ML17223B170: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:ACCELERATED DISTRIBUTION DEMONS~TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)'ACCESSION NBR:9105060103 DOC.DATE: 91/04/30 NOTARIZED:
{{#Wiki_filter:DISTRIBUTION DEMONS~TION SYSTEM ACCELERATED REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
NO FACIL:50-389 St.Lucie Plant, Unit 2, Flor'ida Power&Light Co.AUTH.NAME AUTHOR AFFILIATION, LAUVER,C.Florida Power&Light Co.SAGER,D.A.
'ACCESSION NBR:9105060103                 DOC.DATE: 91/04/30     NOTARIZED: NO         DOCKET FACIL:50-389 St. Lucie Plant, Unit 2, Flor'ida Power               & Light   Co. 05000389 AUTH. NAME           AUTHOR AFFILIATION, LAUVER,C.             Florida     Power & Light Co.
Florida Power&Light Co.~RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000389
SAGER,D.A.           Florida     Power & Light Co.     ~
RECIP.NAME           RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 91-003-00:on 910426,2A shutdown cooling heat exchanger out of.svc due to mispositioned component cooling water valve.Caused by personnel error.Valve correctly realigned&redundant train's valve checked.W/910430 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR J ENCL J SIZE: ,.TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.1 NOTES: A RECIPIENT ID CODE/NAME PD2-2 LA NORRIS,J INTERNAL: ACNW AEOD/DOA.AEOD/ROAB/DSP NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPB11
LER 91-003-00:on 910426,2A shutdown cooling heat exchanger out of. svc due to mispositioned component cooling water valve. Caused by personnel error. Valve correctly realigned
'RR/DST/SICB 7E NRR/DST/SRXB 8E RES/DS IR/EI B EXTERNAL: EG&G BRYCE,J.H NRC PDR NSIC POOREEW COPIES LTTR ENCL 1 1 1 1 2 2 1 1 2 2 1 1 1 1 2 2 1 1 1 1 1 1 3 3 1 1 1 1 RECIPIENT ID CODE/NAME PD2-2 PD ACRS~AEOD/DS P/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB11 NRR/DOEA/OEAB NRR/DST/SELB 8D NRR/DST 2LBBJ31 RE 0M RGN2 FILE 01 L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT'COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 D D'D NOTE TO ALL"RIDS" RECIPIENTS:
                & redundant     train's valve checked.W/910430 ltr.
D D PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 33 ENCL 33 P.O.Box 128, Ft.Pierce, FL 34954-0128 FPL APR 3 0 199'-91-133 10 CFR 50.73 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
  ,.
Re: St.Lucie Unit 2 Docket No.50-389'Reportable Event 91-03 Date of Event: April 26, 1991 2A Shutdown Cooling Heat Exchanger Out of Service Due to Mispositioned Component Coolin Water Outlet Valve Caused b Personnel Error The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.A supplemental report will be submitted at the usual 30 day time interval.Very truly yours, D.A.S ger Vice sident St.Lucie Plant DAS:GRM:kw Attachment cc: Stewart D.Ebneter,.Regional Administrator, USNRC Region II Senior Resident Inspector, USNRC, St.Lucie Plant DAS/PSL N423 9g0c0rr0i03 910430 PDF ADOCK 0 000~89 PDR'"~~men FPL Group company:.:.=t.287&gag FPL FacsilliIC OI.NRCFNITT 666<coy U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)~AffNOIIO CAO NO 01 004100 4000%4: lOtH 0 CSTNHITO 000OOI POI IKKOOC IO DC040T 00TN TN0 04Cf0AATTITI DCUE CDITI IOITNCD 000 1000 ICNWNCT CCINCNTC IKCNIIO CIITXN CTTAIATC TO TIC ICDITITT NO NEIDNTC IWNAINICNI OIANGN I040IL IAL IACITAl IKCIIATOIT
1 J
~WANNNDDN.
TITLE: 50.73/50.9 Licensee Event Report (LER), IncidentJ Rpt, etc.
DC SXk4 AIOTO TIN PAOIACITI ICDUGTIDN ffCICCT I 01NI4OC, Cf INN Cf WNAGTACNT NO ILA0GCT WAONIGTDK DC IIICl FACILITY NAME (1)St.Lucie Unit 2 DOCKET NUMBER (2)PAGE 3 050003891 0 0 4'(4)2A Shutdown Cooling Heat Exchanger Out of Service Due to Mispositioned Component Cooling Water Valve Caused by Personnel Error EVENT DATE (5)LER NUMBER (6)REPORT DATE (7)OTHER FACILITIES INVOLVED (8)MONTH DAY 0 4 2 6 YEAR 9 1.9 1 0 0 3 YEAR S IAL MONTH DAY 0 0 4 3 0 YEAR 9 1 FACILITY NAMES N/A N/A DOCKET NUMBER(S)5 0 0 05000.OPERATING MODE (9)POWER LEVEL, (10)1 0 0 201402(b)20.405(a)(1)(i) 20.405(a)(1)(ii) 20.405(a)(1)(iii)201405(a)(1)(iv) 20.405(c)50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(i) 50.73(a)(2)(ii)50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B)
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR                    ENCL      SIZE:
~THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR: Check one or more of the followin (11)73.71(b)73.71(c)OTHER (Specify in Abstract beloIvandin Text NRC Form 366A)20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
NOTES:                                                                                       A RECIPIENT               COPIES            RECIPIENT          'COPIES          D ID CODE/NAME             LTTR ENCL        ID  CODE/NAME      LTTR ENCL PD2-2 LA                     1    1      PD2-2 PD                1    1          D
NAME LICENSEE CONTACT FOR THIS LER 12 Catherine Lauver, Shift Technical Advisor TELEP ONE NUMBER AREA CODE 4 0 7 465-3550 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 CAUSE SYSTEM COMPONENT MANUFAC-TURER B E I S V P 3 4 0 REPORTABLE TO NPRDS CAUSE SYSTEM COMPONENT I I I REPORTABLE TO NPRDS SUPPLEMENTAL REPORT EXPECTED 14 YES (If yes;complete EXPECTED SUBMISSION DATE)NO EXPECTED MONTH DAY YEAR SUBMISSION DATE (15)0 5 2 6 9 ABSTRACT (Limit to f400 spaces.i.e.
                                                                                                    '
approximately fifteen single-space typewritten lines)(16)This is an interim report.A followup report will be submitted.
NORRIS,J                     1    1 INTERNAL:     ACNW                         2    2      ACRS                    2    2 AEOD/DOA                     1    1    ~ AEOD/DS P/TPAB          1    1
Corrective actions include: the valve was correctly realigned; the redundant train's valve was checked;both units performed a full Valve Status Check.At 0110 on April 26, 1991, with Unit 2 at 100%power, Operations personnel began searching for a DC ground.At 0400, per plant procedure, Operations cycled HCV-14-3A, Component Cooling Water (CCW)outlet from the 2A Shutdown Cooling (SDC)Heat Exchanger (HX)to de-energize its solenoid operator in an effort to locate the DC ground.After the valve opened, no flow through the heat exchanger was indicated.
              .AEOD/ROAB/DSP                 2    2      NRR/DET/ECMB 9H        1    1 NRR/DET/EMEB 7E               1    1      NRR/DLPQ/LHFB11        1    1 NRR/DLPQ/LPEB10               1    1      NRR/DOEA/OEAB          1    1 NRR/DREP/PRPB11               2    2      NRR/DST/SELB 8D        1    1
Upon investigation, the 2A SDC HX CCW return isolation valve SB-14365 was found to be locked closed.This valve is required to be Locked Open.It had been entered into the Valve Switch Deviation Log on October 23, 1990 as Locked Throttled and restored November 29, 1990.As this is the most recent documented manipulation date, it is assumed to have been mispositioned at this time.The valve position pointer was broken and indicated open.The cause of the mispositioning is under investigation.
            'RR/DST/SICB 7E                 1    1      NRR/DST 2LBBJ31        1    1 NRR/DST/SRXB 8E               1    1      RE            0M      1    1 RES/DS IR/EIB                1    1      RGN2    FILE  01      1    1 EXTERNAL: EG&G BRYCE,J.H                     3   3     L ST LOBBY WARD        1     1 NRC PDR                      1   1     NSIC MURPHY,G.A         1     1 NSIC POOREEW                  1   1     NUDOCS FULL TXT        1     1 D
FPL Facsimile of NRC Form 366 (6-89)
D D
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR               33   ENCL   33


FPL Facslmra or NRO Form 666 (6-69)~U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION ASSASNTO CAO ISA$150 0105 EITf saba AITI505 ssrsfATTO usTWN sea tKspQNsc To cCANLT wlTH TNs ssofsfATcN Souse TISH MOICST: 50 0 ISTS ICON f505 CASAOITS fNCAIONO TASSXN Saf WATS TO TIN raxSSIiNetcSCTTTSuuNAmSNT TNANCH 5 Caa ua 55ASSNT NSOAATNTT ofaIASNSN wAsHNCION.
P.O. Box 128, Ft. Pierce, FL 34954-0128 FPL APR 3 0 199'-91-133 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn:     Document Control Desk Washington, D. C. 20555 Gentlemen:
oc 505fa Ncl To TIc sfsTIINcfN MTTucllQH NT55'ci I'150010150frICC of IMWdDCNf AIST 55$5CCT WNSINSTTSAOC 5050$FACILITY NAME (1)DOCKET NUMBER (2)LER NUMBER (6)PAGE (3)St.Lucie Unit 2 05000389 YEAR 9 1 EQUENTIAL NUMBER 0 0 3 REVISION NUMBER 0 0 0 2 0 0 4 TEXT (If more spaceis reriuired, use additional NRC Form 366A's)(17)This is an interim report.A followup report will be submitted At 0110 on April 26, 1991, with Unit 2 at 100%power, Operations personnel began to search for a DC ground.To find a ground, plant toads are individually isolated.Per plant procedure, Operations cycled HCV-14-3A, Component Cooling Water (CCW)(EIIS:CC)from the 2A Shutdown Cooling (SDC)Heat Exchanger (HX)(EIIS:BP).
Re:    St. Lucie Unit 2 Docket No. 50-389
During normal operations there is no flow through the shutdown heat exchanger; opening the valve should have resulted in 4000 gpm flow.There was no flow indicated through the HX.Operations.
              'Reportable Event            91-03 Date of Event: April 26, 1991 2A Shutdown Cooling Heat Exchanger Out of Service Due to Mispositioned Component Coolin Water Outlet Valve Caused b Personnel                      Error The attached          Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.             A supplemental report will be submitted at the usual 30 day time interval.
locally verified movement of HCV-14-3A and position of CCW inlet isolation valve SB-14348.CCW outlet isolation valve SB-14365 is required to be Locked Open, was indicating open by its valve position indicator, but was in fact Locked Closed.The valve was reopened to its proper position.The redundant train's CCW outlet isolation valve position was checked as a precaution.
Very  truly yours, D. A. S    ger Vice        sident St. Lucie Plant DAS:GRM:kw Attachment cc: Stewart D. Ebneter,.Regional Administrator, USNRC Region Senior Resident Inspector, USNRC, St. Lucie Plant II DAS/PSL N423 9g0c0rr0i03 910430 PDF    ADOCK      0  000~89 PDR
The valve was in its proper Locked Open position, but its position indicator was also faulty.An investigation revealed that SB-14365 was entered into the Valve Switch Deviation Log on October 23, 1990, when placed in a Locked Throttled position to balance CCW flow.On November 25, 1990, as Unit 2 was completing a refueling outage, the CCW system was placed in its operating alignment.
                                                                                    &gag
Operating Procedure 2-0310020,"Component Cooling Water-Normal Operation," was performed.
    ' " ~ ~ men
SB-14365 was verified to be Locked Open at this time;On November 29, 1990, the Valve Switch Deviation Log showed that the valve was restored to its Locked Open position.As November 29 is the last recorded date that SB-14365 was manipulated, it is assumed that the valve has been mispositioned since this time.The lack of an OPERABLE 2A SDC HX causes the 2A train of the Containment Spray System (EIIS:BE)to be administratively out of service.From 0455 on February 19 through 0315 on February 20 and 2208 on February 20 through 1700 on February 21, 1991, the 2B Containment Spray System was out of service for routine maintenance and testing.Plant records are being reviewed to see if there are any other periods of time where both trains of the Containment Spray System were out of service.CCW outlet isolation valve SB-14365 is a manually operated butterfly valve located in a horizontal line about twelve feet above the floor.Valve position indication is provided by a pointer which is supposed to move with the valve stem.The pointer was broken.A Plant Work Order was written October 21, 1990 to repair the pointer and was apparently worked January 17, 1991.At the time the mispositioning was discovered, the pointer erroneously indicated Open.Investigation into this valve position indicator failure will continue.A Standing Night Order states that to check the position of a Locked Open valve, the valve shall be unlocked, closed slightly, reopened, and relocked.While the position indicated by the pointer was inaccurate and misleading, the handwheel on the valve indicates which way to turn to open the valve.Since November of 1990, the position of this valve has been checked twice during the quarterly performance of Administrative Procedure 2-0010123,"Administrative Control of Valves, Locks, and Switches," and weekly during Administrative Procedure 2-0010125A,"Surveillance Data Sheets," FPL Facsimile of NRC Form 366 (6-69)
:.:.= t. 287    FPL Group company


FPL FccEIIIIAI ol NR" Form 666 (649)V U.S.NUCLEAR REGUlATORY COMMrsslON LICENSEE EVENT REPORT (LER)'EXT CONTINUATION APPICNTO CAO NCk$1 000 10I E PIKR 00000 ECIPNCTo$$oEN PETI fKSPCtSE To CIEPET PRII TIIC ISP&#xc3;NAATEPI COUEC CIPI IET$ECP.$1$100$RANNO COWRIE IK CAfoRC RTeol ECTCIATE To TIE IECOT$$No IEPOlr$NANIEIEIIT NNN001+0$E oC IAAEEAEIKOAATCAP
FPL FacsilliIC OI.                                          U.S. NUCLEAR REGULATORY COMMISSION                            ~ AffNOIIOCAO NO 01 004100 NRCFNITT 666                                                                                                                        4000%4: lOtH0 CSTNHITO 000OOI POI IKKOOCIO DC040T 00TN TN0 04Cf0AATTITIDCUE CDITI
~~.ocPEN,~TooEP~RoccRP RE0EETI$1$001000 cffcE cP MNIAEEAENT AIA MxET, sEIPATlcR cc$050$FACILITY NAME (1)St.Lucie Unit 2 DOCKET NUMBER (2)YEAR 0500038991 LER NUMBER (6)EQUENTIAL NUMBER 0 0 3 REVISIO NUMBER 0 0 PAGE (3)0 30 0 4 TEXT (lf more spaceis required, use additional NRC Form 366A's)'17)
  <coy                            LICENSEE EVENT REPORT (LER)                                           IOITNCD000 1000 ICNWNCT CCINCNTC IKCNIIOCIITXNCTTAIATCTO TIC ICDITITTNO NEIDNTC IWNAINICNIOIANGNI040ILIALIACITAlIKCIIATOIT
...Data Sheet 36, I At all times it was reported to be Locked Open.The root cause of the event is under investigation.
                                                                                                        ~WANNNDDN.DC SXk4 AIOTOTIN PAOIACITIICDUGTIDNffCICCTI 01NI4OC, CfINN Cf WNAGTACNTNO ILA0GCT WAONIGTDKDC IIICl FACILITYNAME (1)                                                                                                  DOCKET NUMBER (2)                    PAGE 3 St. Lucie Unit 2
A review of plant records, including operator logs, clearances, and Plant Work Orders, is being conducted.
    '      (4) 050003891                                0      0 4 2A Shutdown Cooling Heat Exchanger Out of Service Due to Mispositioned Component Cooling Water Valve Caused by Personnel Error EVENT DATE (5)                    LER NUMBER (6)                    REPORT DATE (7)                OTHER FACILITIES INVOLVED(8)
Personnel will be interviewed to determine the specific nature and cause of the error.An INPO Human Performance Enhancement System evaluation will also be performed.
MONTH DAY YEAR YEAR                    S          IAL                MONTH DAY        YEAR        FACILITYNAMES                        DOCKET NUMBER(S)
V NT This event is reportable under the requirements of 10CFR50.73.a.2.i.B, any condition or operation prohibited by Technical Specifications.
N/A                            5      0 0 0     4    2 6 9    1.
Technical Specification 3.6.2.1"Containment Spray System" requires two independent Containment Spray Systems to be OPERABLE with an OPERABLE Shutdown Cooling Heat Exchanger.
                              ~
A While the exact date of the mispositioning of the CCW outlet isolation valve to the 2A SDC HX is not yet known, November 29, 1990 is the last recorded date of a manipulation of the valve and is assumed to be the date of the mispositioning.
9  1      0 0      3           0     0     4 3 0 9 1 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR:
Over a three day period in February 1991, the 2B Containment Spray System was taken out of service for routine maintenance and testing.The SDC HX is not used until the recirculation phase for decay heat removal.The 2A Containment Spray System was always available to receive cool water from the Refueling Water Tank and deliver it to containment to mitigate a post-LOCA containment pressure rise.An alternate safety system for Containment Heat Removal, the Containment Cooling System, is being further evaluated for decay heat removal capability.
N/A 05000.
St.Lucie equipment sizing is such that the four containment fan coolers will provide the containment heat removal capability necessary to limit and reduce accident containment pressure and temperature during the recirculation phase.Additional analysis are in progress, assuming a single failure, to demonstrate that two containment fan coolers can also remove Large Break LOCA containment heat load during the recirculation phase.This result is expected because of the PSL containment design in which the free standing steel vessel will transfer heat to the environment.
OPERATING                      Check one or more of the followin      (11)
FPL Engineering has performed a first order risk assessment of the CCW to the SDC HX valve being in the closed position.For a medium or large break LOCA, the frequency associated with the loss of the decay heat removal function only increases from 3.6E-8 per reactor year with a normal SDC HX lineup, to 5.8E-7 per reactor year with the shutdown heat exchanger isolated.With operator action to open the valve, the frequency is reduced to 1.5E-7 per reactor year.Therefore, the health and safety of the public was not affected during this condition.
MODE (9) 201402(b)                     20.405(c)                    50.73(a)(2)(iv)                            73.71(b)
FPL Facsimile of NRC Form 366 (6-89)  
POWER LEVEL,                             20.405(a)(1)(i)                50.36(c)(1)                  50.73(a)(2)(v)                            73.71(c)
"t III FPL FocsIITS'AT o.'RC Form 666 (649)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUAllON 0 FFFHOFCO CAO IAS SH0410l CSFSHO: AOWT CNSIATtOOACIHFCHFKSFCSOC TOCCAOSTWOHTIESSFOFSAATCIOOUECSOI FCCACSv:a4 WTS FCHA1AIO CCAACTOSFHOAFOWOHASHH tSISAAIC TOHC FCOrftfS FIAT FCFOITS NQACCAASIT OIAHCH IF4$$OOSrrltAR FHOAAIOHT 00$40$CAI WAOOHOCW.OC Tl&#xc3;OL FFST To SIC FFCFFINASW SDVCOCH FFTSCCT ($110410AS Cf FISC OF AAOCACTITAFO IIAXCT,WASH HOTOA OC SH0$FACILITY NAME (1)St.Lucie Unit 2 DOCKET NUMBER (2)YEAR LER NUMBER (6)EQUENTIAL NUMBER REVISION NUMBER PAGE (3)0500038991 TEXT (If more spaceis rerluired, use additional NRC Form 366A's)(17)0 0 3 0 0 0 4 0 0 4 1.Operations restored SB-14365 to its proper position and verified the position of the redundant train's CCW outlet isolation valve.2.Plant Work Orders were submitted to repair the faulty pointers on each valve and determine the root cause of the faulty pointer.3.All Operations personnel were counseled on the use of the Standing Night Order.Operations is investigating further methods to enhance independent verification.
(10)      1    0  0          20.405(a)(1)(ii)              50.36(c)(2)                  50.73(a)(2)(vii)                          OTHER 20.405(a) (1)(iii)                                                                                      (Specify in Abstract 50.73(a)(2)(i)              50.73(a)(2)(viii)(A) beloIvandin Text 201405(a)(1)(iv)              50.73(a)(2) (ii)            50.73(a)(2)(viii)(B)                        NRC Form 366A) 20.405(a)(1)(v)                50.73(a)(2)(iii)            50.73(a)(2)(x)
4.Operations performed the entire Weekly Valve Status Check on both Unit 1 and Unit 2.No further discepancies were noted.5.An INPO Human Performance Enhancement System evaluation will be performed on this event.'he review will include human factors and work conditions.
LICENSEE CONTACT FOR THIS LER 12 NAME                                                                                                                        TELEP ONE NUMBER Catherine Lauver, Shift Technical Advisor                                                        AREA CODE COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 4      0    7      465 -3550 CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE                                        CAUSE SYSTEM COMPONENT                                          REPORTABLE TURER        TO NPRDS                                                                                  TO NPRDS B      E    I    S  V      P 3    4  0 I      I    I SUPPLEMENTAL REPORT EXPECTED 14                                                                                    MONTH          DAY YEAR EXPECTED YES (Ifyes; complete EXPECTED SUBMISSION DATE)                                                    SUBMISSION NO                          DATE (15)                    0      5    2 6 9 ABSTRACT (Limit to f400 spaces.i.e. approximately fifteen single-space typewritten lines) (16)
Affected Component Identification:
This is an interim report. A followup report will be submitted.
Henry Prat t 14H Butterfly Valve Nuclear MK II with Manual Operator MDT-3 HW Model Number 1001 78 Serial Number C140 Previous Similar Licensee Event Reports: 335-89-002"Inoperable 1B Diesel Generator Due to Fuel Oil System Valve Misalignment" 335-87-012"Loss of Component Cooling Water Redundancy-1A and 1B Component Cooling Water Cross-tie Valves in Open Position" FPL Facsimile of NRC Form 366 (6-69)}}
At 0110 on April 26, 1991, with Unit 2 at 100% power, Operations personnel began searching for a DC ground.
At 0400, per plant procedure, Operations cycled HCV-14-3A, Component Cooling Water (CCW) outlet from the 2A Shutdown Cooling (SDC) Heat Exchanger (HX) to de-energize its solenoid operator in an effort to locate the DC ground. After the valve opened, no flow through the heat exchanger was indicated. Upon investigation, the 2A SDC HX CCW return isolation valve SB-14365 was found to be locked closed. This valve is required to be Locked Open. It had been entered into the Valve Switch Deviation Log on October 23, 1990 as Locked Throttled and restored November 29, 1990. As this is the most recent documented manipulation date, it is assumed to have been mispositioned at this time. The valve position pointer was broken and indicated open.
The cause of the mispositioning is under investigation.
Corrective actions include: the valve was correctly realigned; the redundant train's valve was checked; both units performed a full Valve Status Check.
FPL Facsimile of NRC Form 366 (6-89)
 
FPL Facslmra or                                  ~ U.S. NUCLEAR REGULATORY COMMISSION ASSASNTO CAO ISA$ 150 0105 NRO Form 666 EITf saba AITI505 (6-69)
LICENSEE EVENT REPORT (LER)                                          ssrsfATTO usTWN sea tKspQNsc To cCANLTwlTH TNs ssofsfATcN Souse TISH MOICST: 50 0 ISTS ICONf505 CASAOITS fNCAIONOTASSXN Saf WATS TO TIN TEXT CONTINUATION                                              raxSSIiNetcSCTTTSuuNAmSNT TNANCH 5 Caa ua 55ASSNT NSOAATNTT ofaIASNSN wAsHNCION. oc 505fa Ncl To TIc sfsTIINcfN MTTucllQHNT55'ci I
                                                                                            '150010150frICC of IMWdDCNfAIST 55$5CCT WNSINSTTSAOC 5050$
FACILITYNAME (1)                                                DOCKET NUMBER (2)                LER NUMBER (6)                                        PAGE (3)
YEAR          EQUENTIAL REVISION St. Lucie Unit 2                                                                    NUMBER                      NUMBER 05000389 TEXT (Ifmore spaceis reriuired, use additional NRC Form 366A's) (17) 9 1          0        0      3              0        0  0 2        0    0 4 This is an interim report. A followup report will be submitted At 0110 on April 26, 1991, with Unit 2 at 100% power, Operations personnel began to search for a DC ground. To find a ground, plant toads are individually isolated. Per plant procedure, Operations cycled HCV-14-3A, Component Cooling Water (CCW) (EIIS:CC) from the 2A Shutdown Cooling (
SDC) Heat Exchanger (HX) (EIIS:BP). During normal operations there is no flow through the shutdown heat exchanger; opening the valve should have resulted in 4000 gpm flow. There was no flow indicated through the HX. Operations. locally verified movement of HCV-14-3A and position of CCW inlet isolation valve SB-14348. CCW outlet isolation valve SB-14365 is required to be Locked Open, was indicating open by its valve position indicator, but was in fact Locked Closed.
The valve was reopened to its proper position. The redundant train's CCW outlet isolation valve position was checked as a precaution. The valve was in its proper Locked Open position, but its position indicator was also faulty.
An investigation revealed that SB-14365 was entered into the Valve Switch Deviation Log on October 23, 1990, when placed in a Locked Throttled position to balance CCW flow. On November 25, 1990, as Unit 2 was completing a refueling outage, the CCW system was placed in its operating alignment. Operating Procedure 2-0310020, "Component Cooling Water-Normal Operation," was performed. SB-14365 was verified to be Locked Open at this time; On November 29, 1990, the Valve Switch Deviation Log showed that the valve was restored to its Locked Open position. As November 29 is the last recorded date that SB-14365 was manipulated, it is assumed that the valve has been mispositioned since this time. The lack of an OPERABLE 2A SDC HX causes the 2A train of the Containment Spray System (EIIS:BE) to be administratively out of service.
From 0455 on February 19 through 0315 on February 20 and 2208 on February 20 through 1700 on February 21, 1991, the 2B Containment Spray System was out of service for routine maintenance and testing. Plant records are being reviewed to see if there are any other periods of time where both trains of the Containment Spray System were out of service.
CCW outlet isolation valve SB-14365 is a manually operated butterfly valve located in a horizontal line about twelve feet above the floor. Valve position indication is provided by a pointer which is supposed to move with the valve stem. The pointer was broken. A Plant Work Order was written October 21, 1990 to repair the pointer and was apparently worked January 17, 1991. At the time the mispositioning was discovered, the pointer erroneously indicated Open. Investigation into this valve position indicator failure will continue.
A Standing Night Order states that to check the position of a Locked Open valve, the valve shall be unlocked, closed slightly, reopened, and relocked. While the position indicated by the pointer was inaccurate and misleading, the handwheel on the valve indicates which way to turn to open the valve.
Since November of 1990, the position of this valve has been checked twice during the quarterly performance of Administrative Procedure 2-0010123, "Administrative Control of Valves, Locks, and Switches," and weekly during Administrative Procedure 2-0010125A, "Surveillance Data Sheets,"
FPL Facsimile of NRC Form 366 (6-69)
 
FPL FccEIIIIAIol                                  U.S. NUCLEAR REGUlATORY COMMrsslON APPICNTO CAO NCk $ 1 000 10I NR" Form 666                                                                                                                  PIKR 00000 E
(649)                  LICENSEE EVENT REPORT (LER)                                        ECIPNCTo $ $ oEN PETI fKSPCtSE To CIEPET PRII TIICISP&#xc3;NAATEPI COUEC CIPI V                                                                                        IET$ECP. $ 1$ 100$ RANNO COWRIE IKCAfoRC RTeol ECTCIATE To TIE CONTINUATION            'EXT IECOT$ $ No IEPOlr$ NANIEIEIITNNN001+0$ E oC IAAEEAEIKOAATCAP
                                                                                            ~~.ocPEN,~TooEP~RoccRP                                          RE0EETI
                                                                                            $ 1$ 001000 cffcE cP MNIAEEAENTAIAMxET, sEIPATlcR cc      $ 050$
FACILITYNAME (1)                                              DOCKET NUMBER (2)                  LER NUMBER (6)                                          PAGE (3)
YEAR            EQUENTIAL REVISIO St. Lucie Unit 2                                                                      NUMBER                  NUMBER TEXT (lfmore spaceis required, use additional NRC Form 0500038991 366A's)'17) 0      0      3          0          0    0      30        0 4
                                                                              ...
Data Sheet 36,        I                          At all times it was reported to be Locked Open.
The root cause of the event is under investigation. A review of plant records, including operator logs, clearances, and Plant Work Orders, is being conducted. Personnel will be interviewed to determine the specific nature and cause of the error. An INPO Human Performance Enhancement System evaluation will also be performed.
V NT This event is reportable under the requirements of 10CFR50.73.a.2.i.B, any condition or operation prohibited by Technical Specifications. Technical Specification 3.6.2.1 "Containment Spray System" requires two independent Containment Spray Systems to be OPERABLE with an OPERABLE Shutdown Cooling Heat Exchanger.
A While the exact date of the mispositioning of the CCW outlet isolation valve to the 2A SDC HX is not yet known, November 29, 1990 is the last recorded date of a manipulation of the valve and is assumed to be the date of the mispositioning. Over a three day period in February 1991, the 2B Containment Spray System was taken out of service for routine maintenance and testing.
The SDC HX is not used until the recirculation phase for decay heat removal. The 2A Containment Spray System was always available to receive cool water from the Refueling Water Tank and deliver it to containment to mitigate a post-LOCA containment pressure rise. An alternate safety system for Containment Heat Removal, the Containment Cooling System, is being further evaluated for decay heat removal capability.
St. Lucie equipment sizing is such that the four containment fan coolers will provide the containment heat removal capability necessary to limit and reduce accident containment pressure and temperature during the recirculation phase. Additional analysis are in progress, assuming a single failure, to demonstrate that two containment fan coolers can also remove Large Break LOCA containment heat load during the recirculation phase. This result is expected because of the PSL containment design in which the free standing steel vessel will transfer heat to the environment.
FPL Engineering has performed a first order risk assessment of the CCW to the SDC HX valve being in the closed position. For a medium or large break LOCA, the frequency associated with the loss of the decay heat removal function only increases from 3.6E-8 per reactor year with a normal SDC HX lineup, to 5.8E-7 per reactor year with the shutdown heat exchanger isolated. With operator action to open the valve, the frequency is reduced to 1.5E-7 per reactor year.
Therefore, the health and safety of the public was not affected during this condition.
FPL Facsimile of NRC Form 366 (6-89)
 
    "t III
 
FPL FocsIITS'AT Form 666 o.'RC U.S. NUCLEAR REGULATORY COMMISSION 0              FFFHOFCO CAO IAS SH0410l CSFSHO: AOWT (649)                        LICENSEE EVENT REPORT (LER)                                      CNSIATtOOACIHFCHFKSFCSOC TOCCAOSTWOHTIESSFOFSAATCIOOUECSOI FCCACSv:a4 WTS FCHA1AIO CCAACTOSFHOAFOWOHASHH tSISAAIC TOHC TEXT CONTINUAllON                                          FCOrftfS FIAT FCFOITS NQACCAASITOIAHCH IF4$ $ OOSrrltAR FHOAAIOHT 00$ 40$ CAIWAOOHOCW. OC Tl&#xc3;OL FFST To SIC FFCFFINASW SDVCOCH FFTSCCT (
                                                                                                $ 110410AS Cf FISC OF AAOCACTITAFOIIAXCT,WASHHOTOA OC SH0$
FACILITYNAME (1)                                                    DOCKET NUMBER (2)                LER NUMBER (6)                                      PAGE (3)
YEAR          EQUENTIAL REVISION St. Lucie Unit 2                                                                    NUMBER                  NUMBER 0500038991 TEXT (Ifmore spaceis rerluired, use additional NRC Form 366A's) (17) 0        0    3          0        0      0 4      0      0 4
: 1. Operations restored SB-14365 to its proper position and verified the position of the redundant train's CCW outlet isolation valve.
: 2. Plant Work Orders were submitted to repair the faulty pointers on each valve and determine the root cause of the faulty pointer.
: 3.     All Operations personnel were counseled on the use of the Standing Night Order. Operations is investigating further methods to enhance independent verification.
: 4.     Operations performed the entire Weekly Valve Status Check on both Unit 1 and Unit 2. No further discepancies were noted.
: 5. An INPO Human Performance Enhancement System evaluation will be performed on this event.
review will include human factors and work conditions.
                                                                                                                                                            'he Affected Component Identification:
Henry Prat t 14H Butterfly Valve Nuclear MK II with Manual Operator MDT-3 HW Model Number 1001 78 Serial Number C140 Previous Similar Licensee Event Reports:
335-89-002 "Inoperable 1B Diesel Generator Due to Fuel Oil System Valve Misalignment" 335-87-012 "Loss of Component Cooling Water Redundancy-1A and 1B Component Cooling Water Cross-tie Valves in Open Position" FPL Facsimile of NRC Form 366 (6-69)}}

Revision as of 22:44, 29 October 2019

LER 91-003-00:on 910426,2A Shutdown Cooling Heat Exchanger Out of Svc Due to Mispositioned Component Cooling Water Valve.Caused by Personnel Error.Valve Correctly Realigned & Redundant Train Valve checked.W/910430 Ltr
ML17223B170
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 04/30/1991
From: Lauver C, Sager D
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-91-133, LER-91-003, LER-91-3, NUDOCS 9105060103
Download: ML17223B170 (9)


Text

DISTRIBUTION DEMONS~TION SYSTEM ACCELERATED REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

'ACCESSION NBR:9105060103 DOC.DATE: 91/04/30 NOTARIZED: NO DOCKET FACIL:50-389 St. Lucie Plant, Unit 2, Flor'ida Power & Light Co. 05000389 AUTH. NAME AUTHOR AFFILIATION, LAUVER,C. Florida Power & Light Co.

SAGER,D.A. Florida Power & Light Co. ~

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 91-003-00:on 910426,2A shutdown cooling heat exchanger out of. svc due to mispositioned component cooling water valve. Caused by personnel error. Valve correctly realigned

& redundant train's valve checked.W/910430 ltr.

,.

1 J

TITLE: 50.73/50.9 Licensee Event Report (LER), IncidentJ Rpt, etc.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

NOTES: A RECIPIENT COPIES RECIPIENT 'COPIES D ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 1 PD2-2 PD 1 1 D

'

NORRIS,J 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 ~ AEOD/DS P/TPAB 1 1

.AEOD/ROAB/DSP 2 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFB11 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1

'RR/DST/SICB 7E 1 1 NRR/DST 2LBBJ31 1 1 NRR/DST/SRXB 8E 1 1 RE 0M 1 1 RES/DS IR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G BRYCE,J.H 3 3 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POOREEW 1 1 NUDOCS FULL TXT 1 1 D

D D

NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 33 ENCL 33

P.O. Box 128, Ft. Pierce, FL 34954-0128 FPL APR 3 0 199'-91-133 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:

Re: St. Lucie Unit 2 Docket No. 50-389

'Reportable Event 91-03 Date of Event: April 26, 1991 2A Shutdown Cooling Heat Exchanger Out of Service Due to Mispositioned Component Coolin Water Outlet Valve Caused b Personnel Error The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event. A supplemental report will be submitted at the usual 30 day time interval.

Very truly yours, D. A. S ger Vice sident St. Lucie Plant DAS:GRM:kw Attachment cc: Stewart D. Ebneter,.Regional Administrator, USNRC Region Senior Resident Inspector, USNRC, St. Lucie Plant II DAS/PSL N423 9g0c0rr0i03 910430 PDF ADOCK 0 000~89 PDR

&gag

' " ~ ~ men

.:.= t. 287 FPL Group company

FPL FacsilliIC OI. U.S. NUCLEAR REGULATORY COMMISSION ~ AffNOIIOCAO NO 01 004100 NRCFNITT 666 4000%4: lOtH0 CSTNHITO 000OOI POI IKKOOCIO DC040T 00TN TN0 04Cf0AATTITIDCUE CDITI

<coy LICENSEE EVENT REPORT (LER) IOITNCD000 1000 ICNWNCT CCINCNTC IKCNIIOCIITXNCTTAIATCTO TIC ICDITITTNO NEIDNTC IWNAINICNIOIANGNI040ILIALIACITAlIKCIIATOIT

~WANNNDDN.DC SXk4 AIOTOTIN PAOIACITIICDUGTIDNffCICCTI 01NI4OC, CfINN Cf WNAGTACNTNO ILA0GCT WAONIGTDKDC IIICl FACILITYNAME (1) DOCKET NUMBER (2) PAGE 3 St. Lucie Unit 2

' (4) 050003891 0 0 4 2A Shutdown Cooling Heat Exchanger Out of Service Due to Mispositioned Component Cooling Water Valve Caused by Personnel Error EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED(8)

MONTH DAY YEAR YEAR S IAL MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(S)

N/A 5 0 0 0 4 2 6 9 1.

~

9 1 0 0 3 0 0 4 3 0 9 1 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR:

N/A 05000.

OPERATING Check one or more of the followin (11)

MODE (9) 201402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)

POWER LEVEL, 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)

(10) 1 0 0 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a) (1)(iii) (Specify in Abstract 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) beloIvandin Text 201405(a)(1)(iv) 50.73(a)(2) (ii) 50.73(a)(2)(viii)(B) NRC Form 366A) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER 12 NAME TELEP ONE NUMBER Catherine Lauver, Shift Technical Advisor AREA CODE COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 4 0 7 465 -3550 CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT REPORTABLE TURER TO NPRDS TO NPRDS B E I S V P 3 4 0 I I I SUPPLEMENTAL REPORT EXPECTED 14 MONTH DAY YEAR EXPECTED YES (Ifyes; complete EXPECTED SUBMISSION DATE) SUBMISSION NO DATE (15) 0 5 2 6 9 ABSTRACT (Limit to f400 spaces.i.e. approximately fifteen single-space typewritten lines) (16)

This is an interim report. A followup report will be submitted.

At 0110 on April 26, 1991, with Unit 2 at 100% power, Operations personnel began searching for a DC ground.

At 0400, per plant procedure, Operations cycled HCV-14-3A, Component Cooling Water (CCW) outlet from the 2A Shutdown Cooling (SDC) Heat Exchanger (HX) to de-energize its solenoid operator in an effort to locate the DC ground. After the valve opened, no flow through the heat exchanger was indicated. Upon investigation, the 2A SDC HX CCW return isolation valve SB-14365 was found to be locked closed. This valve is required to be Locked Open. It had been entered into the Valve Switch Deviation Log on October 23, 1990 as Locked Throttled and restored November 29, 1990. As this is the most recent documented manipulation date, it is assumed to have been mispositioned at this time. The valve position pointer was broken and indicated open.

The cause of the mispositioning is under investigation.

Corrective actions include: the valve was correctly realigned; the redundant train's valve was checked; both units performed a full Valve Status Check.

FPL Facsimile of NRC Form 366 (6-89)

FPL Facslmra or ~ U.S. NUCLEAR REGULATORY COMMISSION ASSASNTO CAO ISA$ 150 0105 NRO Form 666 EITf saba AITI505 (6-69)

LICENSEE EVENT REPORT (LER) ssrsfATTO usTWN sea tKspQNsc To cCANLTwlTH TNs ssofsfATcN Souse TISH MOICST: 50 0 ISTS ICONf505 CASAOITS fNCAIONOTASSXN Saf WATS TO TIN TEXT CONTINUATION raxSSIiNetcSCTTTSuuNAmSNT TNANCH 5 Caa ua 55ASSNT NSOAATNTT ofaIASNSN wAsHNCION. oc 505fa Ncl To TIc sfsTIINcfN MTTucllQHNT55'ci I

'150010150frICC of IMWdDCNfAIST 55$5CCT WNSINSTTSAOC 5050$

FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR EQUENTIAL REVISION St. Lucie Unit 2 NUMBER NUMBER 05000389 TEXT (Ifmore spaceis reriuired, use additional NRC Form 366A's) (17) 9 1 0 0 3 0 0 0 2 0 0 4 This is an interim report. A followup report will be submitted At 0110 on April 26, 1991, with Unit 2 at 100% power, Operations personnel began to search for a DC ground. To find a ground, plant toads are individually isolated. Per plant procedure, Operations cycled HCV-14-3A, Component Cooling Water (CCW) (EIIS:CC) from the 2A Shutdown Cooling (

SDC) Heat Exchanger (HX) (EIIS:BP). During normal operations there is no flow through the shutdown heat exchanger; opening the valve should have resulted in 4000 gpm flow. There was no flow indicated through the HX. Operations. locally verified movement of HCV-14-3A and position of CCW inlet isolation valve SB-14348. CCW outlet isolation valve SB-14365 is required to be Locked Open, was indicating open by its valve position indicator, but was in fact Locked Closed.

The valve was reopened to its proper position. The redundant train's CCW outlet isolation valve position was checked as a precaution. The valve was in its proper Locked Open position, but its position indicator was also faulty.

An investigation revealed that SB-14365 was entered into the Valve Switch Deviation Log on October 23, 1990, when placed in a Locked Throttled position to balance CCW flow. On November 25, 1990, as Unit 2 was completing a refueling outage, the CCW system was placed in its operating alignment. Operating Procedure 2-0310020, "Component Cooling Water-Normal Operation," was performed. SB-14365 was verified to be Locked Open at this time; On November 29, 1990, the Valve Switch Deviation Log showed that the valve was restored to its Locked Open position. As November 29 is the last recorded date that SB-14365 was manipulated, it is assumed that the valve has been mispositioned since this time. The lack of an OPERABLE 2A SDC HX causes the 2A train of the Containment Spray System (EIIS:BE) to be administratively out of service.

From 0455 on February 19 through 0315 on February 20 and 2208 on February 20 through 1700 on February 21, 1991, the 2B Containment Spray System was out of service for routine maintenance and testing. Plant records are being reviewed to see if there are any other periods of time where both trains of the Containment Spray System were out of service.

CCW outlet isolation valve SB-14365 is a manually operated butterfly valve located in a horizontal line about twelve feet above the floor. Valve position indication is provided by a pointer which is supposed to move with the valve stem. The pointer was broken. A Plant Work Order was written October 21, 1990 to repair the pointer and was apparently worked January 17, 1991. At the time the mispositioning was discovered, the pointer erroneously indicated Open. Investigation into this valve position indicator failure will continue.

A Standing Night Order states that to check the position of a Locked Open valve, the valve shall be unlocked, closed slightly, reopened, and relocked. While the position indicated by the pointer was inaccurate and misleading, the handwheel on the valve indicates which way to turn to open the valve.

Since November of 1990, the position of this valve has been checked twice during the quarterly performance of Administrative Procedure 2-0010123, "Administrative Control of Valves, Locks, and Switches," and weekly during Administrative Procedure 2-0010125A, "Surveillance Data Sheets,"

FPL Facsimile of NRC Form 366 (6-69)

FPL FccEIIIIAIol U.S. NUCLEAR REGUlATORY COMMrsslON APPICNTO CAO NCk $ 1 000 10I NR" Form 666 PIKR 00000 E

(649) LICENSEE EVENT REPORT (LER) ECIPNCTo $ $ oEN PETI fKSPCtSE To CIEPET PRII TIICISPÃNAATEPI COUEC CIPI V IET$ECP. $ 1$ 100$ RANNO COWRIE IKCAfoRC RTeol ECTCIATE To TIE CONTINUATION 'EXT IECOT$ $ No IEPOlr$ NANIEIEIITNNN001+0$ E oC IAAEEAEIKOAATCAP

~~.ocPEN,~TooEP~RoccRP RE0EETI

$ 1$ 001000 cffcE cP MNIAEEAENTAIAMxET, sEIPATlcR cc $ 050$

FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR EQUENTIAL REVISIO St. Lucie Unit 2 NUMBER NUMBER TEXT (lfmore spaceis required, use additional NRC Form 0500038991 366A's)'17) 0 0 3 0 0 0 30 0 4

...

Data Sheet 36, I At all times it was reported to be Locked Open.

The root cause of the event is under investigation. A review of plant records, including operator logs, clearances, and Plant Work Orders, is being conducted. Personnel will be interviewed to determine the specific nature and cause of the error. An INPO Human Performance Enhancement System evaluation will also be performed.

V NT This event is reportable under the requirements of 10CFR50.73.a.2.i.B, any condition or operation prohibited by Technical Specifications. Technical Specification 3.6.2.1 "Containment Spray System" requires two independent Containment Spray Systems to be OPERABLE with an OPERABLE Shutdown Cooling Heat Exchanger.

A While the exact date of the mispositioning of the CCW outlet isolation valve to the 2A SDC HX is not yet known, November 29, 1990 is the last recorded date of a manipulation of the valve and is assumed to be the date of the mispositioning. Over a three day period in February 1991, the 2B Containment Spray System was taken out of service for routine maintenance and testing.

The SDC HX is not used until the recirculation phase for decay heat removal. The 2A Containment Spray System was always available to receive cool water from the Refueling Water Tank and deliver it to containment to mitigate a post-LOCA containment pressure rise. An alternate safety system for Containment Heat Removal, the Containment Cooling System, is being further evaluated for decay heat removal capability.

St. Lucie equipment sizing is such that the four containment fan coolers will provide the containment heat removal capability necessary to limit and reduce accident containment pressure and temperature during the recirculation phase. Additional analysis are in progress, assuming a single failure, to demonstrate that two containment fan coolers can also remove Large Break LOCA containment heat load during the recirculation phase. This result is expected because of the PSL containment design in which the free standing steel vessel will transfer heat to the environment.

FPL Engineering has performed a first order risk assessment of the CCW to the SDC HX valve being in the closed position. For a medium or large break LOCA, the frequency associated with the loss of the decay heat removal function only increases from 3.6E-8 per reactor year with a normal SDC HX lineup, to 5.8E-7 per reactor year with the shutdown heat exchanger isolated. With operator action to open the valve, the frequency is reduced to 1.5E-7 per reactor year.

Therefore, the health and safety of the public was not affected during this condition.

FPL Facsimile of NRC Form 366 (6-89)

"t III

FPL FocsIITS'AT Form 666 o.'RC U.S. NUCLEAR REGULATORY COMMISSION 0 FFFHOFCO CAO IAS SH0410l CSFSHO: AOWT (649) LICENSEE EVENT REPORT (LER) CNSIATtOOACIHFCHFKSFCSOC TOCCAOSTWOHTIESSFOFSAATCIOOUECSOI FCCACSv:a4 WTS FCHA1AIO CCAACTOSFHOAFOWOHASHH tSISAAIC TOHC TEXT CONTINUAllON FCOrftfS FIAT FCFOITS NQACCAASITOIAHCH IF4$ $ OOSrrltAR FHOAAIOHT 00$ 40$ CAIWAOOHOCW. OC TlÃOL FFST To SIC FFCFFINASW SDVCOCH FFTSCCT (

$ 110410AS Cf FISC OF AAOCACTITAFOIIAXCT,WASHHOTOA OC SH0$

FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR EQUENTIAL REVISION St. Lucie Unit 2 NUMBER NUMBER 0500038991 TEXT (Ifmore spaceis rerluired, use additional NRC Form 366A's) (17) 0 0 3 0 0 0 4 0 0 4

1. Operations restored SB-14365 to its proper position and verified the position of the redundant train's CCW outlet isolation valve.
2. Plant Work Orders were submitted to repair the faulty pointers on each valve and determine the root cause of the faulty pointer.
3. All Operations personnel were counseled on the use of the Standing Night Order. Operations is investigating further methods to enhance independent verification.
4. Operations performed the entire Weekly Valve Status Check on both Unit 1 and Unit 2. No further discepancies were noted.
5. An INPO Human Performance Enhancement System evaluation will be performed on this event.

review will include human factors and work conditions.

'he Affected Component Identification:

Henry Prat t 14H Butterfly Valve Nuclear MK II with Manual Operator MDT-3 HW Model Number 1001 78 Serial Number C140 Previous Similar Licensee Event Reports:

335-89-002 "Inoperable 1B Diesel Generator Due to Fuel Oil System Valve Misalignment" 335-87-012 "Loss of Component Cooling Water Redundancy-1A and 1B Component Cooling Water Cross-tie Valves in Open Position" FPL Facsimile of NRC Form 366 (6-69)