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| {{#Wiki_filter:CATEGORY1REGULATOYINFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESS1'ON NBR:9606260154 DOC.DATE: | | {{#Wiki_filter:CATEGORY 1 REGULATO Y INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESS1'ON NBR:9606260154 DOC.DATE: 96/06/20 NOTARIZED: |
| 96/06/20NOTARIZED: | | NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester AUTH.NAME AUTHOR AFFILIATION ST.MARTIN,J.T. |
| NOFACIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester AUTH.NAMEAUTHORAFFILIATION ST.MARTIN,J.T.
| | Rochester Gas&Electric Corp.MECREDY,R.C. |
| Rochester Gas&ElectricCorp.MECREDY,R.C. | | Rochester Gas&Electric Corp.RECIP.NAME RECIPIENT'AFFILIATION DOCKET G 05000244 |
| Rochester Gas&ElectricCorp.RECIP.NAME RECIPIENT | |
| 'AFFILIATION DOCKETG05000244 | |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER96-006-00:on 960521,discovered containment penetration notinrequiredstatus.Causedbypersonnel error.Installed flangeinsidecontainment penetration 2.W/960620 ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR ENCLSIZE:TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
| | LER 96-006-00:on 960521,discovered containment penetration not in required status.Caused by personnel error.Installed flange inside containment penetration 2.W/960620 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). |
| A'5000244(IRECIPIENT IDCODE/NAME PDl-1PDINTERNAL: | | A'5000244 (I RECIPIENT ID CODE/NAME PDl-1 PD INTERNAL: AEOD/SPD/RAB gF'ZEE CENE E NRR/DE/EEL'B NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN1 FILE 01 EXTERNAL: L ST LOBBY WARD NOAC MURPHYFG~A NRC PDR COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME VISSINGFG. |
| AEOD/SPD/RAB gF'ZEECENEENRR/DE/EEL'B NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN1FILE01EXTERNAL: | | AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DSIR/EIB LITCO BRYCEFJ H NOAC POOREFW.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 D.N NOTE TO ALL"RIDS" RECIPIENTS: |
| LSTLOBBYWARDNOACMURPHYFG~ANRCPDRCOPIESLTTRENCL112211111111111111111111RECIPIENT IDCODE/NAME VISSINGFG.
| | PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK/ROOM OWFN 5D-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25 AND ROCHESTER GAS AND ElECTRIC CORI@RATION |
| AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DSIR/EIB LITCOBRYCEFJHNOACPOOREFW.NUDOCSFULLTXTCOPIESLTTRENCL1111111111111111221111D.NNOTETOALL"RIDS"RECIPIENTS: | | ~89 EAST AVENUE, ROCHESTER, N.Y.IrI64'rr DDT AREA CODE 716 5'-27tXt ROBERT C.MECREDY Vice President Nucte or Operations June 20, 1996 U.S.Nuclear Regulatory Commission Document Control Desk Attn: Guy S.Vissing Project Directorate I-1 Washington, D.C.20555 |
| PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK/ROOMOWFN5D-5(EXT.
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| 415-2083) | |
| TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
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| LTTR25ENCL25 ANDROCHESTER GASANDElECTRICCORI@RATION
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| ~89EASTAVENUE,ROCHESTER, N.Y.IrI64'rrDDTAREACODE7165'-27tXtROBERTC.MECREDYVicePresident NucteorOperations June20,1996U.S.NuclearRegulatory Commission DocumentControlDeskAttn:GuyS.VissingProjectDirectorate I-1Washington, D.C.20555 | |
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| ==Subject:== | | ==Subject:== |
| LER96-006,Containment Penetration NotinRequiredStatus,DuetoPersonnel Errors,ResultsinPotential forUncontrolled ReleaseofRadioactive MaterialR.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordance with10CFR50.73,LicenseeEventReportSystem,items(a)(2)(ii),(a)(2)(v)(C)and(a)(2)(v)(D),whichrequireareportof,"Anyoperation orcondition prohibited bytheplant'sTechnical Specifications" or"Anyeventorcondition thatalonecouldhaveprevented thefulfillment ofthesafetyfunctionofstructures orsystemsthatareneededto...Controlthereleaseofradioactive material; orMitigatetheconsequences ofanaccident",
| | LER 96-006, Containment Penetration Not in Required Status, Due to Personnel Errors, Results in Potential for Uncontrolled Release of Radioactive Material R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, items (a)(2)(ii), (a)(2)(v)(C)and (a)(2)(v)(D), which require a report of,"Any operation or condition prohibited by the plant's Technical Specifications" or"Any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to...Control the release of radioactive material;or Mitigate the consequences of an accident", the attached Licensee Event Report LER 96-006 is hereby submitted. |
| theattachedLicenseeEventReportLER96-006isherebysubmitted.
| | This event has in no way affected the public's health and safety.Very ly yours, Robert C.Mecredy xc: U.S.Nuclear Regulatory Commission Mr.Guy S.Vissing (Mail Stop 14C7)PWR Project Directorate I-1 Washington, D.C.,20555 U.S.Nuclear Regulatory Commission Region I 475 Allendale-Road King of Prussia, PA 19406 U.S.NRC Ginna Senior Resident Inspector 9606260i54 960620 PDR ADQCK 05000244 8 PDR y/~JP NRC FORM 366 (4.95)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)APPROVED BY OMB NO.3150-0104 EXPIRES 04/30/BB ESTIMATED BURDEN PER AESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.REPOATED LESSONS LEARNED ARE INCORPORATED INTO THE UCENSING PROCESS AND FED BACK To INDUSTRY.FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE INFORMATION AND RECORDS MANAGEMENT BRANCH IT-6 F33), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555.0001, AND To THE PAPEAWORK REDUCTION PROJECT FACILITY kAME (1)R.E.Ginna Nuclear Power Plant OOCKET NUMBER (2)05000244 PAGE (3)1OF8 B (4)A Containment Penetration Not in Required Status, Due to Personnel Errors, Results'in Potential for Uncontrolled Release of Radioactive Material MONTH DAY YEAR 05 21 96 EVENT DATE (5)LER NUMBER (6)SEQUENTIAL REVISION NUMBER., NUMBER 96-006-00 MONTH DAY YEAR 06 20 96 REPORT DATE (7)FACILITY NAME FACILITY NAME OTHER FACILITIES INVOLVED (6)OOCKET NUMBER OOCKET NUMBER OPERATING MODE (9)POWER LEVEL (10)kAME 000 THIS REPORT IS SUBMITTED PUR more)(11)50.73(a)(2)(viii]50.73(a)(2)(x)50.73(a)(2)(i)50.73(a)(2)(ii)20.2203(a)(2)(v) 20.2203(a)(3)(i) 20.2201(b) 20.2203ta) tl)73.71 50.73(a)(2)(iii)50.73(a)(2)(iv)20.2203(a) |
| Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verylyyours,RobertC.Mecredyxc:U.S.NuclearRegulatory Commission Mr.GuyS.Vissing(MailStop14C7)PWRProjectDirectorate I-1Washington, D.C.,20555 U.S.NuclearRegulatory Commission RegionI475Allendale-Road KingofPrussia,PA19406U.S.NRCGinnaSeniorResidentInspector 9606260i54 960620PDRADQCK050002448PDRy/~JP NRCFORM366(4.95)U.S.NUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/characters foreachblock)APPROVEDBYOMBNO.3150-0104 EXPIRES04/30/BBESTIMATED BURDENPERAESPONSEToCOMPLYWITHTHISMANDATORY INFORMATION COLLECTION REQUEST:50.0HRS.REPOATEDLESSONSLEARNEDAREINCORPORATED INTOTHEUCENSINGPROCESSANDFEDBACKToINDUSTRY.
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| FORWARDCOMMENTSREGARDING BURDENESTIMATEToTHEINFORMATION ANDRECORDSMANAGEMENT BRANCHIT-6F33),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555.0001, ANDToTHEPAPEAWORK REDUCTION PROJECTFACILITYkAME(1)R.E.GinnaNuclearPowerPlantOOCKETNUMBER(2)05000244PAGE(3)1OF8B(4)AContainment Penetration NotinRequiredStatus,DuetoPersonnel Errors,Results'in Potential forUncontrolled ReleaseofRadioactive MaterialMONTHDAYYEAR052196EVENTDATE(5)LERNUMBER(6)SEQUENTIAL REVISIONNUMBER.,NUMBER96-006-00MONTHDAYYEAR062096REPORTDATE(7)FACILITYNAMEFACILITYNAMEOTHERFACILITIES INVOLVED(6)OOCKETNUMBEROOCKETNUMBEROPERATING MODE(9)POWERLEVEL(10)kAME000THISREPORTISSUBMITTED PURmore)(11)50.73(a)(2)(viii]50.73(a)(2)(x)50.73(a)(2)(i)50.73(a)(2)(ii)20.2203(a)(2)(v) 20.2203(a)(3)(i) 20.2201(b) 20.2203ta) tl)73.7150.73(a)(2)(iii)50.73(a)(2)(iv)20.2203(a)
| |
| (3)(ii)20.2203(a) | | (3)(ii)20.2203(a) |
| (4)20.2203(a) | | (4)20.2203(a) |
| (2)(i)20.2203(a)(2)(ii) | | (2)(i)20.2203(a)(2)(ii) |
| OTHERSpecifyinAbstractbeloworinNRCForm366A20.2203(a)(2)
| | OTHER Specify in Abstract below or in NRC Form 366A 20.2203(a)(2)(iii)50.36(c)(1) 50.73(a)(2)(v)20.2203(a) |
| (iii)50.36(c)(1) 50.73(a)(2) | |
| (v)20.2203(a) | |
| (2)(iv)50.36(c)(2)50.73(a)(2)(vii) | | (2)(iv)50.36(c)(2)50.73(a)(2)(vii) |
| LICENSEECONTACTFORTHISLER(12)ELBPIIOkE NUMBER(IncludeAreaCoda>SUANTTOTHEREQUIREMENTS OF10CFRE:(CheckoneorJohnT.St.Martin-Technical Assistant (716)771-3641COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTURER AEPOATABLE TONPADSCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE ToNPRDSSUPPLEMENTAL REPORTEXPECTED(14)YES(lfyes,completeEXPECTEDSUBMISSION DATE).XNOEXPECTEDSUBMISSION DATE(15)MONTHDAYYEARABSTRACT(Limitto1400spaces,l.e.,approximately 15single-spaced typewritten lines)(16)OnMay21,1996,atapproximately 0900EDST,withtheplantinMode6withcorealterations andmovementofirradiated fuelassemblies withincontainment inprogress, itwasdiscovered thatacontainment penetration wasnotintherequiredstatusforrefueling operations, allowingdirectaccessfromthecontainment atmosphere totheoutsideatmosphere.
| | LICENSEE CONTACT FOR THIS LER (12)ELBPIIOkE NUMBER (Include Area Coda>SUANT TO THE REQUIREMENTS OF 10 CFR E: (Check one or John T.St.Martin-Technical Assistant (716)771-3641 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFACTURER AEPOATABLE TO NPADS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE To NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (lf yes, complete EXPECTED SUBMISSION DATE).X NO EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, l.e., approximately 15 single-spaced typewritten lines)(16)On May 21, 1996, at approximately 0900 EDST, with the plant in Mode 6 with core alterations and movement of irradiated fuel assemblies within containment in progress, it was discovered that a containment penetration was not in the required status for refueling operations, allowing direct access from the containment atmosphere to the outside atmosphere. |
| Immediate corrective actionwastakeninaccordance withGinnaImprovedTechnical Specifications LimitingConditions forOperation 3.9.3.A.1 and3.9.3.A.2 tosuspendcorealterations andsuspendmovementofirradiated fuelassemblies withincontainment. | | Immediate corrective action was taken in accordance with Ginna Improved Technical Specifications Limiting Conditions for Operation 3.9.3.A.1 and 3.9.3.A.2 to suspend core alterations and suspend movement of irradiated fuel assemblies within containment. |
| Thecontainment penetration wasrestoredtotherequiredstatusforrefueling operations, andrefueling operations werepermitted toresume.Theunderlying causeofthepenetration notbeingintherequiredstatusforrefueling operations waspersonnel errors.ThiseventisNUREG-1022 CauseCode(A).Corrective actiontopreventrecurrence isoutlinedinSectionV.B.NRCFORM366(4-95)
| | The containment penetration was restored to the required status for refueling operations, and refueling operations were permitted to resume.The underlying cause of the penetration not being in the required status for refueling operations was personnel errors.This event is NUREG-1022 Cause Code (A).Corrective action to prevent recurrence is outlined in Section V.B.NRC FORM 366 (4-95) |
| NRCFORM366AI4-95)LICENSEEEVENTREPORT(LER),TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAMEIl)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-006-00PAGEI3)2OF8TEXT(Ifmorespaceisrequired, useadditional copiesofNRCForm366A/(17)PRE-EVENT PLANTCONDITIONS:
| | NRC FORM 366A I4-95)LICENSEE EVENT REPORT (LER), TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME Il)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER I6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE I3)2 OF 8 TEXT (If more spaceis required, use additional copies of NRC Form 366A/(17)PRE-EVENT PLANT CONDITIONS: |
| Containment (CNMT)penetration I)'2(referred toasP-2)isthe"S/GCommunications FlangePenetration" normallyusedforsupportofroutinesteamgenerator (S/G)maintenance andinspection activities duringrefueling outages.WheninModes5or6,normallyroutedthroughP-2areclosed-circuit television (CCTV)cablesandothercommunications cables.Forthe1996Refueling outage,P-2wasalsousedtoprovidearouteforadditional CCTVcablesandrigidpipesfrom'theoutsideintoCNMT,toprovideservices(communications, airandargon)foractivities associated withreplacement oftheS/Gs.Thesepipeswerea3"lineforserviceairanda11/2"lineforargon.StationModification procedures SM-10034-10.01 (Temporary ServiceAirSystemforSGRP)andSM-10034-'l0.03 (Installation 5RemovalofTemporary CCTVandCommunications) wereusedtocontrolthetemporary installation andsubsequent removaloftheseservices. | | Containment (CNMT)penetration I)'2 (referred to as P-2)is the"S/G Communications Flange Penetration" normally used for support of routine steam generator (S/G)maintenance and inspection activities during refueling outages.When in Modes 5 or 6, normally routed through P-2 are closed-circuit television (CCTV)cables and other communications cables.For the 1996 Refueling outage, P-2 was also used to provide a route for additional CCTV cables and rigid pipes from'the outside into CNMT, to provide services (communications, air and argon)for activities associated with replacement of the S/Gs.These pipes were a 3" line for service air and a 1 1/2" line for argon.Station Modification procedures SM-10034-10.01 (Temporary Service Air System for SGRP)and SM-10034-'l0.03 (Installation 5 Removal of Temporary CCTV and Communications) were used to control the temporary installation and subsequent removal of these services.On May 19, 1996, in preparation for refueling the reactor, Ginna plant staff checked the configuration of P-2 and verified that the configuration complied with Ginna Improved Technical Specifications (ITS)Limiting Condition for Operation (LCO)3.9.3.c, which states that each penetration providing direct access from the CNMT atmosphere to the outside atmosphere shall be isolated, or closed by an equivalent isolation method.These methods include use of material that can provide a temporary, atmospheric pressure, ventilation barrier.Contractor supervision were subsequently notified not to disturb the configuration of P-2 until after the completion of refueling. |
| OnMay19,1996,inpreparation forrefueling thereactor,Ginnaplantstaffcheckedtheconfiguration ofP-2andverifiedthattheconfiguration compliedwithGinnaImprovedTechnical Specifications (ITS)LimitingCondition forOperation (LCO)3.9.3.c,whichstatesthateachpenetration providing directaccessfromtheCNMTatmosphere totheoutsideatmosphere shallbeisolated, orclosedbyanequivalent isolation method.Thesemethodsincludeuseofmaterialthatcanprovideatemporary, atmospheric
| | During the dayshift on May 20, 1996, as directed by contractor supervision, contractor maintenance personnel removed much of the temporary service air and argon lines inside CNMT, as directed by procedure SM-10034-10.01. |
| : pressure, ventilation barrier.Contractor supervision weresubsequently notifiednottodisturbtheconfiguration ofP-2untilafterthecompletion ofrefueling.
| | Contractor supervision had been cautioned by Ginna staff not to remove the 3" and 1 1/2" pipe spoolpieces that were inside the seal for P-2 and the first valves on each side of P-2 inside and outside of CNMT.Nevertheless, at the end of their shift (at approximately 1800 EDST), the contractor maintenance personnel removed these spoolpieces and valves.Additional piping outside CNMT was left in place until the next day.On May 21, 1996, at approximately 0300 EDST, a utility non-licensed operator was performing Operating Procedure 0-15.2 (Valve Alignment for Reactor Head Lift, Core Component Movement, and Periodic Status Checks), in preparation for the start of refueling operations. |
| DuringthedayshiftonMay20,1996,asdirectedbycontractor supervision, contractor maintenance personnel removedmuchofthetemporary serviceairandargonlinesinsideCNMT,asdirectedbyprocedure SM-10034-10.01.
| | As part of this procedure, the operator performed Step 5.2.1 to verify that P-2 was"adequately sealed", and signed off Step 5.2.1 of procedure 0-15.2.Satisfactory completion of this step ensures compliance with ITS LCO 3.9.3.c.NRG FORM 366A I4-95) |
| Contractor supervision hadbeencautioned byGinnastaffnottoremovethe3"and11/2"pipespoolpieces thatwereinsidethesealforP-2andthefirstvalvesoneachsideofP-2insideandoutsideofCNMT.Nevertheless, attheendoftheirshift(atapproximately 1800EDST),thecontractor maintenance personnel removedthesespoolpieces andvalves.Additional pipingoutsideCNMTwasleftinplaceuntilthenextday.OnMay21,1996,atapproximately 0300EDST,autilitynon-licensed operatorwasperforming Operating Procedure 0-15.2(ValveAlignment forReactorHeadLift,CoreComponent | | NRC FORM 366A (4-95)LXCENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE (3)TEXT (If more spaceis required, use additional copies of NRC Form 366A/(17)DESCRIPTION OF EVENT: A.DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES: |
| : Movement, andPeriodicStatusChecks),inpreparation forthestartofrefueling operations.
| | 0 May 19, 1996: Ginna staff verify that the configuration of P-2 meets the required status of ITS LCO 3.9.3.c.May 20, 1996, 1800 EDST: Contractor maintenance personnel remove pipe spoolpieces from inside the seal for P-2.P-2 configuration does not meet the required status of ITS LCO 3.9.3.c.0 May 21, 1996, 0537 EDST: The plant enters Mode 6 and begins core alterations and movement of irradiated fuel asemblies within CNMT.Event date and time.0 May 21, 1996, 0900 EDST: Discovery date and time.0 May 21, 1996, 0937 EDST: All remaining cables are removed from P-2, and P-2 is flanged off.B.EVENT: On May 21, 1996, all preparations for refueling were completed. |
| Aspartofthisprocedure, theoperatorperformed Step5.2.1toverifythatP-2was"adequately sealed",andsignedoffStep5.2.1ofprocedure 0-15.2.Satisfactory completion ofthisstepensurescompliance withITSLCO3.9.3.c.NRGFORM366AI4-95)
| | Procedure 0-15.2 had been signed off at approximately 0505 EDST, and the Control Room operators notified the Senior Reactor Operator assigned to Refueling (Refueling SRO)to begin refueling. |
| NRCFORM366A(4-95)LXCENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-006-00PAGE(3)TEXT(Ifmorespaceisrequired, useadditional copiesofNRCForm366A/(17)DESCRIPTION OFEVENT:A.DATESANDAPPROXIMATE TIMESOFMAJOROCCURRENCES:
| | The plant entered Mode 6 at approximately 0537 EDST and began refueling operations (core alterations and movement of irradiated fuel assemblies within CNMT).On May 21, 1996, at approximately 0800 EDST, contractor maintenance personnel continued their work from the previous day for removal of lines as per SM-10034-10.01. |
| 0May19,1996:Ginnastaffverifythattheconfiguration ofP-2meetstherequiredstatusofITSLCO3.9.3.c.May20,1996,1800EDST:Contractor maintenance personnel removepipespoolpieces frominsidethesealforP-2.P-2configuration doesnotmeettherequiredstatusofITSLCO3.9.3.c.0May21,1996,0537EDST:TheplantentersMode6andbeginscorealterations andmovementofirradiated fuelasemblies withinCNMT.Eventdateandtime.0May21,1996,0900EDST:Discovery dateandtime.0May21,1996,0937EDST:Allremaining cablesareremovedfromP-2,andP-2isflangedoff.B.EVENT:OnMay21,1996,allpreparations forrefueling werecompleted.
| | Since these lines were potentially contaminated, a Radiation Protection (RP)technician was requested to survey the removed lines prior to disposal.On May 21, 1996, at approximateiy 0900 EDST, with the plant in Mode 6 and refueling operations in progress, the RP technician approached P-2 to survey some materials and discovered that P-2 was not in the required status for refueling operations. |
| Procedure 0-15.2hadbeensignedoffatapproximately 0505EDST,andtheControlRoomoperators notifiedtheSeniorReactorOperatorassignedtoRefueling (Refueling SRO)tobeginrefueling. | | He observed that P-2 was not completely sealed where the 3" and 1 1/2" spoolpieces had been, appearing to allow direct access from the CNMT atmosphere to the outside atmosphere. |
| TheplantenteredMode6atapproximately 0537EDSTandbeganrefueling operations (corealterations andmovementofirradiated fuelassemblies withinCNMT).OnMay21,1996,atapproximately 0800EDST,contractor maintenance personnel continued theirworkfromthepreviousdayforremovaloflinesasperSM-10034-10.01.
| | NRC FORM 366A (4.95) |
| Sincetheselineswerepotentially contaminated, aRadiation Protection (RP)technician wasrequested tosurveytheremovedlinespriortodisposal.
| | NRC FORM 366A (4.95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE (3)4 OF 8 TEXT llf more space is required, use additional copies of NRC Form 386Ai (17)The RP technician notified his supervision. |
| OnMay21,1996,atapproximateiy 0900EDST,withtheplantinMode6andrefueling operations inprogress, theRPtechnician approached P-2tosurveysomematerials anddiscovered thatP-2wasnotintherequiredstatusforrefueling operations.
| | RP supervision notified a member of the plant Outage Management staff, who inspected P-2 and confirmed that it was not adequately sealed.The Control Room operators were notified of the status of P-2 as observed from outside CNMT.Immediate actions were taken per ITS LCO ACTIONs 3.9.3.A.1 and 3.9.3.A.2 to suspend core alterations and suspend movement of irradiated fuel assemblies within CNMT.The Refueling SRO inside CNMT was also notified that P-2 needed to be inspected from inside CNMT for the presence of a flange.The Refueling SRO inspected P-2 and confirmed that the penetration was not isolated inside CNMT by use of a material that can provide a temporary, atmospheric pressure, ventilation barrier.The RP technician verified that the actual flow of air was from the outside into CNMT.Ginna and contractor electricians were notified to remove all remaining cables routed through P-2.When the cables were removed and the penetration was unobstructed inside CNMT, Ginna pipefitters installed a flange over P-2.These actions restored P-2 to the required status for refueling operations, and refueling operations were permitted to resume at approximately 0937 EDST on May 21, 1996.C.INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: None E.METHOD OF DISCOVERY: |
| HeobservedthatP-2wasnotcompletely sealedwherethe3"and11/2"spoolpieces hadbeen,appearing toallowdirectaccessfromtheCNMTatmosphere totheoutsideatmosphere.
| | While performing routine monitoring activities for the removal of potentially contaminated materials from CNMT, a Radiation Protection technician discovered that P-2 was not completely sealed as observed from outside CNMT.The Refueling SRO confirmed that P-2 was not in the required status for refueling operations. |
| NRCFORM366A(4.95)
| | F.OPERATOR ACTION: The Control Room operators, upon being notified that P-2 was not in the required status for refueling operations, immediately complied with the requirements of ITS LCO ACTIONs 3.9.3.A.1. |
| NRCFORM366A(4.95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-006-00PAGE(3)4OF8TEXTllfmorespaceisrequired, useadditional copiesofNRCForm386Ai(17)TheRPtechnician notifiedhissupervision.
| | and 3.9.3.A.2, which require that if one or more CNMT penetrations are not in required status,"Suspend CORE ALTERATIONS" and"Suspend movement of irradiated fuel assemblies within containment". |
| RPsupervision notifiedamemberoftheplantOutageManagement staff,whoinspected P-2andconfirmed thatitwasnotadequately sealed.TheControlRoomoperators werenotifiedofthestatusofP-2asobservedfromoutsideCNMT.Immediate actionsweretakenperITSLCOACTIONs3.9.3.A.1 and3.9.3.A.2 tosuspendcorealterations andsuspendmovementofirradiated fuelassemblies withinCNMT.TheRefueling SROinsideCNMTwasalsonotifiedthatP-2neededtobeinspected frominsideCNMTforthepresenceofaflange.TheRefueling SROinspected P-2andconfirmed thatthepenetration wasnotisolatedinsideCNMTbyuseofamaterialthatcanprovideatemporary, atmospheric
| | Subsequently, the Control Room operators notified higher supervision and the NRC Senior Resident Inspector. |
| : pressure, ventilation barrier.TheRPtechnician verifiedthattheactualflowofairwasfromtheoutsideintoCNMT.Ginnaandcontractor electricians werenotifiedtoremoveallremaining cablesroutedthroughP-2.Whenthecableswereremovedandthepenetration wasunobstructed insideCNMT,Ginnapipefitters installed aflangeoverP-2.TheseactionsrestoredP-2totherequiredstatusforrefueling operations, andrefueling operations werepermitted toresumeatapproximately 0937EDSTonMay21,1996.C.INOPERABLE STRUCTURES, COMPONENTS, ORSYSTEMSTHATCONTRIBUTED TOTHEEVENT:NoneD.OTHERSYSTEMSORSECONDARY FUNCTIONS AFFECTED:
| | At approximately 1226 EDST on May 21, 1996, a 4 hour non-emergency notification was made to the NRC Operations Center as per 10 CFR 50.72 (b)(2)(iii)(C)and 10 CFR 50.72 (b)(2)(iii)(D).NRC FORM 366A (4-95) |
| NoneE.METHODOFDISCOVERY:
| | NRC FORM 366A (4 95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE (3)TEXT llf more space is required, uso additional copies of NRC Form 366Al (17)G.SAFETY SYSTEM RESPONSES: |
| Whileperforming routinemonitoring activities fortheremovalofpotentially contaminated materials fromCNMT,aRadiation Protection technician discovered thatP-2wasnotcompletely sealedasobservedfromoutsideCNMT.TheRefueling SROconfirmed thatP-2wasnotintherequiredstatusforrefueling operations.
| | None III.CAUSE OF EVENT: A.IMMEDIATE CAUSE: The immediate cause of CNMT penetration P-2 not being in the required status for refueling operations was openings in the foam seal where a 3" pipe and 1 1/2" pipe had been removed.This condition was not identified by Operations personnel during performance of procedure 0-15.2.B.INTERMEDIATE CAUSE: The intermediate cause of the openings in the foam seal for P-2 was the unauthorized removal of the pipe spoolpieces and associated valves from the penetration. |
| F.OPERATORACTION:TheControlRoomoperators, uponbeingnotifiedthatP-2wasnotintherequiredstatusforrefueling operations, immediately compliedwiththerequirements ofITSLCOACTIONs3.9.3.A.1. | | The intermediate cause of not identifying this condition during the performance of 0-15.2 was inadequate verification by Operations personnel. |
| and3.9.3.A.2, whichrequirethatifoneormoreCNMTpenetrations arenotinrequiredstatus,"SuspendCOREALTERATIONS" and"Suspendmovementofirradiated fuelassemblies withincontainment".
| | ROOT CAUSE: The underlying cause of the unauthorized removal of the spoolpieces was personnel error.The underlying cause of the inadequate verification by Operations personnel was also personnel error.A Human Performance Enhancement System (HPES)evaluation was performed to determine the causal factors that contributed to these personnel errors.This event is NUREG-1022 Cause Code (A),"Personnel Error".Personnel errors were made by contractor maintenance personnel and a utility non-licensed operator.These errors were cognitive personnel errors on the part of both groups.The contractor maintenance personnel did not recognize the impact on refueling operations of removing the pipe spoolpieces from P-2.The Operations personnel did not recognize the actual configuration of the foam seal in P-2 during 0-15.2 verifications, perceived that they had accurately verified the configuration, and thought that P-2 was in the required status for refueling operations, when, in fact, P-2 was not adequately sealed.NRC FORM 366A (4-95) |
| Subsequently, theControlRoomoperators notifiedhighersupervision andtheNRCSeniorResidentInspector. | | NRC FORM 366A (4-SS)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE (3)6 OF 8 TEXT iif more space is required, use additional copies of NRC Form 366AJ (17).The contractor maintenance error was contrary to approved procedure SM-10034-10.01, and the operator error was contrary to approved procedure 0-15.2.Unusual conditions present during the performance of 0-15.2 included nighttime darkness, a lightning storm, limited access to P-2 (P-2 was enclosed by a wooden protective enclosure), additional cable routed through P-2 for the 1996 outage, and some of the remaining piping and valves still being within the enclosure around P-2.These environmental factors may have obscured the view of the foam seal from outside CNMT, where the 3" and 1 1/2" spoolpieces had been.Access to view P-2 from inside CNMT was partially blocked, due to equipment inside CNMT for the S/G replacement. |
| Atapproximately 1226EDSTonMay21,1996,a4hournon-emergency notification wasmadetotheNRCOperations Centerasper10CFR50.72(b)(2)(iii)(C)and10CFR50.72(b)(2)(iii)(D).NRCFORM366A(4-95)
| | This condition does not meet the NUMARC 93-01,"Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", definition of a"Maintenance Preventable Functional Failure".IV.ANALYSIS OF EVENT: This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, items (a)(2)(ii), (a)(2)(v)(C)and (a)(2)(v)(D), which require a report of,"Any operation or condition prohibited by the plant's Technical Specifications" or"Any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to...Control the release of radioactive material;or Mitigate the consequences of an accident". |
| NRCFORM366A(495)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-006-00PAGE(3)TEXTllfmorespaceisrequired, usoadditional copiesofNRCForm366Al(17)G.SAFETYSYSTEMRESPONSES:
| | Having a CNMT penetration not in the required status for refueling operations with refueling operations in progress is a condition prohibited by the ITS.It is postulated that, in the event of a fuel handling accident at this condition, the resultant radioactive release could be uncontrolled, and that the CNMT could have been ineffective in mitigating the consequences of this postulated accident.i An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions: |
| NoneIII.CAUSEOFEVENT:A.IMMEDIATE CAUSE:Theimmediate causeofCNMTpenetration P-2notbeingintherequiredstatusforrefueling operations wasopeningsinthefoamsealwherea3"pipeand11/2"pipehadbeenremoved.Thiscondition wasnotidentified byOperations personnel duringperformance ofprocedure 0-15.2.B.INTERMEDIATE CAUSE:Theintermediate causeoftheopeningsinthefoamsealforP-2wastheunauthorized removalofthepipespoolpieces andassociated valvesfromthepenetration.
| | There were no operational or safety consequences or implications attributed to this condition because: 0 Though the CNMT penetration allowed direct access from the CNMT atmosphere to the outside atmosphere, a condition did not exist that could have resulted in an uncontrolled radioactive release.A release to the outside atmosphere would have required CNMT pressurization. |
| Theintermediate causeofnotidentifying thiscondition duringtheperformance of0-15.2wasinadequate verification byOperations personnel.
| | Since the fuel had a low decay heat rate due to a sixty day off load and since there was only a small amount of fuel in the core at the time, the energy source to effect a CNMT pressurization was low, making a pressurized conditions unlikely.It was verified that the actual flow of air was from the outside into CNMT.0 CNMT isolation is not credited in the event of a fuel handling accident per the applicable safety analyses bases for ITS LCO 3.9.3.The Ginna Station Updated Final Safety Analysis Report (UFSAR), Section 15.7.3.3, shows that without credit for CNMT and utilizing the conservative assumptions of NRC Regulatory Guide (RG)1.25, the offsite dose consequences following a fuel handling accident are ninety-six (96)REM thyroid, which is within 10 CFR 100 limits for Ginna Station.NRC FORM 366A (4.65) |
| ROOTCAUSE:Theunderlying causeoftheunauthorized removalofthespoolpieces waspersonnel error.Theunderlying causeoftheinadequate verification byOperations personnel wasalsopersonnel error.AHumanPerformance Enhancement System(HPES)evaluation wasperformed todetermine thecausalfactorsthatcontributed tothesepersonnel errors.ThiseventisNUREG-1022 CauseCode(A),"Personnel Error".Personnel errorsweremadebycontractor maintenance personnel andautilitynon-licensed operator.
| | NRC FORM 366A (4-95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME I1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER I6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE I3)7 OF 8 TEXT (lf more speceis required, use eddi tionel copies of NRC Form 366Al (17)0 Ginna Station recently received Amendment 62 to the ITS, which modified the requirements for the CNMT equipment hatch during Mode 6.Included within this ITS amendment request (dated February 9, 1996)was an evaluation of offsite doses, with the following assumptions: |
| Theseerrorswerecognitive personnel errorsonthepartofbothgroups.Thecontractor maintenance personnel didnotrecognize theimpactonrefueling operations ofremovingthepipespoolpieces fromP-2.TheOperations personnel didnotrecognize theactualconfiguration ofthefoamsealinP-2during0-15.2verifications, perceived thattheyhadaccurately verifiedtheconfiguration, andthoughtthatP-2wasintherequiredstatusforrefueling operations, when,infact,P-2wasnotadequately sealed.NRCFORM366A(4-95)
| | b.CNMT was initially pressurized by 0.5 PSIG above the outside atmosphere for the first three minutes following a fuel handling accident, a CNMT leakage rate, based on extreme temperature differences between the inside and the outside of CNMT, existed for the next two hours, and a hole equivalent to 1.83 square feet existed to the outside atmosphere. |
| NRCFORM366A(4-SS)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)SEQUENTIAL REVISIONNUMBERNUMBER96-006-00PAGE(3)6OF8TEXTiifmorespaceisrequired, useadditional copiesofNRCForm366AJ(17).Thecontractor maintenance errorwascontrarytoapprovedprocedure SM-10034-10.01, andtheoperatorerrorwascontrarytoapprovedprocedure 0-15.2.Unusualconditions presentduringtheperformance of0-15.2includednighttime
| | Using these and other assumptions of RG 1.25, the thyroid dose at the exclusion area boundary was calculated to be only 8.1 REM, which is well within 10 CFR 100 limits.The condition of P-2 being open during movement of irradiated fuel assemblies is bounded by this analysis since no fuel handling accident occurred, the CNMT was not pressurized, and the increased leakage path through P-2 was less than 0:1 square foot.Therefore, this condition would not lead to exceeding the dose limits.Based on the above, it can be concluded that the public's health and safety was assured at all times.V.CORRECTIVE ACTION: A.ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: 0 All remaining cables were removed from P-2 and a flange was installed on P-2 inside CNMT, restoring P-2 to compliance with ITS LCO 3.9.3.c.0 Refueling operations were permitted to resume.B.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE: |
| : darkness, alightning storm,limitedaccesstoP-2(P-2wasenclosedbyawoodenprotective enclosure),
| | 0 Procedure 0-15.2 will be revised to require additional controls at P-2, to prevent the configuration of P-2 from being changed during refueling operations. |
| additional cableroutedthroughP-2forthe1996outage,andsomeoftheremaining pipingandvalvesstillbeingwithintheenclosure aroundP-2.Theseenvironmental factorsmayhaveobscuredtheviewofthefoamsealfromoutsideCNMT,wherethe3"and11/2"spoolpieces hadbeen.AccesstoviewP-2frominsideCNMTwaspartially blocked,duetoequipment insideCNMTfortheS/Greplacement. | | 0 A Nuclear Training Work Request will be initiated to train on the lessons learned from this event.VI.ADDITIONAL INFORMATION: |
| Thiscondition doesnotmeettheNUMARC93-01,"Industry Guideline forMonitoring theEffectiveness ofMaintenance atNuclearPowerPlants",definition ofa"Maintenance Preventable Functional Failure".
| | A.FAILED COMPONENTS: |
| IV.ANALYSISOFEVENT:Thiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,items(a)(2)(ii),(a)(2)(v)(C)and(a)(2)(v)(D),whichrequireareportof,"Anyoperation orcondition prohibited bytheplant'sTechnical Specifications" or"Anyeventorcondition thatalonecouldhaveprevented thefulfillment ofthesafetyfunctionofstructures orsystemsthatareneededto...Control thereleaseofradioactive material; orMitigatetheconsequences ofanaccident". | | None IIRC FORM 366A I4.95) |
| HavingaCNMTpenetration notintherequiredstatusforrefueling operations withrefueling operations inprogressisacondition prohibited bytheITS.Itispostulated that,intheeventofafuelhandlingaccidentatthiscondition, theresultant radioactive releasecouldbeuncontrolled, andthattheCNMTcouldhavebeenineffective inmitigating theconsequences ofthispostulated accident.
| | NRC FORM 366A I4-95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME I1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE I3)8 OF 8 TEXT (If more spaceis required, use additional copies of NRC Form 366AJ I17)B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified. |
| iAnassessment wasperformed considering boththesafetyconsequences andimplications ofthiseventwiththefollowing resultsandconclusions:
| | C.SPECIAL COMMENTS: None NAC FOAM 366A I4.95)}} |
| Therewerenooperational orsafetyconsequences orimplications attributed tothiscondition because:0ThoughtheCNMTpenetration alloweddirectaccessfromtheCNMTatmosphere totheoutsideatmosphere, acondition didnotexistthatcouldhaveresultedinanuncontrolled radioactive release.Areleasetotheoutsideatmosphere wouldhaverequiredCNMTpressurization.
| |
| Sincethefuelhadalowdecayheatrateduetoasixtydayoffloadandsincetherewasonlyasmallamountoffuelinthecoreatthetime,theenergysourcetoeffectaCNMTpressurization waslow,makingapressurized conditions unlikely.
| |
| ItwasverifiedthattheactualflowofairwasfromtheoutsideintoCNMT.0CNMTisolation isnotcreditedintheeventofafuelhandlingaccidentpertheapplicable safetyanalysesbasesforITSLCO3.9.3.TheGinnaStationUpdatedFinalSafetyAnalysisReport(UFSAR),Section15.7.3.3, showsthatwithoutcreditforCNMTandutilizing theconservative assumptions ofNRCRegulatory Guide(RG)1.25,theoffsitedoseconsequences following afuelhandlingaccidentareninety-six (96)REMthyroid,whichiswithin10CFR100limitsforGinnaStation.NRCFORM366A(4.65)
| |
| NRCFORM366A(4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-006-00PAGEI3)7OF8TEXT(lfmorespeceisrequired, useedditionelcopiesofNRCForm366Al(17)0GinnaStationrecentlyreceivedAmendment 62totheITS,whichmodifiedtherequirements fortheCNMTequipment hatchduringMode6.IncludedwithinthisITSamendment request(datedFebruary9,1996)wasanevaluation ofoffsitedoses,withthefollowing assumptions:
| |
| b.CNMTwasinitially pressurized by0.5PSIGabovetheoutsideatmosphere forthefirstthreeminutesfollowing afuelhandlingaccident, aCNMTleakagerate,basedonextremetemperature differences betweentheinsideandtheoutsideofCNMT,existedforthenexttwohours,andaholeequivalent to1.83squarefeetexistedtotheoutsideatmosphere. | |
| Usingtheseandotherassumptions ofRG1.25,thethyroiddoseattheexclusion areaboundarywascalculated tobeonly8.1REM,whichiswellwithin10CFR100limits.Thecondition ofP-2beingopenduringmovementofirradiated fuelassemblies isboundedbythisanalysissincenofuelhandlingaccidentoccurred, theCNMTwasnotpressurized, andtheincreased leakagepaththroughP-2waslessthan0:1squarefoot.Therefore, thiscondition wouldnotleadtoexceeding thedoselimits.Basedontheabove,itcanbeconcluded thatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVE ACTION:A.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:0Allremaining cableswereremovedfromP-2andaflangewasinstalled onP-2insideCNMT,restoring P-2tocompliance withITSLCO3.9.3.c.0Refueling operations werepermitted toresume.B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:
| |
| 0Procedure 0-15.2willberevisedtorequireadditional controlsatP-2,topreventtheconfiguration ofP-2frombeingchangedduringrefueling operations.
| |
| 0ANuclearTrainingWorkRequestwillbeinitiated totrainonthelessonslearnedfromthisevent.VI.ADDITIONAL INFORMATION:
| |
| A.FAILEDCOMPONENTS: | |
| NoneIIRCFORM366AI4.95)
| |
| NRCFORM366AI4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)YEARSEQUENTIAL REVISIONNUMBERNUMBER96-006-00PAGEI3)8OF8TEXT(Ifmorespaceisrequired, useadditional copiesofNRCForm366AJI17)B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:Nodocumentation ofsimilarLEReventswiththesamerootcauseatGinnaNuclearPowerPlantcouldbeidentified.
| |
| C.SPECIALCOMMENTS: | |
| NoneNACFOAM366AI4.95)}}
| |
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Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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CATEGORY 1 REGULATO Y INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESS1'ON NBR:9606260154 DOC.DATE: 96/06/20 NOTARIZED:
NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester AUTH.NAME AUTHOR AFFILIATION ST.MARTIN,J.T.
Rochester Gas&Electric Corp.MECREDY,R.C.
Rochester Gas&Electric Corp.RECIP.NAME RECIPIENT'AFFILIATION DOCKET G 05000244
SUBJECT:
LER 96-006-00:on 960521,discovered containment penetration not in required status.Caused by personnel error.Installed flange inside containment penetration 2.W/960620 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
A'5000244 (I RECIPIENT ID CODE/NAME PDl-1 PD INTERNAL: AEOD/SPD/RAB gF'ZEE CENE E NRR/DE/EEL'B NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN1 FILE 01 EXTERNAL: L ST LOBBY WARD NOAC MURPHYFG~A NRC PDR COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME VISSINGFG.
AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DSIR/EIB LITCO BRYCEFJ H NOAC POOREFW.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 D.N NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK/ROOM OWFN 5D-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25 AND ROCHESTER GAS AND ElECTRIC CORI@RATION
~89 EAST AVENUE, ROCHESTER, N.Y.IrI64'rr DDT AREA CODE 716 5'-27tXt ROBERT C.MECREDY Vice President Nucte or Operations June 20, 1996 U.S.Nuclear Regulatory Commission Document Control Desk Attn: Guy S.Vissing Project Directorate I-1 Washington, D.C.20555
Subject:
LER 96-006, Containment Penetration Not in Required Status, Due to Personnel Errors, Results in Potential for Uncontrolled Release of Radioactive Material R.E.Ginna Nuclear Power Plant Docket No.50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, items (a)(2)(ii), (a)(2)(v)(C)and (a)(2)(v)(D), which require a report of,"Any operation or condition prohibited by the plant's Technical Specifications" or"Any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to...Control the release of radioactive material;or Mitigate the consequences of an accident", the attached Licensee Event Report LER 96-006 is hereby submitted.
This event has in no way affected the public's health and safety.Very ly yours, Robert C.Mecredy xc: U.S.Nuclear Regulatory Commission Mr.Guy S.Vissing (Mail Stop 14C7)PWR Project Directorate I-1 Washington, D.C.,20555 U.S.Nuclear Regulatory Commission Region I 475 Allendale-Road King of Prussia, PA 19406 U.S.NRC Ginna Senior Resident Inspector 9606260i54 960620 PDR ADQCK 05000244 8 PDR y/~JP NRC FORM 366 (4.95)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)APPROVED BY OMB NO.3150-0104 EXPIRES 04/30/BB ESTIMATED BURDEN PER AESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.REPOATED LESSONS LEARNED ARE INCORPORATED INTO THE UCENSING PROCESS AND FED BACK To INDUSTRY.FORWARD COMMENTS REGARDING BURDEN ESTIMATE To THE INFORMATION AND RECORDS MANAGEMENT BRANCH IT-6 F33), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555.0001, AND To THE PAPEAWORK REDUCTION PROJECT FACILITY kAME (1)R.E.Ginna Nuclear Power Plant OOCKET NUMBER (2)05000244 PAGE (3)1OF8 B (4)A Containment Penetration Not in Required Status, Due to Personnel Errors, Results'in Potential for Uncontrolled Release of Radioactive Material MONTH DAY YEAR 05 21 96 EVENT DATE (5)LER NUMBER (6)SEQUENTIAL REVISION NUMBER., NUMBER 96-006-00 MONTH DAY YEAR 06 20 96 REPORT DATE (7)FACILITY NAME FACILITY NAME OTHER FACILITIES INVOLVED (6)OOCKET NUMBER OOCKET NUMBER OPERATING MODE (9)POWER LEVEL (10)kAME 000 THIS REPORT IS SUBMITTED PUR more)(11)50.73(a)(2)(viii]50.73(a)(2)(x)50.73(a)(2)(i)50.73(a)(2)(ii)20.2203(a)(2)(v) 20.2203(a)(3)(i) 20.2201(b) 20.2203ta) tl)73.71 50.73(a)(2)(iii)50.73(a)(2)(iv)20.2203(a)
(3)(ii)20.2203(a)
(4)20.2203(a)
(2)(i)20.2203(a)(2)(ii)
OTHER Specify in Abstract below or in NRC Form 366A 20.2203(a)(2)(iii)50.36(c)(1) 50.73(a)(2)(v)20.2203(a)
(2)(iv)50.36(c)(2)50.73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)ELBPIIOkE NUMBER (Include Area Coda>SUANT TO THE REQUIREMENTS OF 10 CFR E: (Check one or John T.St.Martin-Technical Assistant (716)771-3641 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFACTURER AEPOATABLE TO NPADS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE To NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (lf yes, complete EXPECTED SUBMISSION DATE).X NO EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, l.e., approximately 15 single-spaced typewritten lines)(16)On May 21, 1996, at approximately 0900 EDST, with the plant in Mode 6 with core alterations and movement of irradiated fuel assemblies within containment in progress, it was discovered that a containment penetration was not in the required status for refueling operations, allowing direct access from the containment atmosphere to the outside atmosphere.
Immediate corrective action was taken in accordance with Ginna Improved Technical Specifications Limiting Conditions for Operation 3.9.3.A.1 and 3.9.3.A.2 to suspend core alterations and suspend movement of irradiated fuel assemblies within containment.
The containment penetration was restored to the required status for refueling operations, and refueling operations were permitted to resume.The underlying cause of the penetration not being in the required status for refueling operations was personnel errors.This event is NUREG-1022 Cause Code (A).Corrective action to prevent recurrence is outlined in Section V.B.NRC FORM 366 (4-95)
NRC FORM 366A I4-95)LICENSEE EVENT REPORT (LER), TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME Il)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER I6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE I3)2 OF 8 TEXT (If more spaceis required, use additional copies of NRC Form 366A/(17)PRE-EVENT PLANT CONDITIONS:
Containment (CNMT)penetration I)'2 (referred to as P-2)is the"S/G Communications Flange Penetration" normally used for support of routine steam generator (S/G)maintenance and inspection activities during refueling outages.When in Modes 5 or 6, normally routed through P-2 are closed-circuit television (CCTV)cables and other communications cables.For the 1996 Refueling outage, P-2 was also used to provide a route for additional CCTV cables and rigid pipes from'the outside into CNMT, to provide services (communications, air and argon)for activities associated with replacement of the S/Gs.These pipes were a 3" line for service air and a 1 1/2" line for argon.Station Modification procedures SM-10034-10.01 (Temporary Service Air System for SGRP)and SM-10034-'l0.03 (Installation 5 Removal of Temporary CCTV and Communications) were used to control the temporary installation and subsequent removal of these services.On May 19, 1996, in preparation for refueling the reactor, Ginna plant staff checked the configuration of P-2 and verified that the configuration complied with Ginna Improved Technical Specifications (ITS)Limiting Condition for Operation (LCO)3.9.3.c, which states that each penetration providing direct access from the CNMT atmosphere to the outside atmosphere shall be isolated, or closed by an equivalent isolation method.These methods include use of material that can provide a temporary, atmospheric pressure, ventilation barrier.Contractor supervision were subsequently notified not to disturb the configuration of P-2 until after the completion of refueling.
During the dayshift on May 20, 1996, as directed by contractor supervision, contractor maintenance personnel removed much of the temporary service air and argon lines inside CNMT, as directed by procedure SM-10034-10.01.
Contractor supervision had been cautioned by Ginna staff not to remove the 3" and 1 1/2" pipe spoolpieces that were inside the seal for P-2 and the first valves on each side of P-2 inside and outside of CNMT.Nevertheless, at the end of their shift (at approximately 1800 EDST), the contractor maintenance personnel removed these spoolpieces and valves.Additional piping outside CNMT was left in place until the next day.On May 21, 1996, at approximately 0300 EDST, a utility non-licensed operator was performing Operating Procedure 0-15.2 (Valve Alignment for Reactor Head Lift, Core Component Movement, and Periodic Status Checks), in preparation for the start of refueling operations.
As part of this procedure, the operator performed Step 5.2.1 to verify that P-2 was"adequately sealed", and signed off Step 5.2.1 of procedure 0-15.2.Satisfactory completion of this step ensures compliance with ITS LCO 3.9.3.c.NRG FORM 366A I4-95)
NRC FORM 366A (4-95)LXCENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE (3)TEXT (If more spaceis required, use additional copies of NRC Form 366A/(17)DESCRIPTION OF EVENT: A.DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
0 May 19, 1996: Ginna staff verify that the configuration of P-2 meets the required status of ITS LCO 3.9.3.c.May 20, 1996, 1800 EDST: Contractor maintenance personnel remove pipe spoolpieces from inside the seal for P-2.P-2 configuration does not meet the required status of ITS LCO 3.9.3.c.0 May 21, 1996, 0537 EDST: The plant enters Mode 6 and begins core alterations and movement of irradiated fuel asemblies within CNMT.Event date and time.0 May 21, 1996, 0900 EDST: Discovery date and time.0 May 21, 1996, 0937 EDST: All remaining cables are removed from P-2, and P-2 is flanged off.B.EVENT: On May 21, 1996, all preparations for refueling were completed.
Procedure 0-15.2 had been signed off at approximately 0505 EDST, and the Control Room operators notified the Senior Reactor Operator assigned to Refueling (Refueling SRO)to begin refueling.
The plant entered Mode 6 at approximately 0537 EDST and began refueling operations (core alterations and movement of irradiated fuel assemblies within CNMT).On May 21, 1996, at approximately 0800 EDST, contractor maintenance personnel continued their work from the previous day for removal of lines as per SM-10034-10.01.
Since these lines were potentially contaminated, a Radiation Protection (RP)technician was requested to survey the removed lines prior to disposal.On May 21, 1996, at approximateiy 0900 EDST, with the plant in Mode 6 and refueling operations in progress, the RP technician approached P-2 tosurvey some materials and discovered that P-2 was not in the required status for refueling operations.
He observed that P-2 was not completely sealed where the 3" and 1 1/2" spoolpieces had been, appearing to allow direct access from the CNMT atmosphere to the outside atmosphere.
NRC FORM 366A (4.95)
NRC FORM 366A (4.95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE (3)4 OF 8 TEXT llf more space is required, use additional copies of NRC Form 386Ai (17)The RP technician notified his supervision.
RP supervision notified a member of the plant Outage Management staff, who inspected P-2 and confirmed that it was not adequately sealed.The Control Room operators were notified of the status of P-2 as observed from outside CNMT.Immediate actions were taken per ITS LCO ACTIONs 3.9.3.A.1 and 3.9.3.A.2 to suspend core alterations and suspend movement of irradiated fuel assemblies within CNMT.The Refueling SRO inside CNMT was also notified that P-2 needed to be inspected from inside CNMT for the presence of a flange.The Refueling SRO inspected P-2 and confirmed that the penetration was not isolated inside CNMT by use of a material that can provide a temporary, atmospheric pressure, ventilation barrier.The RP technician verified that the actual flow of air was from the outside into CNMT.Ginna and contractor electricians were notified to remove all remaining cables routed through P-2.When the cables were removed and the penetration was unobstructed inside CNMT, Ginna pipefitters installed a flange over P-2.These actions restored P-2 to the required status for refueling operations, and refueling operations were permitted to resume at approximately 0937 EDST on May 21, 1996.C.INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None D.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED: None E.METHOD OF DISCOVERY:
While performing routine monitoring activities for the removal of potentially contaminated materials from CNMT, a Radiation Protection technician discovered that P-2 was not completely sealed as observed from outside CNMT.The Refueling SRO confirmed that P-2 was not in the required status for refueling operations.
F.OPERATOR ACTION: The Control Room operators, upon being notified that P-2 was not in the required status for refueling operations, immediately complied with the requirements of ITS LCO ACTIONs 3.9.3.A.1.
and 3.9.3.A.2, which require that if one or more CNMT penetrations are not in required status,"Suspend CORE ALTERATIONS" and"Suspend movement of irradiated fuel assemblies within containment".
Subsequently, the Control Room operators notified higher supervision and the NRC Senior Resident Inspector.
At approximately 1226 EDST on May 21, 1996, a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> non-emergency notification was made to the NRC Operations Center as per 10 CFR 50.72 (b)(2)(iii)(C)and 10 CFR 50.72 (b)(2)(iii)(D).NRC FORM 366A (4-95)
NRC FORM 366A (4 95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE (3)TEXT llf more space is required, uso additional copies of NRC Form 366Al (17)G.SAFETY SYSTEM RESPONSES:
None III.CAUSE OF EVENT: A.IMMEDIATE CAUSE: The immediate cause of CNMT penetration P-2 not being in the required status for refueling operations was openings in the foam seal where a 3" pipe and 1 1/2" pipe had been removed.This condition was not identified by Operations personnel during performance of procedure 0-15.2.B.INTERMEDIATE CAUSE: The intermediate cause of the openings in the foam seal for P-2 was the unauthorized removal of the pipe spoolpieces and associated valves from the penetration.
The intermediate cause of not identifying this condition during the performance of 0-15.2 was inadequate verification by Operations personnel.
ROOT CAUSE: The underlying cause of the unauthorized removal of the spoolpieces was personnel error.The underlying cause of the inadequate verification by Operations personnel was also personnel error.A Human Performance Enhancement System (HPES)evaluation was performed to determine the causal factors that contributed to these personnel errors.This event is NUREG-1022 Cause Code (A),"Personnel Error".Personnel errors were made by contractor maintenance personnel and a utility non-licensed operator.These errors were cognitive personnel errors on the part of both groups.The contractor maintenance personnel did not recognize the impact on refueling operations of removing the pipe spoolpieces from P-2.The Operations personnel did not recognize the actual configuration of the foam seal in P-2 during 0-15.2 verifications, perceived that they had accurately verified the configuration, and thought that P-2 was in the required status for refueling operations, when, in fact, P-2 was not adequately sealed.NRC FORM 366A (4-95)
NRC FORM 366A (4-SS)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE (3)6 OF 8 TEXT iif more space is required, use additional copies of NRC Form 366AJ (17).The contractor maintenance error was contrary to approved procedure SM-10034-10.01, and the operator error was contrary to approved procedure 0-15.2.Unusual conditions present during the performance of 0-15.2 included nighttime darkness, a lightning storm, limited access to P-2 (P-2 was enclosed by a wooden protective enclosure), additional cable routed through P-2 for the 1996 outage, and some of the remaining piping and valves still being within the enclosure around P-2.These environmental factors may have obscured the view of the foam seal from outside CNMT, where the 3" and 1 1/2" spoolpieces had been.Access to view P-2 from inside CNMT was partially blocked, due to equipment inside CNMT for the S/G replacement.
This condition does not meet the NUMARC 93-01,"Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", definition of a"Maintenance Preventable Functional Failure".IV.ANALYSIS OF EVENT: This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, items (a)(2)(ii), (a)(2)(v)(C)and (a)(2)(v)(D), which require a report of,"Any operation or condition prohibited by the plant's Technical Specifications" or"Any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to...Control the release of radioactive material;or Mitigate the consequences of an accident".
Having a CNMT penetration not in the required status for refueling operations with refueling operations in progress is a condition prohibited by the ITS.It is postulated that, in the event of a fuel handling accident at this condition, the resultant radioactive release could be uncontrolled, and that the CNMT could have been ineffective in mitigating the consequences of this postulated accident.i An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences or implications attributed to this condition because: 0 Though the CNMT penetration allowed direct access from the CNMT atmosphere to the outside atmosphere, a condition did not exist that could have resulted in an uncontrolled radioactive release.A release to the outside atmosphere would have required CNMT pressurization.
Since the fuel had a low decay heat rate due to a sixty day off load and since there was only a small amount of fuel in the core at the time, the energy source to effect a CNMT pressurization was low, making a pressurized conditions unlikely.It was verified that the actual flow of air was from the outside into CNMT.0 CNMT isolation is not credited in the event of a fuel handling accident per the applicable safety analyses bases for ITS LCO 3.9.3.The Ginna Station Updated Final Safety Analysis Report (UFSAR), Section 15.7.3.3, shows that without credit for CNMT and utilizing the conservative assumptions of NRC Regulatory Guide (RG)1.25, the offsite dose consequences following a fuel handling accident are ninety-six (96)REM thyroid, which is within 10 CFR 100 limits for Ginna Station.NRC FORM 366A (4.65)
NRC FORM 366A (4-95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME I1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER I6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE I3)7 OF 8 TEXT (lf more speceis required, use eddi tionel copies of NRC Form 366Al (17)0 Ginna Station recently received Amendment 62 to the ITS, which modified the requirements for the CNMT equipment hatch during Mode 6.Included within this ITS amendment request (dated February 9, 1996)was an evaluation of offsite doses, with the following assumptions:
b.CNMT was initially pressurized by 0.5 PSIG above the outside atmosphere for the first three minutes following a fuel handling accident, a CNMT leakage rate, based on extreme temperature differences between the inside and the outside of CNMT, existed for the next two hours, and a hole equivalent to 1.83 square feet existed to the outside atmosphere.
Using these and other assumptions of RG 1.25, the thyroid dose at the exclusion area boundary was calculated to be only 8.1 REM, which is well within 10 CFR 100 limits.The condition of P-2 being open during movement of irradiated fuel assemblies is bounded by this analysis since no fuel handling accident occurred, the CNMT was not pressurized, and the increased leakage path through P-2 was less than 0:1 square foot.Therefore, this condition would not lead to exceeding the dose limits.Based on the above, it can be concluded that the public's health and safety was assured at all times.V.CORRECTIVE ACTION: A.ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: 0 All remaining cables were removed from P-2 and a flange was installed on P-2 inside CNMT, restoring P-2 to compliance with ITS LCO 3.9.3.c.0 Refueling operations were permitted to resume.B.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
0 Procedure 0-15.2 will be revised to require additional controls at P-2, to prevent the configuration of P-2 from being changed during refueling operations.
0 A Nuclear Training Work Request will be initiated to train on the lessons learned from this event.VI.ADDITIONAL INFORMATION:
A.FAILED COMPONENTS:
None IIRC FORM 366A I4.95)
NRC FORM 366A I4-95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME I1)R.E.Ginna Nuclear Power Plant DOCKET 05000244 LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER 96-006-00 PAGE I3)8 OF 8 TEXT (If more spaceis required, use additional copies of NRC Form 366AJ I17)B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified.
C.SPECIAL COMMENTS: None NAC FOAM 366A I4.95)