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| {{#Wiki_filter:From: Carson, Louis To: Werner, Greg; | | {{#Wiki_filter:From: Carson, Louis To: Werner, Greg; |
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| ==Subject:== | | ==Subject:== |
| River Bend LRW Spills in 2008 Date: Wednesday, FeOuIý18:31:48 AM Greg as Requested: | | River Bend LRW Spills in 2008 Date: Wednesday, FeOuIý18:31:48 AM Greg as Requested: |
| Description of abnormal release event: CWS Blowdown Line break.during LWS discharge January 17, 2008; 70,000 gallons CW plus 700 gal LRW.Groundwater samples: Groundwater samples for gamma radiation and tritium were taken in support of the GPI. These samples are not part of the REMP program. There were two leaks in 2008. These leaks are detailed in the abnormal release section of the Annual Effluent Report. In addition to these two leaks, one other incident occurred on 11/5/2008 while sampling a maintenance pit containing the sampled in 2008. The sample result showed Co-60 at 194 pCi/kg soil contamination and tritium at 2095 pCi/I.The licensee remediated the contamination. | | Description of abnormal release event: CWS Blowdown Line break. |
| Impact of event: At this time there are no impacts to the effluents program that would cause a change in current methodology. | | during LWS discharge January 17, 2008; 70,000 gallons CW plus 700 gal LRW. |
| This is not expected to be a continuing pathway for dose..considerations.-If any positive groundwater-samples are -ever-detected, then additional reviews will be performed and decisions made concerning ODCM changes or any remediation activities. | | Groundwater samples: Groundwater samples for gamma radiation and tritium were taken in support of the GPI. These samples are not part of the REMP program. There were two leaks in 2008. These leaks are detailed in the abnormal release section of the Annual Effluent Report. In addition to these two leaks, one other incident occurred on 11/5/2008 while sampling a maintenance pit containing the sampled in 2008. The sample result showed Co-60 at 194 pCi/kg soil contamination and tritium at 2095 pCi/I. |
| Remediation of event: The hole near the blowdown line break with standing water was pumped into barrels. The remainder of the water is considered to have made its way to the Mississippi River via Outfall 003 and Grants Bayou.Radioactive Contamination contents and level of event: Oniy tritium was detected in the water which leaked from the blowdown line. The maximum level detected in Outfall 003 was 28,043 pCi/L. At this time there is no drinking water pathway between the site and the Mississippi River. Tritium is no longer detected in Outfall 003.Impact on groundwater, if any: Groundwater sampling was performed. | | The licensee remediated the contamination. |
| Additional wells were also used to assist in characterizing any potential groundwater flow from this event. All results for gamma and H-3 were less than MDA.--A L.['SA RC Louis C. Carson, II Sr. Health Physicist US NRC RIV Division of Reactor Safety Plant Support Branch 2.Office No. 817.860.8221 aFx No. 817.860.8188 | | Impact of event: At this time there are no impacts to the effluents program that would cause a change in current methodology. This is not expected to be a continuing pathway for dose |
| .... -o------uis.Carson@ | | ..considerations.-If any positive groundwater- samples are -ever-detected, then additional reviews will be performed and decisions made concerning ODCM changes or any remediation activities. |
| M-C.GOV ,-----}}
| | Remediation of event: The hole near the blowdown line break with standing water was pumped into barrels. The remainder of the water is considered to have made its way to the Mississippi River via Outfall 003 and Grants Bayou. |
| | Radioactive Contamination contents and level of event: Oniy tritium was detected in the water which leaked from the blowdown line. The maximum level detected in Outfall 003 was 28,043 pCi/L. At this time there is no drinking water pathway between the site and the |
| | |
| | Mississippi River. Tritium is no longer detected in Outfall 003. |
| | Impact on groundwater, if any: Groundwater sampling was performed. |
| | Additional wells were also used to assist in characterizing any potential groundwater flow from this event. All results for gamma and H-3 were less than MDA. |
| | A L.['SA RC Louis C. Carson, II Sr. Health Physicist US NRC RIV Division of ReactorSafety Plant Support Branch 2. |
| | Office No. 817.860.8221 aFx No. 817.860.8188 |
| | .... M-C.GOV ,----- -o------uis.Carson@}} |
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Category:Environmental Monitoring Report
MONTHYEARRBG-48220, Submittal of 2022 Annual Radioactive Effluent Release Report2023-04-25025 April 2023 Submittal of 2022 Annual Radioactive Effluent Release Report RBG-48221, 2022 Annual Radiological Environmental Operating Report2023-04-25025 April 2023 2022 Annual Radiological Environmental Operating Report RBG-48149, 2021 Annual Radioactive Effluent Release Report2022-04-27027 April 2022 2021 Annual Radioactive Effluent Release Report RBG-48148, 2021 Annual Radiological Environmental Operating Report2022-04-27027 April 2022 2021 Annual Radiological Environmental Operating Report RBG-48136, Additional Information for the 2020 Annual Radioactive Effluent Release Report2021-11-12012 November 2021 Additional Information for the 2020 Annual Radioactive Effluent Release Report RBG-48137, Additional Information for the 2019 Annual Radioactive Effluent Release Report2021-11-12012 November 2021 Additional Information for the 2019 Annual Radioactive Effluent Release Report RBG-48093, Corrected 2020 Annual Radiological Environmental Operating Report2021-05-20020 May 2021 Corrected 2020 Annual Radiological Environmental Operating Report RBG-48074, Spent Fuel Storage Radioactive Effluent Release Report for 20202021-02-22022 February 2021 Spent Fuel Storage Radioactive Effluent Release Report for 2020 RBG-48019, 2019 Annual Radioactive Effluent Release Report2020-04-30030 April 2020 2019 Annual Radioactive Effluent Release Report RBG-47951, 2018 Annual Radioactive Effluent Release Report2019-05-0101 May 2019 2018 Annual Radioactive Effluent Release Report RBG-47952, 2018 Annual Radiological Environmental Operating Report2019-05-0101 May 2019 2018 Annual Radiological Environmental Operating Report RBG-47837, Spent Fuel Storage Radioactive Effluent Release Report for 20172018-02-26026 February 2018 Spent Fuel Storage Radioactive Effluent Release Report for 2017 RBG-47681, Annual Radiological Environmental Operating Report for 20152016-05-0202 May 2016 Annual Radiological Environmental Operating Report for 2015 RBG-47682, Annual Radioactive Effluent Release Report2016-05-0202 May 2016 Annual Radioactive Effluent Release Report ML16130A5612016-05-0202 May 2016 Submittal of Annual Radiological Environmental Operating Report for 2015 RBG-47563, Annual Radiological Environmental Operating Report for 20142015-05-0101 May 2015 Annual Radiological Environmental Operating Report for 2014 RBG-47562, Annual Radioactive Effluent Release Report for 20142015-05-0101 May 2015 Annual Radioactive Effluent Release Report for 2014 RBG-47544, Spent Fuel Storage Radioactive Effluent Release Report for 20142015-02-23023 February 2015 Spent Fuel Storage Radioactive Effluent Release Report for 2014 RBG-47360, Unit 1 - Annual Radiological Environmental Operating Report for 20122013-05-0101 May 2013 Unit 1 - Annual Radiological Environmental Operating Report for 2012 RBG-47359, Annual Radioactive Effluent Release Report for 20122013-05-0101 May 2013 Annual Radioactive Effluent Release Report for 2012 RBG-47358, Annual Individual Monitoring Report2013-04-22022 April 2013 Annual Individual Monitoring Report RBG-47343, Spent Fuel Storage Radioactive Effluent Release Report for 20122013-02-27027 February 2013 Spent Fuel Storage Radioactive Effluent Release Report for 2012 RBG-47237, Submittal of Radioactive Effluent Release Report for 20112012-04-30030 April 2012 Submittal of Radioactive Effluent Release Report for 2011 RBG-47238, Radiological Environmental Operating Report for 20112012-04-30030 April 2012 Radiological Environmental Operating Report for 2011 RBG-47141, Submittal of Annual Radiological Environmental Operating Report for 20102011-04-29029 April 2011 Submittal of Annual Radiological Environmental Operating Report for 2010 RBG-47142, Radioactive Effluent Release Report for 20102011-04-29029 April 2011 Radioactive Effluent Release Report for 2010 RBG-47025, Radioactive Effluent Release Report for 20092010-04-30030 April 2010 Radioactive Effluent Release Report for 2009 ML1012306272010-04-30030 April 2010 Submittal of Radiological Environmental Operating Report for 2009 RBG-47008, Submittal of Spent Fuel Storage Radioactive Effluent Release Report for 20092010-02-22022 February 2010 Submittal of Spent Fuel Storage Radioactive Effluent Release Report for 2009 ML1016200562010-02-10010 February 2010 Email from Louis Carson to Greg Werner, Subject: River Bend Lrw Spills in 2008 RBG-46912, Submittal of Radiological Environmental Operating Report for 20082009-04-30030 April 2009 Submittal of Radiological Environmental Operating Report for 2008 RBG-46911, Radioactive Effluent Release Report for 20082009-04-30030 April 2009 Radioactive Effluent Release Report for 2008 RBG-46891, Submittal of Spent Fuel Storage Radioactive Effluent Release Report for 20082009-02-26026 February 2009 Submittal of Spent Fuel Storage Radioactive Effluent Release Report for 2008 ML1016200552008-11-0505 November 2008 Entergy Condition Report CR-RBS-2008-06385 RBG-46806, Radiological Environmental Operating Report for 20072008-04-30030 April 2008 Radiological Environmental Operating Report for 2007 RBG-46812, Radioactive Effluent Release Report for January 1, 2007 Through December 31, 20072008-04-30030 April 2008 Radioactive Effluent Release Report for January 1, 2007 Through December 31, 2007 RBG-46691, Radioactive Effluent Release Report for 20062007-05-0101 May 2007 Radioactive Effluent Release Report for 2006 RBG-46660, Spent Fuel Storage Radioactive Effluent Release Report for 20062007-02-28028 February 2007 Spent Fuel Storage Radioactive Effluent Release Report for 2006 RBG-46603, Groundwater Protection Baseline Information2006-07-31031 July 2006 Groundwater Protection Baseline Information RBG-46561, Radiological Environmental Operating Report for 2005, River Bend Unit 12006-04-24024 April 2006 Radiological Environmental Operating Report for 2005, River Bend Unit 1 RBG-46432, Radioactive Effluent Release Report for 20042005-04-27027 April 2005 Radioactive Effluent Release Report for 2004 RBG-46431, Unit 1, Radiological Environmental Operating Report for 20042005-04-27027 April 2005 Unit 1, Radiological Environmental Operating Report for 2004 RBG-46265, Unit 1, Radioactive Effluent Release Report for 20032004-04-23023 April 2004 Unit 1, Radioactive Effluent Release Report for 2003 ML0411901262004-04-20020 April 2004 2003 Annual Effluent Release Report. RBG-46203, Annual Environmental Operating Report (Non-Radiological) for the Period August 29, 2002 to August 28, 20032003-11-26026 November 2003 Annual Environmental Operating Report (Non-Radiological) for the Period August 29, 2002 to August 28, 2003 RBG-46112, Radioactive Effluent Release Report for 2002., River Bend Station, Unit 12003-05-0101 May 2003 Radioactive Effluent Release Report for 2002., River Bend Station, Unit 1 RBG-45938, Radiological Environmental Operating Report for 20012002-04-29029 April 2002 Radiological Environmental Operating Report for 2001 2023-04-25
[Table view] Category:Memoranda
MONTHYEARML23047A3822023-03-21021 March 2023 Summary of December 15, 2022 Periodic Advanced Reactor Stakeholder Public Meeting ML22147A0932022-06-0606 June 2022 2021 Annual Assessment Public Meeting Summary ML21295A0882021-10-21021 October 2021 Fiscal Year 2021 Research and Test Reactors Inspection Program Completion Status ML21288A0392021-10-18018 October 2021 September 14, 2021, Summary of Public Workshop on Scale/Melcor Source Term Demonstration Project - Pebble-Bed Molten-Salt-Cooled Reactor ML21209A0222021-07-29029 July 2021 Closed Predecisional Enforcement Conference with River Bend Station ML21181A3352021-07-0101 July 2021 June 23, 2021, Summary of Public Meeting to Discuss Technology Inclusive Content of Application Project ML21158A2232021-06-0808 June 2021 Meeting Summary for Ticap Workshop 3 ML21140A3892021-05-24024 May 2021 Riv Column 1 EOC 2020 Public Meeting Summary ML21132A2952021-05-14014 May 2021 Summary of Public Meeting to Discuss Technology Inclusive Content of Application Project ML20150A4212020-11-23023 November 2020 Memo to File: Environmental Assessment and Finding of No Significant Impact and NRC Financial Analysis for Entergy Nuclear Company, LLC Decommissioning Funding Plan Submitted in Accordance with 10 CFR 72.30(b) and (C) for Grand Gulf ISFSI ML20155K8142020-11-23023 November 2020 Memo to File: Environmental Assessment and Finding of No. Significant Impact and NRC Financial Analysis for Entergy Operations, Inc., Decommissioning Funding Plan Submitted in Accordance with 10 CFR 72.30(b) and (C) River Bend ISFSI ML20107F7332020-04-27027 April 2020 Summary of April 3, 2020 Meeting with Industry Regarding Changes to Subsequent License Renewal Guidance Documents ML19204A1482019-07-15015 July 2019 FEMA Region VI Memo 07-15-19: Hurricane Barry Preliminary Capabilities Assessment ML18303A2832018-10-30030 October 2018 License Renewal Application ML18173A0082018-06-20020 June 2018 Cancelling Numerous Inspection Report Numbers ML18071A0182018-03-29029 March 2018 Telephone Call Summary RAI 3.2.2.3.2-1a Generic Filtration on 27FEB2018 v1_RBS Edits incorp._030618 ML17160A2042017-06-19019 June 2017 License Renewal Application Receipt FRN Transmittal Letter (Docket Id NRC-2017-0141) ML16088A2042016-03-28028 March 2016 Memo T Bowers from s Ruffin, Technical Assistance Requests - Review 2015 Tri-Annual Decommissioning Funding Plans for Multiple Independent Spent Fuel Storage Installations W/ Encl 2 (Template) ML16088A2052016-03-28028 March 2016 Enclosure 1 - (72.30 DFP Reviews to Be Completed 2015) - Memo T Bowers from s Ruffin, Technial Assistance Requests - Review 2015 Tri-Annual Decommissioning Funding Plans for Multiple Independent Spent Fuel Storage Installations ML15156A8602015-06-30030 June 2015 Safety Evaluation Input - Regarding Application for Change to Technical Specifications 3.8.1, AC Sources - Operating ML13322A4252013-11-25025 November 2013 Transmittal of Final River Bend Station Accident Sequence Precursor Analysis ML13266A3692013-10-0202 October 2013 J. Anderson Memo Request for Technical Assistance on License Amendment Request for Proposed Revision to Emergency Plan for Lacrosse Reactor ML1207500752012-06-13013 June 2012 Nsir/Dps/Mwsb Memo to NMSS Regarding Staff Review of the La Crosse Boiling Water Reactor Independent Spent Fuel Storage Installation Physical Security Plan and Verification of Additional Security Measures Incorporation ML1115704052011-06-0606 June 2011 Notice of Meeting with Entergy Operations, Inc., to Discuss Implementation of Quality Oversight and Verification Programs at Entergy Sites Including Actions Being Taken to Enhance Effectiveness ML1107504052011-03-21021 March 2011 Notice of Meeting with Entergy Operations, Inc., to Discuss Fleetwide Submittal for Proposed Technical Specification and Quality Assurance Program Manual Changes Related to Unit Staff Qualification Requirements ML1028709092010-10-18018 October 2010 Notice of Forthcoming Category 1 Public Meeting with Entergy Operation, Inc. to Discuss River Bend Preliminary Enforcement ML1006010322010-03-0101 March 2010 Cy 2009 Baseline Inspection Completion ML1016200562010-02-10010 February 2010 Email from Louis Carson to Greg Werner, Subject: River Bend Lrw Spills in 2008 ML0829002662008-10-16016 October 2008 Results of Acceptance Review for the River Bend Station, Unit 3 Combined License Application ML0807400842008-03-14014 March 2008 Draft Regulatory Guide for Comment ML0631102342006-11-0303 November 2006 Special Inspection Charter to Evaluate the Loss of Feedwater and Subsequent Reactor Trip at River Bend Station ML0614505922006-05-26026 May 2006 Wits 200600198 - Actions to Be Taken in Response to Hurricane Lessons Learned Task Report ML0607302642006-03-0707 March 2006 Closure Memorandum: Issue for Resolution 2005-083: Evaluation: Part 21 - Engine Systems - Governor Drive Coupling Element ML0529803962005-10-25025 October 2005 Notice of Meeting with Entergy and River Bend Staff Rbs'S Amendment Request for Use of Fuel Building Cask Handling Crane for Dry Spent Fuel Cask Loading Operations ML0516003452005-06-14014 June 2005 Draft Information Memo - May 6 - May 27, 2005 ML0429402412004-10-25025 October 2004 Draft Information for June 1, 2004 to June 30, 2004 ML0427806092004-10-0404 October 2004 Charter for Special Inspection Team at River Bend Station Reactor Scram with Complications ML0421103022004-08-19019 August 2004 Draft Information Memo for April, 2004 - Shirley ML0422602762004-08-12012 August 2004 Meeting Summary of the August 8, 2004 Public Workshop - Region IV Operator Licensing Feedback ML0408209032004-04-15015 April 2004 Draft Information Report from 01/08/04 to 01/31/04 ML0408206822004-04-13013 April 2004 Draft Information Input, Memo from 12/2/03 to 12/28/03 ML0330102972003-11-0707 November 2003 Draft Information for August 4, 2003, to October 2, 2003 ML0322601032003-08-18018 August 2003 Draft Information Inputs for June 3, 2003 to July 31, 2003 ML0311800392003-05-0707 May 2003 Draft Information Inputs for April 2003 (DLPM/LPDIV-1) ML0822807232003-03-18018 March 2003 R. H. Leyse PRMs ML0232401982002-11-20020 November 2002 Evaluation of the Risk Information Used to Support the River Bend Station Request to Modify Technical Specification Surveillance Requirements to Allow Division 3 EDG Testing During Any Mode of Plant Operation (TAC # MB5093) ML0231001312002-11-13013 November 2002 Memo Draft Documents for June 26, 2002 Through October 28, 2002 ML0226705082002-09-25025 September 2002 Meeting with Entergy Operations, Inc. Alternate Source Term License Amendment Application ML0226301922002-09-23023 September 2002 Meeting Canceled Between NRC & Entergy Operations, Inc. River Bend Alternative Source Term License Amendment Application ML0223405642002-09-0404 September 2002 Draft Information Inputs, Memo, from July 8, 2002 to July 25, 2002 2023-03-21
[Table view] |
Text
From: Carson, Louis To: Werner, Greg;
Subject:
River Bend LRW Spills in 2008 Date: Wednesday, FeOuIý18:31:48 AM Greg as Requested:
Description of abnormal release event: CWS Blowdown Line break.
during LWS discharge January 17, 2008; 70,000 gallons CW plus 700 gal LRW.
Groundwater samples: Groundwater samples for gamma radiation and tritium were taken in support of the GPI. These samples are not part of the REMP program. There were two leaks in 2008. These leaks are detailed in the abnormal release section of the Annual Effluent Report. In addition to these two leaks, one other incident occurred on 11/5/2008 while sampling a maintenance pit containing the sampled in 2008. The sample result showed Co-60 at 194 pCi/kg soil contamination and tritium at 2095 pCi/I.
The licensee remediated the contamination.
Impact of event: At this time there are no impacts to the effluents program that would cause a change in current methodology. This is not expected to be a continuing pathway for dose
..considerations.-If any positive groundwater- samples are -ever-detected, then additional reviews will be performed and decisions made concerning ODCM changes or any remediation activities.
Remediation of event: The hole near the blowdown line break with standing water was pumped into barrels. The remainder of the water is considered to have made its way to the Mississippi River via Outfall 003 and Grants Bayou.
Radioactive Contamination contents and level of event: Oniy tritium was detected in the water which leaked from the blowdown line. The maximum level detected in Outfall 003 was 28,043 pCi/L. At this time there is no drinking water pathway between the site and the
Mississippi River. Tritium is no longer detected in Outfall 003.
Impact on groundwater, if any: Groundwater sampling was performed.
Additional wells were also used to assist in characterizing any potential groundwater flow from this event. All results for gamma and H-3 were less than MDA.
A L.['SA RC Louis C. Carson, II Sr. Health Physicist US NRC RIV Division of ReactorSafety Plant Support Branch 2.
Office No. 817.860.8221 aFx No. 817.860.8188
.... M-C.GOV ,----- -o------uis.Carson@