ML17325B574: Difference between revisions

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{{#Wiki_filter:~CATEGORY+REGULATORY INFORMATION DISTRIBUTION SYSTEM(RZDS)ACCESSION NBR:9905050103 DOC.DATE:
{{#Wiki_filter:~CATEGORY+REGULATORY INFORMATION DISTRIBUTION SYSTEM (RZDS)ACCESSION NBR:9905050103 DOC.DATE: 99/05/03 NOTARIZED:
99/05/03NOTARIZED:
NO DOCKET I FACIL:50-315 Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 AUXHTNAME AUTHOR AFFILIATION RENCHECK,M.W.
NODOCKETIFACIL:50-315 DonaldC.CookNuclearPowerPlant,Unit1,IndianaM05000315AUXHTNAME AUTHORAFFILIATION RENCHECK,M.W.
Indiana Michigan Power Co.(formerly Indiana&, Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Records Management Branch (Document Control Desk)
IndianaMichiganPowerCo.(formerly Indiana&,MichiganEleRECIP.NAME RECIPIENT AFFILIATION RecordsManagement Branch(Document ControlDesk)


==SUBJECT:==
==SUBJECT:==
ForwardsLER99-010-00 reRCSleakdetection syssensitivity notinaccoradnce withdesignrequirements.
Forwards LER 99-010-00 re RCS leak detection sys sensitivity not in accoradnce with design requirements.
ListedCcommitments identified insubmittal.
Listed C commitments identified in submittal.
ADZSTRZBUTZON CODE:ZE22TCOPTERRECEZVED:LTR 1ENCLJSZEE:ITITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:ERECIPIENT IDCODE/NAME LPD3-1PDINTERNAL:
A DZSTRZBUTZON CODE: ZE22T COPTER RECEZVED:LTR 1 ENCL J SZEE: I TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: E RECIPIENT ID CODE/NAME LPD3-1 PD INTERNAL: AEOD/SPD/RRAB NRR/DIPM/IOLB NRR/DRIP/REXB RES/DET/EZB EXTERNAL: L ST LOBBY WARD NOAC POORE,W.NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1, 1 1 1 1 1 RECIPIENT ID CODE/NAME STANG,J FIL CENTER QMB NRR/DSSA/SPLB RGN3 FILE 01 LMZTCO MARSHALL NOAC QUEENER,DS NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 R D N NOTE TO ALL"RIDS" RECIPIENTS:
AEOD/SPD/RRAB NRR/DIPM/IOLB NRR/DRIP/REXB RES/DET/EZB EXTERNAL:
PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZAT1ONi CONTACT THE DOCUMENT CONTROE DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 16 ENCL 16 indiana Michigan Power Company Cook Nudger Plere One Cook Bere Bi'dgrnen, ka 491 06 61 6 st66 5901 May 3, 1999 INDIANA IIICHIOiAN IaoM%R United States Nuclear Regulatory Commission Document Control Desk'Washington, DC 20555 Operating r.icense DPR-58 Docket No, 50-315 Document Control Manager: In accordance with the criteria established by10 CFR 50.73 entitled Licensee Event Re ort~Sstem, the following report is being sobmttled:
LSTLOBBYWARDNOACPOORE,W.NRCPDRCOPIESLTTRENCL11111111111,11111RECIPIENT IDCODE/NAME STANG,JFILCENTERQMBNRR/DSSA/SPLB RGN3FILE01LMZTCOMARSHALLNOACQUEENER,DS NUDOCSFULLTXTCOPIESLTTRENCL1111111111111111RDNNOTETOALL"RIDS"RECIPIENTS:
A LER 315/99-010-00,"Reactor Coolant System Leak Detection System Sensitivity Not in Accordance with Design Requirements." The following commitments were identified in this submittal:
PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZAT1ONi CONTACTTHEDOCUMENTCONTROEDESK(DCD)ONEXTENSION 415-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
~An evaluation will be performed to clearly define the design and I'censing bases for the containment sump level and flow leak detection subsystem.
LTTR16ENCL16 indianaMichiganPowerCompanyCookNudgerPlereOneCookBereBi'dgrnen, ka49106616st665901May3,1999INDIANAIIICHIOiAN IaoM%RUnitedStatesNuclearRegulatory Commission DocumentControlDesk'Washington, DC20555Operating r.icenseDPR-58DocketNo,50-315DocumentControlManager:Inaccordance withthecriteriaestablished by10CFR50.73entitledLicenseeEventReort~Sstem,thefollowing reportisbeingsobmttled:
~A supplement to this LER will be provided if the results of the evaluation provide substantial changes to the significance, implications.
ALER315/99-010-00, "ReactorCoolantSystemLeakDetection SystemSensitivity NotinAccordance withDesignRequirements."
consequences or corrective actions.~Action to restore operability to the sump level and flow leak detection subsystem will be taken prior to entry into operational Mode 4.Sincerely, M.W.Rencheck Vice President-Nuclear Engineering Ilrb Attachment c: J.E.Oyer Region Ill R.P.~ower P..A.3arrett D.F.Kunsemiller R.Whale D.Hahn Records Center, INPO NRC Resident Inspector eg1905050i03 990503 PDR ADOCK 050003i5 S PDR sg.4FI'r~l rnerica's Enery I nrlner-}}
Thefollowing commitments wereidentified inthissubmittal:
~Anevaluation willbeperformed toclearlydefinethedesignandI'censing basesforthecontainment sumplevelandflowleakdetection subsystem.
~Asupplement tothisLERwillbeprovidediftheresultsoftheevaluation providesubstantial changestothesignificance, implications.
consequences orcorrective actions.~Actiontorestoreoperability tothesumplevelandflowleakdetection subsystem willbetakenpriortoentryintooperational Mode4.Sincerely, M.W.RencheckVicePresident
-NuclearEngineering IlrbAttachment c:J.E.OyerRegionIllR.P.~owerP..A.3arrettD.F.Kunsemiller R.WhaleD.HahnRecordsCenter,INPONRCResidentInspector eg1905050i03 990503PDRADOCK050003i5SPDRsg.4FI'r~lrnerica's EneryInrlner-}}

Revision as of 08:21, 6 July 2018

Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal
ML17325B574
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 05/03/1999
From: RENCHECK M W
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML17325B575 List:
References
RTR-REGGD-01.045, RTR-REGGD-1.045 NUDOCS 9905050103
Download: ML17325B574 (2)


Text

~CATEGORY+REGULATORY INFORMATION DISTRIBUTION SYSTEM (RZDS)ACCESSION NBR:9905050103 DOC.DATE: 99/05/03 NOTARIZED:

NO DOCKET I FACIL:50-315 Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 AUXHTNAME AUTHOR AFFILIATION RENCHECK,M.W.

Indiana Michigan Power Co.(formerly Indiana&, Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Records Management Branch (Document Control Desk)

SUBJECT:

Forwards LER 99-010-00 re RCS leak detection sys sensitivity not in accoradnce with design requirements.

Listed C commitments identified in submittal.

A DZSTRZBUTZON CODE: ZE22T COPTER RECEZVED:LTR 1 ENCL J SZEE: I TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: E RECIPIENT ID CODE/NAME LPD3-1 PD INTERNAL: AEOD/SPD/RRAB NRR/DIPM/IOLB NRR/DRIP/REXB RES/DET/EZB EXTERNAL: L ST LOBBY WARD NOAC POORE,W.NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1, 1 1 1 1 1 RECIPIENT ID CODE/NAME STANG,J FIL CENTER QMB NRR/DSSA/SPLB RGN3 FILE 01 LMZTCO MARSHALL NOAC QUEENER,DS NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 R D N NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZAT1ONi CONTACT THE DOCUMENT CONTROE DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 16 ENCL 16 indiana Michigan Power Company Cook Nudger Plere One Cook Bere Bi'dgrnen, ka 491 06 61 6 st66 5901 May 3, 1999 INDIANA IIICHIOiAN IaoM%R United States Nuclear Regulatory Commission Document Control Desk'Washington, DC 20555 Operating r.icense DPR-58 Docket No, 50-315 Document Control Manager: In accordance with the criteria established by10 CFR 50.73 entitled Licensee Event Re ort~Sstem, the following report is being sobmttled:

A LER 315/99-010-00,"Reactor Coolant System Leak Detection System Sensitivity Not in Accordance with Design Requirements." The following commitments were identified in this submittal:

~An evaluation will be performed to clearly define the design and I'censing bases for the containment sump level and flow leak detection subsystem.

~A supplement to this LER will be provided if the results of the evaluation provide substantial changes to the significance, implications.

consequences or corrective actions.~Action to restore operability to the sump level and flow leak detection subsystem will be taken prior to entry into operational Mode 4.Sincerely, M.W.Rencheck Vice President-Nuclear Engineering Ilrb Attachment c: J.E.Oyer Region Ill R.P.~ower P..A.3arrett D.F.Kunsemiller R.Whale D.Hahn Records Center, INPO NRC Resident Inspector eg1905050i03 990503 PDR ADOCK 050003i5 S PDR sg.4FI'r~l rnerica's Enery I nrlner-