ML20006D534: Difference between revisions

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                   .                    TENNESSEE VALLEY AUTHORITY
                   .                    TENNESSEE VALLEY AUTHORITY
       -                                            6N 38A Lookout Place February 7, 1990 U.S. Nuclear Regulatory Commission
       -                                            6N 38A Lookout Place February 7, 1990 U.S. Nuclear Regulatory Commission
Line 48: Line 47:
C 80nM aesA                                                U.S. UUCLE A A i t tuLATORY COMMittlON M      ED OMS M WW E XPGE S. 4/30?!2
C 80nM aesA                                                U.S. UUCLE A A i t tuLATORY COMMittlON M      ED OMS M WW E XPGE S. 4/30?!2
                     .            LICENSEE EVENT REPORT (LER)                                          ',8, 2 Tffo',,u" M N ol'f;? M ,To. cg g ,v y ga, gig TEXT CONTINUATlON                                            !?%"n'",'o',"T!'M'" !"Wi!M"c'#^/l35",'Me"f!
                     .            LICENSEE EVENT REPORT (LER)                                          ',8, 2 Tffo',,u" M N ol'f;? M ,To. cg g ,v y ga, gig TEXT CONTINUATlON                                            !?%"n'",'o',"T!'M'" !"Wi!M"c'#^/l35",'Me"f!
                                                                                                              '                                              ;
0?"tA/s'Ji" M t?"a',= i M & m ??ci 0F MANAGEMENT AND SUDGET WASHINGTON, DC 20603.        !
0?"tA/s'Ji" M t?"a',= i M & m ??ci 0F MANAGEMENT AND SUDGET WASHINGTON, DC 20603.        !
F ACILITY PIAME (1)                                                  DOCIL6T NUM0in (21                        LOR NUMSIR (Si                PA00 (3)
F ACILITY PIAME (1)                                                  DOCIL6T NUM0in (21                        LOR NUMSIR (Si                PA00 (3)

Latest revision as of 15:21, 17 February 2020

LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr
ML20006D534
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 02/07/1990
From: Bynum J, Hipp G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-90-001-01, LER-90-1-1, NUDOCS 9002140017
Download: ML20006D534 (5)


Text

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. TENNESSEE VALLEY AUTHORITY

- 6N 38A Lookout Place February 7, 1990 U.S. Nuclear Regulatory Commission

-ATTN -- Document Control Desk Washington :D.C. _20555 Gentlement TENNESSEE VALLEY AUTHORITY - SEQUOYAH NUCLEAR PLANT UNIT 1 - DOCKET NO.

50-327 - FACILITY OPERATING LICENSE DPR LICENSEE EVENT REPORT (LER) 50-327/90001' The enclosed LER provides details of an event wherein several essential raw cooling water valves' servicing safety-related equipment were not verified to be in the correct position at the required frequency. This event is being reported-in accordance with 10 CFR 50.73, paragraph a.2.1.

Very truly yours,

-TENNESSEE VALLEY AUTHORITY R. Bynum.. ice President' Nuclear Power Production Enclosure cc (Enclosure):

Regional Administration U.S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region II 101 Marietta Street, Suite 2900 Atlanta, Georgia 30323 INPO Records Center Institute of Nuclear Power Operations 1100 Circle 75 Parkway, Suite 1500 Atlanta, Georgia 30339 NRC Resident Inspector Sequoyah Nuclear Plant 2600 Igou Ferry Road Soddy Daisy, Tennessee 37379 9002140017 900207 I PDR ADOCK 05000327 S PDC ,,

I An Equal Opportunity Employer

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RgtORM 3es U.S. rUCL E A3 0.01ULA105Y CoeMissION APPROvtD OM6 NO WO44 e KPIRE8- 4'30'92 estiMATf D SURDEN PER Re$PON3E TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) ecI8M* NT ""s'UOAWDi'O A?"RitN $li&'Tt TO' e' REC Ei n'!v"L A N%' COJJ,t!a*W'7?" Rn L'n*TJJ '"

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F ACILtTV NAME til DOCatt NUMetR 436 PAGE[3i Ssquoyah Nuclear Plant, Unit 1 ol610lCl0l3l2l7 1 lOFl 014

"'* Essential raw cooling water valves servicing safety-related equipment not verified to be in-the correct position at the required frequency because of personnel error.

EVENT DAf t (El L E R NUMBE R tel REPORT DAf t m OTHE R F ACILITit$ INVDtVf D 181 MONTH t, A v ytAR vtAR D'Q' , 7],'"$ MONTH DAY vtAR C'LaT v havts DocatT huvatRtsi Sequoyah, Unit 2 0l5l0l010 13l218

~~ ~~

0l1 0l 8 9 0 9l 0 0l 0l 1 0l0 0 l2 0l7 9l0 0 isto toio n l l THis REPORT is susMitTED PuRsvANT TO THE RaOviRIME=T os 10 Cr R 0 rew* e* ., ..<e e, = roa .mas nu o,,,,,,,, l "00'

  • 1 20 4o2m 20 40stel son.H2H.6 n tim 20 406teH1Hal 50.36 teHil 50 73teH2Hel 73 711el no, i O0 i 20 40.Nn1H.,

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{ 60.73tell2 Hit 60.73teH2HviHHA) to 73tepl2HowHel 20 406teH1Havl SO 73teH2Hul .I 20 405teH1 Het 50.73 eH2 Hist, to 731eH2Ha, LICtN886 CONT ACT FOR THIS Lin (til N J.M t TE LEPHONE NUM88R ARE A COQt Gaof Hipp, Compliance Licensing Engineer 61115 8 l 41 31 -l 71716 16 COMPLt ?t ONE LINT FOR ( ACH COMPONENT F AILURE DESCRISED IN THl$ REPORT 113)

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n{0RTA Npn g LE CAu$$ SYSYtM COMPONENT "$$C gpp S I I I 1 l 1 1 I I I I 1 1 I I I I l l 1 I I I l i l l I SUPPLEMENTAL REPORT EXPtCTED (141 MONTH DAY vtAR Ytt lif ves compiere EXPLCTEO $VOMISSION CA TEI NO l l l A..mC T ,-,, ,, , . e. . . . e.,,. . -e-, ,.a.e ~e .,~e ,,-,v ,..e., 0.i At approximately 1700 Eastern standard time (EST) on January 8, 1990, with both Units 1 cnd 2 in Mode 1 at 100 percent power, it was discovered by the Unit i unit operator that the positions of several essential raw cooling water (ERCW) valves in the flowpath supplying the reactor containment building lower compartment vent coolers on both units ware not being periodically verified to be correct as required by technical cpecifications. The correct position of the valves was verified and documented on January 10, 1990. The applicable surveillance instruction (SI-33.1) was placed on administrative hold that same day until revision could be completed and approved. On Jsnuary 12, 1990, during a review of the in-progress Revision 18 of SI-33.1, four cdditional valves that should have been on the SI-33.1 checklists were identified. The correct position of these additional valves was verifled and documented on January 12, 1990. These valves were included in the SI-33.1 valve checklist in Ravision 18 along with the valves previously identified. The SI-33.1 revision was completed and approved on January 12, 1990. The root cause of this event has been attributed to personnel error during procedure revisions and during the review of workplans (WPs). As corrective action to prevent recurrence, an information notice has bsen issued to WP reviewers summarizing this event and reminding them of their rasponsibility for identifying procedure interfaces.

N AC Perm 364 (4697

C 80nM aesA U.S. UUCLE A A i t tuLATORY COMMittlON M ED OMS M WW E XPGE S. 4/30?!2

. LICENSEE EVENT REPORT (LER) ',8, 2 Tffo',,u" M N ol'f;? M ,To. cg g ,v y ga, gig TEXT CONTINUATlON  !?%"n'",'o',"T!'M'" !"Wi!M"c'#^/l35",'Me"f!

0?"tA/s'Ji" M t?"a',= i M & m ??ci 0F MANAGEMENT AND SUDGET WASHINGTON, DC 20603.  !

F ACILITY PIAME (1) DOCIL6T NUM0in (21 LOR NUMSIR (Si PA00 (3)

S:quoyah Nuclear Plant, Unit 1 vEA= " $0. =*J:

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0l 0 0l2 OF 0 l4 f TAT M nesse ansce de respeet we. edstemasmMC form Jmos1071 Description of Event At approximately 1700 Eastern standard time (EST) on January 8, 1990, with both Units 1 cnd 2 in Mode 1 at 100 percent power, 2,235 pounds per square inch gauge, 578 degrees Fahrenheit, it was discovered by the Unit 1 unit operator that the positions of several essential raw cooling water (ERCW) (EIIS Code BI) valves in the flowpath supplying the reactor containment building lower compartment vent coolers (EIIS Code BK) on both units ware not being periodically verified to be correct as required by technical specifications (TSs). Surveillance Requirement (SR) 4.7.4.a requires that the position of ERCW valves, which service safety-related equipment, be verified to be correct every 31 days for all manual, power-operated, or automatic valves not locked, sealed, or otherwise secured in position. This SR is typically satisfied by performance of Surveillance Instruction (SI) 33.1, "ERCW Valves Servicing Safety Related Equipment (Unit)." The valves initially discovered as not having their positions verified were 1-FCV-67-95 (servicing the Unit 1 lower compartment cooler group C) and 2-FCV-67-89, 90, 105, and 107 (servicing Unit 2 lower compartment cooler groups). Although the adequacy of the SI was in question, the physical flowpath was not. Flowpath continuity was confirmed on January 8, 1990, by the presence of normal temperatures on components in containment carrying heat loads. After confirming that the subject valves were not included in any other SI, the correct position of the valves was verified and documented on January 10, 1990. SI-33.1 was placed on administrative hold that same day until ravision could be completed and approved. On January 12, 1990, during a review of the in-progress Revision 18 of SI-33.1, four additional valves were identified that should also have been on the SI-33.1 checklists. These valves were l-FCV-67-523B, 577B, 2-FCV-67-523B, and 577B, which supply the B train lower compartment vent cooler groups on both units. The correct position of these additional valves was verified and documented on January 12, 1990. These valves were included in tt.e SI-33.1 valves checklist in Revision 18 along with the valves previot. sly ident.fied. The SI-33.1 revision was completed and approved on January 12, 1990.

Ceuse of Event The root cause of this event has been attributed to perssnnel error during procedure revisions and during the review of workplans (WPs). A personnel error in the preparation of the procedure revision package for Revision 14 of SI-33.1 resulted in the failure to verify the position of Valve 1-FCV-67-95. This revision, in August 1988, followed the replacement of check valves in the ERCW supply lines to the lower compartment vent coolers on Unit I with motor-operated valves (MOVs). The revision erroneously identified FCV-67-95 as a Unit 2 only valve, thus omitting 1-FCV-67-95 from the SI-33.1 checklist. This error was not identified by the independent qualified reviewer (IQR) or by the cross-disciplinary reviewer (CDR) during processing of the revision package.

A personnel error during the review of the WP that replaced the lower compartment vent cooler ERCW supply check valves with MOVs on Unit 2 resulted in the failure to revise SI-33.1 to include Valves 2-FCV-67-89, 90, 105, and 107, and, consequently, the failure to verify the position of these valves at the required frequency following installation. Review and approval of WPs is administered under Administrative Instruction (AI) 19, Part IV, " Plant Modifications: After Licensing," and AI-19, CRC Feeim 306A (6&H

FORM 306A U S. NUCLlut s,t AUL .TM,Y COMMISSION EX,13f 8 4f300 u

"8E.M"ol'@l's,Mo epi;4v ,gw,inig

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. LICENSEE EVENT REPORT (LER) ,'Q"^,'A"o'o TEXT CONTINUATION CJ"4*,s"@%"oWf'.MflcO,'!M".' "'s"f!

T,,'a".'on"R&#M'Elen?13.c o PM:??ci OF MANAGEMENT AND BUDGif, WASHINGTON.DC 70603 FACILITY NAMG (1) DOCKEi NUMSER (21 gga gyggER (6) PA04 (3)

S2quoyah Nuclear Plant, Unit i vtaa " = P,P Tfeit o l5 l0 l0 j o ] 3 l 217 9]O -

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0l0 0l3 0F 0 l4 ftXT W more ansce e revues ( use espoust NRC Fame JWCsHIM C$use of Event (Continued)-

Part VI, " Modifications: Permanent Design Change Control Program." The review process eslies upon the experience of the reviewer and is dependent upon personnel recognizing the impact of the modification on plant instructions. Review of a WP for instruction revisions can occur at two stages. Any instructions requiring revision because of a modification are supposed to be identified during the first review by the respective section reviewers. If the reviewer does not identify any instruction changes related to the modification, the section will not have any additional opportunity to revise their instructions. During the procedure revision process, a section has the opportunity to complete an in-depth review of the modification's impact on its instructions. This 1 sscond review results in development of the instruction revision package during which cdditional instructions may be identified as being affected by the modification. If additional instructions are identified, revision packages are developed for them at that time. In the case of the ERCW valve modification on Unit 2, neither review identified SI-33.1 as an instruction requiring revision.

Analysis of Event This event is being reported in accordance with 10 CFR 50.73, paragraph a.2.1, as an oparation prohibited by technical specifications because the requirements of SR 4.7.4.a '

wsre not met.

The ERCW system is described in Section 9.2.2 of the SQN Updated Final Safety Analysis Rsport (UFSAR). The lower compartment air cooling system is described in Section 9.4.8 l of the UFSAR. The lower compartment vent coolers are one of three coolers in each of

the four lower compartment cooler groups. Each lower compartment cooler group is comprised of one reactor coolant pump motor cooler, one control rod drive motor cooler, l end one lower compartment vent cooler. These coolers are required to be in operation in

! v:rious combinations during plant operations to maintain component temperatures within l limits. The lower containment vent coolers are required to be operable by TS Limiting Condition for Operation 3.6.2.2. These coolers are required to ensure that adequate hsat removal capacity is available to provide long-term cooling following a non-LOCA (loss of coolant accident) event. Postaccident use of these coolers ensures containment i tcmperatures remain within environmental qualification limits for safety-related equipment.

l All of the ERCW valves that were discovered in this event t.o have not been periodically i varified to be in the correct position were, in fact, found to be in the correct l position when checked on January 10, 1990, and January 12, 1990. These valves had been I

parforming their normal operational functions and were capable of performing their postaccident functions as well. Therefore, there was no adverse effect on the health and safety of the public or plant personnel.

NRC Form 3esA (6496

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EXFlXtl 4/30/92

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. LICENSEE EVENT REPORT (LER) L8'gh',',%8ui8M ","ol'A;sti,' .0 fT.' ,T"J"'s TEXT CONTINUATION 1&,t,'o'."! MN"d OMP'."If/c'*f4'3R 'u"s' "'ic EA PAPERWO ME , ION JC (3 0 0 IC OF MANAGEMENT AND DVDGET WASHINGTON, DC 20603.

, ACitaTY NAME (1) DOCit4T NVMDER (2) LtR huheeth (6) PA06 (3l

-Ssquoyah Nuclear Plant, Unit 1 " ' " " W h" 0'YeU q o ls jo jo jo l3j 2l 7 9l0 -

0[ 0l 1 0l0 0l4 OF 0l4 flNT (# nesse sysse de reeu*our, use setteenst MIC Fwm mii17)

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Corrective Action i

The immediate action taken on January 10, 1990, and on January 12, 1990, was to verify the affected valves were in the correct position and document that verification.

SI-33.1 was placed on administrative hold on January 10, 1990, until revision could be completed and approved on January li, 1990.

As corrective action to prevent recurrence, an information notice has been issued to WP' reviewers summarizing this event and reminding them of their responsibility for  ;

identifying procedure interfaces.

Additional Information There have been two previous reported occurrences of a failure of sis to completely fulfill SRs as a result of personnel error during the procedure revision process (LERs 50-327/84040 and 50-328/86006) and two previously reported occurrences of a failure of sis to completely fulfill SRs as a result of personnel error while processing WPs (LERs 50-327/87008 and 50-328/88002). These occurrences are believed to have been isolated occurrences without any connection to this event.

Commitments None.

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