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| {{#Wiki_filter:ACCELERATED DOCUMENTDISTRIBUTION SYSTEMREGUL>RYINFORMATION DISTRIBUTE SYSTEM(RIDE)ACCESSION NBR:9308120083 DOC.DATE: | | {{#Wiki_filter:ACCELERATED DOCUMENT DISTRIBUTION SYSTEM REGUL>RY INFORMATION DISTRIBUTE SYSTEM (RIDE)ACCESSION NBR:9308120083 DOC.DATE: 93/08/06 NOTARIZED: |
| 93/08/06NOTARIZED: | | NO FACIL 50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION BACKUS,W.H Rochester Gas a Electric Corp.MECREDY,R.C Rochester Gas 6 Electric Corp.RECIP.NAME RECIPIENT AFFILIATION |
| NOFACIL50-244RobertEmmetGinnaNuclearPlant,Unit1,Rochester GAUTH.NAMEAUTHORAFFILIATION BACKUS,W.H Rochester GasaElectricCorp.MECREDY,R.C Rochester Gas6ElectricCorp.RECIP.NAME RECIPIENT AFFILIATION
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER93-004-00:on 930707,Main feedwater isolations occurredduetosecondary side6condensate feedwater pressuretransient.
| | LER 93-004-00:on 930707,Main feedwater isolations occurred due to secondary side 6 condensate feedwater pressure transient. |
| Returnedfeedwater regulating valvestopre-event controlsconfiguration.W/930806 ltr.DISTRIBUTION CODE:ZE22TCOPIESRECEIVED:LTR tENCLrSIZE:LOTITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
| | Returned feedwater regulating valves to pre-event controls configuration.W/930806 ltr.DISTRIBUTION CODE: ZE22T COPIES RECEIVED:LTR t ENCL r SIZE: LO TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). |
| DOCKET¹05000244Ii1I1DlSl'.05000244ARECIPIENT IDCODE/NAME PD1-3LAJOHNSON,A INTERNAL: | | DOCKET¹05000244 I i 1 I 1 Dl S l'.05000244 A RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: ACNW AEOD/DSP/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRIL/RPEB NODS SA/+PLB-BP 02 RGHl FILE 01 EXTERNAL: EGGG BRYCE,J.H NRC PDR NSIC POORE,W.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2'1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DOA AEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB L ST LOBBY WARD NSIC MURPHYFG.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 D D$D D NOTE TO ALL"RIDS" RECIPIENTS: |
| ACNWAEOD/DSP/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRIL/RPEB NODSSA/+PLB-BP02RGHlFILE01EXTERNAL:
| | PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2065)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!D FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30 |
| EGGGBRYCE,J.H NRCPDRNSICPOORE,W.COPIESLTTRENCL11112211111111111111112'1111RECIPIENT IDCODE/NAME PD1-3PDAEOD/DOAAEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB LSTLOBBYWARDNSICMURPHYFG.A NUDOCSFULLTXTCOPIESLTTRENCL111122111111221111111111DD$DDNOTETOALL"RIDS"RECIPIENTS:
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| PLEASEHELPUSTOREDUCEWASTEICONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065)
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| TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!DFULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
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| LTTR30ENCL30
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| rrrnrNr1/r/trl/rr | | rrrnrNr1/r/trl/rr |
| //i////>rr,//'/I/'i"Ii//,''i'" | | //i////>rr,//'/I/'i" Ii//,''i'" i!C!i)ivir~ill!II I/l'lrir, r!r/ROCHESTER GAS AND ELECTRIC CORPORATION |
| i!C!i)ivir~ill!II I/l'lrir, r!r/ROCHESTER GASANDELECTRICCORPORATION | | ~";-',Toe/r., state" 89 EAST AVENUE, ROCHESTER N.K 14649-0001 ROBERT C.MECREOY Vice President Clnna ttuclear Production TELEPHONE ARE/1 COOE 716 5rt6 2700 August 6, 1993 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 |
| ~";-',Toe/r.,state"89EASTAVENUE,ROCHESTER N.K14649-0001 ROBERTC.MECREOYVicePresident ClnnattuclearProduction TELEPHONE ARE/1COOE7165rt62700August6,1993U.S.NuclearRegulatory Commission DocumentControlDeskWashington, DC20555 | |
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| ==Subject:== | | ==Subject:== |
| LER93-004,Feedwater ControlPerturbations, DueToASecondary SideTransient, CausesSteamGenerator HighLevelFeedwater Isolations R.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordance with10CFR50.73,LicenseEventReportSystem,item(a)(2)(iv),
| | LER 93-004, Feedwater Control Perturbations, Due To A Secondary Side Transient, Causes Steam Generator High Level Feedwater Isolations R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, License Event Report System, item (a)(2)(iv), which requires a report of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached event report LER 93-004 i: s hereby submitted. |
| whichrequiresareportof,"anyeventorcondition thatresultedinmanualorautomatic actuation ofanyEngineered SafetyFeature(ESF),including theReactorProtection System(RPS)",theattachedeventreportLER93-004i:sherebysubmitted.
| | This event has in no way affected the public's health and safety.Very truly yours, xco Robert C.Mec edy U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector~r n.h 9308i20083 930806 PDR*DOCK 05000244 8 PDR |
| Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,xcoRobertC.MecedyU.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector
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| ~rn.h9308i20083 930806PDR*DOCK050002448PDR | |
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| NRCFORM366(669)V.S.NUCLEARREGULATORY COMMISSILICENSEEEVENTREPORT(LER)APPROVEDOMBNOA31506104 EXPIRESI4/30/92ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFOAMATION COLLECTION REQUEST:50.0HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANORFPORTSMANAGEMENT BRANCH(F630),V.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTOTHEPAPERWORK REDUCTION PROJECT(31500'l04).
| | NRC FORM 366 (669)V.S.NUCLEAR REGULATORY COMMISSI LICENSEE EVENT REPORT (LER)APPROVED OMB NOA31506104 EXP IR ESI 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFOAMATION COLLECTION REQUEST: 50.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS ANO RFPORTS MANAGEMENT BRANCH (F630), V.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500'l04). |
| OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, OC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBERl2)PAE05000244iOFOFeewaterControerturatons,DueToSeconaryTransent,ausesteamGenerator HighLevelFeedwater Isolations EVENTDATE(5)MONTHDAYYEARYEARLERNUMBER(61:SEQUENTIAL NUMBERREVISIONNUMBERREPORTDATELT)MONTHDAYYEARDOCKETNUMBERIS) 05000FACII.ITV NAMES01'HERFACILITIES INVOLVED(6)0-7793930040008069305000OPERATING MODE(9)NPOWERLEYEL09760n(sl(2)Is>>)50.n(v)(2)
| | OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, OC 20503.FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET NUMBER l2)PA E 0 5 0 0 02 44 iOFO Fee water Contro ertur at ons, Due To Secon ary Trans ent, auses team Generator High Level Feedwater Isolations EVENT DATE (5)MONTH DAY YEAR YEAR LER NUMBER (61: SEQUENTIAL NUMBER REVISION NUMBER REPORT DATE LT)MONTH DAY YEAR DOCKET NUMBERIS)0 5 0 0 0 FACII.ITV NAMES 01'HER FACILITIES INVOLVED (6)0-7 79 393 0 0 4 0 0 0 806 93 0 5 0 0 0 OPERATING MODE (9)N POWER LEYEL 0 9 7 60 n(sl(2)Is>>)50.n(v)(2) |
| Nl5073(s)(2)lvsl)50.73(v)(2)
| | Nl 50 73(s)(2)lvsl)50.73(v)(2)(vill)(Al 50.73(v)l2l(vill)(B) 50.73(~)(2)lsl 0 THE RLQUIAEMENTS OF 10 CFR ((:/Chock ono or moro Ol trss IollovrinP/ |
| (vill)(Al50.73(v)l2l(vill)(B) 50.73(~)(2)lsl0THERLQUIAEMENTS OF10CFR((:/ChockonoormoroOltrssIollovrinP/ | | (11)THIS REPORT IS SVBMITTFD PUASVANT T 20.402(B)20.405(~)(1)(I)20.405 (s)l1)(NI 20.406(~I ('I Hill)20405(s)(1)(lv) 20.405(s I (I)(vl 20.405(c)60M(s)(II 50.36(~)(2)60.73(sl(2((ll 50.73(s)(2)(ill 50.7 3(s)(2)(ill)73,71(B)73.71 I cl OTHER ISpscily In 4osnoct tN/oEN onr/ln Tss I, HRC Form 3664/LICENSEE CONTACT FOR THIS LEA (12I NAME Wesley H.Backus.Technical Assistant to the Operations Mana er TELEPHONE NUMBER AREA CODE 3 155 24-444 6 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAVSE SYS'EM COMPONENT MANUFAC.TVRER REPORTABLE TO NPADS P jQg CAUSE S STEM Xj'>>AA'RC~C.3>>">>T>>~'" IKU'::hl.'.@<COMPONENT MANUFAC.TVRER EPORTABLE TO NPROS?>>o.>>...%R.:.R6)SA'NO 4 PcA.N:: SUPPLEMENTAL REPORT EXPECTED llc)YES Ill y<<, compiots EXPECTED Sl/SSI/SSION DATE/NO AssTRAcT I(.imit to/400 spscsr, l.s., spproslmsrsly lilusn tinpis.rpocs typssvrinon |
| (11)THISREPORTISSVBMITTFD PUASVANTT20.402(B) 20.405(~)(1)(I)20.405(s)l1)(NI20.406(~I('IHill)20405(s)(1)(lv) 20.405(sI(I)(vl20.405(c) 60M(s)(II 50.36(~)(2)60.73(sl(2((ll 50.73(s)(2)(ill50.73(s)(2)(ill)73,71(B)73.71IclOTHERISpscilyIn4osnocttN/oENonr/lnTssI,HRCForm3664/LICENSEECONTACTFORTHISLEA(12INAMEWesleyH.Backus.Technical Assistant totheOperations ManaerTELEPHONE NUMBERAREACODE315524-4446COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAVSESYS'EMCOMPONENT MANUFAC.TVRERREPORTABLE TONPADSPjQgCAUSESSTEMXj'>>AA'RC~C.3>>">>T>>~'"IKU'::hl.'.@<COMPONENT MANUFAC.TVREREPORTABLE TONPROS?>>o.>>...%R.:.R6)SA'NO4PcA.N::SUPPLEMENTAL REPORTEXPECTEDllc)YESIlly<<,compiotsEXPECTEDSl/SSI/SSION DATE/NOAssTRAcTI(.imitto/400spscsr,l.s.,spproslmsrsly lilusntinpis.rpocs typssvrinon | | /inos/(16)EXPECTFD SUBMISSION DATE (15)MONTH DAY YEAR On July 7, 1993-at approximately 0915 EDST, with the reactor at approximately 974 full power, main feedwater isolations occurred on the"BFI Steam Generator (S/G).These feedwater isolations were caused by overfeeding the"B" S/G, following a secondary side condensate and feedwater pressure transient. |
| /inos/(16)EXPECTFDSUBMISSION DATE(15)MONTHDAYYEAROnJuly7,1993-atapproximately 0915EDST,withthereactoratapproximately 974fullpower,mainfeedwater isolations occurredonthe"BFISteamGenerator (S/G).Thesefeedwater isolations werecausedbyoverfeeding the"B"S/G,following asecondary sidecondensate andfeedwater pressuretransient. | | Immediate operator action was to manually control the Feedwater Regulating Valves (FRVs)to restore the S/G water levels and stabilize the plant.The immediate cause of the event was due to a secondary side condensate and feedwater pressure transient. |
| Immediate operatoractionwastomanuallycontroltheFeedwater Regulating Valves(FRVs)torestoretheS/Gwaterlevelsandstabilize theplant.Theimmediate causeoftheeventwasduetoasecondary sidecondensate andfeedwater pressuretransient. | | The underlying cause of the event was determined to be not isolating the 5A heater high level dump valve prior to trouble-shooting.(This event is NUREG-1022 (X)Cause Code).Corrective actions taken or planned are discussed in Section V of the text.NRC Form 366 (669) |
| Theunderlying causeoftheeventwasdetermined tobenotisolating the5Aheaterhighleveldumpvalvepriortotrouble-shooting.
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| (ThiseventisNUREG-1022 (X)CauseCode).Corrective actionstakenorplannedarediscussed inSectionVofthetext.NRCForm366(669) | |
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| NRCFORM388A(SJ)9)US.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORT(LER)TEXTCONTINUATION APPROVEDOMBNO.3(504)04EXPIRES:4/30/92ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUEST:508)HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(F430),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTO1HEPAPERWORK REDUCTION PROJECT(31500)08),
| | NRC FORM 388A (SJ)9)US.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT (LER)TEXT CONTINUATION APPROVED OMB NO.3(504)04 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 508)HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500)08), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (ll DOCKET NUMBER (2)YEAR LER NUMBER (8)SEOUENTIAL o@IIEVISION NUM E II PAGE (3)R.E.Glnna Nuclear Power Plant TEXT/I/more e/reoe/I rer/uuN/, u>>//I/rme/HRC Frurn 35883/()7)o s o o o 24 49 3 004 0 0 0 2 OF 0 9 LANT COND T ONS The plant was at approximately 974 steady state reactor power with the following pertinent activities in progress: o The"B" All Volatile Treatment (AVT)mixed bed demineralizer was being placed in service per operating procedure T-6.9A (Condensate Polishing Mixed Bed DI Unit Start-up). |
| OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20503.FACILITYNAME(llDOCKETNUMBER(2)YEARLERNUMBER(8)SEOUENTIAL o@IIEVISION NUMEIIPAGE(3)R.E.GlnnaNuclearPowerPlantTEXT/I/moree/reoe/Irer/uuN/,
| | Also per T-6.9A, the standby"C" condensate pump start/stop switch was placed in pull stop, and the low pressure heaters condensate bypass valve switch was changed from the auto to closed position.The above switch manipulations were performed to prevent any inadvertent operations during placing the AVT mixed bed demineralizer in service..o The Instrument and Control (I&C)Department was troubleshooting 5A high pressure heater level control problems.DESCRIPTION OP EVENT A.DATES AND APPROXIMATE TIMES OP MAJOR OCCURRENCES: |
| u>>//I/rme/HRC Frurn35883/()7)osooo244930040002OF09LANTCONDTONSTheplantwasatapproximately 974steadystatereactorpowerwiththefollowing pertinent activities inprogress: | | 0 July 7, 1993, 0915 EDST: Event date and approxi-mate time.0 July 7, 1993, 0915 EDST: Discovery date and approximate time.0 July 7, 1993, 0925 EDST: "A" and"B" Steam Generator (S/G)levels restored to pre-event normal operating band.NRC Form 388A (889) |
| oThe"B"AllVolatileTreatment (AVT)mixedbeddemineralizer wasbeingplacedinserviceperoperating procedure T-6.9A(Condensate Polishing MixedBedDIUnitStart-up).
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| AlsoperT-6.9A,thestandby"C"condensate pumpstart/stop switchwasplacedinpullstop,andthelowpressureheaterscondensate bypassvalveswitchwaschangedfromtheautotoclosedposition.
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| Theaboveswitchmanipulations wereperformed topreventanyinadvertent operations duringplacingtheAVTmixedbeddemineralizer inservice..
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| oTheInstrument andControl(I&C)Department wastroubleshooting 5Ahighpressureheaterlevelcontrolproblems.
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| DESCRIPTION OPEVENTA.DATESANDAPPROXIMATE TIMESOPMAJOROCCURRENCES: | |
| 0July7,1993,0915EDST:Eventdateandapproxi-matetime.0July7,1993,0915EDST:Discovery dateandapproximate time.0July7,1993,0925EDST:"A"and"B"SteamGenerator (S/G)levelsrestoredtopre-event normaloperating band.NRCForm388A(889)
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| NRCFORM388A(SJ)9)US.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORT(LER)TEXTCONTINUATION APPROVEDOMBNO.31600108EXPIRES:E/30/92ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUEST:60.0HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(PW30),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20666,ANDTO1'HEPAPERWORK REDUCTION PROJECT(3160410E).
| | NRC FORM 388A (SJ)9)US.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT (LER)TEXT CONTINUATION APPROVED OMB NO.31600108 EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 60.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (PW30), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20666, AND TO 1'HE PAPERWORK REDUCTION PROJECT (3160410E). |
| OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20603.FACILITYNAME('I)DOCKETNUMBER12)YEARLERNl/MBER(8).'os:sEovENTIAL NVMSERREVISIONNVMERPAGE(3)R.E.GlnnaNuclearPowerPlantTEXT///marog>>coJInq>>)ed,1>>o~H/ICFomI38SAB/(ll) osooo244930040003QF09B.EVENTOnJuly7,1993,atapproximately 0800EDST,anInstrument andControl(I&C)Technician begantrouble-shooting5Ahighpressureheaterlevelcontrolproblems, inaccordance withMaintenance WorkOrder(MWO)9301086.TheI&CTechnician suspected therewasanairleakintheairsupplytubingorinthevalvepositioner foroneofthe5Aheaterlevelcontrolvalves.Withconcurrence fromaControlRoomoperator, thetechnician disconnected andpluggedthetubingtothenormallevelcontrolvalve,andobservedthatthehighleveldumpvalve(whichfailsopenonlossofair)brieflyopenedforafew.seconds(untilthetubingwasplugged)andthenclosed,Seeingnoimprovement inairpressure, thetubingwasthenunplugged andrestoredtonormal.Shortlybefore0915EDST,thetechnician disconnected andpluggedthetubingtothehighleveldumpvalve.Withairpressuretothevalveplugged,thedumpvalvewentfullopenandremainedfullyopen.Approximately ten(10)secondslater,thetechnician notedthattheHeaterDrainTank(HDT)discharge valvebeganclosing,andexpeditious'ly unplugged thetubingandrestorednormalairsupplytothedumpvalve.Uponrestoration ofairpressure, thedumpvalveclosed.OnJuly7,1993atapproximately 0915EDST,withthereactoratapproximately 974fullpower,asecondary sidecondensate andfeedwater systemdecreasing pressuretransient occurred.
| | OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20603.FACILITY NAME ('I)DOCKET NUMBER 12)YEAR LER Nl/MBER (8).'os: sEovENTIAL NVMSER REVISION NVM ER PAGE (3)R.E.Glnna Nuclear Power Plant TEXT///maro g>>co JI nq>>)ed, 1>>o~H/IC FomI 38SAB/(ll) o s o o o 2 4 4 9 3 004 0 0 0 3 QF0 9 B.EVENT On July 7, 1993, at approximately 0800 EDST, an Instrument and Control (I&C)Technician began trouble-shooting 5A high pressure heater level control problems, in accordance with Maintenance Work Order (MWO)9301086.The I&C Technician suspected there was an air leak in the air supply tubing or in the valve positioner for one of the 5A heater level control valves.With concurrence from a Control Room operator, the technician disconnected and plugged the tubing to the normal level control valve, and observed that the high level dump valve (which fails open on loss of air)briefly opened for a few.seconds (until the tubing was plugged)and then closed, Seeing no improvement in air pressure, the tubing was then unplugged and restored to normal.Shortly before 0915 EDST, the technician disconnected and plugged the tubing to the high level dump valve.With air pressure to the valve plugged, the dump valve went full open and remained fully open.Approximately ten (10)seconds later, the technician noted that the Heater Drain Tank (HDT)discharge valve began closing, and expeditious'ly unplugged the tubing and restored normal air supply to the dump valve.Upon restoration of air pressure, the dump valve closed.On July 7, 1993 at approximately 0915 EDST, with the reactor at approximately 974 full power, a secondary side condensate and feedwater system decreasing pressure transient occurred.At this time the configuration of the S/G feedwater regulating valves were as follows: o The"A" S/G Main Feedwater Regulating Valve (FRV)was in manual mode (approximately 454 open)to reduce feedwater system flow oscillations that were occurring. |
| Atthistimetheconfiguration oftheS/Gfeedwater regulating valveswereasfollows:oThe"A"S/GMainFeedwater Regulating Valve(FRV)wasinmanualmode(approximately 454open)toreducefeedwater systemflowoscillations thatwereoccurring.
| | NR C F oIRI 388A (689) |
| NRCFoIRI388A(689)
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| NRCFORM366A(SSS)U.S.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORTILER)TEXTCONTINUATION APPROVEDOMSNO.31600104EXPIRES:4/30/02ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUEST:50A)HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(P430),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20655,ANDTO1HEPAPERWORK REDUCTION PROJECT(3150d)04),
| | NRC FORM 366A (SSS)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT ILER)TEXT CONTINUATION APPROVED OMS NO.31600104 EXPIRES: 4/30/02 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 50A)HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P430), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20655, AND TO 1HE PAPERWORK REDUCTION PROJECT (3150d)04), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (<<DOCKET NUMBER (2)YEAR LER NUMBER (6)'SOUSNTIAL NUMSSII 4 IISVIS ION NUMSSII PAGE (3)R.E.Gonna Nuclear Power Plant TEXT///mau Spuce/4 Isqu/>>I/, u>>a/dc0htuh4/I/RC FumI 36643/((Tl 0 5 0 0 0 2 4 4'004 0 0 0 4oF 0 9 o The<<A<<S/G Bypass FRV was in the auto mode controlling the<<A<<S/G level (approximately 804 open).o The<<B<<S/G Main FRV was in the auto mode controlling the<<B<<S/G level (approximately 464 open).o The<<B<<S/G Bypass FRV was in the auto mode (full open).The secondary side condensate and feedwater system decreasing pressure transient was initiated by a significant momentary decrease in HDT pump flow due to the closing of the HDT discharge valve.(HDT pump flow decreased approximately 754 from normal).HDT pump flow normally supplies approximately one third of the suction flow to the S/G main feedwater pumps.The other two thirds of the suction flow to the S/G main feedwater pumps is supplied by the condensate pumps through the low pressure feedwater heaters.The decreased flow coupled with the inability of the standby condensate pump to start and/or the low pressure heaters condensate bypass valve to open, (this line-up explained in Pre-Event Plant Conditions, Section I), decreased pressure throughout the con-.densate and feedwater system.The<<B<<S/G Main FRV (in auto)followed the loss of main feedwater pressure by opening more (approximately 574 open)to maintain main feedwater flow to the<<B<<S/G.The<<A<<S/G Main FRV (in manual)remained at approximately 454 open.Approximately 40-50 seconds after initiation of the transient, HDT pump flow was restored to normal, restoring condensate and feedwater pressure to normal, and causing<<B<<S/G feedwater flow to exceed the calibration range of the flow transmitters |
| OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20503.FACILITYNAME(<<DOCKETNUMBER(2)YEARLERNUMBER(6)'SOUSNTIAL NUMSSII4IISVISIONNUMSSIIPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///mauSpuce/4Isqu/>>I/,
| | (<<B".S/G FRV had opened to 574).Because the"B<<S/G feedwater flow values exceeded the calibration range of the flow transmitters, the"B<<FRV automatically switched to manual mode.The preceding events occurred in a short period of time.During this short period of NRC FoIm 366A (640) 0 NRC FORM 366A (6BB)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT (LER)TEXT CONTINUATION APPROVEO DMS NO.3)504(OE EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUESTI 508)HRS.FORWARD COMMENTS REGARDING BURDEN FSTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504)04). |
| u>>a/dc0htuh4/I/RC FumI36643/((Tl05000244'0040004oF09oThe<<A<<S/GBypassFRVwasintheautomodecontrolling the<<A<<S/Glevel(approximately 804open).oThe<<B<<S/GMainFRVwasintheautomodecontrolling the<<B<<S/Glevel(approximately 464open).oThe<<B<<S/GBypassFRVwasintheautomode(fullopen).Thesecondary sidecondensate andfeedwater systemdecreasing pressuretransient wasinitiated byasignificant momentary decreaseinHDTpumpflowduetotheclosingoftheHDTdischarge valve.(HDTpumpflowdecreased approximately 754fromnormal).HDTpumpflownormallysuppliesapproximately onethirdofthesuctionflowtotheS/Gmainfeedwater pumps.TheothertwothirdsofthesuctionflowtotheS/Gmainfeedwater pumpsissuppliedbythecondensate pumpsthroughthelowpressurefeedwater heaters.Thedecreased flowcoupledwiththeinability ofthestandbycondensate pumptostartand/orthelowpressureheaterscondensate bypassvalvetoopen,(thisline-upexplained inPre-Event PlantConditions, SectionI),decreased pressurethroughout thecon-.densateandfeedwater system.The<<B<<S/GMainFRV(inauto)followedthelossofmainfeedwater pressurebyopeningmore(approximately 574open)tomaintainmainfeedwater flowtothe<<B<<S/G.The<<A<<S/GMainFRV(inmanual)remainedatapproximately 454open.Approximately 40-50secondsafterinitiation ofthetransient, HDTpumpflowwasrestoredtonormal,restoring condensate andfeedwater pressuretonormal,andcausing<<B<<S/Gfeedwater flowtoexceedthecalibration rangeoftheflowtransmitters | | OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (I)DOCKET NUMBER 12)YEAR LER NUMBER (6)I'oR'j SEQUENTIAL S>NUMBER REVISION NUM ER PAGE (3)R.E.Gonna Nuclear Power Plant TEXT/II mort Epoco/E IEOVPEI/ooo ea//I/ono/HRC FomI 366AB/(17)o s o o o 24 49 3 004 0 0 0 50F 09 time the"B" S/G was being supplied with more feedwater than required, and at approximately 0917 EDST (approxi-mately two (2)minutes into the transient) main feedwater isolation on high level (i.e.>/=674 narrow range level)occurred five (5)times to the"BL(S/G over a period of fourteen (14)seconds.The Control Room operators took immediate manual actions to restore S/G levels and at approximately 0925 EDST the"A" and"B" S/G levels were restored to their normal operating band and the plant stabilized. |
| (<<B".S/GFRVhadopenedto574).Becausethe"B<<S/Gfeedwater flowvaluesexceededthecalibration rangeoftheflowtransmitters, the"B<<FRVautomatically switchedtomanualmode.Thepreceding eventsoccurredinashortperiodoftime.DuringthisshortperiodofNRCFoIm366A(640) 0 NRCFORM366A(6BB)U.S.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORT(LER)TEXTCONTINUATION APPROVEODMSNO.3)504(OEEXPIRES:E/30/92ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUESTI508)HRS.FORWARDCOMMENTSREGARDING BURDENFSTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(PJ)30),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTOTHEPAPERWORK REDUCTION PROJECT(31504)04). | | Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Com-mission per 10 CFR 50.72, non-emergency 4 hour notification. |
| OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20503.FACILITYNAME(I)DOCKETNUMBER12)YEARLERNUMBER(6)I'oR'jSEQUENTIAL S>NUMBERREVISIONNUMERPAGE(3)R.E.GonnaNuclearPowerPlantTEXT/IImortEpoco/EIEOVPEI/oooea//I/ono/HRC FomI366AB/(17)osooo2449300400050F09timethe"B"S/Gwasbeingsuppliedwithmorefeedwater thanrequired, andatapproximately 0917EDST(approxi-matelytwo(2)minutesintothetransient) mainfeedwater isolation onhighlevel(i.e.>/=674narrowrangelevel)occurredfive(5)timestothe"BL(S/Goveraperiodoffourteen(14)seconds.TheControlRoomoperators tookimmediate manualactionstorestoreS/Glevelsandatapproximately 0925EDSTthe"A"and"B"S/Glevelswererestoredtotheirnormaloperating bandandtheplantstabilized.
| | C.INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT The 5A high pressure heater high level dump valve to the HDT inoperability, due to troubleshooting efforts, in accordance with MWO 9301086, contributed to the event.Inoperability of the"C" Standby condensate pump and condensate bypass valve, due to procedure T-6.9A'equirements, contributed to the difficulty in responding to the event.D.CÃHiER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: None.NRC FoIIn 366A (649) |
| Subsequently, theControlRoomoperators notifiedhighersupervision andtheNuclearRegulatory Com-missionper10CFR50.72,non-emergency 4hournotification. | |
| C.INOPERABLE STRUCTURES, COMPONENTS, ORSYSTEMSTHATCONTRIBUTED TOTHEEVENTThe5AhighpressureheaterhighleveldumpvalvetotheHDTinoperability, duetotroubleshooting efforts,inaccordance withMWO9301086,contributed totheevent.Inoperability ofthe"C"Standbycondensate pumpandcondensate bypassvalve,duetoprocedure T-6.9A'equirements, contributed tothedifficulty inresponding totheevent.D.CÃHiERSYSTEMSORSECONDARY FUNCTIONS AFFECTED: | |
| None.NRCFoIIn366A(649) | |
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| NAGFOAMSKSA(5$9)U$.NUCLEARREGULATORY COMMISSION LICENSEENTREPORT(LER)TEXTCONTINUATION APPROVEDOMBNO.3)500(04EXPIRES:r/30/92TIMATEDBUADENPEARESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REGUEST:50A)HRS.FORWARDCOMMENTSREGARDING BUAOENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(P$30),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON.
| | NAG FOAM SKSA (5$9)U$.NUCLEAR REGULATORY COMMISSION LICENSEE NT REPORT (LER)TEXT CONTINUATION APPROVED OMB NO.3)500(04 EXPIRES: r/30/92 TIMATED BUADEN PEA RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REGUEST: 50A)HRS.FORWARD COMMENTS REGARDING BUAOEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P$30), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON. |
| OC20555.ANDTO'IHEPAPERWORK REDUCTION PROJECT(31500(04),
| | OC 20555.AND TO'IHE PAPERWORK REDUCTION PROJECT (31500(04), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503 FACILITY NAME (II DOCKET NUMBER (2)YEAR LER NUMBER FS)SKQVKNTIAI NVMSKR RKVIKION NUMSKR PAGE (3)R.E.Gonna Nuclear Power Plant TEXT///mao r/vcr/r rrqokaf, uw edcVdoIN/HRC Fomr 35SA'r/(Ill o s o o o 2 449 3 004 0 0 0 6 OF 0 9 E.METHOD OP DISCOVERY The event was immediately apparent due to alarms and indications in the Control Room and indications at the 5A high pressure heater high level dump valve to the Heater Drain Tank.OPERATOR ACTION: The Control Room operators took immediate manual actions to control S/G levels and stabilize the plant.Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10 CFR 50.72, non-emergency 4 hour notification. |
| OFFICEOFMANAGEMENT ANDBUDGETWASHINGTON DC20503FACILITYNAME(IIDOCKETNUMBER(2)YEARLERNUMBERFS)SKQVKNTIAI NVMSKRRKVIKIONNUMSKRPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///maor/vcr/rrrqokaf,uwedcVdoIN/
| | G SAFETY SYSTEM RESPONSES: |
| HRCFomr35SA'r/(Illosooo244930040006OF09E.METHODOPDISCOVERY Theeventwasimmediately apparentduetoalarmsandindications intheControlRoomandindications atthe5AhighpressureheaterhighleveldumpvalvetotheHeaterDrainTank.OPERATORACTION:TheControlRoomoperators tookimmediate manualactionstocontrolS/Glevelsandstabilize theplant.Subsequently, theControlRoomoperators notifiedhighersupervision andtheNuclearRegulatory Commission per10CFR50.72,non-emergency 4hournotification.
| | The>>B>>S/G Main and Bypass FRVs began to close automatically as a result of the feedwater isolation signals.Due to the short duration that the signals were present, the FRVs never fully closed.III.CAUSE OP EVERT A.IMMEDIATE CAUSE: The feedwater isolation signal to the>>B>>S/G Main and Bypass FRVs was due to the>>B>>S/G narrow range level being>/=67%.B.INTERMEDIATE CAUSE: The>>B>>S/G narrow range level was>/=674 due to increased flow to the>>B>>S/G caused by the perturba-tions in main feedwater header pressure and automatic FRV operation. |
| GSAFETYSYSTEMRESPONSES:
| | This situation resulted in overfeeding the>>B>>S/G.NRC FomI 358A (5$9) |
| The>>B>>S/GMainandBypassFRVsbegantocloseautomatically asaresultofthefeedwater isolation signals.Duetotheshortdurationthatthesignalswerepresent,theFRVsneverfullyclosed.III.CAUSEOPEVERTA.IMMEDIATE CAUSE:Thefeedwater isolation signaltothe>>B>>S/GMainandBypassFRVswasduetothe>>B>>S/Gnarrowrangelevelbeing>/=67%.B.INTERMEDIATE CAUSE:The>>B>>S/Gnarrowrangelevelwas>/=674duetoincreased flowtothe>>B>>S/Gcausedbytheperturba-tionsinmainfeedwater headerpressureandautomatic FRVoperation. | |
| Thissituation resultedinoverfeeding the>>B>>S/G.NRCFomI358A(5$9)
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| NRCFORM366A(609)US.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORT(LER)TEXTCONTINUATION APPROVEDOMBNO.31500104EXPIRES:4/30/92ESTIMATED BURDENPERRESPONSETOCOMPI.YWTHTHISINFORMATION COLLECTION REQUEST:60glHRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(PJ)30),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTO1HEPAPERWORK REDUCTION PROJECT(31500104),
| | NRC FORM 366A (609)US.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT (LER)TEXT CONTINUATION APPROVED OMB NO.31500104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPI.Y WTH THIS INFORMATION COLLECTION REQUEST: 60gl HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. |
| OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON.
| | DC 20503.FACILITY NAME (II DOCKET NUMBER (2)YEAR LER NUMBER (6)(I63: SEQUENTIAL NUM664+p REVISION NUM 64 PAGE (3)R.E.Gonna Nuclear Power Plant TEXT///RNVP 4/>>Ce/4 JNIUPN/II>>PIS/OR4/HRC FORR 36542/((7)0 s 0 o 0 2 4 4~3 004-0 0 7oF 09 The perturbations in main feedwater header pressure were caused by a momentary large reduction in HDT pump flow followed by a rapid return to normal flow.The"B" S/G Main FRV (in auto)followed the loss of main feedwater header pressure by opening more to maintain feedwater flow and when HDT pump flow was rapidly restored, main feedwater header pressure returned to normal.When main feedwater header pressure returned to normal, the"B" S/G FRV was open approximately 114 more than normal and the"B" S/G feedwater flows exceeded the calibration range of the flow transmitters and by design the"B" S/G FRV switched to manual mode.In the manual mode'he"B" S/G Main FRV could not control the"BLI S/G level without operator intervention. |
| DC20503.FACILITYNAME(IIDOCKETNUMBER(2)YEARLERNUMBER(6)(I63:SEQUENTIAL NUM664+pREVISIONNUM64PAGE(3)R.E.GonnaNuclearPowerPlantTEXT///RNVP4/>>Ce/4JNIUPN/II>>PIS/OR4/HRC FORR36542/((7)0s0o0244~3004-007oF09Theperturbations inmainfeedwater headerpressurewerecausedbyamomentary largereduction inHDTpumpflowfollowedbyarapidreturntonormalflow.The"B"S/GMainFRV(inauto)followedthelossofmainfeedwater headerpressurebyopeningmoretomaintainfeedwater flowandwhenHDTpumpflowwasrapidlyrestored, mainfeedwater headerpressurereturnedtonormal.Whenmainfeedwater headerpressurereturnedtonormal,the"B"S/GFRVwasopenapproximately 114morethannormalandthe"B"S/Gfeedwater flowsexceededthecalibration rangeoftheflowtransmitters andbydesignthe"B"S/GFRVswitchedtomanualmode.Inthemanualmode'he"B"S/GMainFRVcouldnotcontrolthe"BLIS/Glevelwithoutoperatorintervention.
| | It should be noted here that if the low pressure heaters condensate bypass valve had been capable of opening, the above transient could have been less severe and the"BFI S/G would most likely have not sustained a high level feedwater isolation. |
| Itshouldbenotedherethatifthelowpressureheaterscondensate bypassvalvehadbeencapableofopening,theabovetransient couldhavebeenlesssevereandthe"BFIS/Gwouldmostlikelyhavenotsustained ahighlevelfeedwater isolation.
| | The momentary large reduction in HDT pump flow, followed by a rapid return to normal flow, was caused by the opening and subsequent closing of the 5A high pressure heater high level dump valve to the HDT, due to the actions of the I&C Technician's troubleshooting activities. |
| Themomentary largereduction inHDTpumpflow,followedbyarapidreturntonormalflow,wascausedbytheopeningandsubsequent closingofthe5AhighpressureheaterhighleveldumpvalvetotheHDT,duetotheactionsoftheI&CTechnician's troubleshooting activities.
| | It is believed that the opening of this dump valve, coupled with the 5A high pressure heater low level condition, decreased the HDT level substan-tially.This level decrease was sensed by the HDT level control system and it began to close the HDT pump discharge control valve to reduce flow and return the HDT level to its operating band.The closing of the 5A high pressure heater high level dump valve, due to the actions of the ISC Technician, reversed the above conditions and the HDT pump flow returned to normal.NRC FoIRI 366A (64)9) |
| Itisbelievedthattheopeningofthisdumpvalve,coupledwiththe5Ahighpressureheaterlowlevelcondition, decreased theHDTlevelsubstan-tially.ThisleveldecreasewassensedbytheHDTlevelcontrolsystemanditbegantoclosetheHDTpumpdischarge controlvalvetoreduceflowandreturntheHDTleveltoitsoperating band.Theclosingofthe5Ahighpressureheaterhighleveldumpvalve,duetotheactionsoftheISCTechnician, reversedtheaboveconditions andtheHDTpumpflowreturnedtonormal.NRCFoIRI366A(64)9)
| | J 0 NRC FOAM 368A (649)FACILITY NAME (1)U.S NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT ILER)TEXT CONTINUATION DOCKET NUMBER (2)APPROVED 0MB NO.31504(OS EXPIRES;S/30/92 ESTIMATED BUADEN PER AESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50J)HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430).U.S.NUCLEAR REGULATORY COMMISSION. |
| J0 NRCFOAM368A(649)FACILITYNAME(1)U.SNUCLEARREGULATORY COMMISSION LICENSEEENTREPORTILER)TEXTCONTINUATION DOCKETNUMBER(2)APPROVED0MBNO.31504(OSEXPIRES;S/30/92ESTIMATED BUADENPERAESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REQUEST:50J)HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(F430).U.S.NUCLEARREGULATORY COMMISSION.
| | WASHINGTON, DC 205S5, AND TO THE PAPERWORK REDUCTION PROJECT (3(504104). |
| WASHINGTON, DC205S5,ANDTOTHEPAPERWORK REDUCTION PROJECT(3(504104). | | OFFICE OF MANAGEMENT AND 8UDG ET, WASHINGTON. |
| OFFICEOFMANAGEMENT AND8UDGET,WASHINGTON.
| | DC 20503.PAGE (3)LER NUMBER IS)R.E.Glnna'NUclear Power Plant TEXT///mare Saece/e re/a/rerL Iree~HRC Farm 355AB/(12)YEARo s o o o 24 493 SEQUENTIAL.oA NUMSSR CN 004 REVISION NUM SR 0 0 0 8 oF 09 ROOT CAUSE: The underlying cause of the event was determined to be not isolating the 5A high pressure heater high level dump valve to the HDT prior to commencement of troubleshooting the air supply concerns for the'dump valve.ANALYSTS OP&TENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of,"any event or conditi'on that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)including the Reactor Protection System (RPS)".The feedwater isolation of the"B" S/G was an automatic actuation of an ESF system.An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions: |
| DC20503.PAGE(3)LERNUMBERIS)R.E.Glnna'NUclear PowerPlantTEXT///mareSaece/ere/a/rerL Iree~HRCFarm355AB/(12)YEARosooo24493SEQUENTIAL
| | There were no operational or safety consequences or implications attributed to the feedwater isolations because: o The feedwater isolations occurred at the required S/G level.0 0 The plant was quickly stabilized and manual control of FRVs was accomplished to mitigate any consequences of the event.I, As the feedwater isolations occurred as designed, the assumptions of the FSAR for steam line break were met.Based on the above, it can be concluded that the public's health and safety was assured at all times.NRC FomI 365A (589) |
| .oANUMSSRCN004REVISIONNUMSR0008oF09ROOTCAUSE:Theunderlying causeoftheeventwasdetermined tobenotisolating the5AhighpressureheaterhighleveldumpvalvetotheHDTpriortocommencement oftroubleshooting theairsupplyconcernsforthe'dumpvalve.ANALYSTSOP&TENTThiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv), | |
| whichrequiresreporting of,"anyeventorconditi'on thatresultedinmanualorautomatic actuation ofanyEngineered SafetyFeature(ESF)including theReactorProtection System(RPS)".Thefeedwater isolation ofthe"B"S/Gwasanautomatic actuation ofanESFsystem.Anassessment wasperformed considering boththesafetyconsequences andimplications ofthiseventwiththefollowing resultsandconclusions:
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| Therewerenooperational orsafetyconsequences orimplications attributed tothefeedwater isolations because:oThefeedwater isolations occurredattherequiredS/Glevel.00Theplantwasquicklystabilized andmanualcontrolofFRVswasaccomplished tomitigateanyconsequences oftheevent.I,Asthefeedwater isolations occurredasdesigned, theassumptions oftheFSARforsteamlinebreakweremet.Basedontheabove,itcanbeconcluded thatthepublic'shealthandsafetywasassuredatalltimes.NRCFomI365A(589)
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| NRCFORM366A(BJIS)UA.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORTILER)TEXTCONTINUATION APPROVEDOMBNO.3(500106EXPIRES:6/30/62ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUEST:60.0HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(F430),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTO1MEPAPERWORK REDUCTION PROJECT(3(500106).
| | NRC FORM 366A (BJIS)UA.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT ILER)TEXT CONTINUATION APPROVED OMB NO.3(500106 E XP I R ES: 6/30/62 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 60.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1ME PAPERWORK REDUCTION PROJECT (3(500106). |
| OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBERLSIYEARr~r'SEOUENTIAL P~SREVISIONNUMBER"~NUMERPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///momJpon/1mqII/mI/II'////JJN/I HRC%%dmI36MB/l(7)osooo2449300400090FV.CORRECTIVE ACTIONAACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:AftertheS/Glevelswerestabilized, theFRVswerereturnedtotheirpre-event controlconfiguration.
| | OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (1)DOCKET NUMBER (2)LER NUMBER LSI YEAR r~r'SEOUENTIAL P~S REVISION NUMBER"~NUM ER PAGE (3)R.E.Gonna Nuclear Power Plant TEXT///mom Jpon/1 mqII/mI/II'////JJN/I HRC%%dmI 36M B/l(7)o s o o o 2 449 3 004 00 0 90F V.CORRECTIVE ACTION A ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: After the S/G levels were stabilized, the FRVs were returned to their pre-event control configuration. |
| B.ACTIONTAKENORPLANNEDTOPREVENTRECERMFNCE: | | B.ACTION TAKEN OR PLANNED TO PREVENT RECERMFNCE: |
| Toensureamorerapidmitigation ofthistypeofeventandpossiblyeliminate thefeedwater isolation, operating procedure T-6.9Awillbechangedtodeletethestepsthatplacethelowpressureheaterscondensate bypassvalveswitchtotheclosedposition.
| | To ensure a more rapid mitigation of this type of event and possibly eliminate the feedwater isolation, operating procedure T-6.9A will be changed to delete the steps that place the low pressure heaters condensate bypass valve switch to the closed position.Operations, Planning, and I&C personnel have been notified that isolation of a heater high level dump valve, prior to troubleshooting, should be considered a normal practice.ADDITIONAL INFORMATION A.FAILED COMPONENTS: |
| Operations, | | None.B PREVIOUS LERs ON SIMILAR EVENTS A similar LER event historical search was conducted with the following results: LER 91-009 and LER-92-006 (Revision 1)were similar events with different root causes.C SPECIAL COMMENTS: LER 92-006 (Revision 1)indicates the problems that have been experienced with the Advanced Digital Feedwater Control System (ADFCS), the causes and corrective actions taken or planned.NRC Form 366A (686) h T}} |
| : Planning, andI&Cpersonnel havebeennotifiedthatisolation ofaheaterhighleveldumpvalve,priortotroubleshooting, shouldbeconsidered anormalpractice.
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| ADDITIONAL INFORMATION A.FAILEDCOMPONENTS: | |
| None.BPREVIOUSLERsONSIMILAREVENTSAsimilarLEReventhistorical searchwasconducted withthefollowing results:LER91-009andLER-92-006(Revision 1)weresimilareventswithdifferent rootcauses.CSPECIALCOMMENTS: | |
| LER92-006(Revision 1)indicates theproblemsthathavebeenexperienced withtheAdvancedDigitalFeedwater ControlSystem(ADFCS),thecausesandcorrective actionstakenorplanned.NRCForm366A(686) hT}}
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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ACCELERATED DOCUMENT DISTRIBUTION SYSTEM REGUL>RY INFORMATION DISTRIBUTE SYSTEM (RIDE)ACCESSION NBR:9308120083 DOC.DATE: 93/08/06 NOTARIZED:
NO FACIL 50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION BACKUS,W.H Rochester Gas a Electric Corp.MECREDY,R.C Rochester Gas 6 Electric Corp.RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 93-004-00:on 930707,Main feedwater isolations occurred due to secondary side 6 condensate feedwater pressure transient.
Returned feedwater regulating valves to pre-event controls configuration.W/930806 ltr.DISTRIBUTION CODE: ZE22T COPIES RECEIVED:LTR t ENCL r SIZE: LO TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
DOCKET¹05000244 I i 1 I 1 Dl S l'.05000244 A RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: ACNW AEOD/DSP/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRIL/RPEB NODS SA/+PLB-BP 02 RGHl FILE 01 EXTERNAL: EGGG BRYCE,J.H NRC PDR NSIC POORE,W.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2'1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DOA AEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB L ST LOBBY WARD NSIC MURPHYFG.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 D D$D D NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2065)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!D FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30
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//i////>rr,//'/I/'i" Ii//,i'" i!C!i)ivir~ill!II I/l'lrir, r!r/ROCHESTER GAS AND ELECTRIC CORPORATION
~";-',Toe/r., state" 89 EAST AVENUE, ROCHESTER N.K 14649-0001 ROBERT C.MECREOY Vice President Clnna ttuclear Production TELEPHONE ARE/1 COOE 716 5rt6 2700 August 6, 1993 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 93-004, Feedwater Control Perturbations, Due To A Secondary Side Transient, Causes Steam Generator High Level Feedwater Isolations R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, License Event Report System, item (a)(2)(iv), which requires a report of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached event report LER 93-004 i: s hereby submitted.
This event has in no way affected the public's health and safety.Very truly yours, xco Robert C.Mec edy U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector~r n.h 9308i20083 930806 PDR*DOCK 05000244 8 PDR
NRC FORM 366 (669)V.S.NUCLEAR REGULATORY COMMISSI LICENSEE EVENT REPORT (LER)APPROVED OMB NOA31506104 EXP IR ESI 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFOAMATION COLLECTION REQUEST: 50.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS ANO RFPORTS MANAGEMENT BRANCH (F630), V.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500'l04).
OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, OC 20503.FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET NUMBER l2)PA E 0 5 0 0 02 44 iOFO Fee water Contro ertur at ons, Due To Secon ary Trans ent, auses team Generator High Level Feedwater Isolations EVENT DATE (5)MONTH DAY YEAR YEAR LER NUMBER (61: SEQUENTIAL NUMBER REVISION NUMBER REPORT DATE LT)MONTH DAY YEAR DOCKET NUMBERIS)0 5 0 0 0 FACII.ITV NAMES 01'HER FACILITIES INVOLVED (6)0-7 79 393 0 0 4 0 0 0 806 93 0 5 0 0 0 OPERATING MODE (9)N POWER LEYEL 0 9 7 60 n(sl(2)Is>>)50.n(v)(2)
Nl 50 73(s)(2)lvsl)50.73(v)(2)(vill)(Al 50.73(v)l2l(vill)(B) 50.73(~)(2)lsl 0 THE RLQUIAEMENTS OF 10 CFR ((:/Chock ono or moro Ol trss IollovrinP/
(11)THIS REPORT IS SVBMITTFD PUASVANT T 20.402(B)20.405(~)(1)(I)20.405 (s)l1)(NI 20.406(~I ('I Hill)20405(s)(1)(lv) 20.405(s I (I)(vl 20.405(c)60M(s)(II 50.36(~)(2)60.73(sl(2((ll 50.73(s)(2)(ill 50.7 3(s)(2)(ill)73,71(B)73.71 I cl OTHER ISpscily In 4osnoct tN/oEN onr/ln Tss I, HRC Form 3664/LICENSEE CONTACT FOR THIS LEA (12I NAME Wesley H.Backus.Technical Assistant to the Operations Mana er TELEPHONE NUMBER AREA CODE 3 155 24-444 6 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAVSE SYS'EM COMPONENT MANUFAC.TVRER REPORTABLE TO NPADS P jQg CAUSE S STEM Xj'>>AA'RC~C.3>>">>T>>~'" IKU'::hl.'.@<COMPONENT MANUFAC.TVRER EPORTABLE TO NPROS?>>o.>>...%R.:.R6)SA'NO 4 PcA.N:: SUPPLEMENTAL REPORT EXPECTED llc)YES Ill y<<, compiots EXPECTED Sl/SSI/SSION DATE/NO AssTRAcT I(.imit to/400 spscsr, l.s., spproslmsrsly lilusn tinpis.rpocs typssvrinon
/inos/(16)EXPECTFD SUBMISSION DATE (15)MONTH DAY YEAR On July 7, 1993-at approximately 0915 EDST, with the reactor at approximately 974 full power, main feedwater isolations occurred on the"BFI Steam Generator (S/G).These feedwater isolations were caused by overfeeding the"B" S/G, following a secondary side condensate and feedwater pressure transient.
Immediate operator action was to manually control the Feedwater Regulating Valves (FRVs)to restore the S/G water levels and stabilize the plant.The immediate cause of the event was due to a secondary side condensate and feedwater pressure transient.
The underlying cause of the event was determined to be not isolating the 5A heater high level dump valve prior to trouble-shooting.(This event is NUREG-1022 (X)Cause Code).Corrective actions taken or planned are discussed in Section V of the text.NRC Form 366 (669)
NRC FORM 388A (SJ)9)US.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT (LER)TEXT CONTINUATION APPROVED OMB NO.3(504)04 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 508)HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500)08), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (ll DOCKET NUMBER (2)YEAR LER NUMBER (8)SEOUENTIAL o@IIEVISION NUM E II PAGE (3)R.E.Glnna Nuclear Power Plant TEXT/I/more e/reoe/I rer/uuN/, u>>//I/rme/HRC Frurn 35883/()7)o s o o o 24 49 3 004 0 0 0 2 OF 0 9 LANT COND T ONS The plant was at approximately 974 steady state reactor power with the following pertinent activities in progress: o The"B" All Volatile Treatment (AVT)mixed bed demineralizer was being placed in service per operating procedure T-6.9A (Condensate Polishing Mixed Bed DI Unit Start-up).
Also per T-6.9A, the standby"C" condensate pump start/stop switch was placed in pull stop, and the low pressure heaters condensate bypass valve switch was changed from the auto to closed position.The above switch manipulations were performed to prevent any inadvertent operations during placing the AVT mixed bed demineralizer in service..o The Instrument and Control (I&C)Department was troubleshooting 5A high pressure heater level control problems.DESCRIPTION OP EVENT A.DATES AND APPROXIMATE TIMES OP MAJOR OCCURRENCES:
0 July 7, 1993, 0915 EDST: Event date and approxi-mate time.0 July 7, 1993, 0915 EDST: Discovery date and approximate time.0 July 7, 1993, 0925 EDST: "A" and"B" Steam Generator (S/G)levels restored to pre-event normal operating band.NRC Form 388A (889)
NRC FORM 388A (SJ)9)US.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT (LER)TEXT CONTINUATION APPROVED OMB NO.31600108 EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 60.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (PW30), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20666, AND TO 1'HE PAPERWORK REDUCTION PROJECT (3160410E).
OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20603.FACILITY NAME ('I)DOCKET NUMBER 12)YEAR LER Nl/MBER (8).'os: sEovENTIAL NVMSER REVISION NVM ER PAGE (3)R.E.Glnna Nuclear Power Plant TEXT///maro g>>co JI nq>>)ed, 1>>o~H/IC FomI 38SAB/(ll) o s o o o 2 4 4 9 3 004 0 0 0 3 QF0 9 B.EVENT On July 7, 1993, at approximately 0800 EDST, an Instrument and Control (I&C)Technician began trouble-shooting 5A high pressure heater level control problems, in accordance with Maintenance Work Order (MWO)9301086.The I&C Technician suspected there was an air leak in the air supply tubing or in the valve positioner for one of the 5A heater level control valves.With concurrence from a Control Room operator, the technician disconnected and plugged the tubing to the normal level control valve, and observed that the high level dump valve (which fails open on loss of air)briefly opened for a few.seconds (until the tubing was plugged)and then closed, Seeing no improvement in air pressure, the tubing was then unplugged and restored to normal.Shortly before 0915 EDST, the technician disconnected and plugged the tubing to the high level dump valve.With air pressure to the valve plugged, the dump valve went full open and remained fully open.Approximately ten (10)seconds later, the technician noted that the Heater Drain Tank (HDT)discharge valve began closing, and expeditious'ly unplugged the tubing and restored normal air supply to the dump valve.Upon restoration of air pressure, the dump valve closed.On July 7, 1993 at approximately 0915 EDST, with the reactor at approximately 974 full power, a secondary side condensate and feedwater system decreasing pressure transient occurred.At this time the configuration of the S/G feedwater regulating valves were as follows: o The"A" S/G Main Feedwater Regulating Valve (FRV)was in manual mode (approximately 454 open)to reduce feedwater system flow oscillations that were occurring.
NR C F oIRI 388A (689)
NRC FORM 366A (SSS)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT ILER)TEXT CONTINUATION APPROVED OMS NO.31600104 EXPIRES: 4/30/02 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 50A)HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P430), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20655, AND TO 1HE PAPERWORK REDUCTION PROJECT (3150d)04), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (<<DOCKET NUMBER (2)YEAR LER NUMBER (6)'SOUSNTIAL NUMSSII 4 IISVIS ION NUMSSII PAGE (3)R.E.Gonna Nuclear Power Plant TEXT///mau Spuce/4 Isqu/>>I/, u>>a/dc0htuh4/I/RC FumI 36643/((Tl 0 5 0 0 0 2 4 4'004 0 0 0 4oF 0 9 o The<<A<<S/G Bypass FRV was in the auto mode controlling the<<A<<S/G level (approximately 804 open).o The<<B<<S/G Main FRV was in the auto mode controlling the<<B<<S/G level (approximately 464 open).o The<<B<<S/G Bypass FRV was in the auto mode (full open).The secondary side condensate and feedwater system decreasing pressure transient was initiated by a significant momentary decrease in HDT pump flow due to the closing of the HDT discharge valve.(HDT pump flow decreased approximately 754 from normal).HDT pump flow normally supplies approximately one third of the suction flow to the S/G main feedwater pumps.The other two thirds of the suction flow to the S/G main feedwater pumps is supplied by the condensate pumps through the low pressure feedwater heaters.The decreased flow coupled with the inability of the standby condensate pump to start and/or the low pressure heaters condensate bypass valve to open, (this line-up explained in Pre-Event Plant Conditions,Section I), decreased pressure throughout the con-.densate and feedwater system.The<<B<<S/G Main FRV (in auto)followed the loss of main feedwater pressure by opening more (approximately 574 open)to maintain main feedwater flow to the<<B<<S/G.The<<A<<S/G Main FRV (in manual)remained at approximately 454 open.Approximately 40-50 seconds after initiation of the transient, HDT pump flow was restored to normal, restoring condensate and feedwater pressure to normal, and causing<<B<<S/G feedwater flow to exceed the calibration range of the flow transmitters
(<<B".S/G FRV had opened to 574).Because the"B<<S/G feedwater flow values exceeded the calibration range of the flow transmitters, the"B<<FRV automatically switched to manual mode.The preceding events occurred in a short period of time.During this short period of NRC FoIm 366A (640) 0 NRC FORM 366A (6BB)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT (LER)TEXT CONTINUATION APPROVEO DMS NO.3)504(OE EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUESTI 508)HRS.FORWARD COMMENTS REGARDING BURDEN FSTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504)04).
OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (I)DOCKET NUMBER 12)YEAR LER NUMBER (6)I'oR'j SEQUENTIAL S>NUMBER REVISION NUM ER PAGE (3)R.E.Gonna Nuclear Power Plant TEXT/II mort Epoco/E IEOVPEI/ooo ea//I/ono/HRC FomI 366AB/(17)o s o o o 24 49 3 004 0 0 0 50F 09 time the"B" S/G was being supplied with more feedwater than required, and at approximately 0917 EDST (approxi-mately two (2)minutes into the transient) main feedwater isolation on high level (i.e.>/=674 narrow range level)occurred five (5)times to the"BL(S/G over a period of fourteen (14)seconds.The Control Room operators took immediate manual actions to restore S/G levels and at approximately 0925 EDST the"A" and"B" S/G levels were restored to their normal operating band and the plant stabilized.
Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Com-mission per 10 CFR 50.72, non-emergency 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification.
C.INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT The 5A high pressure heater high level dump valve to the HDT inoperability, due to troubleshooting efforts, in accordance with MWO 9301086, contributed to the event.Inoperability of the"C" Standby condensate pump and condensate bypass valve, due to procedure T-6.9A'equirements, contributed to the difficulty in responding to the event.D.CÃHiER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: None.NRC FoIIn 366A (649)
NAG FOAM SKSA (5$9)U$.NUCLEAR REGULATORY COMMISSION LICENSEE NT REPORT (LER)TEXT CONTINUATION APPROVED OMB NO.3)500(04 EXPIRES: r/30/92 TIMATED BUADEN PEA RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REGUEST: 50A)HRS.FORWARD COMMENTS REGARDING BUAOEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P$30), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON.
OC 20555.AND TO'IHE PAPERWORK REDUCTION PROJECT (31500(04), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503 FACILITY NAME (II DOCKET NUMBER (2)YEAR LER NUMBER FS)SKQVKNTIAI NVMSKR RKVIKION NUMSKR PAGE (3)R.E.Gonna Nuclear Power Plant TEXT///mao r/vcr/r rrqokaf, uw edcVdoIN/HRC Fomr 35SA'r/(Ill o s o o o 2 449 3 004 0 0 0 6 OF 0 9 E.METHOD OP DISCOVERY The event was immediately apparent due to alarms and indications in the Control Room and indications at the 5A high pressure heater high level dump valve to the Heater Drain Tank.OPERATOR ACTION: The Control Room operators took immediate manual actions to control S/G levels and stabilize the plant.Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10 CFR 50.72, non-emergency 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification.
G SAFETY SYSTEM RESPONSES:
The>>B>>S/G Main and Bypass FRVs began to close automatically as a result of the feedwater isolation signals.Due to the short duration that the signals were present, the FRVs never fully closed.III.CAUSE OP EVERT A.IMMEDIATE CAUSE: The feedwater isolation signal to the>>B>>S/G Main and Bypass FRVs was due to the>>B>>S/G narrow range level being>/=67%.B.INTERMEDIATE CAUSE: The>>B>>S/G narrow range level was>/=674 due to increased flow to the>>B>>S/G caused by the perturba-tions in main feedwater header pressure and automatic FRV operation.
This situation resulted in overfeeding the>>B>>S/G.NRC FomI 358A (5$9)
NRC FORM 366A (609)US.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT (LER)TEXT CONTINUATION APPROVED OMB NO.31500104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPI.Y WTH THIS INFORMATION COLLECTION REQUEST: 60gl HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON.
DC 20503.FACILITY NAME (II DOCKET NUMBER (2)YEAR LER NUMBER (6)(I63: SEQUENTIAL NUM664+p REVISION NUM 64 PAGE (3)R.E.Gonna Nuclear Power Plant TEXT///RNVP 4/>>Ce/4 JNIUPN/II>>PIS/OR4/HRC FORR 36542/((7)0 s 0 o 0 2 4 4~3 004-0 0 7oF 09 The perturbations in main feedwater header pressure were caused by a momentary large reduction in HDT pump flow followed by a rapid return to normal flow.The"B" S/G Main FRV (in auto)followed the loss of main feedwater header pressure by opening more to maintain feedwater flow and when HDT pump flow was rapidly restored, main feedwater header pressure returned to normal.When main feedwater header pressure returned to normal, the"B" S/G FRV was open approximately 114 more than normal and the"B" S/G feedwater flows exceeded the calibration range of the flow transmitters and by design the"B" S/G FRV switched to manual mode.In the manual mode'he"B" S/G Main FRV could not control the"BLI S/G level without operator intervention.
It should be noted here that if the low pressure heaters condensate bypass valve had been capable of opening, the above transient could have been less severe and the"BFI S/G would most likely have not sustained a high level feedwater isolation.
The momentary large reduction in HDT pump flow, followed by a rapid return to normal flow, was caused by the opening and subsequent closing of the 5A high pressure heater high level dump valve to the HDT, due to the actions of the I&C Technician's troubleshooting activities.
It is believed that the opening of this dump valve, coupled with the 5A high pressure heater low level condition, decreased the HDT level substan-tially.This level decrease was sensed by the HDT level control system and it began to close the HDT pump discharge control valve to reduce flow and return the HDT level to its operating band.The closing of the 5A high pressure heater high level dump valve, due to the actions of the ISC Technician, reversed the above conditions and the HDT pump flow returned to normal.NRC FoIRI 366A (64)9)
J 0 NRC FOAM 368A (649)FACILITY NAME (1)U.S NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT ILER)TEXT CONTINUATION DOCKET NUMBER (2)APPROVED 0MB NO.31504(OS EXPIRES;S/30/92 ESTIMATED BUADEN PER AESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50J)HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430).U.S.NUCLEAR REGULATORY COMMISSION.
WASHINGTON, DC 205S5, AND TO THE PAPERWORK REDUCTION PROJECT (3(504104).
OFFICE OF MANAGEMENT AND 8UDG ET, WASHINGTON.
DC 20503.PAGE (3)LER NUMBER IS)R.E.Glnna'NUclear Power Plant TEXT///mare Saece/e re/a/rerL Iree~HRC Farm 355AB/(12)YEARo s o o o 24 493 SEQUENTIAL.oA NUMSSR CN 004 REVISION NUM SR 0 0 0 8 oF 09 ROOT CAUSE: The underlying cause of the event was determined to be not isolating the 5A high pressure heater high level dump valve to the HDT prior to commencement of troubleshooting the air supply concerns for the'dump valve.ANALYSTS OP&TENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of,"any event or conditi'on that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)including the Reactor Protection System (RPS)".The feedwater isolation of the"B" S/G was an automatic actuation of an ESF system.An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences or implications attributed to the feedwater isolations because: o The feedwater isolations occurred at the required S/G level.0 0 The plant was quickly stabilized and manual control of FRVs was accomplished to mitigate any consequences of the event.I, As the feedwater isolations occurred as designed, the assumptions of the FSAR for steam line break were met.Based on the above, it can be concluded that the public's health and safety was assured at all times.NRC FomI 365A (589)
NRC FORM 366A (BJIS)UA.NUCLEAR REGULATORY COMMISSION LICENSEE ENT REPORT ILER)TEXT CONTINUATION APPROVED OMB NO.3(500106 E XP I R ES: 6/30/62 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 60.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1ME PAPERWORK REDUCTION PROJECT (3(500106).
OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (1)DOCKET NUMBER (2)LER NUMBER LSI YEAR r~r'SEOUENTIAL P~S REVISION NUMBER"~NUM ER PAGE (3)R.E.Gonna Nuclear Power Plant TEXT///mom Jpon/1 mqII/mI/II'////JJN/I HRC%%dmI 36M B/l(7)o s o o o 2 449 3 004 00 0 90F V.CORRECTIVE ACTION A ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: After the S/G levels were stabilized, the FRVs were returned to their pre-event control configuration.
B.ACTION TAKEN OR PLANNED TO PREVENT RECERMFNCE:
To ensure a more rapid mitigation of this type of event and possibly eliminate the feedwater isolation, operating procedure T-6.9A will be changed to delete the steps that place the low pressure heaters condensate bypass valve switch to the closed position.Operations, Planning, and I&C personnel have been notified that isolation of a heater high level dump valve, prior to troubleshooting, should be considered a normal practice.ADDITIONAL INFORMATION A.FAILED COMPONENTS:
None.B PREVIOUS LERs ON SIMILAR EVENTS A similar LER event historical search was conducted with the following results: LER 91-009 and LER-92-006 (Revision 1)were similar events with different root causes.C SPECIAL COMMENTS: LER 92-006 (Revision 1)indicates the problems that have been experienced with the Advanced Digital Feedwater Control System (ADFCS), the causes and corrective actions taken or planned.NRC Form 366A (686) h T