ML17263A352: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(3 intermediate revisions by the same user not shown)
Line 3: Line 3:
| issue date = 08/06/1993
| issue date = 08/06/1993
| title = LER 93-004-00:on 930707,Main Feedwater Isolations Occurred Due to Secondary Side & Condensate Feedwater Pressure Transient.Returned Feedwater Regulating Valves to pre-event Controls configuration.W/930806 Ltr
| title = LER 93-004-00:on 930707,Main Feedwater Isolations Occurred Due to Secondary Side & Condensate Feedwater Pressure Transient.Returned Feedwater Regulating Valves to pre-event Controls configuration.W/930806 Ltr
| author name = BACKUS W H, MECREDY R C
| author name = Backus W, Mecredy R
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:ACCELERATED DOCUMENTDISTRIBUTION SYSTEMREGUL>RYINFORMATION DISTRIBUTE SYSTEM(RIDE)ACCESSION NBR:9308120083 DOC.DATE:
{{#Wiki_filter:ACCELERATED DOCUMENT DISTRIBUTION SYSTEM REGUL>RY      INFORMATION DISTRIBUTE         SYSTEM (RIDE)
93/08/06NOTARIZED:
ACCESSION NBR:9308120083             DOC.DATE: 93/08/06      NOTARIZED: NO          DOCKET  ¹ FACIL 50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester                   G 05000244 AUTH. NAME          AUTHOR AFFILIATION BACKUS,W.H           Rochester Gas a Electric Corp.
NOFACIL50-244RobertEmmetGinnaNuclearPlant,Unit1,Rochester GAUTH.NAMEAUTHORAFFILIATION BACKUS,W.H Rochester GasaElectricCorp.MECREDY,R.C Rochester Gas6ElectricCorp.RECIP.NAME RECIPIENT AFFILIATION
MECREDY,R.C         Rochester Gas 6 Electric Corp.
RECIP.NAME           RECIPIENT AFFILIATION I  i


==SUBJECT:==
==SUBJECT:==
LER93-004-00:on 930707,Main feedwater isolations occurredduetosecondary side6condensate feedwater pressuretransient.
LER    93-004-00:on 930707,Main feedwater isolations occurred                          1 I
Returnedfeedwater regulating valvestopre-event controlsconfiguration.W/930806 ltr.DISTRIBUTION CODE:ZE22TCOPIESRECEIVED:LTR tENCLrSIZE:LOTITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
to secondary side 6 condensate feedwater pressure 1
DOCKET¹05000244Ii1I1DlSl'.05000244ARECIPIENT IDCODE/NAME PD1-3LAJOHNSON,A INTERNAL:
due                                                                                  Dl transient. Returned feedwater regulating valves to pre-event controls configuration.W/930806             ltr.                                     S DISTRIBUTION CODE: ZE22T          COPIES RECEIVED:LTR       t ENCL r    SIZE: LO TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.                             l  '.
ACNWAEOD/DSP/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRIL/RPEB NODSSA/+PLB-BP02RGHlFILE01EXTERNAL:
NOTES:License Exp date      in accordance with 10CFR2,2.109(9/19/72).               05000244  A RECIPIENT              COPIES              RECIPIENT          COPIES              D ID CODE/NAME            LTTR ENCL        ID CODE/NAME       LTTR ENCL PD1-3 LA                    1      1      PD1-3 PD              1    1            D JOHNSON,A                   1      1 INTERNAL: ACNW                        2      2      AEOD/DOA              1    1 AEOD/DSP/TPAB               1      1      AEOD/ROAB/DSP          2    2 NRR/DE/EELB                 1      1      NRR/DE/EMEB            1    1 NRR/DORS/OEAB               1      1      NRR/DRCH/HHFB          1    1 NRR/DRCH/HICB                1      1      NRR/DRCH/HOLB          1    1 NRR/DRIL/RPEB                1      1      NRR/DRSS/PRPB         2    2 NODS SA/+PLB
EGGGBRYCE,J.H NRCPDRNSICPOORE,W.COPIESLTTRENCL11112211111111111111112'1111RECIPIENT IDCODE/NAME PD1-3PDAEOD/DOAAEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB LSTLOBBYWARDNSICMURPHYFG.A NUDOCSFULLTXTCOPIESLTTRENCL111122111111221111111111DD$DDNOTETOALL"RIDS"RECIPIENTS:
                  -BP 1      1      NRR/DSSA/SRXB         1    1 02          1      1      RES/DSIR/EIB           1    1 RGHl      FILE  01          1      1 EXTERNAL: EGGG BRYCE,J.H                2            L ST LOBBY WARD        1    1 NRC PDR                      1      1      NSIC MURPHYFG.A       1    1 NSIC POORE,W.                1      1      NUDOCS FULL TXT        1    1 D
PLEASEHELPUSTOREDUCEWASTEICONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065)
D D
TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!DFULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
NOTE TO ALL"RIDS" RECIPIENTS:
LTTR30ENCL30
PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR                30  ENCL    30


rrrnrNr1/r/trl/rr
rrrnrNr1/r/trl/rr //i//// > rr,
//i////>rr,//'/I/'i"Ii//,''i'"
                                          //'/
i!C!i)ivir~ill!II I/l'lrir, r!r/ROCHESTER GASANDELECTRICCORPORATION
I/ 'i" Ii//,''i'" i                                                                                    ";- ',Toe/r .,
~";-',Toe/r.,state"89EASTAVENUE,ROCHESTER N.K14649-0001 ROBERTC.MECREOYVicePresident ClnnattuclearProduction TELEPHONE ARE/1COOE7165rt62700August6,1993U.S.NuclearRegulatory Commission DocumentControlDeskWashington, DC20555
      !C!i)ivir~ill!III/l'lrir,r! r/
state" ROCHESTER GAS AND ELECTRIC CORPORATION                                ~  89 EAST AVENUE, ROCHESTER N. K 14649-0001 ROBERT C. MECREOY                                                                                        TELEPHONE Vice President                                                                                    ARE/1 COOE 716 5rt6 2700 Clnna ttuclear Production August 6, 1993 U.S. Nuclear Regulatory Commission Document                                Control Desk Washington,                                 DC  20555


==Subject:==
==Subject:==
LER93-004,Feedwater ControlPerturbations, DueToASecondary SideTransient, CausesSteamGenerator HighLevelFeedwater Isolations R.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordance with10CFR50.73,LicenseEventReportSystem,item(a)(2)(iv),
LER  93-004, Feedwater Control Perturbations, Due To A Secondary Side Transient, Causes Steam Generator High Level Feedwater Isolations R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, License Event Report System,                               item (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered                                    Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached event report LER 93-004 i:s hereby submitted.
whichrequiresareportof,"anyeventorcondition thatresultedinmanualorautomatic actuation ofanyEngineered SafetyFeature(ESF),including theReactorProtection System(RPS)",theattachedeventreportLER93-004i:sherebysubmitted.
This event has in no way affected the public's health and safety.
Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,xcoRobertC.MecedyU.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector
Very  truly  yours, Robert C. Mec edy xco                            U.S. Nuclear Regulatory Commission Region I 475        Allendale  Road King of Prussia,         PA 19406 Ginna        USNRC  Senior Resident Inspector
~rn.h9308i20083 930806PDR*DOCK050002448PDR
                                                    ~r n.h 9308i20083 930806 PDR            *DOCK                          05000244 8                                                PDR


NRCFORM366(669)V.S.NUCLEARREGULATORY COMMISSILICENSEEEVENTREPORT(LER)APPROVEDOMBNOA31506104 EXPIRESI4/30/92ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFOAMATION COLLECTION REQUEST:50.0HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANORFPORTSMANAGEMENT BRANCH(F630),V.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTOTHEPAPERWORK REDUCTION PROJECT(31500'l04).
NRC FORM 366                                                                    V.S. NUCLEAR REGULATORY COMMISSI (669)                                                                                                                                           APPROVED OMB NOA31506104 EXP IR ESI 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFOAMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER)                                                                  COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS ANO RFPORTS MANAGEMENT BRANCH (F630), V.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500'l04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, OC 20503.
OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, OC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBERl2)PAE05000244iOFOFeewaterControerturatons,DueToSeconaryTransent,ausesteamGenerator HighLevelFeedwater Isolations EVENTDATE(5)MONTHDAYYEARYEARLERNUMBER(61:SEQUENTIAL NUMBERREVISIONNUMBERREPORTDATELT)MONTHDAYYEARDOCKETNUMBERIS) 05000FACII.ITV NAMES01'HERFACILITIES INVOLVED(6)0-7793930040008069305000OPERATING MODE(9)NPOWERLEYEL09760n(sl(2)Is>>)50.n(v)(2)
FACILITY NAME (1)                                                                                                                         DOCKET NUMBER l2)                            PA E R.E. Ginna Nuclear Power Plant                                                                                                            0 5    0  0    02        44 iOFO Fee water Contro                            ertur at ons, Due To Secon ary Trans ent,                                                   auses          team Generator High Level Feedwater Isolations EVENT DATE (5)                       LER NUMBER (61                           REPORT DATE LT)                             01'HER FACILITIES INVOLVED (6)
Nl5073(s)(2)lvsl)50.73(v)(2)
: SEQUENTIAL          REVISION MONTH    DAY      YEAR      YEAR                                                            DAY        YEAR          FACII.ITVNAMES                    DOCKET NUMBERIS)
(vill)(Al50.73(v)l2l(vill)(B) 50.73(~)(2)lsl0THERLQUIAEMENTS OF10CFR((:/ChockonoormoroOltrssIollovrinP/
NUMBER        NUMBER MONTH 0    5    0      0      0 0-7          79 393                            0 0      4        0 0 0            806 93                                                                0    5    0      0      0 THIS REPORT IS SVBMITTFD PUASVANT T0 THE RLQUIAEMENTS OF 10 CFR ((: /Chock ono or moro Ol trss IollovrinP/ (11)
(11)THISREPORTISSVBMITTFD PUASVANTT20.402(B) 20.405(~)(1)(I)20.405(s)l1)(NI20.406(~I('IHill)20405(s)(1)(lv) 20.405(sI(I)(vl20.405(c) 60M(s)(II 50.36(~)(2)60.73(sl(2((ll 50.73(s)(2)(ill50.73(s)(2)(ill)73,71(B)73.71IclOTHERISpscilyIn4osnocttN/oENonr/lnTssI,HRCForm3664/LICENSEECONTACTFORTHISLEA(12INAMEWesleyH.Backus.Technical Assistant totheOperations ManaerTELEPHONE NUMBERAREACODE315524-4446COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAVSESYS'EMCOMPONENT MANUFAC.TVRERREPORTABLE TONPADSPjQgCAUSESSTEMXj'>>AA'RC~C.3>>">>T>>~'"IKU'::hl.'.@<COMPONENT MANUFAC.TVREREPORTABLE TONPROS?>>o.>>...%R.:.R6)SA'NO4PcA.N::SUPPLEMENTAL REPORTEXPECTEDllc)YESIlly<<,compiotsEXPECTEDSl/SSI/SSION DATE/NOAssTRAcTI(.imitto/400spscsr,l.s.,spproslmsrsly lilusntinpis.rpocs typssvrinon
OPERATING MODE (9)           N        20.402(B)                                  20.405(c)                              60 n(sl(2) Is>>)                           73,71(B)
/inos/(16)EXPECTFDSUBMISSION DATE(15)MONTHDAYYEAROnJuly7,1993-atapproximately 0915EDST,withthereactoratapproximately 974fullpower,mainfeedwater isolations occurredonthe"BFISteamGenerator (S/G).Thesefeedwater isolations werecausedbyoverfeeding the"B"S/G,following asecondary sidecondensate andfeedwater pressuretransient.
POWER                            20.405( ~ )(1)(I)                           60M(s)(II                              50.n(v)(2) Nl                              73.71 I cl LEYEL 0 9 7              20.405 (s ) l1 ) (NI                        50.36( ~ )(2)                           50 73(s)(2) lvsl)                          OTHER ISpscily In 4osnoct tN/oEN onr/ ln Tss I, HRC Form 20.406( ~ I ('I Hill)                       60.73(sl(2((ll                          50.73(v)(2) (vill)(Al                    3664/
Immediate operatoractionwastomanuallycontroltheFeedwater Regulating Valves(FRVs)torestoretheS/Gwaterlevelsandstabilize theplant.Theimmediate causeoftheeventwasduetoasecondary sidecondensate andfeedwater pressuretransient.
20405(s)(1)(lv)                             50.73(s) (2)(ill                        50.73(v)l2l(vill)(B) 20.405(s  I (I)(vl                          50.7 3(s) (2) (ill)                    50.73( ~ )(2)lsl LICENSEE CONTACT FOR THIS LEA (12I NAME                                                                                                                                                      TELEPHONE NUMBER AREA CODE Wesley H. Backus.
Theunderlying causeoftheeventwasdetermined tobenotisolating the5Aheaterhighleveldumpvalvepriortotrouble-shooting.
Technical Assistant to the Operations                                                  Mana        er                                  3    155 24- 444                                  6 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
(ThiseventisNUREG-1022 (X)CauseCode).Corrective actionstakenorplannedarediscussed inSectionVofthetext.NRCForm366(669)  
CAVSE SYS'EM        COMPONENT MANUFAC.
TVRER REPORTABLE TO NPADS            PjQg                  CAUSE S STEM  COMPONENT MANUFAC.
TVRER EPORTABLE TO NPROS
                                                                                                                                                                                ?>>o.>>... %R .:. R6)
SA'NO Xj
                                                                              ">>T>>~'
AA  'RC~C.
                                                                                          " IKU '
3>>                                                                      4      PcA. N::
::hl  .'.            @<
SUPPLEMENTAL REPORT EXPECTED              llc)                                                                   MONTH          DAY    YEAR EXPECTFD SUBMISSION DATE (15)
YES Illy<<, compiots EXPECTED Sl/SSI/SSION DATE/                                           NO AssTRAcT I(.imit to /400 spscsr, l.s., spproslmsrsly lilusn tinpis.rpocs typssvrinon /inos/ (16)
On      July 7, 1993 -at approximately 0915 EDST, with the reactor at approximately 974 full power, main feedwater isolations occurred on the "BFI Steam Generator (S/G).                                                                     These feedwater isolations were caused by overfeeding the "B" S/G, following a secondary side condensate and feedwater pressure transient.
Immediate operator action was to manually control the Feedwater Regulating Valves (FRVs) to restore the S/G water levels and stabilize the plant.
The immediate cause of the event was due to a secondary side condensate and feedwater pressure transient.
The underlying cause of the event was determined to be not isolating the 5A heater high level dump valve prior to trouble-shooting. (This event is NUREG-1022 (X) Cause Code).
Corrective actions taken or planned are discussed in Section V of the text.
NRC Form 366 (669)


NRCFORM388A(SJ)9)US.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORT(LER)TEXTCONTINUATION APPROVEDOMBNO.3(504)04EXPIRES:4/30/92ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUEST:508)HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(F430),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTO1HEPAPERWORK REDUCTION PROJECT(31500)08),
NRC FORM 388A                                                        US. NUCLEAR REGULATORY COMMISSION (SJ)9)                                                                                                               APPROVED OMB NO. 3(504)04 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE              ENT REPORT (LER)                              INFORMATION COLLECTION REOUEST: 508) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION                                              AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500)08), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20503.FACILITYNAME(llDOCKETNUMBER(2)YEARLERNUMBER(8)SEOUENTIAL o@IIEVISION NUMEIIPAGE(3)R.E.GlnnaNuclearPowerPlantTEXT/I/moree/reoe/Irer/uuN/,
FACILITYNAME (ll                                                            DOCKET NUMBER (2)                   LER NUMBER (8)                 PAGE (3)
u>>//I/rme/HRC Frurn35883/()7)osooo244930040002OF09LANTCONDTONSTheplantwasatapproximately 974steadystatereactorpowerwiththefollowing pertinent activities inprogress:
YEAR      SEOUENTIAL o@ IIEVISION NUM E II R.E. Glnna Nuclear Power Plant                                            o  s  o  o  o  24 49          3      004          0 0      0  2 OF    0 9 TEXT /I/more e/reoe /I rer/uuN/, u>> //I/rme/HRC Frurn 35883/ ()7)
oThe"B"AllVolatileTreatment (AVT)mixedbeddemineralizer wasbeingplacedinserviceperoperating procedure T-6.9A(Condensate Polishing MixedBedDIUnitStart-up).
LANT COND T ONS The        plant was at approximately 974 steady state reactor power        with the following pertinent activities in progress:
AlsoperT-6.9A,thestandby"C"condensate pumpstart/stop switchwasplacedinpullstop,andthelowpressureheaterscondensate bypassvalveswitchwaschangedfromtheautotoclosedposition.
o          The "B" All Volatile Treatment                                    (AVT) mixed bed demineralizer was being placed in service per operating procedure T-6.9A (Condensate Polishing Mixed Bed DI Unit Start-up).                   Also per T-6.9A, the standby "C" condensate pump start/stop switch was placed in pull stop, and the low pressure heaters condensate bypass valve switch was changed from the auto to closed position.               The above switch manipulations                                      were performed to prevent any inadvertent operations during placing the AVT mixed bed demineralizer in service..
Theaboveswitchmanipulations wereperformed topreventanyinadvertent operations duringplacingtheAVTmixedbeddemineralizer inservice..
o          The          Instrument        and      Control (I&C) Department was troubleshooting                5A  high pressure heater level control problems.
oTheInstrument andControl(I&C)Department wastroubleshooting 5Ahighpressureheaterlevelcontrolproblems.
DESCRIPTION OP EVENT A.         DATES AND APPROXIMATE TIMES OP MAJOR OCCURRENCES:
DESCRIPTION OPEVENTA.DATESANDAPPROXIMATE TIMESOPMAJOROCCURRENCES:
0            July 7, 1993, 0915 EDST: Event date and approxi-mate  time.
0July7,1993,0915EDST:Eventdateandapproxi-matetime.0July7,1993,0915EDST:Discovery dateandapproximate time.0July7,1993,0925EDST:"A"and"B"SteamGenerator (S/G)levelsrestoredtopre-event normaloperating band.NRCForm388A(889)  
0            July 7, 1993, 0915 EDST: Discovery date and approximate time.
0            July 7, 1993, 0925 EDST:                           "A" and "B" Steam Generator (S/G) levels restored to pre-event normal operating band.
NRC Form 388A (889)


NRCFORM388A(SJ)9)US.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORT(LER)TEXTCONTINUATION APPROVEDOMBNO.31600108EXPIRES:E/30/92ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUEST:60.0HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(PW30),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20666,ANDTO1'HEPAPERWORK REDUCTION PROJECT(3160410E).
NRC FORM 388A                                                US. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31600108 (SJ)9)
OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20603.FACILITYNAME('I)DOCKETNUMBER12)YEARLERNl/MBER(8).'os:sEovENTIAL NVMSERREVISIONNVMERPAGE(3)R.E.GlnnaNuclearPowerPlantTEXT///marog>>coJInq>>)ed,1>>o~H/ICFomI38SAB/(ll) osooo244930040003QF09B.EVENTOnJuly7,1993,atapproximately 0800EDST,anInstrument andControl(I&C)Technician begantrouble-shooting5Ahighpressureheaterlevelcontrolproblems, inaccordance withMaintenance WorkOrder(MWO)9301086.TheI&CTechnician suspected therewasanairleakintheairsupplytubingorinthevalvepositioner foroneofthe5Aheaterlevelcontrolvalves.Withconcurrence fromaControlRoomoperator, thetechnician disconnected andpluggedthetubingtothenormallevelcontrolvalve,andobservedthatthehighleveldumpvalve(whichfailsopenonlossofair)brieflyopenedforafew.seconds(untilthetubingwasplugged)andthenclosed,Seeingnoimprovement inairpressure, thetubingwasthenunplugged andrestoredtonormal.Shortlybefore0915EDST,thetechnician disconnected andpluggedthetubingtothehighleveldumpvalve.Withairpressuretothevalveplugged,thedumpvalvewentfullopenandremainedfullyopen.Approximately ten(10)secondslater,thetechnician notedthattheHeaterDrainTank(HDT)discharge valvebeganclosing,andexpeditious'ly unplugged thetubingandrestorednormalairsupplytothedumpvalve.Uponrestoration ofairpressure, thedumpvalveclosed.OnJuly7,1993atapproximately 0915EDST,withthereactoratapproximately 974fullpower,asecondary sidecondensate andfeedwater systemdecreasing pressuretransient occurred.
EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE        ENT REPORT (LER)                                INFORMATION COLLECTION REOUEST: 60.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION                                            AND REPORTS MANAGEMENT BRANCH (PW30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20666, AND TO 1'HE PAPERWORK REDUCTION PROJECT (3160410E). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20603.
Atthistimetheconfiguration oftheS/Gfeedwater regulating valveswereasfollows:oThe"A"S/GMainFeedwater Regulating Valve(FRV)wasinmanualmode(approximately 454open)toreducefeedwater systemflowoscillations thatwereoccurring.
FACILITY NAME ('I)                                                 DOCKET NUMBER 12)                       LER Nl/MBER (8)                 PAGE (3)
NRCFoIRI388A(689)  
YEAR  .'os: sEovENTIAL     REVISION NVMSER        NVM ER R.E. Glnna Nuclear Power Plant                                  o  s  o  o  o  2 4    4 9 3            004            0 0      0  3 QF0    9 TEXT ///maro g>>co JI nq>>)ed, 1>>o ~H/IC  FomI 38SAB/(ll)
B. EVENT On      July 7, 1993,               at approximately                    0800        EDST,         an Instrument and Control (I&C) Technician began trouble-shooting 5A high pressure heater level control problems, in accordance with Maintenance Work Order (MWO) 9301086.                 The I&C Technician suspected there was an air leak in the air supply tubing or in the valve positioner for one of the 5A heater level control valves. With concurrence from a Control Room operator, the technician disconnected and plugged the tubing to the normal level control valve, and observed that the high level dump valve (which fails open on loss of air) briefly opened for a few .seconds (until the tubing was plugged) and then closed, Seeing no improvement in air pressure, the tubing was then unplugged and restored to normal.
Shortly before 0915 EDST, the technician disconnected and plugged the tubing to the high level dump valve.
With air pressure to the valve plugged, the dump valve went full open and remained fully open.
Approximately ten (10) seconds later, the technician noted that the Heater Drain Tank (HDT) discharge valve began closing, and expeditious'ly unplugged the tubing and restored normal air supply to the dump valve. Upon restoration of air pressure, the dump valve closed.
On July 7, 1993 at approximately 0915 EDST, with the reactor at approximately 974 full power, a secondary side condensate and feedwater system decreasing pressure transient occurred.                                   At this time the configuration of the S/G                        feedwater            regulating valves were as          follows:
o          The      "A" S/G Main Feedwater                            Regulating Valve (FRV)     was      in    manual      mode        (approximately 454 open)     to reduce feedwater system flow oscillations that    were occurring.
NR C F oIRI 388A (689)


NRCFORM366A(SSS)U.S.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORTILER)TEXTCONTINUATION APPROVEDOMSNO.31600104EXPIRES:4/30/02ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUEST:50A)HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(P430),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20655,ANDTO1HEPAPERWORK REDUCTION PROJECT(3150d)04),
NRC FORM 366A                                                        U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO. 31600104 (SSS)
OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20503.FACILITYNAME(<<DOCKETNUMBER(2)YEARLERNUMBER(6)'SOUSNTIAL NUMSSII4IISVISIONNUMSSIIPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///mauSpuce/4Isqu/>>I/,
EXPIRES: 4/30/02 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE                ENT REPORT ILER)                                  INFORMATION COLLECTION REOUEST: 50A) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION                                                  AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20655, AND TO 1HE PAPERWORK REDUCTION PROJECT (3150d)04), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
u>>a/dc0htuh4/I/RC FumI36643/((Tl05000244'0040004oF09oThe<<A<<S/GBypassFRVwasintheautomodecontrolling the<<A<<S/Glevel(approximately 804open).oThe<<B<<S/GMainFRVwasintheautomodecontrolling the<<B<<S/Glevel(approximately 464open).oThe<<B<<S/GBypassFRVwasintheautomode(fullopen).Thesecondary sidecondensate andfeedwater systemdecreasing pressuretransient wasinitiated byasignificant momentary decreaseinHDTpumpflowduetotheclosingoftheHDTdischarge valve.(HDTpumpflowdecreased approximately 754fromnormal).HDTpumpflownormallysuppliesapproximately onethirdofthesuctionflowtotheS/Gmainfeedwater pumps.TheothertwothirdsofthesuctionflowtotheS/Gmainfeedwater pumpsissuppliedbythecondensate pumpsthroughthelowpressurefeedwater heaters.Thedecreased flowcoupledwiththeinability ofthestandbycondensate pumptostartand/orthelowpressureheaterscondensate bypassvalvetoopen,(thisline-upexplained inPre-Event PlantConditions, SectionI),decreased pressurethroughout thecon-.densateandfeedwater system.The<<B<<S/GMainFRV(inauto)followedthelossofmainfeedwater pressurebyopeningmore(approximately 574open)tomaintainmainfeedwater flowtothe<<B<<S/G.The<<A<<S/GMainFRV(inmanual)remainedatapproximately 454open.Approximately 40-50secondsafterinitiation ofthetransient, HDTpumpflowwasrestoredtonormal,restoring condensate andfeedwater pressuretonormal,andcausing<<B<<S/Gfeedwater flowtoexceedthecalibration rangeoftheflowtransmitters
FACILITY NAME (<<                                                             DOCKET NUMBER (2)                     LER NUMBER (6)                   PAGE (3)
(<<B".S/GFRVhadopenedto574).Becausethe"B<<S/Gfeedwater flowvaluesexceededthecalibration rangeoftheflowtransmitters, the"B<<FRVautomatically switchedtomanualmode.Thepreceding eventsoccurredinashortperiodoftime.DuringthisshortperiodofNRCFoIm366A(640) 0 NRCFORM366A(6BB)U.S.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORT(LER)TEXTCONTINUATION APPROVEODMSNO.3)504(OEEXPIRES:E/30/92ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUESTI508)HRS.FORWARDCOMMENTSREGARDING BURDENFSTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(PJ)30),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTOTHEPAPERWORK REDUCTION PROJECT(31504)04).
YEAR      'SOUSNTIAL      IISVIS ION NUMSSII    4 NUMSSII R.E. Gonna Nuclear Power Plant                                            0  5  0  0    0  2  4 4 004            0      0 0  4oF 0    9 TEXT ///mau Spuce /4 Isqu/>>I/, u>> a/dc0htuh4/I/RC FumI 36643/ ((Tl o          The    <<A<<     S/G      Bypass        FRV was          in the auto mode controlling the             <<A<< S/G level              (approximately 804 open) .
OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20503.FACILITYNAME(I)DOCKETNUMBER12)YEARLERNUMBER(6)I'oR'jSEQUENTIAL S>NUMBERREVISIONNUMERPAGE(3)R.E.GonnaNuclearPowerPlantTEXT/IImortEpoco/EIEOVPEI/oooea//I/ono/HRC FomI366AB/(17)osooo2449300400050F09timethe"B"S/Gwasbeingsuppliedwithmorefeedwater thanrequired, andatapproximately 0917EDST(approxi-matelytwo(2)minutesintothetransient) mainfeedwater isolation onhighlevel(i.e.>/=674narrowrangelevel)occurredfive(5)timestothe"BL(S/Goveraperiodoffourteen(14)seconds.TheControlRoomoperators tookimmediate manualactionstorestoreS/Glevelsandatapproximately 0925EDSTthe"A"and"B"S/Glevelswererestoredtotheirnormaloperating bandandtheplantstabilized.
o          The    <<B<<     S/G      Main FRV was                in the auto mode controlling the             <<B<< S/G        level (approximately 464 open) .
Subsequently, theControlRoomoperators notifiedhighersupervision andtheNuclearRegulatory Com-missionper10CFR50.72,non-emergency 4hournotification.
o          The    <<B<<     S/G      Bypass        FRV was          in the auto                  mode (full open)       .
C.INOPERABLE STRUCTURES, COMPONENTS, ORSYSTEMSTHATCONTRIBUTED TOTHEEVENTThe5AhighpressureheaterhighleveldumpvalvetotheHDTinoperability, duetotroubleshooting efforts,inaccordance withMWO9301086,contributed totheevent.Inoperability ofthe"C"Standbycondensate pumpandcondensate bypassvalve,duetoprocedure T-6.9A'equirements, contributed tothedifficulty inresponding totheevent.D.C&#xc3;HiERSYSTEMSORSECONDARY FUNCTIONS AFFECTED:
The      secondary          side condensate and feedwater system decreasing          pressure transient was initiated by a significant momentary decrease in HDT pump flow due to the closing of the HDT discharge valve. (HDT pump flow decreased approximately 754 from normal). HDT pump        flow normally supplies approximately one third of the suction flow to the S/G main feedwater pumps.
None.NRCFoIIn366A(649)  
The other two thirds of the suction flow to the S/G main feedwater pumps is supplied by the condensate pumps through the low pressure                                    feedwater heaters.
The decreased flow coupled with the inability of the standby condensate pump to start and/or the low pressure heaters condensate bypass valve to open, (this line-up explained in Pre-Event Plant Conditions, Section I), decreased pressure throughout the con-.
densate and feedwater system.                                 The <<B<< S/G Main FRV (in auto) followed the loss of main feedwater pressure by opening more (approximately 574 open) to maintain main feedwater flow to the <<B<< S/G. The <<A<< S/G Main FRV (in manual) remained at approximately 454 open.
Approximately 40-50 seconds after initiation of the transient, HDT pump flow was restored to normal, restoring condensate and feedwater pressure to normal, and causing <<B<< S/G feedwater flow to exceed the calibration range of the flow transmitters                                              (<<B". S/G FRV had opened to 574).                       Because the            "B<<   S/G feedwater flow values exceeded the calibration range of the flow transmitters, the "B<< FRV automatically switched to manual mode. The preceding events occurred in a short period of time. During this short period of NRC FoIm 366A (640)


NAGFOAMSKSA(5$9)U$.NUCLEARREGULATORY COMMISSION LICENSEENTREPORT(LER)TEXTCONTINUATION APPROVEDOMBNO.3)500(04EXPIRES:r/30/92TIMATEDBUADENPEARESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REGUEST:50A)HRS.FORWARDCOMMENTSREGARDING BUAOENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(P$30),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON.
0 NRC FORM 366A                                                      U.S. NUCLEAR REGULATORY COMMISSION APPROVEO DMS NO. 3)504(OE (6BB)
OC20555.ANDTO'IHEPAPERWORK REDUCTION PROJECT(31500(04),
EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE              ENT REPORT (LER)                              INFORMATION    COLLECTION REOUESTI 508) HRS. FORWARD COMMENTS REGARDING BURDEN FSTIMATE TO THE RECORDS TEXT CONTINUATION                                            AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504)04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
OFFICEOFMANAGEMENT ANDBUDGETWASHINGTON DC20503FACILITYNAME(IIDOCKETNUMBER(2)YEARLERNUMBERFS)SKQVKNTIAI NVMSKRRKVIKIONNUMSKRPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///maor/vcr/rrrqokaf,uwedcVdoIN/
FACILITY NAME (I)                                                          DOCKET NUMBER 12)                      LER NUMBER (6)                                 PAGE (3)
HRCFomr35SA'r/(Illosooo244930040006OF09E.METHODOPDISCOVERY Theeventwasimmediately apparentduetoalarmsandindications intheControlRoomandindications atthe5AhighpressureheaterhighleveldumpvalvetotheHeaterDrainTank.OPERATORACTION:TheControlRoomoperators tookimmediate manualactionstocontrolS/Glevelsandstabilize theplant.Subsequently, theControlRoomoperators notifiedhighersupervision andtheNuclearRegulatory Commission per10CFR50.72,non-emergency 4hournotification.
YEAR  I'oR'j SEQUENTIAL    REVISION S>      NUMBER      NUM ER R.E. Gonna Nuclear Power Plant                                          o  s  o  o  o  24 49          3          004          0 0                      0  50F      09 TEXT /IImort Epoco /E IEOVPEI/ ooo ea //I/ono/HRC FomI 366AB/ (17) time the "B" S/G was being supplied with more feedwater than required, and at approximately 0917 EDST (approxi-mately two (2) minutes into the transient) main feedwater isolation on high level (i.e. >/ = 674 narrow range level) occurred five (5) times to the "BL(
GSAFETYSYSTEMRESPONSES:
S/G over a period of fourteen (14) seconds.
The>>B>>S/GMainandBypassFRVsbegantocloseautomatically asaresultofthefeedwater isolation signals.Duetotheshortdurationthatthesignalswerepresent,theFRVsneverfullyclosed.III.CAUSEOPEVERTA.IMMEDIATE CAUSE:Thefeedwater isolation signaltothe>>B>>S/GMainandBypassFRVswasduetothe>>B>>S/Gnarrowrangelevelbeing>/=67%.B.INTERMEDIATE CAUSE:The>>B>>S/Gnarrowrangelevelwas>/=674duetoincreased flowtothe>>B>>S/Gcausedbytheperturba-tionsinmainfeedwater headerpressureandautomatic FRVoperation.
The Control Room operators took immediate manual actions to restore S/G levels and at approximately 0925 EDST the "A" and "B" S/G levels were restored to their normal operating band and the plant stabilized.
Thissituation resultedinoverfeeding the>>B>>S/G.NRCFomI358A(5$9)  
Subsequently,             the Control Room operators notified higher supervision and the Nuclear Regulatory Com-mission per 10 CFR 50.72, non-emergency 4 hour notification.
C.          INOPERABLE STRUCTURES, COMPONENTS,                                    OR    SYSTEMS                          THAT CONTRIBUTED TO THE EVENT The 5A high pressure heater high level dump valve to the HDT inoperability, due to troubleshooting efforts, in accordance with MWO 9301086, contributed to the event.
Inoperability of the "C" Standby condensate pump and condensate bypass valve, due to procedure contributed to the difficulty in                            T-6.9A'equirements, responding        to    the    event.
D.           C&#xc3;HiER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
NRC FoIIn 366A (649)


NRCFORM366A(609)US.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORT(LER)TEXTCONTINUATION APPROVEDOMBNO.31500104EXPIRES:4/30/92ESTIMATED BURDENPERRESPONSETOCOMPI.YWTHTHISINFORMATION COLLECTION REQUEST:60glHRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(PJ)30),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTO1HEPAPERWORK REDUCTION PROJECT(31500104),
NAG FOAM SKSA                                                        U$ . NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3)500(04 (5$ 9)
OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON.
EXPIRES: r/30/92 TIMATED BUADEN PEA RESPONSE TO COMPLY WTH THIS LICENSEE                NT REPORT (LER)                                  INFORMATION COLLECTION REGUEST: 50A) HRS. FORWARD COMMENTS REGARDING BUAOEN ESTIMATE TO THE RECORDS TEXT CONTINUATION                                                  AND REPORTS MANAGEMENT BRANCH (P$ 30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. OC 20555. AND TO
DC20503.FACILITYNAME(IIDOCKETNUMBER(2)YEARLERNUMBER(6)(I63:SEQUENTIAL NUM664+pREVISIONNUM64PAGE(3)R.E.GonnaNuclearPowerPlantTEXT///RNVP4/>>Ce/4JNIUPN/II>>PIS/OR4/HRC FORR36542/((7)0s0o0244~3004-007oF09Theperturbations inmainfeedwater headerpressurewerecausedbyamomentary largereduction inHDTpumpflowfollowedbyarapidreturntonormalflow.The"B"S/GMainFRV(inauto)followedthelossofmainfeedwater headerpressurebyopeningmoretomaintainfeedwater flowandwhenHDTpumpflowwasrapidlyrestored, mainfeedwater headerpressurereturnedtonormal.Whenmainfeedwater headerpressurereturnedtonormal,the"B"S/GFRVwasopenapproximately 114morethannormalandthe"B"S/Gfeedwater flowsexceededthecalibration rangeoftheflowtransmitters andbydesignthe"B"S/GFRVswitchedtomanualmode.Inthemanualmode'he"B"S/GMainFRVcouldnotcontrolthe"BLIS/Glevelwithoutoperatorintervention.
                                                                                                            'IHE PAPERWORK REDUCTION PROJECT (31500(04), OFFICE OF MANAGEMENTAND BUDGET WASHINGTON DC 20503 FACILITY NAME (II                                                          DOCKET NUMBER (2)                     LER NUMBER  FS)                 PAGE (3)
Itshouldbenotedherethatifthelowpressureheaterscondensate bypassvalvehadbeencapableofopening,theabovetransient couldhavebeenlesssevereandthe"BFIS/Gwouldmostlikelyhavenotsustained ahighlevelfeedwater isolation.
YEAR      SKQVKNTIAI      RKVIKION NVMSKR        NUMSKR R.E. Gonna Nuclear Power Plant                                            o  s  o  o    o  2  449        3      004            0 0      0  6 OF    0  9 TEXT /// mao r/vcr /r rrqokaf, uw edcVdoIN/ HRC Fomr 35SA'r/ (Ill E.          METHOD OP DISCOVERY The event was immediately apparent                                  due to alarms and indications in the Control                            Room        and      indications at the 5A high pressure heater high level                                        dump      valve to the Heater Drain Tank.
Themomentary largereduction inHDTpumpflow,followedbyarapidreturntonormalflow,wascausedbytheopeningandsubsequent closingofthe5AhighpressureheaterhighleveldumpvalvetotheHDT,duetotheactionsoftheI&CTechnician's troubleshooting activities.
OPERATOR ACTION:
Itisbelievedthattheopeningofthisdumpvalve,coupledwiththe5Ahighpressureheaterlowlevelcondition, decreased theHDTlevelsubstan-tially.ThisleveldecreasewassensedbytheHDTlevelcontrolsystemanditbegantoclosetheHDTpumpdischarge controlvalvetoreduceflowandreturntheHDTleveltoitsoperating band.Theclosingofthe5Ahighpressureheaterhighleveldumpvalve,duetotheactionsoftheISCTechnician, reversedtheaboveconditions andtheHDTpumpflowreturnedtonormal.NRCFoIRI366A(64)9)
The       Control Room operators took immediate manual actions to control S/G levels and stabilize the plant.                Subsequently,             the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10 CFR 50.72, non-emergency 4 hour notification.
J0 NRCFOAM368A(649)FACILITYNAME(1)U.SNUCLEARREGULATORY COMMISSION LICENSEEENTREPORTILER)TEXTCONTINUATION DOCKETNUMBER(2)APPROVED0MBNO.31504(OSEXPIRES;S/30/92ESTIMATED BUADENPERAESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REQUEST:50J)HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(F430).U.S.NUCLEARREGULATORY COMMISSION.
G          SAFETY SYSTEM RESPONSES:
WASHINGTON, DC205S5,ANDTOTHEPAPERWORK REDUCTION PROJECT(3(504104).
The        >>B>>      S/G  Main and Bypass FRVs began                                  to close automatically as a result of the feedwater                                            isolation signals.               Due    to the short duration that the signals were present,               the      FRVs    never      fully closed.
OFFICEOFMANAGEMENT AND8UDGET,WASHINGTON.
III.             CAUSE OP EVERT A.         IMMEDIATE CAUSE:
DC20503.PAGE(3)LERNUMBERIS)R.E.Glnna'NUclear PowerPlantTEXT///mareSaece/ere/a/rerL Iree~HRCFarm355AB/(12)YEARosooo24493SEQUENTIAL
The feedwater isolation                          signal to the                >>B>>      S/G Main and Bypass FRVs was due                          to the        >>B>> S/G          narrow range level being >/                 = 67%.
.oANUMSSRCN004REVISIONNUMSR0008oF09ROOTCAUSE:Theunderlying causeoftheeventwasdetermined tobenotisolating the5AhighpressureheaterhighleveldumpvalvetotheHDTpriortocommencement oftroubleshooting theairsupplyconcernsforthe'dumpvalve.ANALYSTSOP&TENTThiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),
B.         INTERMEDIATE CAUSE:
whichrequiresreporting of,"anyeventorconditi'on thatresultedinmanualorautomatic actuation ofanyEngineered SafetyFeature(ESF)including theReactorProtection System(RPS)".Thefeedwater isolation ofthe"B"S/Gwasanautomatic actuation ofanESFsystem.Anassessment wasperformed considering boththesafetyconsequences andimplications ofthiseventwiththefollowing resultsandconclusions:
The >>B>> S/G narrow range                            level      was >/ = 674 due to increased flow to the                      >>B>> S/G        caused        by the perturba-tions in main feedwater header                              pressure          and automatic FRV      operation.             This situation resulted in overfeeding the      >>B>>      S/G.
Therewerenooperational orsafetyconsequences orimplications attributed tothefeedwater isolations because:oThefeedwater isolations occurredattherequiredS/Glevel.00Theplantwasquicklystabilized andmanualcontrolofFRVswasaccomplished tomitigateanyconsequences oftheevent.I,Asthefeedwater isolations occurredasdesigned, theassumptions oftheFSARforsteamlinebreakweremet.Basedontheabove,itcanbeconcluded thatthepublic'shealthandsafetywasassuredatalltimes.NRCFomI365A(589)  
NRC FomI 358A (5$ 9)


NRCFORM366A(BJIS)UA.NUCLEARREGULATORY COMMISSION LICENSEEENTREPORTILER)TEXTCONTINUATION APPROVEDOMBNO.3(500106EXPIRES:6/30/62ESTIMATED BURDENPERRESPONSETOCOMPLYWTHTHISINFORMATION COLLECTION REOUEST:60.0HRS.FORWARDCOMMENTSREGARDING BURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENT BRANCH(F430),U.S.NUCLEARREGULATORY COMMISSION, WASHINGTON, DC20555,ANDTO1MEPAPERWORK REDUCTION PROJECT(3(500106).
NRC FORM 366A                                                    US. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31500104 (609)
OFFICEOFMANAGEMENT ANDBUDGET,WASHINGTON, DC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBERLSIYEARr~r'SEOUENTIAL P~SREVISIONNUMBER"~NUMERPAGE(3)R.E.GonnaNuclearPowerPlantTEXT///momJpon/1mqII/mI/II'////JJN/I HRC%%dmI36MB/l(7)osooo2449300400090FV.CORRECTIVE ACTIONAACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:AftertheS/Glevelswerestabilized, theFRVswerereturnedtotheirpre-event controlconfiguration.
EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPI.Y WTH THIS LICENSEE              ENT REPORT (LER)                              INFORMATION COLLECTION REQUEST: 60gl HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION                                            AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.
B.ACTIONTAKENORPLANNEDTOPREVENTRECERMFNCE:
FACILITY NAME (II                                                      DOCKET NUMBER (2)                      LER NUMBER (6)                  PAGE (3)
Toensureamorerapidmitigation ofthistypeofeventandpossiblyeliminate thefeedwater isolation, operating procedure T-6.9Awillbechangedtodeletethestepsthatplacethelowpressureheaterscondensate bypassvalveswitchtotheclosedposition.
(I63: SEQUENTIAL    REVISION YEAR          NUM664  +p  NUM 64 R.E. Gonna Nuclear Power Plant                                      0  s  0  o    0  2 4    4 ~
Operations,
3        004 0            0        7oF      09 TEXT /// RNVP 4/>>Ce /4 JNIUPN/ II>> PIS/OR4/HRC  FORR 36542/ ((7)
: Planning, andI&Cpersonnel havebeennotifiedthatisolation ofaheaterhighleveldumpvalve,priortotroubleshooting, shouldbeconsidered anormalpractice.
The      perturbations in main feedwater header pressure were caused by a momentary large reduction in HDT pump flow followed by a rapid return to normal flow.
ADDITIONAL INFORMATION A.FAILEDCOMPONENTS:
The "B" S/G Main FRV (in auto) followed the loss of main feedwater header pressure by opening more to maintain feedwater flow and when HDT pump flow was rapidly restored, main feedwater header pressure returned to normal.                        When main feedwater                            header pressure returned to normal, the                            "B"      S/G    FRV    was        open approximately 114 more than normal and                                      the      "B"      S/G feedwater flows exceeded the calibration range of the flow transmitters and by design the "B" S/G FRV switched to manual mode. In the manual"BLI                                  mode'he "B" S/G Main FRV could not control                                the                S/G level without operator intervention.                              It      should        be noted here that          if    the low pressure bypass valve had been capable of opening, the"BFI heaters          condensate above transient could have been                    less      severe          and    the              S/G would most likely have not                          sustained              a    high          level feedwater isolation.
None.BPREVIOUSLERsONSIMILAREVENTSAsimilarLEReventhistorical searchwasconducted withthefollowing results:LER91-009andLER-92-006(Revision 1)weresimilareventswithdifferent rootcauses.CSPECIALCOMMENTS:
The        momentary large reduction in HDT pump flow, followed by a rapid return to normal flow, was caused by the opening and subsequent closing of the 5A high pressure heater high level dump valve to the HDT, due to the actions of the I&C Technician's troubleshooting activities.
LER92-006(Revision 1)indicates theproblemsthathavebeenexperienced withtheAdvancedDigitalFeedwater ControlSystem(ADFCS),thecausesandcorrective actionstakenorplanned.NRCForm366A(686) hT}}
dump valve, It    is believed that the coupled with the 5A high opening of pressure heater this low level condition, decreased                        the      HDT      level substan-tially. This level decrease                  it      was        sensed to    close by the HDT the HDT level control system and                            began pump discharge              control valve                to      reduce        flow        and return the HDT level to its operating                                          band.          The closing of the 5A high pressure heater high level dump valve, due to the actions of the ISC Technician, reversed the above conditions and the HDT pump flow returned to normal.
NRC FoIRI 366A (64)9)
 
0 J
 
NRC FOAM 368A                                                      U.S NUCLEAR REGULATORY COMMISSION (649)                                                                                                              APPROVED 0MB NO. 31504(OS EXPIRES; S/30/92 ESTIMATED BUADEN PER AESPONSE TO COMPLY WTH THIS LICENSEE          ENT REPORT ILER)                              INFORMATION COLLECTION REQUEST: 50J) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION                                            AND REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, DC 205S5, AND TO THE PAPERWORK REDUCTION PROJECT (3(504104). OFFICE OF MANAGEMENT AND 8UDG ET, WASHINGTON. DC 20503.
FACILITY NAME (1)                                                      DOCKET NUMBER (2)                    LER NUMBER IS)                    PAGE (3)
YEAR      SEQUENTIAL  .oA REVISION NUMSSR    CN  NUM SR R.E. Glnna'NUclear Power Plant TEXT /// mare Saece /e re/a/rerL Iree ~    HRC Farm 355AB/ (12) o  s  o  o  o  24 493                004            0 0      0    8 oF    09 ROOT CAUSE:
The      underlying cause of the event was determined to be      not isolating the 5A high pressure heater high level dump valve to the HDT prior to commencement of troubleshooting the air supply concerns for the'dump valve.
ANALYSTS OP &TENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of, "any event or conditi'on that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF) including the Reactor Protection System (RPS)". The feedwater isolation of the "B" S/G was an automatic actuation of an ESF system.
An assessment              was performed considering both the safety consequences              and implications of this event with the following results and conclusions:
There were no operational or safety consequences                                                        or implications attributed to the feedwater isolations because:
o      The feedwater            isolations occurred at the required S/G level.
0      The plant was quickly stabilized and manual control of FRVs was accomplished to mitigate any consequences of the event.
I, 0      As the feedwater isolations occurred as designed, the assumptions of the FSAR for steam line break were met.
Based on the above, it can be concluded that the public's health and safety was assured at all times.
NRC FomI 365A (589)
 
NRC FORM 366A                                                UA. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3(500106 (BJIS)
E XP I R ES: 6/30/62 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE            ENT REPORT ILER)                            INFORMATION COLLECTION REOUEST: 60.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION                                        AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1ME PAPERWORK REDUCTION PROJECT (3(500106). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1)                                                   DOCKET NUMBER (2)                     LER NUMBER LSI                      PAGE (3) r~r' YEAR          NUMBER    "~
SEOUENTIAL P~S REVISION NUM ER R.E. Gonna Nuclear Power Plant                                    o  s  o  o  o  2  449        3        004                00      0 90F TEXT /// mom Jpon /1 mqII/mI/ II' ////JJN/I HRC 36M B/ l(7)
                                              %%dmI V.               CORRECTIVE ACTION A            ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
After the    S/G    levels were stabilized, the FRVs were returned to their pre-event control configuration.
B.           ACTION TAKEN OR PLANNED TO PREVENT RECERMFNCE:
To ensure      a more        rapid mitigation of this type of event and    possibly eliminate the feedwater isolation, operating procedure T-6.9A will be changed to delete the steps that place the low pressure heaters condensate bypass valve switch to the closed position.
Operations,     Planning,           and    I&C personnel                  have          been notified that isolation of a heater high level dump valve, prior to troubleshooting, should be considered a normal practice.
ADDITIONAL INFORMATION A.           FAILED COMPONENTS:
None.
B            PREVIOUS LERs ON SIMILAR EVENTS A    similar LER event historical search was conducted with the following results: LER 91-009 and LER                                              006 (Revision 1) were similar events with different root causes.
C            SPECIAL COMMENTS:
LER 92-006     (Revision 1) indicates the problems that have been experienced with the Advanced Digital Feedwater Control System (ADFCS), the causes and corrective actions taken or planned.
NRC Form 366A (686)
 
h T}}

Latest revision as of 09:35, 4 February 2020

LER 93-004-00:on 930707,Main Feedwater Isolations Occurred Due to Secondary Side & Condensate Feedwater Pressure Transient.Returned Feedwater Regulating Valves to pre-event Controls configuration.W/930806 Ltr
ML17263A352
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/06/1993
From: Backus W, Mecredy R
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-93-004, LER-93-4, NUDOCS 9308120083
Download: ML17263A352 (22)


Text

ACCELERATED DOCUMENT DISTRIBUTION SYSTEM REGUL>RY INFORMATION DISTRIBUTE SYSTEM (RIDE)

ACCESSION NBR:9308120083 DOC.DATE: 93/08/06 NOTARIZED: NO DOCKET ¹ FACIL 50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION BACKUS,W.H Rochester Gas a Electric Corp.

MECREDY,R.C Rochester Gas 6 Electric Corp.

RECIP.NAME RECIPIENT AFFILIATION I i

SUBJECT:

LER 93-004-00:on 930707,Main feedwater isolations occurred 1 I

to secondary side 6 condensate feedwater pressure 1

due Dl transient. Returned feedwater regulating valves to pre-event controls configuration.W/930806 ltr. S DISTRIBUTION CODE: ZE22T COPIES RECEIVED:LTR t ENCL r SIZE: LO TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. l '.

NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 A RECIPIENT COPIES RECIPIENT COPIES D ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 D JOHNSON,A 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 NODS SA/+PLB

-BP 1 1 NRR/DSSA/SRXB 1 1 02 1 1 RES/DSIR/EIB 1 1 RGHl FILE 01 1 1 EXTERNAL: EGGG BRYCE,J.H 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHYFG.A 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 D

D D

NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30

rrrnrNr1/r/trl/rr //i//// > rr,

//'/

I/ 'i" Ii//,i'" i ";- ',Toe/r .,

!C!i)ivir~ill!III/l'lrir,r! r/

state" ROCHESTER GAS AND ELECTRIC CORPORATION ~ 89 EAST AVENUE, ROCHESTER N. K 14649-0001 ROBERT C. MECREOY TELEPHONE Vice President ARE/1 COOE 716 5rt6 2700 Clnna ttuclear Production August 6, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Subject:

LER 93-004, Feedwater Control Perturbations, Due To A Secondary Side Transient, Causes Steam Generator High Level Feedwater Isolations R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, License Event Report System, item (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached event report LER 93-004 i:s hereby submitted.

This event has in no way affected the public's health and safety.

Very truly yours, Robert C. Mec edy xco U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector

~r n.h 9308i20083 930806 PDR *DOCK 05000244 8 PDR

NRC FORM 366 V.S. NUCLEAR REGULATORY COMMISSI (669) APPROVED OMB NOA31506104 EXP IR ESI 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFOAMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS ANO RFPORTS MANAGEMENT BRANCH (F630), V.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500'l04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, OC 20503.

FACILITY NAME (1) DOCKET NUMBER l2) PA E R.E. Ginna Nuclear Power Plant 0 5 0 0 02 44 iOFO Fee water Contro ertur at ons, Due To Secon ary Trans ent, auses team Generator High Level Feedwater Isolations EVENT DATE (5) LER NUMBER (61 REPORT DATE LT) 01'HER FACILITIES INVOLVED (6)

SEQUENTIAL REVISION MONTH DAY YEAR YEAR DAY YEAR FACII.ITVNAMES DOCKET NUMBERIS)

NUMBER NUMBER MONTH 0 5 0 0 0 0-7 79 393 0 0 4 0 0 0 806 93 0 5 0 0 0 THIS REPORT IS SVBMITTFD PUASVANT T0 THE RLQUIAEMENTS OF 10 CFR ((: /Chock ono or moro Ol trss IollovrinP/ (11)

OPERATING MODE (9) N 20.402(B) 20.405(c) 60 n(sl(2) Is>>) 73,71(B)

POWER 20.405( ~ )(1)(I) 60M(s)(II 50.n(v)(2) Nl 73.71 I cl LEYEL 0 9 7 20.405 (s ) l1 ) (NI 50.36( ~ )(2) 50 73(s)(2) lvsl) OTHER ISpscily In 4osnoct tN/oEN onr/ ln Tss I, HRC Form 20.406( ~ I ('I Hill) 60.73(sl(2((ll 50.73(v)(2) (vill)(Al 3664/

20405(s)(1)(lv) 50.73(s) (2)(ill 50.73(v)l2l(vill)(B) 20.405(s I (I)(vl 50.7 3(s) (2) (ill) 50.73( ~ )(2)lsl LICENSEE CONTACT FOR THIS LEA (12I NAME TELEPHONE NUMBER AREA CODE Wesley H. Backus.

Technical Assistant to the Operations Mana er 3 155 24- 444 6 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

CAVSE SYS'EM COMPONENT MANUFAC.

TVRER REPORTABLE TO NPADS PjQg CAUSE S STEM COMPONENT MANUFAC.

TVRER EPORTABLE TO NPROS

?>>o.>>... %R .:. R6)

SA'NO Xj

">>T>>~'

AA 'RC~C.

" IKU '

3>> 4 PcA. N::

hl .'. @<

SUPPLEMENTAL REPORT EXPECTED llc) MONTH DAY YEAR EXPECTFD SUBMISSION DATE (15)

YES Illy<<, compiots EXPECTED Sl/SSI/SSION DATE/ NO AssTRAcT I(.imit to /400 spscsr, l.s., spproslmsrsly lilusn tinpis.rpocs typssvrinon /inos/ (16)

On July 7, 1993 -at approximately 0915 EDST, with the reactor at approximately 974 full power, main feedwater isolations occurred on the "BFI Steam Generator (S/G). These feedwater isolations were caused by overfeeding the "B" S/G, following a secondary side condensate and feedwater pressure transient.

Immediate operator action was to manually control the Feedwater Regulating Valves (FRVs) to restore the S/G water levels and stabilize the plant.

The immediate cause of the event was due to a secondary side condensate and feedwater pressure transient.

The underlying cause of the event was determined to be not isolating the 5A heater high level dump valve prior to trouble-shooting. (This event is NUREG-1022 (X) Cause Code).

Corrective actions taken or planned are discussed in Section V of the text.

NRC Form 366 (669)

NRC FORM 388A US. NUCLEAR REGULATORY COMMISSION (SJ)9) APPROVED OMB NO. 3(504)04 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE ENT REPORT (LER) INFORMATION COLLECTION REOUEST: 508) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500)08), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.

FACILITYNAME (ll DOCKET NUMBER (2) LER NUMBER (8) PAGE (3)

YEAR SEOUENTIAL o@ IIEVISION NUM E II R.E. Glnna Nuclear Power Plant o s o o o 24 49 3 004 0 0 0 2 OF 0 9 TEXT /I/more e/reoe /I rer/uuN/, u>> //I/rme/HRC Frurn 35883/ ()7)

LANT COND T ONS The plant was at approximately 974 steady state reactor power with the following pertinent activities in progress:

o The "B" All Volatile Treatment (AVT) mixed bed demineralizer was being placed in service per operating procedure T-6.9A (Condensate Polishing Mixed Bed DI Unit Start-up). Also per T-6.9A, the standby "C" condensate pump start/stop switch was placed in pull stop, and the low pressure heaters condensate bypass valve switch was changed from the auto to closed position. The above switch manipulations were performed to prevent any inadvertent operations during placing the AVT mixed bed demineralizer in service..

o The Instrument and Control (I&C) Department was troubleshooting 5A high pressure heater level control problems.

DESCRIPTION OP EVENT A. DATES AND APPROXIMATE TIMES OP MAJOR OCCURRENCES:

0 July 7, 1993, 0915 EDST: Event date and approxi-mate time.

0 July 7, 1993, 0915 EDST: Discovery date and approximate time.

0 July 7, 1993, 0925 EDST: "A" and "B" Steam Generator (S/G) levels restored to pre-event normal operating band.

NRC Form 388A (889)

NRC FORM 388A US. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31600108 (SJ)9)

EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE ENT REPORT (LER) INFORMATION COLLECTION REOUEST: 60.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (PW30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20666, AND TO 1'HE PAPERWORK REDUCTION PROJECT (3160410E). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20603.

FACILITY NAME ('I) DOCKET NUMBER 12) LER Nl/MBER (8) PAGE (3)

YEAR .'os: sEovENTIAL REVISION NVMSER NVM ER R.E. Glnna Nuclear Power Plant o s o o o 2 4 4 9 3 004 0 0 0 3 QF0 9 TEXT ///maro g>>co JI nq>>)ed, 1>>o ~H/IC FomI 38SAB/(ll)

B. EVENT On July 7, 1993, at approximately 0800 EDST, an Instrument and Control (I&C) Technician began trouble-shooting 5A high pressure heater level control problems, in accordance with Maintenance Work Order (MWO) 9301086. The I&C Technician suspected there was an air leak in the air supply tubing or in the valve positioner for one of the 5A heater level control valves. With concurrence from a Control Room operator, the technician disconnected and plugged the tubing to the normal level control valve, and observed that the high level dump valve (which fails open on loss of air) briefly opened for a few .seconds (until the tubing was plugged) and then closed, Seeing no improvement in air pressure, the tubing was then unplugged and restored to normal.

Shortly before 0915 EDST, the technician disconnected and plugged the tubing to the high level dump valve.

With air pressure to the valve plugged, the dump valve went full open and remained fully open.

Approximately ten (10) seconds later, the technician noted that the Heater Drain Tank (HDT) discharge valve began closing, and expeditious'ly unplugged the tubing and restored normal air supply to the dump valve. Upon restoration of air pressure, the dump valve closed.

On July 7, 1993 at approximately 0915 EDST, with the reactor at approximately 974 full power, a secondary side condensate and feedwater system decreasing pressure transient occurred. At this time the configuration of the S/G feedwater regulating valves were as follows:

o The "A" S/G Main Feedwater Regulating Valve (FRV) was in manual mode (approximately 454 open) to reduce feedwater system flow oscillations that were occurring.

NR C F oIRI 388A (689)

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO. 31600104 (SSS)

EXPIRES: 4/30/02 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE ENT REPORT ILER) INFORMATION COLLECTION REOUEST: 50A) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20655, AND TO 1HE PAPERWORK REDUCTION PROJECT (3150d)04), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.

FACILITY NAME (<< DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR 'SOUSNTIAL IISVIS ION NUMSSII 4 NUMSSII R.E. Gonna Nuclear Power Plant 0 5 0 0 0 2 4 4 004 0 0 0 4oF 0 9 TEXT ///mau Spuce /4 Isqu/>>I/, u>> a/dc0htuh4/I/RC FumI 36643/ ((Tl o The <<A<< S/G Bypass FRV was in the auto mode controlling the <<A<< S/G level (approximately 804 open) .

o The <<B<< S/G Main FRV was in the auto mode controlling the <<B<< S/G level (approximately 464 open) .

o The <<B<< S/G Bypass FRV was in the auto mode (full open) .

The secondary side condensate and feedwater system decreasing pressure transient was initiated by a significant momentary decrease in HDT pump flow due to the closing of the HDT discharge valve. (HDT pump flow decreased approximately 754 from normal). HDT pump flow normally supplies approximately one third of the suction flow to the S/G main feedwater pumps.

The other two thirds of the suction flow to the S/G main feedwater pumps is supplied by the condensate pumps through the low pressure feedwater heaters.

The decreased flow coupled with the inability of the standby condensate pump to start and/or the low pressure heaters condensate bypass valve to open, (this line-up explained in Pre-Event Plant Conditions,Section I), decreased pressure throughout the con-.

densate and feedwater system. The <<B<< S/G Main FRV (in auto) followed the loss of main feedwater pressure by opening more (approximately 574 open) to maintain main feedwater flow to the <<B<< S/G. The <<A<< S/G Main FRV (in manual) remained at approximately 454 open.

Approximately 40-50 seconds after initiation of the transient, HDT pump flow was restored to normal, restoring condensate and feedwater pressure to normal, and causing <<B<< S/G feedwater flow to exceed the calibration range of the flow transmitters (<<B". S/G FRV had opened to 574). Because the "B<< S/G feedwater flow values exceeded the calibration range of the flow transmitters, the "B<< FRV automatically switched to manual mode. The preceding events occurred in a short period of time. During this short period of NRC FoIm 366A (640)

0 NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVEO DMS NO. 3)504(OE (6BB)

EXPIRES: E/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE ENT REPORT (LER) INFORMATION COLLECTION REOUESTI 508) HRS. FORWARD COMMENTS REGARDING BURDEN FSTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504)04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.

FACILITY NAME (I) DOCKET NUMBER 12) LER NUMBER (6) PAGE (3)

YEAR I'oR'j SEQUENTIAL REVISION S> NUMBER NUM ER R.E. Gonna Nuclear Power Plant o s o o o 24 49 3 004 0 0 0 50F 09 TEXT /IImort Epoco /E IEOVPEI/ ooo ea //I/ono/HRC FomI 366AB/ (17) time the "B" S/G was being supplied with more feedwater than required, and at approximately 0917 EDST (approxi-mately two (2) minutes into the transient) main feedwater isolation on high level (i.e. >/ = 674 narrow range level) occurred five (5) times to the "BL(

S/G over a period of fourteen (14) seconds.

The Control Room operators took immediate manual actions to restore S/G levels and at approximately 0925 EDST the "A" and "B" S/G levels were restored to their normal operating band and the plant stabilized.

Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Com-mission per 10 CFR 50.72, non-emergency 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification.

C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT The 5A high pressure heater high level dump valve to the HDT inoperability, due to troubleshooting efforts, in accordance with MWO 9301086, contributed to the event.

Inoperability of the "C" Standby condensate pump and condensate bypass valve, due to procedure contributed to the difficulty in T-6.9A'equirements, responding to the event.

D. CÃHiER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:

None.

NRC FoIIn 366A (649)

NAG FOAM SKSA U$ . NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3)500(04 (5$ 9)

EXPIRES: r/30/92 TIMATED BUADEN PEA RESPONSE TO COMPLY WTH THIS LICENSEE NT REPORT (LER) INFORMATION COLLECTION REGUEST: 50A) HRS. FORWARD COMMENTS REGARDING BUAOEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P$ 30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. OC 20555. AND TO

'IHE PAPERWORK REDUCTION PROJECT (31500(04), OFFICE OF MANAGEMENTAND BUDGET WASHINGTON DC 20503 FACILITY NAME (II DOCKET NUMBER (2) LER NUMBER FS) PAGE (3)

YEAR SKQVKNTIAI RKVIKION NVMSKR NUMSKR R.E. Gonna Nuclear Power Plant o s o o o 2 449 3 004 0 0 0 6 OF 0 9 TEXT /// mao r/vcr /r rrqokaf, uw edcVdoIN/ HRC Fomr 35SA'r/ (Ill E. METHOD OP DISCOVERY The event was immediately apparent due to alarms and indications in the Control Room and indications at the 5A high pressure heater high level dump valve to the Heater Drain Tank.

OPERATOR ACTION:

The Control Room operators took immediate manual actions to control S/G levels and stabilize the plant. Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10 CFR 50.72, non-emergency 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification.

G SAFETY SYSTEM RESPONSES:

The >>B>> S/G Main and Bypass FRVs began to close automatically as a result of the feedwater isolation signals. Due to the short duration that the signals were present, the FRVs never fully closed.

III. CAUSE OP EVERT A. IMMEDIATE CAUSE:

The feedwater isolation signal to the >>B>> S/G Main and Bypass FRVs was due to the >>B>> S/G narrow range level being >/ = 67%.

B. INTERMEDIATE CAUSE:

The >>B>> S/G narrow range level was >/ = 674 due to increased flow to the >>B>> S/G caused by the perturba-tions in main feedwater header pressure and automatic FRV operation. This situation resulted in overfeeding the >>B>> S/G.

NRC FomI 358A (5$ 9)

NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31500104 (609)

EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPI.Y WTH THIS LICENSEE ENT REPORT (LER) INFORMATION COLLECTION REQUEST: 60gl HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (PJ)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.

FACILITY NAME (II DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

(I63: SEQUENTIAL REVISION YEAR NUM664 +p NUM 64 R.E. Gonna Nuclear Power Plant 0 s 0 o 0 2 4 4 ~

3 004 0 0 7oF 09 TEXT /// RNVP 4/>>Ce /4 JNIUPN/ II>> PIS/OR4/HRC FORR 36542/ ((7)

The perturbations in main feedwater header pressure were caused by a momentary large reduction in HDT pump flow followed by a rapid return to normal flow.

The "B" S/G Main FRV (in auto) followed the loss of main feedwater header pressure by opening more to maintain feedwater flow and when HDT pump flow was rapidly restored, main feedwater header pressure returned to normal. When main feedwater header pressure returned to normal, the "B" S/G FRV was open approximately 114 more than normal and the "B" S/G feedwater flows exceeded the calibration range of the flow transmitters and by design the "B" S/G FRV switched to manual mode. In the manual"BLI mode'he "B" S/G Main FRV could not control the S/G level without operator intervention. It should be noted here that if the low pressure bypass valve had been capable of opening, the"BFI heaters condensate above transient could have been less severe and the S/G would most likely have not sustained a high level feedwater isolation.

The momentary large reduction in HDT pump flow, followed by a rapid return to normal flow, was caused by the opening and subsequent closing of the 5A high pressure heater high level dump valve to the HDT, due to the actions of the I&C Technician's troubleshooting activities.

dump valve, It is believed that the coupled with the 5A high opening of pressure heater this low level condition, decreased the HDT level substan-tially. This level decrease it was sensed to close by the HDT the HDT level control system and began pump discharge control valve to reduce flow and return the HDT level to its operating band. The closing of the 5A high pressure heater high level dump valve, due to the actions of the ISC Technician, reversed the above conditions and the HDT pump flow returned to normal.

NRC FoIRI 366A (64)9)

0 J

NRC FOAM 368A U.S NUCLEAR REGULATORY COMMISSION (649) APPROVED 0MB NO. 31504(OS EXPIRES; S/30/92 ESTIMATED BUADEN PER AESPONSE TO COMPLY WTH THIS LICENSEE ENT REPORT ILER) INFORMATION COLLECTION REQUEST: 50J) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, DC 205S5, AND TO THE PAPERWORK REDUCTION PROJECT (3(504104). OFFICE OF MANAGEMENT AND 8UDG ET, WASHINGTON. DC 20503.

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER IS) PAGE (3)

YEAR SEQUENTIAL .oA REVISION NUMSSR CN NUM SR R.E. Glnna'NUclear Power Plant TEXT /// mare Saece /e re/a/rerL Iree ~ HRC Farm 355AB/ (12) o s o o o 24 493 004 0 0 0 8 oF 09 ROOT CAUSE:

The underlying cause of the event was determined to be not isolating the 5A high pressure heater high level dump valve to the HDT prior to commencement of troubleshooting the air supply concerns for the'dump valve.

ANALYSTS OP &TENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of, "any event or conditi'on that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF) including the Reactor Protection System (RPS)". The feedwater isolation of the "B" S/G was an automatic actuation of an ESF system.

An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:

There were no operational or safety consequences or implications attributed to the feedwater isolations because:

o The feedwater isolations occurred at the required S/G level.

0 The plant was quickly stabilized and manual control of FRVs was accomplished to mitigate any consequences of the event.

I, 0 As the feedwater isolations occurred as designed, the assumptions of the FSAR for steam line break were met.

Based on the above, it can be concluded that the public's health and safety was assured at all times.

NRC FomI 365A (589)

NRC FORM 366A UA. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3(500106 (BJIS)

E XP I R ES: 6/30/62 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE ENT REPORT ILER) INFORMATION COLLECTION REOUEST: 60.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1ME PAPERWORK REDUCTION PROJECT (3(500106). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER LSI PAGE (3) r~r' YEAR NUMBER "~

SEOUENTIAL P~S REVISION NUM ER R.E. Gonna Nuclear Power Plant o s o o o 2 449 3 004 00 0 90F TEXT /// mom Jpon /1 mqII/mI/ II' ////JJN/I HRC 36M B/ l(7)

%%dmI V. CORRECTIVE ACTION A ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:

After the S/G levels were stabilized, the FRVs were returned to their pre-event control configuration.

B. ACTION TAKEN OR PLANNED TO PREVENT RECERMFNCE:

To ensure a more rapid mitigation of this type of event and possibly eliminate the feedwater isolation, operating procedure T-6.9A will be changed to delete the steps that place the low pressure heaters condensate bypass valve switch to the closed position.

Operations, Planning, and I&C personnel have been notified that isolation of a heater high level dump valve, prior to troubleshooting, should be considered a normal practice.

ADDITIONAL INFORMATION A. FAILED COMPONENTS:

None.

B PREVIOUS LERs ON SIMILAR EVENTS A similar LER event historical search was conducted with the following results: LER 91-009 and LER 006 (Revision 1) were similar events with different root causes.

C SPECIAL COMMENTS:

LER 92-006 (Revision 1) indicates the problems that have been experienced with the Advanced Digital Feedwater Control System (ADFCS), the causes and corrective actions taken or planned.

NRC Form 366A (686)

h T