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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr ML17229A7381998-05-21021 May 1998 LER 98-006-00:on 980421,missed EDG Fuel Oil Sample Surveillance Was Noted.Caused by Personnel Error.Revised Fuel Oil Sampling Service Purchase Order & Revised Site procedure.W/980521 Ltr ML17229A7011998-04-27027 April 1998 LER 98-003-00:on 980326,discovered Containment Pressure Instrumentation Design Single Failure Vulnerability.Caused by Inadequate Design by Personnel Error.Removed RPS & ESFAS Containment Pressure Bypass Keys immediately.W/980427 Ltr ML17229A6761998-04-0202 April 1998 LER 98-005-00:on 980305,identified Two Conditions That Were Outside App R Design Bases.Caused by Design Oversight During Development of Original App R Safe SD Design.Established 30 Minute Roving Fire Watches & Provided training.W/980402 Ltr ML17229A6731998-03-26026 March 1998 LER 98-002-00:on 980224,radiation Monitor Surveillance Inadequacies Led to Operating of Facility Prohibited by Tss. Caused by Congnitive Personnel Error.Permanent Procedure Changes Were implemented.W/980326 Ltr ML17229A6551998-03-0505 March 1998 LER 98-001-00:on 980206,high/low Pressure Shutdown Cooling Interface Was Noted Outside App R Design Bases.Caused by Personnel Error.Addl Guidance Was Provided to Engineering Dept personnel.W/980305 Ltr ML17229A6281998-02-19019 February 1998 LER 98-004-00:on 980121,emergency Lighting Outside App R Design Bases Occurred.Caused by Congnitive Personnel Error During Translation of App R Section Iii.Procedures Onop 1 & 2 ONP-100.01 Were Issued for Use on 980206.W/980219 Ltr ML17229A6211998-02-0909 February 1998 LER 98-003-00:on 980110,manual Rt Due to DEH Leak at Turbine Test Block Was Noted.Caused by o-ring Extrusion.Shortened Bolts by About 0.125 & Reinstalled at Correct Torque values.W/980209 Ltr ML17229A6191998-02-0404 February 1998 LER 98-002-00:on 980105,CIS Bistable in Bypass Resulted in Condition Prohibited by Tss.Caused by Personnel Error. Radiation Monitor Was Restored to service.W/980204 Ltr ML17229A6161998-02-0303 February 1998 LER 98-001-00:on 980104,inadvertent RPS Actuation Occurred Due to Personnel Error.Caused by Procedural Inadequacies & Inadequate self-checking by Licensed Utility Personnel. Placards Have Been Placed in CRs.W/980203 Ltr ML17229A6051998-01-27027 January 1998 LER 97-010-01:on 971027,inadvertent Core Alteration Prohibited by TSs Were Noted Due to Stuck Cea.Caused by Personnel Error.Cea #24 Was Dislodged & Transferred to Spent Pool for insp.W/980127 Ltr ML17229A5501997-12-0505 December 1997 LER 97-008-00:on 971107,inadequate CR Ventilation Surveillance Resulted in Condition Prohibited by Ts.Caused by non-cognitive Personnel Error.Operating Procedure 2-1900050 Was revised.W/971205 Ltr ML17309A9091997-12-0202 December 1997 LER 97-011-00:on 971102,non-conservative RAS Set Point Resulted in Operation Prohibited by Ts.Caused by Inadequate Set Point & Instrument Loop Scaling Process.Revised ESFAS Functional Tp W/Proper Set point.W/971202 Ltr ML17229A5391997-11-26026 November 1997 LER 97-010-00:on 971027,inadvertant Core Alteration Prohibited by TS Occurred.Caused by CEA Failure to Detach from Ugs.Safety Evaluation Was Performed & Procedural Rev Made to Continue Upper Guide Structure move.W/971126 Ltr ML17229A5151997-11-0707 November 1997 LER 97-007-00:on 971008,inoperable Containment Cooling Fan Resulted in Operation of Facility Outside Design Basis. Caused by non-cognitive Personnel Error.Ccs Operation Was Revised & Issued on 971013.W/971107 Ltr ML17229A4991997-10-17017 October 1997 LER 97-009-00:on 970917,inoperable PORV Block Valve Resulted in Operation Prohibited by Tech Specs Occurred.Caused by Plant GL 89-10 Program Plan to Review Plant Manager Action Item Sys.Porv Block Valve V-1403 restored.W/971017 Ltr ML17309A9011997-08-27027 August 1997 LER 97-008-00:on 970728,mechanical Fire Penetrations Were Inoperable & Outside App R Design Bases.Caused by Seal Mfg Not Providing Formal Documentation for Installed Seals. Modified Inoperable Fire penetrations.W/970827 Ltr ML17229A4311997-07-29029 July 1997 LER 97-006-00:on 970630,discovered Inadequate Testing of Engineered Safety Features Subgroup Relays.Caused by Inadequacy in Implementing TS Requirements in Surveillance Procedures.Revised Surveillance procedures.W/970729 Ltr ML17229A4241997-07-25025 July 1997 LER 97-005-00:on 970625,discovered That Hot Shutdown Control Panel Shutdown Cooling Flow indicator,FI-3306 Inoperable. Caused by Weakness in Work Order & Procedure Used to Repair FI-3306.Section Meeting W/I&C Planners held.W/970725 Ltr ML17229A3971997-07-11011 July 1997 LER 97-004-00:on 970611,discovered Incorrect Original Cable Tray Fire Stop Assembly Installation Was Outside App R Design Basis.Caused by Personnel Error.Hourly Fire Watch Patrols Will Be posted.W/970711 Ltr ML17229A3871997-06-19019 June 1997 LER 97-003-00:on 970521,determined Required Post Maint Open Stroke Test for Valve V3245,2B2 SIT Discharge Check Valve, Had Not Been Performed.Caused by Personnel Error.Procedure revised.W/970619 Ltr ML17229A3841997-06-17017 June 1997 LER 97-002-00:on 970518,containment Sump Debris Screen Was Not IAW Design Due to Gaps in Screen Encl.Performed SER to Document Containment Sump Design requirements.W/970617 Ltr ML17229A3751997-06-0202 June 1997 LER 97-006-00:on 970501,operation Was Prohibited by TS Due to Inadequately Tested Degraded Voltage Sys.Revised Unit 1 ESFAS Surveillance Test procedure.W/970602 Ltr ML17229A3611997-05-29029 May 1997 LER 97-007-00:on 970502,reactor Coolant Pump Oil Collection Sys Was Outside App R Design Bases.Identified Leak Sites Were Repaired & Mods to RCP Oil Collection Sys to Capture Any Future Leakage from areas.W/970529 Ltr ML17229A3491997-05-21021 May 1997 LER 97-001-00:on 970423,containment Isolation Actuation Occurred.Caused by Increased Radiation Levels During Removal of Upper Guide Structure.Proper Actuation of Containment Isolation Components Was verified.W/970521 Ltr ML17229A3441997-05-13013 May 1997 LER 97-005-00:on 970419,reactor Was Shutdown Due to Reactor Coolant Pressure Boundary Leakage.Hot Cracking Was Caused by Weld Contamination.Repairs to RCPB Were Completed & 1A SDC Train Was Restored to Svc ML17229A3141997-04-30030 April 1997 LER 97-004-00:on 970402,refueling Machine Was Operating in Manner Prohibited by TS Due to Original Design of Refueling Machine Bypass Feature Conflicting W/Ts Requirements. Eliminated Overload Cut Off Limit bypass.W/970430 Ltr ML17229A2951997-03-31031 March 1997 LER 97-003-00:on 970304,automatic Rt Resulted from Loss of Electrical Power to 1A2 Rc Pump.Rcp Breaker Was Replaced & Pump Was Returned to svc.W/970331 Ltr ML17229A2721997-03-21021 March 1997 LER 97-002-00:on 970221,operation in Excess of Max Rated Thermal Power Occurred Due to Digital Data Processing Sys (Ddps) Calorimetric Error.Verified Acceptable Performance of Ddps Functions & Reviewed Software mods.W/970321 Ltr 1999-07-06
[Table view] Category:RO)
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr ML17229A7381998-05-21021 May 1998 LER 98-006-00:on 980421,missed EDG Fuel Oil Sample Surveillance Was Noted.Caused by Personnel Error.Revised Fuel Oil Sampling Service Purchase Order & Revised Site procedure.W/980521 Ltr ML17229A7011998-04-27027 April 1998 LER 98-003-00:on 980326,discovered Containment Pressure Instrumentation Design Single Failure Vulnerability.Caused by Inadequate Design by Personnel Error.Removed RPS & ESFAS Containment Pressure Bypass Keys immediately.W/980427 Ltr ML17229A6761998-04-0202 April 1998 LER 98-005-00:on 980305,identified Two Conditions That Were Outside App R Design Bases.Caused by Design Oversight During Development of Original App R Safe SD Design.Established 30 Minute Roving Fire Watches & Provided training.W/980402 Ltr ML17229A6731998-03-26026 March 1998 LER 98-002-00:on 980224,radiation Monitor Surveillance Inadequacies Led to Operating of Facility Prohibited by Tss. Caused by Congnitive Personnel Error.Permanent Procedure Changes Were implemented.W/980326 Ltr ML17229A6551998-03-0505 March 1998 LER 98-001-00:on 980206,high/low Pressure Shutdown Cooling Interface Was Noted Outside App R Design Bases.Caused by Personnel Error.Addl Guidance Was Provided to Engineering Dept personnel.W/980305 Ltr ML17229A6281998-02-19019 February 1998 LER 98-004-00:on 980121,emergency Lighting Outside App R Design Bases Occurred.Caused by Congnitive Personnel Error During Translation of App R Section Iii.Procedures Onop 1 & 2 ONP-100.01 Were Issued for Use on 980206.W/980219 Ltr ML17229A6211998-02-0909 February 1998 LER 98-003-00:on 980110,manual Rt Due to DEH Leak at Turbine Test Block Was Noted.Caused by o-ring Extrusion.Shortened Bolts by About 0.125 & Reinstalled at Correct Torque values.W/980209 Ltr ML17229A6191998-02-0404 February 1998 LER 98-002-00:on 980105,CIS Bistable in Bypass Resulted in Condition Prohibited by Tss.Caused by Personnel Error. Radiation Monitor Was Restored to service.W/980204 Ltr ML17229A6161998-02-0303 February 1998 LER 98-001-00:on 980104,inadvertent RPS Actuation Occurred Due to Personnel Error.Caused by Procedural Inadequacies & Inadequate self-checking by Licensed Utility Personnel. Placards Have Been Placed in CRs.W/980203 Ltr ML17229A6051998-01-27027 January 1998 LER 97-010-01:on 971027,inadvertent Core Alteration Prohibited by TSs Were Noted Due to Stuck Cea.Caused by Personnel Error.Cea #24 Was Dislodged & Transferred to Spent Pool for insp.W/980127 Ltr ML17229A5501997-12-0505 December 1997 LER 97-008-00:on 971107,inadequate CR Ventilation Surveillance Resulted in Condition Prohibited by Ts.Caused by non-cognitive Personnel Error.Operating Procedure 2-1900050 Was revised.W/971205 Ltr ML17309A9091997-12-0202 December 1997 LER 97-011-00:on 971102,non-conservative RAS Set Point Resulted in Operation Prohibited by Ts.Caused by Inadequate Set Point & Instrument Loop Scaling Process.Revised ESFAS Functional Tp W/Proper Set point.W/971202 Ltr ML17229A5391997-11-26026 November 1997 LER 97-010-00:on 971027,inadvertant Core Alteration Prohibited by TS Occurred.Caused by CEA Failure to Detach from Ugs.Safety Evaluation Was Performed & Procedural Rev Made to Continue Upper Guide Structure move.W/971126 Ltr ML17229A5151997-11-0707 November 1997 LER 97-007-00:on 971008,inoperable Containment Cooling Fan Resulted in Operation of Facility Outside Design Basis. Caused by non-cognitive Personnel Error.Ccs Operation Was Revised & Issued on 971013.W/971107 Ltr ML17229A4991997-10-17017 October 1997 LER 97-009-00:on 970917,inoperable PORV Block Valve Resulted in Operation Prohibited by Tech Specs Occurred.Caused by Plant GL 89-10 Program Plan to Review Plant Manager Action Item Sys.Porv Block Valve V-1403 restored.W/971017 Ltr ML17309A9011997-08-27027 August 1997 LER 97-008-00:on 970728,mechanical Fire Penetrations Were Inoperable & Outside App R Design Bases.Caused by Seal Mfg Not Providing Formal Documentation for Installed Seals. Modified Inoperable Fire penetrations.W/970827 Ltr ML17229A4311997-07-29029 July 1997 LER 97-006-00:on 970630,discovered Inadequate Testing of Engineered Safety Features Subgroup Relays.Caused by Inadequacy in Implementing TS Requirements in Surveillance Procedures.Revised Surveillance procedures.W/970729 Ltr ML17229A4241997-07-25025 July 1997 LER 97-005-00:on 970625,discovered That Hot Shutdown Control Panel Shutdown Cooling Flow indicator,FI-3306 Inoperable. Caused by Weakness in Work Order & Procedure Used to Repair FI-3306.Section Meeting W/I&C Planners held.W/970725 Ltr ML17229A3971997-07-11011 July 1997 LER 97-004-00:on 970611,discovered Incorrect Original Cable Tray Fire Stop Assembly Installation Was Outside App R Design Basis.Caused by Personnel Error.Hourly Fire Watch Patrols Will Be posted.W/970711 Ltr ML17229A3871997-06-19019 June 1997 LER 97-003-00:on 970521,determined Required Post Maint Open Stroke Test for Valve V3245,2B2 SIT Discharge Check Valve, Had Not Been Performed.Caused by Personnel Error.Procedure revised.W/970619 Ltr ML17229A3841997-06-17017 June 1997 LER 97-002-00:on 970518,containment Sump Debris Screen Was Not IAW Design Due to Gaps in Screen Encl.Performed SER to Document Containment Sump Design requirements.W/970617 Ltr ML17229A3751997-06-0202 June 1997 LER 97-006-00:on 970501,operation Was Prohibited by TS Due to Inadequately Tested Degraded Voltage Sys.Revised Unit 1 ESFAS Surveillance Test procedure.W/970602 Ltr ML17229A3611997-05-29029 May 1997 LER 97-007-00:on 970502,reactor Coolant Pump Oil Collection Sys Was Outside App R Design Bases.Identified Leak Sites Were Repaired & Mods to RCP Oil Collection Sys to Capture Any Future Leakage from areas.W/970529 Ltr ML17229A3491997-05-21021 May 1997 LER 97-001-00:on 970423,containment Isolation Actuation Occurred.Caused by Increased Radiation Levels During Removal of Upper Guide Structure.Proper Actuation of Containment Isolation Components Was verified.W/970521 Ltr ML17229A3441997-05-13013 May 1997 LER 97-005-00:on 970419,reactor Was Shutdown Due to Reactor Coolant Pressure Boundary Leakage.Hot Cracking Was Caused by Weld Contamination.Repairs to RCPB Were Completed & 1A SDC Train Was Restored to Svc ML17229A3141997-04-30030 April 1997 LER 97-004-00:on 970402,refueling Machine Was Operating in Manner Prohibited by TS Due to Original Design of Refueling Machine Bypass Feature Conflicting W/Ts Requirements. Eliminated Overload Cut Off Limit bypass.W/970430 Ltr ML17229A2951997-03-31031 March 1997 LER 97-003-00:on 970304,automatic Rt Resulted from Loss of Electrical Power to 1A2 Rc Pump.Rcp Breaker Was Replaced & Pump Was Returned to svc.W/970331 Ltr ML17229A2721997-03-21021 March 1997 LER 97-002-00:on 970221,operation in Excess of Max Rated Thermal Power Occurred Due to Digital Data Processing Sys (Ddps) Calorimetric Error.Verified Acceptable Performance of Ddps Functions & Reviewed Software mods.W/970321 Ltr 1999-07-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for St Lucie,Units 1 & 2.With 991014 Ltr ML17241A4741999-08-31031 August 1999 Rev 1 to PCM 99016, St Lucie Unit 1,Cycle 16 Colr. ML17241A4591999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for St Lucie,Units 1 & 2.With 990913 Ltr ML17241A4301999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for St Lucie Units 1 & 2.With 990805 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A4091999-06-30030 June 1999 Monthly Operating Repts for June 1999 for St Lucie,Units 1 & 2.With 990712 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3631999-05-31031 May 1999 Monthly Operating Repts for May 1999 for St Lucie Units 1 & 2.With 990610 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17241A3331999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for St Lucie,Units 1 & 2.With 990517 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0841999-04-0707 April 1999 Rev 2 to PSL-ENG-SEMS-98-102, Engineering Evaluation of ECCS Suction Lines. ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0961999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for St Lucie,Units 1 & 2.With 990408 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229B0461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for St Lucie,Units 1 & 2.With 990310 Ltr ML17229B0051999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for St Lucie,Units 1 & 2.With 990211 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9961999-01-14014 January 1999 SG Tube Inservice Insp Special Rept. ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9831998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for St Lucie,Units 1 & 2.With 990111 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17241A3581998-12-0909 December 1998 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period of 970526-981209. ML17229A9421998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for St Lucie,Units 1 & 2.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17241A4931998-11-0101 November 1998 Statement of Account for Period of 981101-990930 for Suntrust Bank,As Trustee for Florida Municipal Power Agency Nuclear Decommissioning Trust (St Lucie Project). ML17229A9051998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for St Lucie,Units 1 & 2.With 981110 Ltr ML17229A8871998-10-19019 October 1998 Part 21 Rept Re Potential Defect in Swagelok Stainless Steel Front Ferrule,Part Number SS-503-1 Which Was Machined with Improper Length.C/A Includes Insp Equipment That Will 100% Identify Short Length ML17229A8781998-10-19019 October 1998 Part 21 Rept Re Potential Defect in Swagelok Stainless Steel Front Ferrule,Part Number SS-503-1,which Was Machined with Improper Length.Insp Equipment That Will 100% Identify Short Length ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8721998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for St Lucie Units 1 & 2.With 981009 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8611998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for St Lucie,Units 1 & 2.With 980911 Ltr ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17229A8481998-08-0707 August 1998 Rev 1 to PSL-ENG-SEFJ-98-013, St Lucie Unit 2,Cycle 10 Colr. ML17229A9461998-08-0707 August 1998 Rev 0 to PCM 98016, St Lucie Unit 2,Cycle 11 Colr. ML17229A8301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for St Lucie,Units 1 & 2.W/980814 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7981998-06-30030 June 1998 Monthly Operating Repts for June 1998 for St Lucie,Units 1 & 2.W/980713 Ltr ML17229A7701998-05-31031 May 1998 Monthly Operating Repts for May 1998 for St Lucie,Units 1 & 2.W/980612 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr 1999-09-30
[Table view] |
Text
i 1 CATEGORY 1 Q INFORMATION l REGULATORY DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9705200337 DOC.DATE: 97/05/13 NOTARIZED: NO DOCKET FACIL: --.3-335 St. Lucie Plant, Unit 1, Florida Po~er & Light Co. 05000335 AUTH. NAME AUTHOR AFFILIATION BENKEN,E.J. Florida Power & Light Co.
STALL,J.A. Florida Power & Light'o.
RECIP.NAME RECIPIENT AFFILIATION E
SUBJECT:
I ER 97-005-00:on 970419,reactor was shutdown due to reactor coolant pressure boundary leakage. Repairs to RCPB was completed & la SDC train was restored to svc.W/970513 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES G ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3 PD 1 1 WIENS,L. 1 1 0 INTERNAL: ACRS 1 1 2 2 AEOD/SPD/RRAB 1 1 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 1 RGN2 FILE 01 1 1 EXTEi NAL: L ST LOBBY WARD 1 1 LITCC BRYCE,J H 1 1 D NOAC POORE g W ~ 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 0 N
NOTE TO ALL "RIDS" RECIPIENTS:
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FULL TEXT CONVERSIQN REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25
,J Florida Power 8 Light Company, 6501 South Ocean Drive, Jensen Beach. FL34957 May 13, 1997 L-97-130 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: St. Lucie Unit 1 Docket No. 50-335 Reportable Event: 97-005 Date of Event: April 19, 1997 Reactor Shutdown Required by Technical Specifications The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.
Very truly yours, J. A. Stall Vice President St. Lucie Plant JAS/EJB Attachment cc: Regional Administrator, USNRC Region II I (
Senior Resident Inspector, USNRC, St. Lucie Plant 9705200337 9705i3 PDR ADOCK 05000335 S PDR p QttUQ(i 4
IIIIIIIIIIIIIIIIIIIIIIIIIIIIIIIIIIIIIIII an FPL Group company
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED SY OIM No. 31604104 EKFNIES 04nolss (4.95)
ESTIMATED SVROEN PER RESPONSE To COMPLY WITH THIS MANDATO INFORMATION COLLECTION REQUEST: 60.0 HRS. REPORTED LESSON LEARNED ARE INCORPORATED INTO THE UCENSING PROCESS ANO F SACK To eIOUSTRY. FORWARD COMMDITS REGARDING SURD EN ESTIMAT LICENBEE EVENT REPORT (LER) TO THE INFORMATION ANO RECORDS MANAGEMENT BRANCH IT.e F33)
VN. NUCLEAR REGIAATORY COMMISSION. WASHINGTON, OC 206660001 AND TO THE PAPERWORK REDUCTION PROJECT I31600104b OFRCE 0 (See reverse for required number of MANAGEMENTAND BUDGET, WASHINGTON, OC 20603.
digits/characters for each block)
FACIUTY NAME (1) DOCKET NNASBE 12l PAGE Isl ST LUCIE UNIT 1 05000335 1 OF 7 TITLE 14l Reactor Shutdown Required by TechnicaI Specifications due to Reactor Coolant Pressure Boundary Leakage FACIUTY NAME DOCKETNUMSER MONTH DAY SEauENTIAL REVISION MONTH DAY YEAR NUM9ER NUMBER N/A FACIUTY NAME DOCKETNVMSER 04 19 97, 97 005 00 05 13 97 N/A OPERAT)NQ MODE (6) 20.2201(b) 20.2203 (0) (2) (v) 50.73 (0) (2) (i) 50.73(n) (2)(viii)
POWER LEVEL l10) 20.2203(e) l2)(i) 20.2203(o) l3) Iii) 50.73(n) (2)(iii) 73.71 OTHER 20.2203 (0) l2) (iii) 50.36(c)ll) 50.73(n)(2)(v) Specify ln Abstract below or lri NRC Form 3SSA 20.2203(n) (2) (iv) 50.36(c)(2) 50.73(n)(2)(vii)
NAME TELEPHONE NVMSER Onc4de Ates Coal Edwin J. Benken, Licensing Engineer (561) 467 - 7156 REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TO NPRDS TO NPRDS
'.jViE:kj BP N/A N MONTH DAY YEAR EXPECTED YES SUBMISSION (lf yes, complete EXPECTED SUBMISSION DATE) ~
X No DATE l15)
ABSTRACT (Umit to 1400 spnces, i.o., npproximote(y 15 single-specod typowritten lines) l16)
On April 18, 1997, St, Lucie Unit 1 was operating in Mode 1 at 100 percent reactor power. Leakage from a one inch line on a safety injection (Sl) pipe vent was identified and subsequently determined to be reactor coolant pressure boundary (RCPB) leakage. The leakage was restricted to Safety Injection
~ Tank 1B2 inventory, and no reactor coolant leakage resulted. A reactor. shutdown was initiated on April 19, 1997, and was completed in accordance with Technical Specification requirements. The Unit was placed in Mode 5 on April 20, 1997, to implement repairs. During the plant cooldown, shutdown cooling (SDC) train 1A was declared inoperable and the redundant train was used to complete the cooldown. The RCPB leakage was repaired and the Unit was subsequently returned to Mode 1 operation on April 23, 1997.
The plant shutdown was required by Technical Specifications due to the, presence of pressure boundary leakage. The failure mechanism associated with the pressure boundary leakage was determined to be hot cracking of a socket weld associated with the Sl vent line. The hot cracking was caused by weld contamination. The inoperability of the 1A SDC train was due to the misalignment of a minimum flow recirculation line, and the presence of gas voids in the high points of the 1A SDC suction line.
Corrective Actions Include: 1) Repairs were completed to the RCPB and the 1A SDC train was restored to service. 2) Additional analysis was performed to confirm the failure mechanism for the affected socket weld. 3) Weld testing is being performed to evaluate for potential improvements. 4) The 1A SDC train was restored to operation following venting and inspection. 5) SDC system venting procedures are being revised to include additional frequency and temperature requirements, NRc FORM 38$ I4.95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSIO I4 95I LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 2 OF 7 97 005 00 TEXT llfmore speceis required, use eddi tionel copies of OftC Form 366AJ I17I On April 17, 1997, St. Lucie Unit 1 was operating in Mode 1 at 100 percent reactor power. At 1037, a High Pressure Safety Injection (HPSI) Pump [EIIS:BQ:P] was started and inventory was added to the Safety Injection Tanks (SIT) in accordance with normal operating procedures. Following the SIT fill evolution, operators noted that the 1B2 SIT [EIIS:BP:TK] level was slowly decreasing. The rate of inventory loss in the SIT was observed to be approximately 2.5 percent over a 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> period.
Additionally, operators noticed an increase in reactor cavity leakage from approximately 0.2 gpm to 0.45 gpm. Based on the indicated increase in reactor cavity leakage, a reactor coolant system (RCS)
[EIIS:AB] inventory balance was performed to evaluate and quantify RCS leakage. The inventory balance determined that no change in RCS leakage rate had occurred and values were consistent with those determined prior to filling the SITs. An investigation was initiated to determine the source of the indicated increase in reactor cavity leakage.
On April 18, 1997, while conducting a containment inspection to identify the source of the leakage, water was observed in the area of the 1B2 SIT pipe trench. To minimize radiological exposure, a robotic camera was deployed to determine the source of the leakage, which appeared to originate from
+he vicinity of vent valve V-3" 15 [EIIS:BP:VTV]. This vent valve is located within the reactor containment building (RCB) on the 1B2 safety injection pipe, upstream of the 1B2 safety injection loop check valve (Refer to Figure 1). A sample of leakage was obtained and analyzed, which indicated a boron concentration in the sample of 2915 parts per million (ppm). RCS boron concentration at the time was approximately 840 ppm.
t A reduction in reactor power was initiated at 2020 on'April 18, 1997, to allow personnel to access V-3815 and characterize the source of the leakage. At 0150 on April 19, 1997, with the reactor in Mode 2 at approximately 10'ercent power, a containment entry was made to inspect V-3815. The inspection revealed a failure. of the socket weld joining the one inch vent line for V-3815 to the sockolet in the safety injection loop line. This was determined to be reactor coolant pressure boundary (RCPB) leakage, in accordance with 10 CFR 50.2, and the action statement for Technical Specification (TS) 3.4.6.2 was entered at 0217 hours0.00251 days <br />0.0603 hours <br />3.587963e-4 weeks <br />8.25685e-5 months <br />. Action Statement 3.4.6.2.a, specifies, "With any PRESSURE BOUNDARY LEAKAGE, be in at least HOT STANDBY within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."
A reactor shutdown was commenced and St. Lucie Unit 1 entered Mode 3 (Hot Standby) at 0228 on April 19, 1997. A Notification of Unusual Event was made to the State of Florida at 0229'and to the USNRC at 0245, in accordance with the requirements of the St. Lucie Emergency Plan for events involving RCS pressure boundary leakage. The Unit entered Mode 4 at 1405 and the 1B shutdown cooling (SDC) train [EIIS:BP] was placed in service at 2322 hours0.0269 days <br />0.645 hours <br />0.00384 weeks <br />8.83521e-4 months <br /> on April 19, 1997. Operators attempted, but were unable, to place the 1A SDC train in service due to a decrease in pressurizer
[EIIS:AB:PZR] level when the suction valves for the 1A SDC train were opened. The 1A SDC train was subsequently declared inoperable, and the plant cooldown was continued using the 1B SDC train. Unit 1 entered Mode 5 on April 20, 1997, at 0315 and the Unusual Event was terminated at that time.
Following repaiI af the affected weld on the 182 safety injection line and resto.dtion of the
'A SDC train, St. Lucie Unit 1 retuined to Mode 1 power operation at 0153 on April 23, 1997.
NRC FOIIM 366A U.S. NUCLEAR REGULATORY COMMISSIO (4-95)
LICENSEE EVENT REPORT (LER)
. TEXT CONTINUATION YEAR SEOUENTIAL REVISION ST. LUCIE UNIT 1 05000335 3 OF 7 97 005 00 TEXT Iifmore speceis required, use edditionel copies of IVRC Form 366AI I17I The reactor shut down was completed in accordance with TS requirements for RCS leakage involving the reactor coolant pressure boundary. 'he RCPB leakage originated from a socket weld on a one inch vent line to V-3815, located on the 1B2 safety injection header. While only 1B2 safety injection tank volume was affected, and no reactor coolant inventory was lost as a result of the leak, the site of the leakage is classified as reactor coolant pressure boundary, as further discussed in this report.
Failure analysis of the affected weld on the vent line to V-3815 was performed following the event.
The analysis concluded that the initiating failure mechanism was hot cracking of the weld due to contamination. Boric acid residue is considered to be the most likely cause of this contamination.
The 1A SDC train was declared inoperable when operations personnel observed decreases in pressurizer
. level while opening the SDC suction isolation valves. Local observations identified that system pressure in the 1A SDC train was fluctuating during attempts to open the valves, and a safety relief valve on the 1A SDC train, V-3483, temporarily lifted as designed in response to the system pressure transient.
Subsequent inspection and trouble shooting of flow noises in system piping by operations personnel identified that a manual recirculation isolation valve (V-3"<4) for the 1A low pressure safety injection (LPSI) pump was not fully shut as required for SDC operation. This resulted in a flow path from the RCS to the refueling water tank (RWT) when the SDC suction valves to the pump were opened, and was the primary cause of the indicated decreases in pressurizer level previously discussed. Upon inspection, the handwheel for V-3204 was found to be difficult to operate and appeared to be closed, however operators using a valve wrench were able to manipulate the valve an additional two turns to the fully closed position. A work order was written to repair the defective valve and preventive maintenance practices are being reviewed to address generic aspects.
System venting and inspections performed following the event determined that the pressure response observed in the 1A SDC train was caused by the presence of gas voids in the high points of the 1A SDC suction piping in conjunction with a partially open LPSI pump recirculation valve. The presence of voids, along with the partially open recirculation valve would provide conditions conducive to steam flashing and pressure fluctuations in the LPSI pump suction line when reactor coolant was initially aligned to the system. Venting of the SDC piping is required to be performed following system use as the result of a similar event in 1995, however the procedures did not specifically require that this be performed at ambient temperature. The completion of venting following the last use of the SDC system may therefore not have been adequate to prevent subsequent degassing (voiding) of reactor coolant in the SDC suction lines. Consequently, procedural inadequacy was a contributing factor by not preventing conditions which were favorable to the formation of the'gas voids in the 1A SDC system.
TS 3.4.6.2 requires that no pressure boundary leakage be present in Modes 1,2,3 and 4. TS Action Statement 3 4.6.2.a, further specifies, "With any PRESSURE BOUNDARY LEAKAGE, be in at least HOT STANDBY within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />." St. Lucie Unit 1 vas placed in Mode 3, HOT S ANDBY e';0228, on April 19 1997, approximately 23 minutes following the identification of RCPB leakage.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSIO I4.96)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 4 OF 7 97 005 00 TEXT le more speoeis required, use eddidonel copies of NRC Farm 386AJ I17)
The plant'entered Mode 5 at 0315 on April 20, 1997, approximately 25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br /> after entry into Mode 3.
Based on the above, this event is reportable under 10 CFR 50.73 (a) (2) (i) (A), as a completion of a plant shutdown required by the Technical Specifications.
According to the definition provided in the St. Lucie Unit 1 TS, PRESSURE BOUNDARY LEAKAGE is defined as "...leakage (except steam generator tube leakage) through a non-isolable fault in a Reactor Coolant System component body, pipe wall or vessel. wall." Additionally, 10 CFR 50.2 defines the "reactor coolant pressure boundary" as follows:
...all those pressure-containing components of boiling or pressurized water-cooled nuclear power reactors such as pressure vessels, 'piping, pumps and valves, which are:
(1) Part of the reactor coolant system, or (2) Connected to the reactor coolant system, up to and including any and all of the following:
The outermost containment isolation valve in system piping which penetrates primary reactor containment, The second of two valves normally closed during normal reactor operation in system piping which does not penetrate primary reactor containment, The reactor coolant system safety and relief valves.
During this event, a small amount of inventory from the 1B2 SIT was observed leaking from a weld associated with a one inch vent,- V-3815, located on the 1B2 safety injection pipe, upstream of the 1B2 safety injection loop check valve. Per the above definition, this vent is a part of the reactor coolant pressure boundary since it is located on a system connected to the RCS and is within the outermost containment isolation valve in system piping penetrating the primary reactor containment.
Additionally, V-3815 is located in the Quality Group A portion of the safety injection system. This Quality Group is described by the St. Lucie Unit 1 Updated Final Safety Analysis Report (UFSAR),
Section 3.2, as specifically applying to reactor coolant pressure boundary components.
The St. Lucie Unit 1 TS bases related to RCPB leakage specify that pressure boundary leakage of any magnitude is unacceptable as it may be indicative of impending further pressure boundary the presence of any pressure boundary leakage requires that the plant be promptly placed in failure.'herefore, a cold shutdown (Mode 5) condition. Compliance with the Limiting Conditions for Operation (LCO) as specified in the Technical Specifications assures that the functional capability of equipment required for the safe operation of the plant is maintained. Following the identification of pressure boundary leakage during this event, operators promptly implemented the applicable TS Action requirements.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSIO I4.95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 5 OF 7 97 005 00 TEXT llfmore spece is required, use eddi tianel copies of fVRC Form 366A J I17I A review of similar documented maintenance weld failures at St. Lucie was performed following the event. Based on available information, it was determined that no significant failure rate existed for this failure mechanism, therefore the socket weld leakage from the vent line for V-3815 is considered to be a random failure. As a result of the RCBP leakage, no loss of reactor coolant system inv'entory occurred, and the area of leakage was isolated from the RCS by the 1B safety injection header loop check valve (V-3247) [EIIS:BP:VJ. V-3247 is also addressed by the St. Lucie Unit 1 TS and is required to meet periodic surveillance criteria for leakage which provides added assurance of valve integrity.
Leakage from the 1B2 SIT during the event was limited to approximately one-half gallon per minute and makeup was provided as necessary to maintain the required tank volume. The operability of the 182 Sl was not affected by the weld leakage.
N With regard to the 1A SDC system, St. Lucie Unit 1 Updated Final Safety Analysis (UFSAR), Section 9.1.5.3.2, states that " No single failure of an active component during residual heat removal will result in a loss of core cooling capability. The reactor coolant system can be brought to refueling temperature IIsing one Iow pressure safety injection pump and one shutdown cooling heat exchanger." The 1B SDC system remained operational at all times during this event, and was not affected by the inoperability of the 1A SDC train. The 1B SDC train was placed in service to facilitate the RCS cooldown and functioned properly in establishing Mode 5 conditions. The RCS heat removal safety function was maintained at all times during the event.
Following the event, FPL engineering personnel performed a walkdown of the 1A SDC system and reviewed data observed during efforts to place the 1A SD system in service. Based on the pressures in the system observed during the event, a review of the design and hydrostatic testing for this system, and local inspection, the 1A SDC train was determined to be functional and acceptable for operation.
Based on the above, this event did not adversely affect the protection of the health and safety of the public.
Following the identification of the pressure boundary leakage on the 182 safety injection header, St. Lucie Unit 1 was placed in Cold Shutdown in accordance with the requirements of plant Technical Specifications.
- 2. The affected '! B2 safety injection header vent line weld was removed and repairs were implemented. The Unit was returned to Mode 1 power operation on April 23, 1997,
~
following completion of the repairs.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSI I4-95I I
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 6 OF 7 97 005 00 TEXT fifmore speceis required, use additional copies of NRC Farm 366AJ I17I
- 3. An inspection and failure analysis was performed for the failed socket weld associated with V-3815 vent line. The analysis determined that the initiating failure mechanism of the socket weld was hot cracking, due to contamination of the weld. While this failure is considered to be random at St. Lucie, additional testing will be done to evaluate boric acid weld contamination and determine if additional preventive measures are necessary to minimize the potential for recurrence.
The 1A SDC train was returned to service following system venting and the realignment of the minimum flow recirculation valve for the 1A LPSI pump. A caution tag was placed on the recirculation valve and a plant work order was initiated to repair and restore the valve to satisfactory operation.
- 5. Venting of the 1A LPSI pump suction line is currently being performed at an increased frequency and the results will be evaluated to determine if additional changes to venting periodicity are required.
- 6. To further preclude the possibility of gas formation in the SDC suction lines, St. Lucie Unit 1 and 2 shutdown cooling system procedures are being revised to require that system venting following SDC operation be conducted at ambient temperatures. FPL engineering will review the procedure revisions for incorporation of adequate guidance and corrective actions prior to issue.
Component: Safety Injection Pipe 1 inch Vent Line - Socket Weld Material: Piping - 304/316 stainless steel with ER 308/316 filler material Sockolet - 304 stainless steel LER - 389/95-001 St. Lucie Unit 2 (2/21/95) - The event describes the failure of a low pressure safety injection (LPSI) pump during a surveillance, due to air binding of the pump. The root cause was attributed to the migration of trapped air in the emergency core cooling system (ECCS) header following maintenance.
In-house Event 95-09 St. Lucie Unit 1 (2/27/95) - This event involved the lifting of safety relief valve V-3483 at St. Lucie Unit 1 following the initiation of flow from the 1A LPSI pump during SDC operation. The primary cause was pressure spiking in the hot leg suction line due to a rapid increase in system flow rate following LPSI pump start. Gas voiding was considered as a possible contributor. Corrective actions were implemented following the event to minimize transient fluid flow effects.
NKC FORM 366A I4.95]
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSI I4 95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIF UNIT 1 05000335 7 OF 7 97 005 00 TEXT /ff more speceis required, use edditionel copies of iVRC Form 388A/ I17I BQUB~
SAFETY INJECTION TANK (SIT 1B2)
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S SAMPLE O SIAS CLOSE B-e I M
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SIAS hs'ROM V3815 AREA OF LEAKAGE RCS LOOP 182 HPSI PUMP