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{{#Wiki_filter:NRC FisIsssM 366 I7.77 I U.S.NUCLEAR REGULATORY COMMISSION t 79-015/03L-0 LICENSEE EV ENT REPORT'~O 7 8 CON'T ,"~O'1, 7 8 ,'~0'Qi (PLEASE P 6 0-0 0 0 0 0-0 0 Qs4 1 1 1 1 ps~ps 25 26 LICENSE TYPE 30 57 CAT 58 air lock was not tested until 12/26/79~This exceeded the 48 hour re uirement of CONTROL BLOCK: AINT OR TYPE ALL REQUIRED INFORMATION)
{{#Wiki_filter:NRC FisIsssM 366 I7.77 I CONTROL BLOCK:
I NY RE G1Q20 9 LICENSEE CODE 14 15 LICENSE NUMBER~LQB 0 5 0 0 0 2 4 4 7 1 2 2 3 7 9 8 0 1 2 2 8 0 Qg 60 61 DOCKET NUMBER'8 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO An at power containment entry was made on 12/23/79 but the containment personnel Tech.Spec.4.4.2.4.The test on 12/26/79 was acceptable.
I t       6 Qi 79-015/03L-0 LICENSEE EV ENT REPORT (PLEASE    P AINT OR U. S. NUCLEAR REGULATORY COMMISSION TYPE ALL REQUIRED INFORMATION)
'~OS~O7 80 7 8 9 g personnel air lock is open.A new procedure in check off form requires this notifica-SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~SA Q1>D Qa~ZQ>>R E N E T R Q4~AQ>>~Z Qis 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERiRO EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REPORT~79~~Q2 5~m~03~E~~0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATI'ACHMENT NPRDP PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER Qlll~~ping gpss~Z p>>0 0 0 0~N pss gpss~A pss C 3 1 0 p;33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o The existing procedure does not re uire notification of test and results ersonnel when 2 tion.3~l4 7 8 9 FACILITY STATUS%POWER OTHER STATUS QSO E 1 0 0 NA s Qs~Qs 7 8 9 10 12 13 44 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY 6~Z Q33~2Q34 NA 7 8 9 10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q3g~00 0 P'~ZP'8 9 11 12 13 PERSONNEL INJURIES METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32 Q31 Review of plant activities 45 46 LOCATION OF RELEASE Q3 NA 45 80 80 80 80 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION
  '~O 7         8   9 NY          RE LICENSEE CODE G1Q20    14      15 0   0         0   0     0 LICENSE NUMBER 0     -   0     0 25 Qs4 26 1     1   1 LICENSE TYPE 1
[ii~]Z Qss NA 7 8 9 10 PUBLICITY ISSUED DESCRIPTION Q~2~~NQ44 NA 8 9 io NRC USE ONLY 80 80 NAME OF PREPARER Carl H.Peck 68 69 80 ss PHQNE.716/546-2700, ext.291-205 0}}
30 ps~ps 57 CAT 58 7
CON'T
  "~O'1,
  '~0' 8
                                      ~LQB 60          61 0     5 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES 0   0   0 DOCKET NUMBER 2
                                                                                    '8 4   4 QIO 7
An at power containment entry was made on 12/23/79 but the containment personnel 69 1   2     2 EVENT DATE 3     7     9 74 8
75 0     1     2 REPORT DATE 2   8   0 80 Qg air lock was not tested until 12/26/79                                   ~    This exceeded the 48 hour re uirement of Tech. Spec.               4.4.2.4.             The   test on 12/26/79 was acceptable.
    '~OS
    ~O7 7         8 9                                                                                                                                                                       80 SYSTEM               CAUSE         CAUSE                                                           COMP.           VALVE CODE               CODE       SUBCODE                   COMPONENT CODE                       SUBCODE           SUBCODE g                          ~SA           Q1>         D   Qa   ~ZQ>>               R     E     N     E   T     R Q4           ~AQ>>             ~Z     Qis 7         8                       9           10           11           12             13                                 18           19               20 SEQUENTIAL                           OCCURRENCE             REPORT                       REVISION Q17 LERiRO REPORT ACTION FUTURE EVENT YEAR
                                        ~79 21        22 EFFECT
                                                                ~
23 SHUTDOWN
                                                                              ~Q2 24 REPORT NO.
5 26
                                                                                                        ~m 27
                                                                                                                      ~03 28 ATI'ACHMENT CODE 29 NPRDP TYPE
                                                                                                                                                ~E 30 PRIME COMP.
                                                                                                                                                                ~
31 NO.
                                                                                                                                                                              ~0 32 COMPONENT TAKEN ACTION                   ON PLANT           METHOD                 HOURS Q22           SUBMITTED           FORM SUB.         SUPPLIER             MANUFACTURER Qlll ~~     ping       gpss               ~Z p>>             0   0     0     0       ~N     pss         gpss             ~A     pss         C 3       1 0   p; 33         34                 35                 36             37                     40     41                 42               43               44             47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o         The existing procedure does not re uire                                       notification of test and results ersonnel when personnel air lock is open. A new procedure in check off form requires this notifica-2           tion.
3
    ~l4 7         8   9                                                                                                                                                                     80
                                  ~Qs FACILITY                                                                       METHOD OF STATUS             % POWER                       OTHER STATUS QSO           DISCOVERY                                  DISCOVERY DESCRIPTION Q32 s          E Qs          1     0     0                       NA                               Q31    Review of plant activities 7       8   9               10               12       13                           44       45          46                                                                        80 ACTIVITY CONTENT RELEASED OF RELEASE                           AMOUNTOF ACTIVITY                                                            LOCATION OF RELEASE        Q3 6       ~Z     Q33     ~2Q34                               NA                                                                NA 7       8   9               10           11                                         44             45                                                                            80 PERSONNEL EXPOSURES NUMBER               TYPE         DESCRIPTION Q3g
                  ~00           0   P'~ZP' 8   9               11       12           13                                                                                                                             80 PERSONNEL INJURIES 7         8   9               11       12                                                                                                                                           80 LOSS OF OR DAMAGE TO FACILITY               43 TYPE         DESCRIPTION
[ii~]
7         8   9 Z  Qss 10 NA 80 PUBLICITY
  ~2     ~
ISSUED
                  ~NQ44 DESCRIPTION      Q                    NA NRC USE ONLY 8   9           io                                                                                                                       68    69                          80 ss NAME OF PREPARER                         Carl H. Peck                                                   PHQNE. 716/546-2700, ext. 291-205
 
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Latest revision as of 10:04, 4 February 2020

LER 79-025/03L-0:on 791223,containment Entry Was Made But Personnel Air Lock Not Tested Until 791226,exceeding 48-h Tech Spec Requirement.Caused by Existing Procedural Inadequacy
ML17261A165
Person / Time
Site: Ginna Constellation icon.png
Issue date: 01/22/1980
From: Peck C
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17249A507 List:
References
LER-79-025-03L, LER-79-25-3L, NUDOCS 8001280246
Download: ML17261A165 (2)


Text

NRC FisIsssM 366 I7.77 I CONTROL BLOCK:

I t 6 Qi 79-015/03L-0 LICENSEE EV ENT REPORT (PLEASE P AINT OR U. S. NUCLEAR REGULATORY COMMISSION TYPE ALL REQUIRED INFORMATION)

'~O 7 8 9 NY RE LICENSEE CODE G1Q20 14 15 0 0 0 0 0 LICENSE NUMBER 0 - 0 0 25 Qs4 26 1 1 1 LICENSE TYPE 1

30 ps~ps 57 CAT 58 7

CON'T

"~O'1,

'~0' 8

~LQB 60 61 0 5 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES 0 0 0 DOCKET NUMBER 2

'8 4 4 QIO 7

An at power containment entry was made on 12/23/79 but the containment personnel 69 1 2 2 EVENT DATE 3 7 9 74 8

75 0 1 2 REPORT DATE 2 8 0 80 Qg air lock was not tested until 12/26/79 ~ This exceeded the 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> re uirement of Tech. Spec. 4.4.2.4. The test on 12/26/79 was acceptable.

'~OS

~O7 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE g ~SA Q1> D Qa ~ZQ>> R E N E T R Q4 ~AQ>> ~Z Qis 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Q17 LERiRO REPORT ACTION FUTURE EVENT YEAR

~79 21 22 EFFECT

~

23 SHUTDOWN

~Q2 24 REPORT NO.

5 26

~m 27

~03 28 ATI'ACHMENT CODE 29 NPRDP TYPE

~E 30 PRIME COMP.

~

31 NO.

~0 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER Qlll ~~ ping gpss ~Z p>> 0 0 0 0 ~N pss gpss ~A pss C 3 1 0 p; 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o The existing procedure does not re uire notification of test and results ersonnel when personnel air lock is open. A new procedure in check off form requires this notifica-2 tion.

3

~l4 7 8 9 80

~Qs FACILITY METHOD OF STATUS  % POWER OTHER STATUS QSO DISCOVERY DISCOVERY DESCRIPTION Q32 s E Qs 1 0 0 NA Q31 Review of plant activities 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY LOCATION OF RELEASE Q3 6 ~Z Q33 ~2Q34 NA NA 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q3g

~00 0 P'~ZP' 8 9 11 12 13 80 PERSONNEL INJURIES 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION

[ii~]

7 8 9 Z Qss 10 NA 80 PUBLICITY

~2 ~

ISSUED

~NQ44 DESCRIPTION Q NA NRC USE ONLY 8 9 io 68 69 80 ss NAME OF PREPARER Carl H. Peck PHQNE. 716/546-2700, ext. 291-205

0