| NO DOCKET¹FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH.NAME AUTHOR AFFILIATION GRABO,B.A. | | CATEGORY j. |
| Arizona Public Service Co.(formerly Arizona Nuclear Power LEVINE,J.M. | | REGULATO Y INFORMATION DISTRIBUTION STEM (RIDS) |
| Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION | | ACCESSION NBR:9601160059 DOC.DATE: 95/12/31 NOTARIZED: NO DOCKET ¹ FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME AUTHOR AFFILIATION GRABO,B.A. Arizona Public Service Co. (formerly Arizona Nuclear Power LEVINE,J.M. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION |
|
| |
|
| ==SUBJECT:== | | ==SUBJECT:== |
| LER 95-013-00:on 951201,AFW sys was outside design basis of.plant.Caused by design error.Performed assessment to demonstrate that existing condition does not pose addi safety concerns.W/951231 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR | | LER 95-013-00:on 951201,AFW sys was outside design basis of. |
| )ENCI i SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.05000528 NOTES:STANDARDIZED PLANT RECIPIENT ID CODE/NAME PD4-2 PD INTERNAL: ACRS AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DSIR/EIB EXTERNAL: L ST LOBBY WARD NOAC MURPHYPG.A NRC PDR COPIES RECIPIENT LTTR ENCI ID CODE/NAME 1 1 HOLIAN, B 1 GD~B B 1 FILE CENTER 1~~BB 1 NRR/DRCH/HHFB 1 NRR/DRCH/HOLB NRR/DRPM/PECB 1 NRR/DSSA/SRXB 1 RGN4 FILE 01 1 1 LITCO BRYCEPJ H 1 1 NOAC POOREPW.1 1 NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENTS: | | plant. Caused by design error. Performed assessment to demonstrate that existing condition does not pose addi safety concerns.W/951231 ltr. |
| PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 26 4k~1 JAMES M.LEVINE VICE PRESIDENT NUCLEAR PRODUCTION Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O.BOX 52034~PHOENIX.ARIZONA 850?2-=i3 192-00955-JML/BAG/DLK December 31, 1995 U.S.Nuclear Regulatory Commission ATTN: Document Control Desk Mail Station-P1-37 Washington, DC 20555-0001 | | DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ) ENCI i SIZE: |
| | TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. |
| | NOTES:STANDARDIZED PLANT 05000528 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCI ID CODE/NAME LTTR ENCL PD4-2 PD 1 1 HOLIAN, B 1 1 INTERNAL: ACRS 1 GD~B B 2 2 AEOD/SPD/RRAB 1 FILE CENTER 1 1 NRR/DE/ECGB NRR/DE/EMEB 1 |
| | 1 |
| | ~~BB NRR/DRCH/HHFB 1 |
| | 1 1 |
| | 1 NRR/DRCH/HICB 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 RGN4 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCEPJ H 2 2 NOAC MURPHYPG.A 1 1 NOAC POOREPW. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS: |
| | PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED! |
| | FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 26 |
| | |
| | ~ 1 4k |
| | |
| | Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O. BOX 52034 ~ PHOENIX. ARIZONA 850?2-=i3 192-00955-JML/BAG/DLK JAMES M. LEVINE December 31, 1995 VICE PRESIDENT NUCLEAR PRODUCTION U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Station-P1-37 Washington, DC 20555-0001 |
|
| |
|
| ==Dear Sirs:== | | ==Dear Sirs:== |
|
| |
|
| ==Subject:== | | ==Subject:== |
| Palo Verde Nuclear Generating Station (PVNGS)Units 1, 2, and 3 Docket Nos.STN 50-528, 50-529, 50-530 License Nos.NPF41, NPF-51, NPF-74 Licensee Event Report.95-013-00 Attached please find, Licensee Event Report (LER)95-013 prepared and submitted pursuant to 10 CFR 50.73.This LER reports a condition where an intermediate sized steam line break accident scenario was discovered that could result in the loss of both steam generators as an available heat sink to remove decay heat under limited accident conditions. | | Palo Verde Nuclear Generating Station (PVNGS) |
| In accordance with 10 CFR 50.73(d), a copy of this LER is being forwarded to the Regional Administrator, NRC Region IV.If you have any questions, please contact Burton A.Grabo, Section Leader, Nuclear Regulatory Affairs, at (602)393-6492.Sincerely, JML/BAG/DLK Attachment (all with attachment) cc: L.J.Callan K.E.Perkins K.E.Johnston INPO Records Center 960ii60059 95i23i PDR ADOCK 05000528 S PDR zg>p | | Units 1, 2, and 3 Docket Nos. STN 50-528, 50-529, 50-530 License Nos. NPF41, NPF-51, NPF-74 Licensee Event Report.95-013-00 Attached please find, Licensee Event Report (LER) 95-013 prepared and submitted pursuant to 10 CFR 50.73. This LER reports a condition where an intermediate sized steam line break accident scenario was discovered that could result in the loss of both steam generators as an available heat sink to remove decay heat under limited accident conditions. |
| | In accordance with 10 CFR 50.73(d), a copy of this LER is being forwarded to the Regional Administrator, NRC Region IV. If you have any questions, please contact Burton A. Grabo, Section Leader, Nuclear Regulatory Affairs, at (602) 393-6492. |
| | Sincerely, JML/BAG/DLK Attachment cc: L. J. Callan (all with attachment) |
| | K. E. Perkins K. E. Johnston INPO Records Center 960ii60059 95i23i PDR ADOCK 05000528 S PDR zg> |
| | p |
| | |
| | LICENSEE EVENT REPORT (LER) |
| | ACIUTYNAME (1) DOCKET NUMBER (2) PAGE (3) |
| | Palo Verde Unit 1 0 5 0 0 0 5 2 8 1OFO'6 TLE (4) |
| | Accident Condition Identified Puts Auxiliary Feedwater Beyond Component Level Design Basis EVENT DATE 5 LER NUMBER 6 REPORT DATE 7 OTHER FACIUTIES INVOLVED 6 MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FACIUIYNAMES KET NUMBERS NUMBER NUMBER Palo Verde Unit 2 0 5 0 0 0 5 2 9 1 2 0 1 9 5 9 5 0 1 3 0 0 1 2 3 1 9 5 Palo Verde Unit 3 0 5 0 0 0 5'3 0 OPE RATING HIS REPORT IS SUBMITTED PURSUANT TO THE RED UIREMENTs 0F 10 cFR 4: (chedt one or more of the fosowng) (11) |
| | MODE (6) 20.402(b) 20.405(c) 50.73(aX2XN) 73.71(b) |
| | POWER 20.405(aX1Xi) 50.36(cX I) 50,73(aX2Xv) 73.71(c) |
| | LEVEL(10) 9 9 20.405(sX1X i) 50.36(cX2) 50.73(aX2Xvi) OTHER (Spectfy in Abstract 20.405(aXIXB) 50.73(aX2XI) 50.73(aX2XvtnXA) below snd in Text, NRC Form 20.405(sXI Xiv) 50.73(aX2Xn) M.73(sX2XvntXB) 20.405(aXI Xv) 50.73(aX2XB) 50.73(aX2Xx) |
| | LICENSEE CONTACT FOR THIS LER (12) |
| | ELEPHONE NUMBER Burton A. Grabo, Section Leader, Nuclear. Regulatory Affairs EA CODE 6 0 2 3'9 3 - 6 4 92 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| | CAUSE SYSTEM COMPONENT MANUFAC REPORTABLE SYSTEM COMPONENT MANUFAC REPORTABLE ', |
| | TURER TT) NPRDS TURER TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY . YEAR SUBMISSION YES (E yes, complete EXPECTED SUBMISSION DATE) NO DATE (15) |
| | X BS TRACT (Uma to 1400 spaces, Le., spproxnnately fsteen sny~ typewntten Ines) (16) |
| | On December 1, 1995, at approximately 1245 MST, Palo Verde Units 1, 2, and 3 were in Mode 1 (POWER OPERATlON) operating at approximately 99, 100, and 42 percent power, respectively, when the Auxiliary Feedwater (AFW) system was found to be unable to perform a component-level design basis function to. |
| | automatically provide water to the Steam Generator (SG) upon .an Auxiliary Feedwater Actuation Signal (AFAS). This condition is valid for a limited range of Main Steam Line Break sizes with a Loss of Power (LOP), single failure on the motor driven AFW pump, and below-normal SG level leading to a very low probability event - approximately 4E-12. Emergency Operating Procedures (EOP) and operator actions are fully capable of mitigating the event with the reset of the turbine overspeed and/or start of the non-seismic motor driven AFW pump from the control room.. |
| | This low probability event was not ful'ly appreciated during the original design, leading to this LER. A design change will be installed to correct the design deficiency. As interim corrective action, an assessment was performed to demonstrate that the existing condition does not pose a safety concern while permanent corrective actions are being developed and implemented. Existing EOPs and operator training preclude a complete loss of AFW under accident conditions and the heat removal capabilities of the SGs are met. |
| | |
| | 0 I' |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION |
| | 'GILITY NAME ,DOCKETNUMBER LER NUMBER PAGE |
| | 'fEAR ';";;:; SEQUENTIAL,;., EVISIO NUMBER,"w, NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9'5 - 0 1 3 0 0 0 2 of 0 6 EXT |
| | : 1. REPORTING REQUIREMENTS: |
| | This LER 528/95-013-00 is being written to report a'ondition outside the design basis of the plant. |
| | Specifically, at approximately 1245 MST on December 1, 1995, Palo Verde Units 1, 2, and 3 were in Mode 1 (POWER OPERATION) operating at approximately 99, 100, and 42 percent power, respectively, when the Auxiliary Feedwater (AFW) (BA) system was found to be unable to- perform a component-level design basis function to automatically provide water to the Steam Generator (SG) (AB) upon an Auxiliary Feedwater Actuation Signal (AFAS). This condition is valid for a limited range of Main Steam Line Break (MSLB) sizes with a Loss of Power (LOP), single failure on the motor driven AFW pump (BA), and below-normal SG level leading to a very low probability event - approximately 4E-12. |
| | : 2. EVENT DESCRIPTIONI On December 1, 1995, engineering personnel (utility, non licensed) completed an evaluation of a previously identified nonconforming condition and found that the AFW system was outside the design basis of the plant. |
| | Section 10.4.9.3 of the PVNGS Updated Final Safety Analysis Report. (UFSAR) states in part, "The AFS [Auxiliary Feedwater System] is designed to maintain adequate water level in the steam generators under the following operating modes and accident conditions:...3. Reactor Coolant System (AB) cooldown using the intact steam generator following a main st'~am line break or main feedwater line break inside the containment (NH) with a loss-of-offsite, power and normal onsite power...." Section 15.0.3.2 of the PVNGS UFSAR specifies the range of initial principle process values that must be considered when performing accident analysis. From a design perspective, postulated accidents are required to be analyzed over the range of initial steam generator inventories of 40 percent to 88 percent Wide Range (WR) indication (LI). [Note - From an operational perspective, the AFW system ensures that the Reactor Coolant System can be cooled down to less than 350 degrees Fahrenheit from normal operating conditions (i.e., 45 percent to 55 percent Narrow Range (NR) indication (LI) which corresponds to 78.5 percent WR and 82 percent WR respectively) in the event of a total loss-of-offsite power.] A postulated accident was discovered that could cause an overspeed trip of the AFW pump turbine (BA) |
| | (TRB) following a second AFAS during an intermediate sized steam line break scenario. The postulated accident would result in a loss of both |
| | |
| | 0 0 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITY NAME DOCKETNUMBER LER NUMBER PAGE YEAR 0,"":,: SEQUENTIAL EVISIO NUMBER ., NUMBER Palo Verde Unit 1 0 5 0 0 0.5 2 8 9 5 0 1 3 0 0 03of06 steam generators as an available heat sink to remove decay heat. The accident scenario reads as follows: |
| | The initial water inventory in both steam generators is assumed to be less than 163,479 pounds mass which corresponds to less than 39.2 percent NR (76 percent WR). The initial water inventory assumed for the postulated accident is below the normal band of 45 percent NR and includes instrument uncertainties plus added margin for additional conservatism. (Note - An initial water level in both steam generators of 76 percent WR or greater has been demonstrated through accident analysis to provide enough water to maintain the steam generator heat sink for 30 minutes without crediting operator action. The reportable condition is for an initial water level between 76 percent WR and 40 percent WR.) |
| | A intermediate steam line break, approximately 0.64 through 1.0 square feet, to trip the reactor (AC) is postulated. This is substantially more than the flow area of one fully stuck open Main Steam Safety Valve (MSSV) (SB) (RV) or Atmospheric Dump Valve (SB). |
| | The break is of sufficient size to generate an AFAS from the affected steam generator before the Delta-P (pressure differential between steam generators) lockout (ZEL) signals are generated. The Delta-p lockout is designed to lock out the AFAS from the affected steam generator to prevent feeding the fault. An AFAS is not ini"ially generated from the intact steam generator due to the higher inventory in the intact steam generator and the eventual Main Steam Zsolation Signal which reduces further inventory loss. |
| | A Loss of Power (LOP) is postulated as a consequence of the reactor trip which results in a loss of main feedwater (SJ). |
| | The non-seismic, "N" train AFW pump (BA) is not credited for the first thirty (30) minutes of the accident. The "N" train pump. must be manually loaded on the "A" train diesel generator (EK) following a LOP. The single active failure is postulated to be a failure of the "B" train AFW pump (the safety related electric driven AFW pump) . |
| | The steam line break size is such that steam supply to the turbine driven AFW pump from the affected steam generator terminates due to |
| | |
| | !I |
| | ,v |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITYNAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAL EVISIO |
| | 'UMBER NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 5 0 1 3 0 0 0 4 of 0 6 TEXT dryout/loss of pressure resulting in the turbine governor valve (TRB) (65) being fully open, the turbine speed setpoint at a steady state speed setting of approximately 3560 rpm, and the actual speed of the turbine at or near 0 rpm. The intact steam generator will continue to gradually lose inventory through the MSSVs until a second AFAS is generated from the intact steam generator. |
| | The second AFAS initiates steam flow from the intact steam generator to the idle turbine driven AFW pump. With the pump speed demand set at 3560 rpm verses the normal starting value of 900 rpm, the governor valve will not respond quickly enough to control speed. As a result, the .turbine driven AFW pump will ramp up and trip on overspeed. |
| | The overspeed trip will prevent the only available AFW pump (the turbine drive pump) from automatically delivering flow to the intact steam generator. |
| | The intact steam generator could steam dry and result in a loss of both steam generators as an available heat sink -to remove decay heat. |
| | An assessment was performed to demonstrate that the existing condition would not pose additional safety concerns while permanent corrective acti:ons are being developed and implemented. The assessment considered the following items: |
| | The availability of redundant or backup equipment, The compensatory measures including limited administrative controls, The safety function and events protected against, The conservatism and margins, The probabili.ty of needing the safety function, and The PRA or Individual Plant Evaluation (IPE) results that determine how operating the facility in the manner proposed in the Justification for Continued Operation (JCO) will impact the core damage frequency. |
| | The assessment concluded that success paths do exist that ensure the heat removal capabilities of the steam generating system are retained and that |
| | |
| | II 0 Y |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITYNAME DOCKET NUMBER LER NUMBER PAGE YEAR '~+, SEQUENTIAL EVISIO NUMBER NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 5 0 1 3 0 0 05of06 the bounding analyses found in Chapter 15 on the UFSAR will not be changed. The success paths identified in the assessment require operator action; however, these actions are not required prior to 30 minutes into the event and administrative controls are sufficiently proceduralized to preclude a total loss of AFW. Based on the conclusions of the assessment and very low probability of occurrence (i.e., 4E-12), the existing condition does not result in a safety concern for the period of time needed to develop and implement permanent corrective actions. |
| | : 3. ASSESSMENT OF THE SAFETY CONSEQUENCES AND THE IMPLICATIONS OF THIS EVENT: |
| | The safety function of the AFW system is to ensure that the Reactor Coolant System (RCS) can be cooled down to less than 350 degrees Fahrenheit from normal operating conditions in the event of a total loss-of-offsite power. The conditions necessary for the postulated accident to result in a complete loss of steam generator inventory include an initial steam generator water level of less than 39.2 percent NR which is below the lower normal operating level of 45 percent NR. From an operational perspective, there were no safety consequences or implications as a result of this event - existing Emergency Operating Procedures (EOP) and operator training are sufficient to preclude a complete loss of AFW under accident conditions and the heat removal capabilities of the SGs are met. From a design perspective, the existing condition does not result in additional safety concerns based on the assessment and very low probability of occurrence (i.e., 4E-12). |
| | The condition did not result in any challenges to the fission product barriers or result in any releases of radioactive materials. This condition did not adversely affect the safe operation of the plant or the health and safety of the public. |
| | : 4. CAUSE OF THE EVENT: |
| | An independent investigation of this event is being conducted in accordance with the APS Corrective Action Program. Based'n the results of the investigation, the cause of the condition was attributed to design error (SALP Cause Code BI Design Error). The postulated accident scenario was not considered during the initial plant design. No unusual characteristics of the work location (e.g., noise, heat, poor lighting) directly contributed to this event. There were no procedural errors involved. |
| | |
| | 0 II LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITY NAME DOCKETNUMBER LER NUMBER PAGE YEAR SMUENTIAL EVISIO NUMBER NUMSER Palo Verde Unit 1 0 5 0 0.0 5 2 8 9 5, 0 1 3 -'0 0 0 6 of 0 6 |
| | : 5. STRUCTURES, SYSTEMS, OR COMPONENT ZNFORMATZON: |
| | No structures, systems, or components were inoperable at the start of the event that contributed to the event. No component or system failures were involved. No failures of components with multiple functions were involved. No failures that rendered a train of a safety system inoperable were involved. There were no component or system failures or procedural errors identified. There were no safety system responses and none were necessary. |
| | : 6. CORRECTZVE ACTION TO PREVENT RECURRENCE: |
| | An assessment was performed to demonstrate that the existing condition does not pose additional safety concerns. The Plant Review Board (PRB) reviewed the event scenario and the assessment and determined that the postulated accident did not raise an Unreviewed Safety Question. Based on recommendations from the PRB, a JCO was prepared to support continued plant operation until permanent corrective action is implemented. |
| | As permanent corrective action, a design change will be installed in each unit during the next outage of sufficient. duration beginning with refueling outage 1R6 currently scheduled to start in November 1996.. The design change will preclude the steam driven AFN pump from tripping on overspeed during an, intermediate steam line break accident. |
| | PREVZOUS SZMZLAR EVENTS: |
| | There have been no previous similar events reported pursuant to 10CFR50.73 in the last three years. |
|
| |
|
| LICENSEE EVENT REPORT (LER)ACIUTY NAME (1)Palo Verde Unit 1 DOCKET NUMBER (2)PAGE (3)0 5 0 0 0 5 2 8 1OFO'6 TLE (4)Accident Condition Identified Puts Auxiliary Feedwater Beyond Component Level Design Basis EVENT DATE 5 LER NUMBER 6 REPORT DATE 7 OTHER FACIUTIES INVOLVED 6 MONTH 1 2 DAY YEAR YEAR 0 1 9 5 9 5 SEQUENTIAL NUMBER 0 1 3 REVISION NUMBER 0 0 MONTH DAY YEAR 1 2 3 1 9 5 FACIUIY NAMES Palo Verde Unit 2 Palo Verde Unit 3 KET NUMBERS 0 5 0 0 0 5 2 9 0 5 0 0 0 5'3 0 OPE RATING HIS REPORT IS SUBMITTED PURSUANT TO THE RED UIREMENTs 0F 10 cFR 4: (chedt one or more of the fosowng)(11)MODE (6)POWER LEVEL(10)9 9 20.402(b)20.405(aX1Xi) 20.405(sX1X i)20.405(aXIXB) 20.405(sXI Xiv)20.405(aXI Xv)20.405(c)50.36(cX I)50.36(cX2) 50.73(aX2XI) 50.73(aX2Xn) 50.73(aX2XB)
| |
| LICENSEE CONTACT FOR THIS LER (12)50.73(aX2XN) 50,73(aX2Xv) 50.73(aX2Xvi) 50.73(aX2XvtnXA)
| |
| M.73(sX2XvntXB) 50.73(aX2Xx) 73.71(b)73.71(c)OTHER (Spectfy in Abstract below snd in Text, NRC Form Burton A.Grabo, Section Leader, Nuclear.Regulatory Affairs ELEPHONE NUMBER EA CODE 6 0 2 3'9 3-6 4 92 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFAC TURER REPORTABLE TT)NPRDS SYSTEM COMPONENT MANU FAC TURER REPORTABLE
| |
| ', TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (E yes, complete EXPECTED SUBMISSION DATE)X NO BS TRACT (Uma to 1400 spaces, Le., spproxnnately fsteen sny~typewntten Ines)(16)EXPECTED SUBMISSION DATE (15)MONTH DAY.YEAR On December 1, 1995, at approximately 1245 MST, Palo Verde Units 1, 2, and 3 were in Mode 1 (POWER OPERATlON) operating at approximately 99, 100, and 42 percent power, respectively, when the Auxiliary Feedwater (AFW)system was found to be unable to perform a component-level design basis function to.automatically provide water to the Steam Generator (SG)upon.an Auxiliary Feedwater Actuation Signal (AFAS).This condition is valid for a limited range of Main Steam Line Break sizes with a Loss of Power (LOP), single failure on the motor driven AFW pump, and below-normal SG level leading to a very low probability event-approximately 4E-12.Emergency Operating Procedures (EOP)and operator actions are fully capable of mitigating the event with the reset of the turbine overspeed and/or start of the non-seismic motor driven AFW pump from the control room..This low probability event was not ful'ly appreciated during the original design, leading to this LER.A design change will be installed to correct the design deficiency.
| |
| As interim corrective action, an assessment was performed to demonstrate that the existing condition does not pose a safety concern while permanent corrective actions are being developed and implemented.
| |
| Existing EOPs and operator training preclude a complete loss of AFW under accident conditions and the heat removal capabilities of the SGs are met.
| |
| 0 I' LICENSEE EVENT REPORT (LER)TEXT CONTINUATION
| |
| 'GILITY NAME Palo Verde Unit 1 ,DOCKETNUMBER LER NUMBER'f EAR';";;:;SEQUENTIAL,;., EVISIO NUMBER,"w, NUMBER PAGE EXT 1.REPORTING REQUIREMENTS:
| |
| 0 5 0 0 0 5 2 8 9'5-0 1 3 0 0 0 2 of 0 6 This LER 528/95-013-00 is being written to report a'ondition outside the design basis of the plant.Specifically, at approximately 1245 MST on December 1, 1995, Palo Verde Units 1, 2, and 3 were in Mode 1 (POWER OPERATION) operating at approximately 99, 100, and 42 percent power, respectively, when the Auxiliary Feedwater (AFW)(BA)system was found to be unable to-perform a component-level design basis function to automatically provide water to the Steam Generator (SG)(AB)upon an Auxiliary Feedwater Actuation Signal (AFAS).This condition is valid for a limited range of Main Steam Line Break (MSLB)sizes with a Loss of Power (LOP), single failure on the motor driven AFW pump (BA), and below-normal SG level leading to a very low probability event-approximately 4E-12.2.EVENT DESCRIPTIONI On December 1, 1995, engineering personnel (utility, non licensed)completed an evaluation of a previously identified nonconforming condition and found that the AFW system was outside the design basis of the plant.Section 10.4.9.3 of the PVNGS Updated Final Safety Analysis Report.(UFSAR)states in part,"The AFS[Auxiliary Feedwater System]is designed to maintain adequate water level in the steam generators under the following operating modes and accident conditions:...3.
| |
| Reactor Coolant System (AB)cooldown using the intact steam generator following a main st'~am line break or main feedwater line break inside the containment (NH)with a loss-of-offsite, power and normal onsite power...." Section 15.0.3.2 of the PVNGS UFSAR specifies the range of initial principle process values that must be considered when performing accident analysis.From a design perspective, postulated accidents are required to be analyzed over the range of initial steam generator inventories of 40 percent to 88 percent Wide Range (WR)indication (LI).[Note-From an operational perspective, the AFW system ensures that the Reactor Coolant System can be cooled down to less than 350 degrees Fahrenheit from normal operating conditions (i.e., 45 percent to 55 percent Narrow Range (NR)indication (LI)which corresponds to 78.5 percent WR and 82 percent WR respectively) in the event of a total loss-of-offsite power.]A postulated accident was discovered that could cause an overspeed trip of the AFW pump turbine (BA)(TRB)following a second AFAS during an intermediate sized steam line break scenario.The postulated accident would result in a loss of both 0 0 LICENSEE EVENT REPORT (LER)TEXT CONTINUATION AGILITY NAME DOCKETNUMBER LER NUMBER PAGE Palo Verde Unit 1 YEAR 0,"":,: SEQUENTIAL NUMBER EVISIO., NUMBER 0 5 0 0 0.5 2 8 9 5 0 1 3 0 0 03of06 steam generators as an available heat sink to remove decay heat.The accident scenario reads as follows: The initial water inventory in both steam generators is assumed to be less than 163,479 pounds mass which corresponds to less than 39.2 percent NR (76 percent WR).The initial water inventory assumed for the postulated accident is below the normal band of 45 percent NR and includes instrument uncertainties plus added margin for additional conservatism.(Note-An initial water level in both steam generators of 76 percent WR or greater has been demonstrated through accident analysis to provide enough water to maintain the steam generator heat sink for 30 minutes without crediting operator action.The reportable condition is for an initial water level between 76 percent WR and 40 percent WR.)A intermediate steam line break, approximately 0.64 through 1.0 square feet, to trip the reactor (AC)is postulated.
| |
| This is substantially more than the flow area of one fully stuck open Main Steam Safety Valve (MSSV)(SB)(RV)or Atmospheric Dump Valve (SB).The break is of sufficient size to generate an AFAS from the affected steam generator before the Delta-P (pressure differential between steam generators) lockout (ZEL)signals are generated.
| |
| The Delta-p lockout is designed to lock out the AFAS from the affected steam generator to prevent feeding the fault.An AFAS is not ini"ially generated from the intact steam generator due to the higher inventory in the intact steam generator and the eventual Main Steam Zsolation Signal which reduces further inventory loss.A Loss of Power (LOP)is postulated as a consequence of the reactor trip which results in a loss of main feedwater (SJ).The non-seismic,"N" train AFW pump (BA)is not credited for the first thirty (30)minutes of the accident.The"N" train pump.must be manually loaded on the"A" train diesel generator (EK)following a LOP.The single active failure is postulated to be a failure of the"B" train AFW pump (the safety related electric driven AFW pump).The steam line break size is such that steam supply to the turbine driven AFW pump from the affected steam generator terminates due to
| |
| !I ,v LICENSEE EVENT REPORT (LER)TEXT CONTINUATION AGILITY NAME Palo Verde Unit 1 DOCKET NUMBER LER NUMBER SEQUENTIAL
| |
| 'UMBER EVISIO NUMBER PAGE 0 5 0 0 0 5 2 8 9 5 0 1 3 0 0 0 4 of 0 6 TEXT dryout/loss of pressure resulting in the turbine governor valve (TRB)(65)being fully open, the turbine speed setpoint at a steady state speed setting of approximately 3560 rpm, and the actual speed of the turbine at or near 0 rpm.The intact steam generator will continue to gradually lose inventory through the MSSVs until a second AFAS is generated from the intact steam generator.
| |
| The second AFAS initiates steam flow from the intact steam generator to the idle turbine driven AFW pump.With the pump speed demand set at 3560 rpm verses the normal starting value of 900 rpm, the governor valve will not respond quickly enough to control speed.As a result, the.turbine driven AFW pump will ramp up and trip on overspeed.
| |
| The overspeed trip will prevent the only available AFW pump (the turbine drive pump)from automatically delivering flow to the intact steam generator.
| |
| The intact steam generator could steam dry and result in a loss of both steam generators as an available heat sink-to remove decay heat.An assessment was performed to demonstrate that the existing condition would not pose additional safety concerns while permanent corrective acti:ons are being developed and implemented.
| |
| The assessment considered the following items: The availability of redundant or backup equipment, The compensatory measures including limited administrative controls, The safety function and events protected against, The conservatism and margins, The probabili.ty of needing the safety function, and The PRA or Individual Plant Evaluation (IPE)results that determine how operating the facility in the manner proposed in the Justification for Continued Operation (JCO)will impact the core damage frequency.
| |
| The assessment concluded that success paths do exist that ensure the heat removal capabilities of the steam generating system are retained and that II 0 Y LICENSEE EVENT REPORT (LER)TEXT CONTINUATION AGILITY NAME Palo Verde Unit 1 DOCKET NUMBER LER NUMBER YEAR'~+, SEQUENTIAL NUMBER EVISIO NUMBER PAGE 0 5 0 0 0 5 2 8 9 5 0 1 3 0 0 05of06 the bounding analyses found in Chapter 15 on the UFSAR will not be changed.The success paths identified in the assessment require operator action;however, these actions are not required prior to 30 minutes into the event and administrative controls are sufficiently proceduralized to preclude a total loss of AFW.Based on the conclusions of the assessment and very low probability of occurrence (i.e., 4E-12), the existing condition does not result in a safety concern for the period of time needed to develop and implement permanent corrective actions.3.ASSESSMENT OF THE SAFETY CONSEQUENCES AND THE IMPLICATIONS OF THIS EVENT: The safety function of the AFW system is to ensure that the Reactor Coolant System (RCS)can be cooled down to less than 350 degrees Fahrenheit from normal operating conditions in the event of a total loss-of-offsite power.The conditions necessary for the postulated accident to result in a complete loss of steam generator inventory include an initial steam generator water level of less than 39.2 percent NR which is below the lower normal operating level of 45 percent NR.From an operational perspective, there were no safety consequences or implications as a result of this event-existing Emergency Operating Procedures (EOP)and operator training are sufficient to preclude a complete loss of AFW under accident conditions and the heat removal capabilities of the SGs are met.From a design perspective, the existing condition does not result in additional safety concerns based on the assessment and very low probability of occurrence (i.e., 4E-12).The condition did not result in any challenges to the fission product barriers or result in any releases of radioactive materials.
| |
| This condition did not adversely affect the safe operation of the plant or the health and safety of the public.4.CAUSE OF THE EVENT: An independent investigation of this event is being conducted in accordance with the APS Corrective Action Program.Based'n the results of the investigation, the cause of the condition was attributed to design error (SALP Cause Code BI Design Error).The postulated accident scenario was not considered during the initial plant design.No unusual characteristics of the work location (e.g., noise, heat, poor lighting)directly contributed to this event.There were no procedural errors involved.
| |
| 0 II LICENSEE EVENT REPORT (LER)TEXT CONTINUATION AGILITY NAME DOCKETNUMBER LER NUMBER PAGE Palo Verde Unit 1 YEAR SMUENTIAL NUMBER EVISIO NUMSER 0 5 0 0.0 5 2 8 9 5, 0 1 3-'0 0 0 6 of 0 6 5.STRUCTURES, SYSTEMS, OR COMPONENT ZNFORMATZON:
| |
| No structures, systems, or components were inoperable at the start of the event that contributed to the event.No component or system failures were involved.No failures of components with multiple functions were involved.No failures that rendered a train of a safety system inoperable were involved.There were no component or system failures or procedural errors identified.
| |
| There were no safety system responses and none were necessary.
| |
| 6.CORRECTZVE ACTION TO PREVENT RECURRENCE:
| |
| An assessment was performed to demonstrate that the existing condition does not pose additional safety concerns.The Plant Review Board (PRB)reviewed the event scenario and the assessment and determined that the postulated accident did not raise an Unreviewed Safety Question.Based on recommendations from the PRB, a JCO was prepared to support continued plant operation until permanent corrective action is implemented.
| |
| As permanent corrective action, a design change will be installed in each unit during the next outage of sufficient.
| |
| duration beginning with refueling outage 1R6 currently scheduled to start in November 1996..The design change will preclude the steam driven AFN pump from tripping on overspeed during an, intermediate steam line break accident.PREVZOUS SZMZLAR EVENTS: There have been no previous similar events reported pursuant to 10CFR50.73 in the last three years.
| |
| 4l t}} | | 4l t}} |
|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
[Table view] |
Text
~
CATEGORY j.
REGULATO Y INFORMATION DISTRIBUTION STEM (RIDS)
ACCESSION NBR:9601160059 DOC.DATE: 95/12/31 NOTARIZED: NO DOCKET ¹ FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME AUTHOR AFFILIATION GRABO,B.A. Arizona Public Service Co. (formerly Arizona Nuclear Power LEVINE,J.M. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 95-013-00:on 951201,AFW sys was outside design basis of.
plant. Caused by design error. Performed assessment to demonstrate that existing condition does not pose addi safety concerns.W/951231 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ) ENCI i SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:STANDARDIZED PLANT 05000528 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCI ID CODE/NAME LTTR ENCL PD4-2 PD 1 1 HOLIAN, B 1 1 INTERNAL: ACRS 1 GD~B B 2 2 AEOD/SPD/RRAB 1 FILE CENTER 1 1 NRR/DE/ECGB NRR/DE/EMEB 1
1
~~BB NRR/DRCH/HHFB 1
1 1
1 NRR/DRCH/HICB 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 RGN4 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCEPJ H 2 2 NOAC MURPHYPG.A 1 1 NOAC POOREPW. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 26
~ 1 4k
Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O. BOX 52034 ~ PHOENIX. ARIZONA 850?2-=i3 192-00955-JML/BAG/DLK JAMES M. LEVINE December 31, 1995 VICE PRESIDENT NUCLEAR PRODUCTION U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Station-P1-37 Washington, DC 20555-0001
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Units 1, 2, and 3 Docket Nos. STN 50-528, 50-529, 50-530 License Nos. NPF41, NPF-51, NPF-74 Licensee Event Report.95-013-00 Attached please find, Licensee Event Report (LER)95-013 prepared and submitted pursuant to 10 CFR 50.73. This LER reports a condition where an intermediate sized steam line break accident scenario was discovered that could result in the loss of both steam generators as an available heat sink to remove decay heat under limited accident conditions.
In accordance with 10 CFR 50.73(d), a copy of this LER is being forwarded to the Regional Administrator, NRC Region IV. If you have any questions, please contact Burton A. Grabo, Section Leader, Nuclear Regulatory Affairs, at (602) 393-6492.
Sincerely, JML/BAG/DLK Attachment cc: L. J. Callan (all with attachment)
K. E. Perkins K. E. Johnston INPO Records Center 960ii60059 95i23i PDR ADOCK 05000528 S PDR zg>
p
LICENSEE EVENT REPORT (LER)
ACIUTYNAME (1) DOCKET NUMBER (2) PAGE (3)
Palo Verde Unit 1 0 5 0 0 0 5 2 8 1OFO'6 TLE (4)
Accident Condition Identified Puts Auxiliary Feedwater Beyond Component Level Design Basis EVENT DATE 5 LER NUMBER 6 REPORT DATE 7 OTHER FACIUTIES INVOLVED 6 MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FACIUIYNAMES KET NUMBERS NUMBER NUMBER Palo Verde Unit 2 0 5 0 0 0 5 2 9 1 2 0 1 9 5 9 5 0 1 3 0 0 1 2 3 1 9 5 Palo Verde Unit 3 0 5 0 0 0 5'3 0 OPE RATING HIS REPORT IS SUBMITTED PURSUANT TO THE RED UIREMENTs 0F 10 cFR 4: (chedt one or more of the fosowng) (11)
MODE (6) 20.402(b) 20.405(c) 50.73(aX2XN) 73.71(b)
POWER 20.405(aX1Xi) 50.36(cX I) 50,73(aX2Xv) 73.71(c)
LEVEL(10) 9 9 20.405(sX1X i) 50.36(cX2) 50.73(aX2Xvi) OTHER (Spectfy in Abstract 20.405(aXIXB) 50.73(aX2XI) 50.73(aX2XvtnXA) below snd in Text, NRC Form 20.405(sXI Xiv) 50.73(aX2Xn) M.73(sX2XvntXB) 20.405(aXI Xv) 50.73(aX2XB) 50.73(aX2Xx)
LICENSEE CONTACT FOR THIS LER (12)
ELEPHONE NUMBER Burton A. Grabo, Section Leader, Nuclear. Regulatory Affairs EA CODE 6 0 2 3'9 3 - 6 4 92 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC REPORTABLE SYSTEM COMPONENT MANUFAC REPORTABLE ',
TURER TT) NPRDS TURER TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY . YEAR SUBMISSION YES (E yes, complete EXPECTED SUBMISSION DATE) NO DATE (15)
X BS TRACT (Uma to 1400 spaces, Le., spproxnnately fsteen sny~ typewntten Ines) (16)
On December 1, 1995, at approximately 1245 MST, Palo Verde Units 1, 2, and 3 were in Mode 1 (POWER OPERATlON) operating at approximately 99, 100, and 42 percent power, respectively, when the Auxiliary Feedwater (AFW) system was found to be unable to perform a component-level design basis function to.
automatically provide water to the Steam Generator (SG) upon .an Auxiliary Feedwater Actuation Signal (AFAS). This condition is valid for a limited range of Main Steam Line Break sizes with a Loss of Power (LOP), single failure on the motor driven AFW pump, and below-normal SG level leading to a very low probability event - approximately 4E-12. Emergency Operating Procedures (EOP) and operator actions are fully capable of mitigating the event with the reset of the turbine overspeed and/or start of the non-seismic motor driven AFW pump from the control room..
This low probability event was not ful'ly appreciated during the original design, leading to this LER. A design change will be installed to correct the design deficiency. As interim corrective action, an assessment was performed to demonstrate that the existing condition does not pose a safety concern while permanent corrective actions are being developed and implemented. Existing EOPs and operator training preclude a complete loss of AFW under accident conditions and the heat removal capabilities of the SGs are met.
0 I'
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
'GILITY NAME ,DOCKETNUMBER LER NUMBER PAGE
'fEAR ';";;:; SEQUENTIAL,;., EVISIO NUMBER,"w, NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9'5 - 0 1 3 0 0 0 2 of 0 6 EXT
- 1. REPORTING REQUIREMENTS:
This LER 528/95-013-00 is being written to report a'ondition outside the design basis of the plant.
Specifically, at approximately 1245 MST on December 1, 1995, Palo Verde Units 1, 2, and 3 were in Mode 1 (POWER OPERATION) operating at approximately 99, 100, and 42 percent power, respectively, when the Auxiliary Feedwater (AFW) (BA) system was found to be unable to- perform a component-level design basis function to automatically provide water to the Steam Generator (SG) (AB) upon an Auxiliary Feedwater Actuation Signal (AFAS). This condition is valid for a limited range of Main Steam Line Break (MSLB) sizes with a Loss of Power (LOP), single failure on the motor driven AFW pump (BA), and below-normal SG level leading to a very low probability event - approximately 4E-12.
- 2. EVENT DESCRIPTIONI On December 1, 1995, engineering personnel (utility, non licensed) completed an evaluation of a previously identified nonconforming condition and found that the AFW system was outside the design basis of the plant.
Section 10.4.9.3 of the PVNGS Updated Final Safety Analysis Report. (UFSAR) states in part, "The AFS [Auxiliary Feedwater System] is designed to maintain adequate water level in the steam generators under the following operating modes and accident conditions:...3. Reactor Coolant System (AB) cooldown using the intact steam generator following a main st'~am line break or main feedwater line break inside the containment (NH) with a loss-of-offsite, power and normal onsite power...." Section 15.0.3.2 of the PVNGS UFSAR specifies the range of initial principle process values that must be considered when performing accident analysis. From a design perspective, postulated accidents are required to be analyzed over the range of initial steam generator inventories of 40 percent to 88 percent Wide Range (WR) indication (LI). [Note - From an operational perspective, the AFW system ensures that the Reactor Coolant System can be cooled down to less than 350 degrees Fahrenheit from normal operating conditions (i.e., 45 percent to 55 percent Narrow Range (NR) indication (LI) which corresponds to 78.5 percent WR and 82 percent WR respectively) in the event of a total loss-of-offsite power.] A postulated accident was discovered that could cause an overspeed trip of the AFW pump turbine (BA)
(TRB) following a second AFAS during an intermediate sized steam line break scenario. The postulated accident would result in a loss of both
0 0 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITY NAME DOCKETNUMBER LER NUMBER PAGE YEAR 0,"":,: SEQUENTIAL EVISIO NUMBER ., NUMBER Palo Verde Unit 1 0 5 0 0 0.5 2 8 9 5 0 1 3 0 0 03of06 steam generators as an available heat sink to remove decay heat. The accident scenario reads as follows:
The initial water inventory in both steam generators is assumed to be less than 163,479 pounds mass which corresponds to less than 39.2 percent NR (76 percent WR). The initial water inventory assumed for the postulated accident is below the normal band of 45 percent NR and includes instrument uncertainties plus added margin for additional conservatism. (Note - An initial water level in both steam generators of 76 percent WR or greater has been demonstrated through accident analysis to provide enough water to maintain the steam generator heat sink for 30 minutes without crediting operator action. The reportable condition is for an initial water level between 76 percent WR and 40 percent WR.)
A intermediate steam line break, approximately 0.64 through 1.0 square feet, to trip the reactor (AC) is postulated. This is substantially more than the flow area of one fully stuck open Main Steam Safety Valve (MSSV) (SB) (RV) or Atmospheric Dump Valve (SB).
The break is of sufficient size to generate an AFAS from the affected steam generator before the Delta-P (pressure differential between steam generators) lockout (ZEL) signals are generated. The Delta-p lockout is designed to lock out the AFAS from the affected steam generator to prevent feeding the fault. An AFAS is not ini"ially generated from the intact steam generator due to the higher inventory in the intact steam generator and the eventual Main Steam Zsolation Signal which reduces further inventory loss.
A Loss of Power (LOP) is postulated as a consequence of the reactor trip which results in a loss of main feedwater (SJ).
The non-seismic, "N" train AFW pump (BA) is not credited for the first thirty (30) minutes of the accident. The "N" train pump. must be manually loaded on the "A" train diesel generator (EK) following a LOP. The single active failure is postulated to be a failure of the "B" train AFW pump (the safety related electric driven AFW pump) .
The steam line break size is such that steam supply to the turbine driven AFW pump from the affected steam generator terminates due to
!I
,v
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITYNAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAL EVISIO
'UMBER NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 5 0 1 3 0 0 0 4 of 0 6 TEXT dryout/loss of pressure resulting in the turbine governor valve (TRB) (65) being fully open, the turbine speed setpoint at a steady state speed setting of approximately 3560 rpm, and the actual speed of the turbine at or near 0 rpm. The intact steam generator will continue to gradually lose inventory through the MSSVs until a second AFAS is generated from the intact steam generator.
The second AFAS initiates steam flow from the intact steam generator to the idle turbine driven AFW pump. With the pump speed demand set at 3560 rpm verses the normal starting value of 900 rpm, the governor valve will not respond quickly enough to control speed. As a result, the .turbine driven AFW pump will ramp up and trip on overspeed.
The overspeed trip will prevent the only available AFW pump (the turbine drive pump) from automatically delivering flow to the intact steam generator.
The intact steam generator could steam dry and result in a loss of both steam generators as an available heat sink -to remove decay heat.
An assessment was performed to demonstrate that the existing condition would not pose additional safety concerns while permanent corrective acti:ons are being developed and implemented. The assessment considered the following items:
The availability of redundant or backup equipment, The compensatory measures including limited administrative controls, The safety function and events protected against, The conservatism and margins, The probabili.ty of needing the safety function, and The PRA or Individual Plant Evaluation (IPE) results that determine how operating the facility in the manner proposed in the Justification for Continued Operation (JCO) will impact the core damage frequency.
The assessment concluded that success paths do exist that ensure the heat removal capabilities of the steam generating system are retained and that
II 0 Y
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITYNAME DOCKET NUMBER LER NUMBER PAGE YEAR '~+, SEQUENTIAL EVISIO NUMBER NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 5 0 1 3 0 0 05of06 the bounding analyses found in Chapter 15 on the UFSAR will not be changed. The success paths identified in the assessment require operator action; however, these actions are not required prior to 30 minutes into the event and administrative controls are sufficiently proceduralized to preclude a total loss of AFW. Based on the conclusions of the assessment and very low probability of occurrence (i.e., 4E-12), the existing condition does not result in a safety concern for the period of time needed to develop and implement permanent corrective actions.
- 3. ASSESSMENT OF THE SAFETY CONSEQUENCES AND THE IMPLICATIONS OF THIS EVENT:
The safety function of the AFW system is to ensure that the Reactor Coolant System (RCS) can be cooled down to less than 350 degrees Fahrenheit from normal operating conditions in the event of a total loss-of-offsite power. The conditions necessary for the postulated accident to result in a complete loss of steam generator inventory include an initial steam generator water level of less than 39.2 percent NR which is below the lower normal operating level of 45 percent NR. From an operational perspective, there were no safety consequences or implications as a result of this event - existing Emergency Operating Procedures (EOP) and operator training are sufficient to preclude a complete loss of AFW under accident conditions and the heat removal capabilities of the SGs are met. From a design perspective, the existing condition does not result in additional safety concerns based on the assessment and very low probability of occurrence (i.e., 4E-12).
The condition did not result in any challenges to the fission product barriers or result in any releases of radioactive materials. This condition did not adversely affect the safe operation of the plant or the health and safety of the public.
- 4. CAUSE OF THE EVENT:
An independent investigation of this event is being conducted in accordance with the APS Corrective Action Program. Based'n the results of the investigation, the cause of the condition was attributed to design error (SALP Cause Code BI Design Error). The postulated accident scenario was not considered during the initial plant design. No unusual characteristics of the work location (e.g., noise, heat, poor lighting) directly contributed to this event. There were no procedural errors involved.
0 II LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITY NAME DOCKETNUMBER LER NUMBER PAGE YEAR SMUENTIAL EVISIO NUMBER NUMSER Palo Verde Unit 1 0 5 0 0.0 5 2 8 9 5, 0 1 3 -'0 0 0 6 of 0 6
- 5. STRUCTURES, SYSTEMS, OR COMPONENT ZNFORMATZON:
No structures, systems, or components were inoperable at the start of the event that contributed to the event. No component or system failures were involved. No failures of components with multiple functions were involved. No failures that rendered a train of a safety system inoperable were involved. There were no component or system failures or procedural errors identified. There were no safety system responses and none were necessary.
- 6. CORRECTZVE ACTION TO PREVENT RECURRENCE:
An assessment was performed to demonstrate that the existing condition does not pose additional safety concerns. The Plant Review Board (PRB) reviewed the event scenario and the assessment and determined that the postulated accident did not raise an Unreviewed Safety Question. Based on recommendations from the PRB, a JCO was prepared to support continued plant operation until permanent corrective action is implemented.
As permanent corrective action, a design change will be installed in each unit during the next outage of sufficient. duration beginning with refueling outage 1R6 currently scheduled to start in November 1996.. The design change will preclude the steam driven AFN pump from tripping on overspeed during an, intermediate steam line break accident.
PREVZOUS SZMZLAR EVENTS:
There have been no previous similar events reported pursuant to 10CFR50.73 in the last three years.
4l t