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J0 NRCFOAM368A(649)FACILITYNAME(1)U.SNUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORTILER)TEXTCONTINUATIONDOCKETNUMBER(2)APPROVED0MBNO.31504(OSEXPIRES;S/30/92ESTIMATEDBUADENPERAESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUEST:50J)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430).U.S.NUCLEARREGULATORYCOMMISSION.WASHINGTON,DC205S5,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3(504104).OFFICEOFMANAGEMENTAND8UDGET,WASHINGTON.DC20503.PAGE(3)LERNUMBERIS)R.E.Glnna'NUclearPowerPlantTEXT///mareSaece/ere/a/rerLIree~HRCFarm355AB/(12)YEARosooo24493SEQUENTIAL.oANUMSSRCN004REVISIONNUMSR0008oF09ROOTCAUSE:Theunderlyingcauseoftheeventwasdeterminedtobenotisolatingthe5AhighpressureheaterhighleveldumpvalvetotheHDTpriortocommencementoftroubleshootingtheairsupplyconcernsforthe'dumpvalve.ANALYSTSOP&TENTThiseventisreportableinaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresreportingof,"anyeventorconditi'onthatresultedinmanualorautomaticactuationofanyEngineeredSafetyFeature(ESF)includingtheReactorProtectionSystem(RPS)".Thefeedwaterisolationofthe"B"S/GwasanautomaticactuationofanESFsystem.Anassessmentwasperformedconsideringboththesafetyconsequencesandimplicationsofthiseventwiththefollowingresultsandconclusions:Therewerenooperationalorsafetyconsequencesorimplicationsattributedtothefeedwaterisolationsbecause:oThefeedwaterisolationsoccurredattherequiredS/Glevel.00TheplantwasquicklystabilizedandmanualcontrolofFRVswasaccomplishedtomitigateanyconsequencesoftheevent.I,Asthefeedwaterisolationsoccurredasdesigned,theassumptionsoftheFSARforsteamlinebreakweremet.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassuredatalltimes.NRCFomI365A(589)  
J0 NRCFOAM368A(649)FACILITYNAME(1)U.SNUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORTILER)TEXTCONTINUATIONDOCKETNUMBER(2)APPROVED0MBNO.31504(OSEXPIRES;S/30/92ESTIMATEDBUADENPERAESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUEST:50J)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430).U.S.NUCLEARREGULATORYCOMMISSION.WASHINGTON,DC205S5,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3(504104).OFFICEOFMANAGEMENTAND8UDGET,WASHINGTON.DC20503.PAGE(3)LERNUMBERIS)R.E.Glnna'NUclearPowerPlantTEXT///mareSaece/ere/a/rerLIree~HRCFarm355AB/(12)YEARosooo24493SEQUENTIAL.oANUMSSRCN004REVISIONNUMSR0008oF09ROOTCAUSE:Theunderlyingcauseoftheeventwasdeterminedtobenotisolatingthe5AhighpressureheaterhighleveldumpvalvetotheHDTpriortocommencementoftroubleshootingtheairsupplyconcernsforthe'dumpvalve.ANALYSTSOP&TENTThiseventisreportableinaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresreportingof,"anyeventorconditi'onthatresultedinmanualorautomaticactuationofanyEngineeredSafetyFeature(ESF)includingtheReactorProtectionSystem(RPS)".Thefeedwaterisolationofthe"B"S/GwasanautomaticactuationofanESFsystem.Anassessmentwasperformedconsideringboththesafetyconsequencesandimplicationsofthiseventwiththefollowingresultsandconclusions:Therewerenooperationalorsafetyconsequencesorimplicationsattributedtothefeedwaterisolationsbecause:oThefeedwaterisolationsoccurredattherequiredS/Glevel.00TheplantwasquicklystabilizedandmanualcontrolofFRVswasaccomplishedtomitigateanyconsequencesoftheevent.I,Asthefeedwaterisolationsoccurredasdesigned,theassumptionsoftheFSARforsteamlinebreakweremet.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassuredatalltimes.NRCFomI365A(589)  


NRCFORM366A(BJIS)UA.NUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORTILER)TEXTCONTINUATIONAPPROVEDOMBNO.3(500106EXPIRES:6/30/62ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREOUEST:60.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1MEPAPERWORKREDUCTIONPROJECT(3(500106).OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBERLSIYEARr~r'SEOUENTIALP~SREVISIONNUMBER"~NUMERPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///momJpon/1mqII/mI/II'////JJN/IHRC%%dmI36MB/l(7)osooo2449300400090FV.CORRECTIVEACTIONAACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUS:AftertheS/Glevelswerestabilized,theFRVswerereturnedtotheirpre-eventcontrolconfiguration.B.ACTIONTAKENORPLANNEDTOPREVENTRECERMFNCE:Toensureamorerapidmitigationofthistypeofeventandpossiblyeliminatethefeedwaterisolation,operatingprocedureT-6.9Awillbechangedtodeletethestepsthatplacethelowpressureheaterscondensatebypassvalveswitchtotheclosedposition.Operations,Planning,andI&Cpersonnelhavebeennotifiedthatisolationofaheaterhighleveldumpvalve,priortotroubleshooting,shouldbeconsideredanormalpractice.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:None.BPREVIOUSLERsONSIMILAREVENTSAsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:LER91-009andLER-92-006(Revision1)weresimilareventswithdifferentrootcauses.CSPECIALCOMMENTS:LER92-006(Revision1)indicatestheproblemsthathavebeenexperiencedwiththeAdvancedDigitalFeedwaterControlSystem(ADFCS),thecausesandcorrectiveactionstakenorplanned.NRCForm366A(686) hT  
NRCFORM366A(BJIS)UA.NUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORTILER)TEXTCONTINUATIONAPPROVEDOMBNO.3(500106EXPIRES:6/30/62ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREOUEST:60.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1MEPAPERWORKREDUCTIONPROJECT(3(500106).OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBERLSIYEARr~r'SEOUENTIALP~SREVISIONNUMBER"~NUMERPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///momJpon/1mqII/mI/II'////JJN/IHRC%%dmI36MB/l(7)osooo2449300400090FV.CORRECTIVEACTIONAACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUS:AftertheS/Glevelswerestabilized,theFRVswerereturnedtotheirpre-eventcontrolconfiguration.B.ACTIONTAKENORPLANNEDTOPREVENTRECERMFNCE:Toensureamorerapidmitigationofthistypeofeventandpossiblyeliminatethefeedwaterisolation,operatingprocedureT-6.9Awillbechangedtodeletethestepsthatplacethelowpressureheaterscondensatebypassvalveswitchtotheclosedposition.Operations,Planning,andI&Cpersonnelhavebeennotifiedthatisolationofaheaterhighleveldumpvalve,priortotroubleshooting,shouldbeconsideredanormalpractice.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:None.BPREVIOUSLERsONSIMILAREVENTSAsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:LER91-009andLER-92-006(Revision1)weresimilareventswithdifferentrootcauses.CSPECIALCOMMENTS:LER92-006(Revision1)indicatestheproblemsthathavebeenexperiencedwiththeAdvancedDigitalFeedwaterControlSystem(ADFCS),thecausesandcorrectiveactionstakenorplanned.NRCForm366A(686) hT}}
}}

Revision as of 12:33, 18 May 2018

LER 93-004-00:on 930707,Main Feedwater Isolations Occurred Due to Secondary Side & Condensate Feedwater Pressure Transient.Returned Feedwater Regulating Valves to pre-event Controls configuration.W/930806 Ltr
ML17263A352
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/06/1993
From: BACKUS W H, MECREDY R C
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-93-004, LER-93-4, NUDOCS 9308120083
Download: ML17263A352 (22)


Text

ACCELERATEDDOCUMENTDISTRIBUTIONSYSTEMREGUL>RYINFORMATIONDISTRIBUTESYSTEM(RIDE)ACCESSIONNBR:9308120083DOC.DATE:93/08/06NOTARIZED:NOFACIL50-244RobertEmmetGinnaNuclearPlant,Unit1,RochesterGAUTH.NAMEAUTHORAFFILIATIONBACKUS,W.HRochesterGasaElectricCorp.MECREDY,R.CRochesterGas6ElectricCorp.RECIP.NAMERECIPIENTAFFILIATION

SUBJECT:

LER93-004-00:on930707,Mainfeedwaterisolationsoccurredduetosecondaryside6condensatefeedwaterpressuretransient.Returnedfeedwaterregulatingvalvestopre-eventcontrolsconfiguration.W/930806ltr.DISTRIBUTIONCODE:ZE22TCOPIESRECEIVED:LTRtENCLrSIZE:LOTITLE:50.73/50.9LicenseeEventReport(LER),IncidentRpt,etc.NOTES:LicenseExpdateinaccordancewith10CFR2,2.109(9/19/72).DOCKET¹05000244Ii1I1DlSl'.05000244ARECIPIENTIDCODE/NAMEPD1-3LAJOHNSON,AINTERNAL:ACNWAEOD/DSP/TPABNRR/DE/EELBNRR/DORS/OEABNRR/DRCH/HICBNRR/DRIL/RPEBNODSSA/+PLB-BP02RGHlFILE01EXTERNAL:EGGGBRYCE,J.HNRCPDRNSICPOORE,W.COPIESLTTRENCL11112211111111111111112'1111RECIPIENTIDCODE/NAMEPD1-3PDAEOD/DOAAEOD/ROAB/DSPNRR/DE/EMEBNRR/DRCH/HHFBNRR/DRCH/HOLBNRR/DRSS/PRPBNRR/DSSA/SRXBRES/DSIR/EIBLSTLOBBYWARDNSICMURPHYFG.ANUDOCSFULLTXTCOPIESLTTRENCL111122111111221111111111DD$DDNOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWASTEICONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065)TOELIMINATEYOURNAMEFROMDISTRIBUTIONLISTSFORDOCUMENTSYOUDON'TNEED!DFULLTEXTCONVERSIONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR30ENCL30

rrrnrNr1/r/trl/rr//i////>rr,//'/I/'i"Ii//,i'"i!C!i)ivir~ill!III/l'lrir,r!r/ROCHESTERGASANDELECTRICCORPORATION~";-',Toe/r.,state"89EASTAVENUE,ROCHESTERN.K14649-0001ROBERTC.MECREOYVicePresidentClnnattuclearProductionTELEPHONEARE/1COOE7165rt62700August6,1993U.S.NuclearRegulatoryCommissionDocumentControlDeskWashington,DC20555

Subject:

LER93-004,FeedwaterControlPerturbations,DueToASecondarySideTransient,CausesSteamGeneratorHighLevelFeedwaterIsolationsR.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordancewith10CFR50.73,LicenseEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"anyeventorconditionthatresultedinmanualorautomaticactuationofanyEngineeredSafetyFeature(ESF),includingtheReactorProtectionSystem(RPS)",theattachedeventreportLER93-004i:sherebysubmitted.Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,xcoRobertC.MecedyU.S.NuclearRegulatoryCommissionRegionI475AllendaleRoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector~rn.h9308i20083930806PDR*DOCK050002448PDR

NRCFORM366(669)V.S.NUCLEARREGULATORYCOMMISSILICENSEEEVENTREPORT(LER)APPROVEDOMBNOA31506104EXPIRESI4/30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFOAMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANORFPORTSMANAGEMENTBRANCH(F630),V.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTOTHEPAPERWORKREDUCTIONPROJECT(31500'l04).OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,OC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBERl2)PAE05000244iOFOFeewaterControerturatons,DueToSeconaryTransent,ausesteamGeneratorHighLevelFeedwaterIsolationsEVENTDATE(5)MONTHDAYYEARYEARLERNUMBER(61:SEQUENTIALNUMBERREVISIONNUMBERREPORTDATELT)MONTHDAYYEARDOCKETNUMBERIS)05000FACII.ITVNAMES01'HERFACILITIESINVOLVED(6)0-7793930040008069305000OPERATINGMODE(9)NPOWERLEYEL09760n(sl(2)Is>>)50.n(v)(2)Nl5073(s)(2)lvsl)50.73(v)(2)(vill)(Al50.73(v)l2l(vill)(B)50.73(~)(2)lsl0THERLQUIAEMENTSOF10CFR((:/ChockonoormoroOltrssIollovrinP/(11)THISREPORTISSVBMITTFDPUASVANTT20.402(B)20.405(~)(1)(I)20.405(s)l1)(NI20.406(~I('IHill)20405(s)(1)(lv)20.405(sI(I)(vl20.405(c)60M(s)(II50.36(~)(2)60.73(sl(2((ll50.73(s)(2)(ill50.73(s)(2)(ill)73,71(B)73.71IclOTHERISpscilyIn4osnocttN/oENonr/lnTssI,HRCForm3664/LICENSEECONTACTFORTHISLEA(12INAMEWesleyH.Backus.TechnicalAssistanttotheOperationsManaerTELEPHONENUMBERAREACODE315524-4446COMPLETEONELINEFOREACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAVSESYS'EMCOMPONENTMANUFAC.TVRERREPORTABLETONPADSPjQgCAUSESSTEMXj'>>AA'RC~C.3>>">>T>>~'"IKU'::hl.'.@<COMPONENTMANUFAC.TVREREPORTABLETONPROS?>>o.>>...%R.:.R6)SA'NO4PcA.N::SUPPLEMENTALREPORTEXPECTEDllc)YESIlly<<,compiotsEXPECTEDSl/SSI/SSIONDATE/NOAssTRAcTI(.imitto/400spscsr,l.s.,spproslmsrslylilusntinpis.rpocstypssvrinon/inos/(16)EXPECTFDSUBMISSIONDATE(15)MONTHDAYYEAROnJuly7,1993-atapproximately0915EDST,withthereactoratapproximately974fullpower,mainfeedwaterisolationsoccurredonthe"BFISteamGenerator(S/G).Thesefeedwaterisolationswerecausedbyoverfeedingthe"B"S/G,followingasecondarysidecondensateandfeedwaterpressuretransient.ImmediateoperatoractionwastomanuallycontroltheFeedwaterRegulatingValves(FRVs)torestoretheS/Gwaterlevelsandstabilizetheplant.Theimmediatecauseoftheeventwasduetoasecondarysidecondensateandfeedwaterpressuretransient.Theunderlyingcauseoftheeventwasdeterminedtobenotisolatingthe5Aheaterhighleveldumpvalvepriortotrouble-shooting.(ThiseventisNUREG-1022(X)CauseCode).CorrectiveactionstakenorplannedarediscussedinSectionVofthetext.NRCForm366(669)

NRCFORM388A(SJ)9)US.NUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORT(LER)TEXTCONTINUATIONAPPROVEDOMBNO.3(504)04EXPIRES:4/30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREOUEST:508)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1HEPAPERWORKREDUCTIONPROJECT(31500)08),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(llDOCKETNUMBER(2)YEARLERNUMBER(8)SEOUENTIALo@IIEVISIONNUMEIIPAGE(3)R.E.GlnnaNuclearPowerPlantTEXT/I/moree/reoe/Irer/uuN/,u>>//I/rme/HRCFrurn35883/()7)osooo244930040002OF09LANTCONDTONSTheplantwasatapproximately974steadystatereactorpowerwiththefollowingpertinentactivitiesinprogress:oThe"B"AllVolatileTreatment(AVT)mixedbeddemineralizerwasbeingplacedinserviceperoperatingprocedureT-6.9A(CondensatePolishingMixedBedDIUnitStart-up).AlsoperT-6.9A,thestandby"C"condensatepumpstart/stopswitchwasplacedinpullstop,andthelowpressureheaterscondensatebypassvalveswitchwaschangedfromtheautotoclosedposition.TheaboveswitchmanipulationswereperformedtopreventanyinadvertentoperationsduringplacingtheAVTmixedbeddemineralizerinservice..oTheInstrumentandControl(I&C)Departmentwastroubleshooting5Ahighpressureheaterlevelcontrolproblems.DESCRIPTIONOPEVENTA.DATESANDAPPROXIMATETIMESOPMAJOROCCURRENCES:0July7,1993,0915EDST:Eventdateandapproxi-matetime.0July7,1993,0915EDST:Discoverydateandapproximatetime.0July7,1993,0925EDST:"A"and"B"SteamGenerator(S/G)levelsrestoredtopre-eventnormaloperatingband.NRCForm388A(889)

NRCFORM388A(SJ)9)US.NUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORT(LER)TEXTCONTINUATIONAPPROVEDOMBNO.31600108EXPIRES:E/30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREOUEST:60.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(PW30),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20666,ANDTO1'HEPAPERWORKREDUCTIONPROJECT(3160410E).OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20603.FACILITYNAME('I)DOCKETNUMBER12)YEARLERNl/MBER(8).'os:sEovENTIALNVMSERREVISIONNVMERPAGE(3)R.E.GlnnaNuclearPowerPlantTEXT///marog>>coJInq>>)ed,1>>o~H/ICFomI38SAB/(ll)osooo244930040003QF09B.EVENTOnJuly7,1993,atapproximately0800EDST,anInstrumentandControl(I&C)Technicianbegantrouble-shooting5Ahighpressureheaterlevelcontrolproblems,inaccordancewithMaintenanceWorkOrder(MWO)9301086.TheI&CTechniciansuspectedtherewasanairleakintheairsupplytubingorinthevalvepositionerforoneofthe5Aheaterlevelcontrolvalves.WithconcurrencefromaControlRoomoperator,thetechniciandisconnectedandpluggedthetubingtothenormallevelcontrolvalve,andobservedthatthehighleveldumpvalve(whichfailsopenonlossofair)brieflyopenedforafew.seconds(untilthetubingwasplugged)andthenclosed,Seeingnoimprovementinairpressure,thetubingwasthenunpluggedandrestoredtonormal.Shortlybefore0915EDST,thetechniciandisconnectedandpluggedthetubingtothehighleveldumpvalve.Withairpressuretothevalveplugged,thedumpvalvewentfullopenandremainedfullyopen.Approximatelyten(10)secondslater,thetechniciannotedthattheHeaterDrainTank(HDT)dischargevalvebeganclosing,andexpeditious'lyunpluggedthetubingandrestorednormalairsupplytothedumpvalve.Uponrestorationofairpressure,thedumpvalveclosed.OnJuly7,1993atapproximately0915EDST,withthereactoratapproximately974fullpower,asecondarysidecondensateandfeedwatersystemdecreasingpressuretransientoccurred.AtthistimetheconfigurationoftheS/Gfeedwaterregulatingvalveswereasfollows:oThe"A"S/GMainFeedwaterRegulatingValve(FRV)wasinmanualmode(approximately454open)toreducefeedwatersystemflowoscillationsthatwereoccurring.NRCFoIRI388A(689)

NRCFORM366A(SSS)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORTILER)TEXTCONTINUATIONAPPROVEDOMSNO.31600104EXPIRES:4/30/02ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREOUEST:50A)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(P430),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20655,ANDTO1HEPAPERWORKREDUCTIONPROJECT(3150d)04),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(<<DOCKETNUMBER(2)YEARLERNUMBER(6)'SOUSNTIALNUMSSII4IISVISIONNUMSSIIPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///mauSpuce/4Isqu/>>I/,u>>a/dc0htuh4/I/RCFumI36643/((Tl05000244'0040004oF09oThe<<A<<S/GBypassFRVwasintheautomodecontrollingthe<<A<<S/Glevel(approximately804open).oThe<<B<<S/GMainFRVwasintheautomodecontrollingthe<<B<<S/Glevel(approximately464open).oThe<<B<<S/GBypassFRVwasintheautomode(fullopen).ThesecondarysidecondensateandfeedwatersystemdecreasingpressuretransientwasinitiatedbyasignificantmomentarydecreaseinHDTpumpflowduetotheclosingoftheHDTdischargevalve.(HDTpumpflowdecreasedapproximately754fromnormal).HDTpumpflownormallysuppliesapproximatelyonethirdofthesuctionflowtotheS/Gmainfeedwaterpumps.TheothertwothirdsofthesuctionflowtotheS/Gmainfeedwaterpumpsissuppliedbythecondensatepumpsthroughthelowpressurefeedwaterheaters.Thedecreasedflowcoupledwiththeinabilityofthestandbycondensatepumptostartand/orthelowpressureheaterscondensatebypassvalvetoopen,(thisline-upexplainedinPre-EventPlantConditions,SectionI),decreasedpressurethroughoutthecon-.densateandfeedwatersystem.The<<B<<S/GMainFRV(inauto)followedthelossofmainfeedwaterpressurebyopeningmore(approximately574open)tomaintainmainfeedwaterflowtothe<<B<<S/G.The<<A<<S/GMainFRV(inmanual)remainedatapproximately454open.Approximately40-50secondsafterinitiationofthetransient,HDTpumpflowwasrestoredtonormal,restoringcondensateandfeedwaterpressuretonormal,andcausing<<B<<S/Gfeedwaterflowtoexceedthecalibrationrangeoftheflowtransmitters(<<B".S/GFRVhadopenedto574).Becausethe"B<<S/Gfeedwaterflowvaluesexceededthecalibrationrangeoftheflowtransmitters,the"B<<FRVautomaticallyswitchedtomanualmode.Theprecedingeventsoccurredinashortperiodoftime.DuringthisshortperiodofNRCFoIm366A(640) 0 NRCFORM366A(6BB)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORT(LER)TEXTCONTINUATIONAPPROVEODMSNO.3)504(OEEXPIRES:E/30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREOUESTI508)HRS.FORWARDCOMMENTSREGARDINGBURDENFSTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(PJ)30),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTOTHEPAPERWORKREDUCTIONPROJECT(31504)04).OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(I)DOCKETNUMBER12)YEARLERNUMBER(6)I'oR'jSEQUENTIALS>NUMBERREVISIONNUMERPAGE(3)R.E.GonnaNuclearPowerPlantTEXT/IImortEpoco/EIEOVPEI/oooea//I/ono/HRCFomI366AB/(17)osooo2449300400050F09timethe"B"S/Gwasbeingsuppliedwithmorefeedwaterthanrequired,andatapproximately0917EDST(approxi-matelytwo(2)minutesintothetransient)mainfeedwaterisolationonhighlevel(i.e.>/=674narrowrangelevel)occurredfive(5)timestothe"BL(S/Goveraperiodoffourteen(14)seconds.TheControlRoomoperatorstookimmediatemanualactionstorestoreS/Glevelsandatapproximately0925EDSTthe"A"and"B"S/Glevelswererestoredtotheirnormaloperatingbandandtheplantstabilized.Subsequently,theControlRoomoperatorsnotifiedhighersupervisionandtheNuclearRegulatoryCom-missionper10CFR50.72,non-emergency4hournotification.C.INOPERABLESTRUCTURES,COMPONENTS,ORSYSTEMSTHATCONTRIBUTEDTOTHEEVENTThe5AhighpressureheaterhighleveldumpvalvetotheHDTinoperability,duetotroubleshootingefforts,inaccordancewithMWO9301086,contributedtotheevent.Inoperabilityofthe"C"Standbycondensatepumpandcondensatebypassvalve,duetoprocedureT-6.9A'equirements,contributedtothedifficultyinrespondingtotheevent.D.CÃHiERSYSTEMSORSECONDARYFUNCTIONSAFFECTED:None.NRCFoIIn366A(649)

NAGFOAMSKSA(5$9)U$.NUCLEARREGULATORYCOMMISSIONLICENSEENTREPORT(LER)TEXTCONTINUATIONAPPROVEDOMBNO.3)500(04EXPIRES:r/30/92TIMATEDBUADENPEARESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREGUEST:50A)HRS.FORWARDCOMMENTSREGARDINGBUAOENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(P$30),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON.OC20555.ANDTO'IHEPAPERWORKREDUCTIONPROJECT(31500(04),OFFICEOFMANAGEMENTANDBUDGETWASHINGTONDC20503FACILITYNAME(IIDOCKETNUMBER(2)YEARLERNUMBERFS)SKQVKNTIAINVMSKRRKVIKIONNUMSKRPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///maor/vcr/rrrqokaf,uwedcVdoIN/HRCFomr35SA'r/(Illosooo244930040006OF09E.METHODOPDISCOVERYTheeventwasimmediatelyapparentduetoalarmsandindicationsintheControlRoomandindicationsatthe5AhighpressureheaterhighleveldumpvalvetotheHeaterDrainTank.OPERATORACTION:TheControlRoomoperatorstookimmediatemanualactionstocontrolS/Glevelsandstabilizetheplant.Subsequently,theControlRoomoperatorsnotifiedhighersupervisionandtheNuclearRegulatoryCommissionper10CFR50.72,non-emergency4hournotification.GSAFETYSYSTEMRESPONSES:The>>B>>S/GMainandBypassFRVsbegantocloseautomaticallyasaresultofthefeedwaterisolationsignals.Duetotheshortdurationthatthesignalswerepresent,theFRVsneverfullyclosed.III.CAUSEOPEVERTA.IMMEDIATECAUSE:Thefeedwaterisolationsignaltothe>>B>>S/GMainandBypassFRVswasduetothe>>B>>S/Gnarrowrangelevelbeing>/=67%.B.INTERMEDIATECAUSE:The>>B>>S/Gnarrowrangelevelwas>/=674duetoincreasedflowtothe>>B>>S/Gcausedbytheperturba-tionsinmainfeedwaterheaderpressureandautomaticFRVoperation.Thissituationresultedinoverfeedingthe>>B>>S/G.NRCFomI358A(5$9)

NRCFORM366A(609)US.NUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORT(LER)TEXTCONTINUATIONAPPROVEDOMBNO.31500104EXPIRES:4/30/92ESTIMATEDBURDENPERRESPONSETOCOMPI.YWTHTHISINFORMATIONCOLLECTIONREQUEST:60glHRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(PJ)30),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1HEPAPERWORKREDUCTIONPROJECT(31500104),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON.DC20503.FACILITYNAME(IIDOCKETNUMBER(2)YEARLERNUMBER(6)(I63:SEQUENTIALNUM664+pREVISIONNUM64PAGE(3)R.E.GonnaNuclearPowerPlantTEXT///RNVP4/>>Ce/4JNIUPN/II>>PIS/OR4/HRCFORR36542/((7)0s0o0244~3004-007oF09TheperturbationsinmainfeedwaterheaderpressurewerecausedbyamomentarylargereductioninHDTpumpflowfollowedbyarapidreturntonormalflow.The"B"S/GMainFRV(inauto)followedthelossofmainfeedwaterheaderpressurebyopeningmoretomaintainfeedwaterflowandwhenHDTpumpflowwasrapidlyrestored,mainfeedwaterheaderpressurereturnedtonormal.Whenmainfeedwaterheaderpressurereturnedtonormal,the"B"S/GFRVwasopenapproximately114morethannormalandthe"B"S/Gfeedwaterflowsexceededthecalibrationrangeoftheflowtransmittersandbydesignthe"B"S/GFRVswitchedtomanualmode.Inthemanualmode'he"B"S/GMainFRVcouldnotcontrolthe"BLIS/Glevelwithoutoperatorintervention.Itshouldbenotedherethatifthelowpressureheaterscondensatebypassvalvehadbeencapableofopening,theabovetransientcouldhavebeenlesssevereandthe"BFIS/Gwouldmostlikelyhavenotsustainedahighlevelfeedwaterisolation.ThemomentarylargereductioninHDTpumpflow,followedbyarapidreturntonormalflow,wascausedbytheopeningandsubsequentclosingofthe5AhighpressureheaterhighleveldumpvalvetotheHDT,duetotheactionsoftheI&CTechnician'stroubleshootingactivities.Itisbelievedthattheopeningofthisdumpvalve,coupledwiththe5Ahighpressureheaterlowlevelcondition,decreasedtheHDTlevelsubstan-tially.ThisleveldecreasewassensedbytheHDTlevelcontrolsystemanditbegantoclosetheHDTpumpdischargecontrolvalvetoreduceflowandreturntheHDTleveltoitsoperatingband.Theclosingofthe5Ahighpressureheaterhighleveldumpvalve,duetotheactionsoftheISCTechnician,reversedtheaboveconditionsandtheHDTpumpflowreturnedtonormal.NRCFoIRI366A(64)9)

J0 NRCFOAM368A(649)FACILITYNAME(1)U.SNUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORTILER)TEXTCONTINUATIONDOCKETNUMBER(2)APPROVED0MBNO.31504(OSEXPIRES;S/30/92ESTIMATEDBUADENPERAESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUEST:50J)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430).U.S.NUCLEARREGULATORYCOMMISSION.WASHINGTON,DC205S5,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3(504104).OFFICEOFMANAGEMENTAND8UDGET,WASHINGTON.DC20503.PAGE(3)LERNUMBERIS)R.E.Glnna'NUclearPowerPlantTEXT///mareSaece/ere/a/rerLIree~HRCFarm355AB/(12)YEARosooo24493SEQUENTIAL.oANUMSSRCN004REVISIONNUMSR0008oF09ROOTCAUSE:Theunderlyingcauseoftheeventwasdeterminedtobenotisolatingthe5AhighpressureheaterhighleveldumpvalvetotheHDTpriortocommencementoftroubleshootingtheairsupplyconcernsforthe'dumpvalve.ANALYSTSOP&TENTThiseventisreportableinaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresreportingof,"anyeventorconditi'onthatresultedinmanualorautomaticactuationofanyEngineeredSafetyFeature(ESF)includingtheReactorProtectionSystem(RPS)".Thefeedwaterisolationofthe"B"S/GwasanautomaticactuationofanESFsystem.Anassessmentwasperformedconsideringboththesafetyconsequencesandimplicationsofthiseventwiththefollowingresultsandconclusions:Therewerenooperationalorsafetyconsequencesorimplicationsattributedtothefeedwaterisolationsbecause:oThefeedwaterisolationsoccurredattherequiredS/Glevel.00TheplantwasquicklystabilizedandmanualcontrolofFRVswasaccomplishedtomitigateanyconsequencesoftheevent.I,Asthefeedwaterisolationsoccurredasdesigned,theassumptionsoftheFSARforsteamlinebreakweremet.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassuredatalltimes.NRCFomI365A(589)

NRCFORM366A(BJIS)UA.NUCLEARREGULATORYCOMMISSIONLICENSEEENTREPORTILER)TEXTCONTINUATIONAPPROVEDOMBNO.3(500106EXPIRES:6/30/62ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREOUEST:60.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1MEPAPERWORKREDUCTIONPROJECT(3(500106).OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBERLSIYEARr~r'SEOUENTIALP~SREVISIONNUMBER"~NUMERPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///momJpon/1mqII/mI/II'////JJN/IHRC%%dmI36MB/l(7)osooo2449300400090FV.CORRECTIVEACTIONAACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUS:AftertheS/Glevelswerestabilized,theFRVswerereturnedtotheirpre-eventcontrolconfiguration.B.ACTIONTAKENORPLANNEDTOPREVENTRECERMFNCE:Toensureamorerapidmitigationofthistypeofeventandpossiblyeliminatethefeedwaterisolation,operatingprocedureT-6.9Awillbechangedtodeletethestepsthatplacethelowpressureheaterscondensatebypassvalveswitchtotheclosedposition.Operations,Planning,andI&Cpersonnelhavebeennotifiedthatisolationofaheaterhighleveldumpvalve,priortotroubleshooting,shouldbeconsideredanormalpractice.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:None.BPREVIOUSLERsONSIMILAREVENTSAsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:LER91-009andLER-92-006(Revision1)weresimilareventswithdifferentrootcauses.CSPECIALCOMMENTS:LER92-006(Revision1)indicatestheproblemsthathavebeenexperiencedwiththeAdvancedDigitalFeedwaterControlSystem(ADFCS),thecausesandcorrectiveactionstakenorplanned.NRCForm366A(686) hT