ML20206G374: Difference between revisions

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        /        ' ' - c t.,'c.                         UNITED STATES NUCLEAR REGULATORY COMMISSION
UNITED STATES
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NUCLEAR REGULATORY COMMISSION
SAFET) EVALUATION REPORT BY THE OFFICE OF SPECIAL PROJECTS I                                          EMPLOYEE C0' i CERN ELEMENT REPORT 22110 (B) i USE OF SNUBBERS TENSESSEE VALLEY AUTHORITY                             ;
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SECUOVAH NUCLEAR POWER PLAET . UNIT 1 DOCKET NO.: 50-327
i wasmNotoN, o. c. 20sss a
: 1.     STATEMENT Or EP:LOYEE C0' ctRN The basis for Element Repert 22110 (B), Rev.1. Dated December .'s0,1956 is enleyee cencern SQN.F.6-001-02 which states that the Upper d'ead injection Systen vertical riser requires a rigid support where a snubber     '
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a                        was usec.
SAFET) EVALUATION REPORT BY THE OFFICE OF SPECIAL PROJECTS EMPLOYEE C0' CERN ELEMENT REPORT 22110 (B)
i                !!. SUw?M Y OF ISSUE                                                                  [
I i
;                        A rigid type sup; ort is specified in the piping analysis for a specific location on the vertical riser of the Upper Head Injectica (VHI) system, but the detail drawings and as-built condition show use of a snubber at this location. UH! has a plant safety-related function.                      ,
USE OF SNUBBERS i
                  !!!. EVALLATION l                          In Merch 1986, this discrepancy was identified by TVA in a significant ccrdition report SCR SQN CEB 8615. Elernent report 22110 (B), Rev.1.          ;
TENSESSEE VALLEY AUTHORITY SECUOVAH NUCLEAR POWER PLAET. UNIT 1 DOCKET NO.: 50-327 1.
recognizec the empic                            In a subsequent letter l
STATEMENT Or EP:LOYEE C0' ctRN The basis for Element Repert 22110 (B), Rev.1. Dated December.'s0,1956 is enleyee cencern SQN.F.6-001-02 which states that the Upper 'ead d
J.A. McEenald (TVA) yee concern as valid.to B.J. Youngblood (NRC), Dated i                          responding to an NRC request for additional inforr.ation, the root cause    i 2                          of this disparity between thk pipe support analysih and the al built          !
injection Systen vertical riser requires a rigid support where a snubber a
1 concition was given as a lack of attention to detail, specifically, that    !
was usec.
;                          Jn engineering judgeFent w3s made regarding support orientation and design  ;
without proper documentation and comunication to in erfacing groups.        :
I The letter also identified a 100t (nginee-ing revies of all snubbers in      t the plant against the piping analyses, and confirme this instance to be a single, isolatec case. The T'.A re-analysis (060v104 15 01) of the UH!    3 pipe restraint at this location utilizirig a snubber demonstrated the use    ;
of the snubber to be an adequate design, able to sustain required seismic    j and therr.al stress levels. TVA has identified this as an acceptable        ;
)'
resciution to the issue. Tre st:ff believes the depth and extent of the      !
review tc be adecuate and concurs that installation of the snubber is j                          acceptatie, and the rt;iace ant of the snutbet' is not necessary.            [
l                                                                                                        i
)        8011220253 88;104 PDR        AfOCK 05000327 P                          FDL                                                                l I
i
i
!!. SUw?M Y OF ISSUE
[
A rigid type sup; ort is specified in the piping analysis for a specific location on the vertical riser of the Upper Head Injectica (VHI) system, but the detail drawings and as-built condition show use of a snubber at this location.
UH! has a plant safety-related function.
!!!. EVALLATION l
In Merch 1986, this discrepancy was identified by TVA in a significant ccrdition report SCR SQN CEB 8615. Elernent report 22110 (B), Rev.1.
recognizec the empic In a subsequent letter J.A. McEenald (TVA) yee concern as valid.to B.J. Youngblood (NRC), Dated l
i i
responding to an NRC request for additional inforr.ation, the root cause of this disparity between thk pipe support analysih and the al built 2
1 concition was given as a lack of attention to detail, specifically, that Jn engineering judgeFent w3s made regarding support orientation and design I
without proper documentation and comunication to in erfacing groups.
t The letter also identified a 100t (nginee-ing revies of all snubbers in the plant against the piping analyses, and confirme this instance to be a single, isolatec case. The T'.A re-analysis (060v104 15 01) of the UH!
3 pipe restraint at this location utilizirig a snubber demonstrated the use of the snubber to be an adequate design, able to sustain required seismic j
and therr.al stress levels. TVA has identified this as an acceptable
)
resciution to the issue. Tre st:ff believes the depth and extent of the review tc be adecuate and concurs that installation of the snubber is j
acceptatie, and the rt;iace ant of the snutbet' is not necessary.
[
l i
)
8011220253 88;104 PDR AfOCK 05000327 P
FDL l
I i


7 2                                         L The corrective action has been tracked under terrective Action Track.ng Docurer: (CATD) 2211~ SON 01, and was reported as completed and verified for Secucyah Unit 1 on July 11, 1988.                                       ;
7 2
The proble- described in the CATD has also been tracxed by SCR SON CEB FE15. The piping analysis 0600104-15-01 was r',norted as completed and       ,
L The corrective action has been tracked under terrective Action Track.ng (CATD) 2211~ SON 01, and was reported as completed and verified Docurer:
verified in the Tracking and Reporting of Open Items (TROI) document dated September 12, 1958.
for Secucyah Unit 1 on July 11, 1988.
IV. CONCL US10'.                                                                 i The issue conc 3rning ER 22110 (B), Use of Snubbers, has been substantiated.
The proble-described in the CATD has also been tracxed by SCR SON CEB FE15.
The piping analysis 0600104-15-01 was r',norted as completed and verified in the Tracking and Reporting of Open Items (TROI) document dated September 12, 1958.
IV.
CONCL US10'.
i The issue conc 3rning ER 22110 (B), Use of Snubbers, has been substantiated.
The staff finds the licensee's corrective action to be adequate and acceptable for SON, Unit I restart.
The staff finds the licensee's corrective action to be adequate and acceptable for SON, Unit I restart.
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Latest revision as of 01:20, 7 December 2024

SER Supporting Employee Concern Element Rept 22110 (B), Use of Snubbers
ML20206G374
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 11/04/1988
From:
NRC OFFICE OF SPECIAL PROJECTS
To:
Shared Package
ML20206G037 List: ... further results
References
NUDOCS 8811220253
Download: ML20206G374 (2)


Text

_ - - -

i

,s. ' ' - c t.,'c.

UNITED STATES

/

NUCLEAR REGULATORY COMMISSION

! if, /b,f" i.

i wasmNotoN, o. c. 20sss a

k/

SAFET) EVALUATION REPORT BY THE OFFICE OF SPECIAL PROJECTS EMPLOYEE C0' CERN ELEMENT REPORT 22110 (B)

I i

USE OF SNUBBERS i

TENSESSEE VALLEY AUTHORITY SECUOVAH NUCLEAR POWER PLAET. UNIT 1 DOCKET NO.: 50-327 1.

STATEMENT Or EP:LOYEE C0' ctRN The basis for Element Repert 22110 (B), Rev.1. Dated December.'s0,1956 is enleyee cencern SQN.F.6-001-02 which states that the Upper 'ead d

injection Systen vertical riser requires a rigid support where a snubber a

was usec.

i

!!. SUw?M Y OF ISSUE

[

A rigid type sup; ort is specified in the piping analysis for a specific location on the vertical riser of the Upper Head Injectica (VHI) system, but the detail drawings and as-built condition show use of a snubber at this location.

UH! has a plant safety-related function.

!!!. EVALLATION l

In Merch 1986, this discrepancy was identified by TVA in a significant ccrdition report SCR SQN CEB 8615. Elernent report 22110 (B), Rev.1.

recognizec the empic In a subsequent letter J.A. McEenald (TVA) yee concern as valid.to B.J. Youngblood (NRC), Dated l

i i

responding to an NRC request for additional inforr.ation, the root cause of this disparity between thk pipe support analysih and the al built 2

1 concition was given as a lack of attention to detail, specifically, that Jn engineering judgeFent w3s made regarding support orientation and design I

without proper documentation and comunication to in erfacing groups.

t The letter also identified a 100t (nginee-ing revies of all snubbers in the plant against the piping analyses, and confirme this instance to be a single, isolatec case. The T'.A re-analysis (060v104 15 01) of the UH!

3 pipe restraint at this location utilizirig a snubber demonstrated the use of the snubber to be an adequate design, able to sustain required seismic j

and therr.al stress levels. TVA has identified this as an acceptable

)

resciution to the issue. Tre st:ff believes the depth and extent of the review tc be adecuate and concurs that installation of the snubber is j

acceptatie, and the rt;iace ant of the snutbet' is not necessary.

[

l i

)

8011220253 88;104 PDR AfOCK 05000327 P

FDL l

I i

7 2

L The corrective action has been tracked under terrective Action Track.ng (CATD) 2211~ SON 01, and was reported as completed and verified Docurer:

for Secucyah Unit 1 on July 11, 1988.

The proble-described in the CATD has also been tracxed by SCR SON CEB FE15.

The piping analysis 0600104-15-01 was r',norted as completed and verified in the Tracking and Reporting of Open Items (TROI) document dated September 12, 1958.

IV.

CONCL US10'.

i The issue conc 3rning ER 22110 (B), Use of Snubbers, has been substantiated.

The staff finds the licensee's corrective action to be adequate and acceptable for SON, Unit I restart.

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,