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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr ML17229A7381998-05-21021 May 1998 LER 98-006-00:on 980421,missed EDG Fuel Oil Sample Surveillance Was Noted.Caused by Personnel Error.Revised Fuel Oil Sampling Service Purchase Order & Revised Site procedure.W/980521 Ltr ML17229A7011998-04-27027 April 1998 LER 98-003-00:on 980326,discovered Containment Pressure Instrumentation Design Single Failure Vulnerability.Caused by Inadequate Design by Personnel Error.Removed RPS & ESFAS Containment Pressure Bypass Keys immediately.W/980427 Ltr ML17229A6761998-04-0202 April 1998 LER 98-005-00:on 980305,identified Two Conditions That Were Outside App R Design Bases.Caused by Design Oversight During Development of Original App R Safe SD Design.Established 30 Minute Roving Fire Watches & Provided training.W/980402 Ltr ML17229A6731998-03-26026 March 1998 LER 98-002-00:on 980224,radiation Monitor Surveillance Inadequacies Led to Operating of Facility Prohibited by Tss. Caused by Congnitive Personnel Error.Permanent Procedure Changes Were implemented.W/980326 Ltr ML17229A6551998-03-0505 March 1998 LER 98-001-00:on 980206,high/low Pressure Shutdown Cooling Interface Was Noted Outside App R Design Bases.Caused by Personnel Error.Addl Guidance Was Provided to Engineering Dept personnel.W/980305 Ltr ML17229A6281998-02-19019 February 1998 LER 98-004-00:on 980121,emergency Lighting Outside App R Design Bases Occurred.Caused by Congnitive Personnel Error During Translation of App R Section Iii.Procedures Onop 1 & 2 ONP-100.01 Were Issued for Use on 980206.W/980219 Ltr ML17229A6211998-02-0909 February 1998 LER 98-003-00:on 980110,manual Rt Due to DEH Leak at Turbine Test Block Was Noted.Caused by o-ring Extrusion.Shortened Bolts by About 0.125 & Reinstalled at Correct Torque values.W/980209 Ltr ML17229A6191998-02-0404 February 1998 LER 98-002-00:on 980105,CIS Bistable in Bypass Resulted in Condition Prohibited by Tss.Caused by Personnel Error. Radiation Monitor Was Restored to service.W/980204 Ltr ML17229A6161998-02-0303 February 1998 LER 98-001-00:on 980104,inadvertent RPS Actuation Occurred Due to Personnel Error.Caused by Procedural Inadequacies & Inadequate self-checking by Licensed Utility Personnel. Placards Have Been Placed in CRs.W/980203 Ltr ML17229A6051998-01-27027 January 1998 LER 97-010-01:on 971027,inadvertent Core Alteration Prohibited by TSs Were Noted Due to Stuck Cea.Caused by Personnel Error.Cea #24 Was Dislodged & Transferred to Spent Pool for insp.W/980127 Ltr ML17229A5501997-12-0505 December 1997 LER 97-008-00:on 971107,inadequate CR Ventilation Surveillance Resulted in Condition Prohibited by Ts.Caused by non-cognitive Personnel Error.Operating Procedure 2-1900050 Was revised.W/971205 Ltr ML17309A9091997-12-0202 December 1997 LER 97-011-00:on 971102,non-conservative RAS Set Point Resulted in Operation Prohibited by Ts.Caused by Inadequate Set Point & Instrument Loop Scaling Process.Revised ESFAS Functional Tp W/Proper Set point.W/971202 Ltr ML17229A5391997-11-26026 November 1997 LER 97-010-00:on 971027,inadvertant Core Alteration Prohibited by TS Occurred.Caused by CEA Failure to Detach from Ugs.Safety Evaluation Was Performed & Procedural Rev Made to Continue Upper Guide Structure move.W/971126 Ltr ML17229A5151997-11-0707 November 1997 LER 97-007-00:on 971008,inoperable Containment Cooling Fan Resulted in Operation of Facility Outside Design Basis. Caused by non-cognitive Personnel Error.Ccs Operation Was Revised & Issued on 971013.W/971107 Ltr ML17229A4991997-10-17017 October 1997 LER 97-009-00:on 970917,inoperable PORV Block Valve Resulted in Operation Prohibited by Tech Specs Occurred.Caused by Plant GL 89-10 Program Plan to Review Plant Manager Action Item Sys.Porv Block Valve V-1403 restored.W/971017 Ltr ML17309A9011997-08-27027 August 1997 LER 97-008-00:on 970728,mechanical Fire Penetrations Were Inoperable & Outside App R Design Bases.Caused by Seal Mfg Not Providing Formal Documentation for Installed Seals. Modified Inoperable Fire penetrations.W/970827 Ltr ML17229A4311997-07-29029 July 1997 LER 97-006-00:on 970630,discovered Inadequate Testing of Engineered Safety Features Subgroup Relays.Caused by Inadequacy in Implementing TS Requirements in Surveillance Procedures.Revised Surveillance procedures.W/970729 Ltr ML17229A4241997-07-25025 July 1997 LER 97-005-00:on 970625,discovered That Hot Shutdown Control Panel Shutdown Cooling Flow indicator,FI-3306 Inoperable. Caused by Weakness in Work Order & Procedure Used to Repair FI-3306.Section Meeting W/I&C Planners held.W/970725 Ltr ML17229A3971997-07-11011 July 1997 LER 97-004-00:on 970611,discovered Incorrect Original Cable Tray Fire Stop Assembly Installation Was Outside App R Design Basis.Caused by Personnel Error.Hourly Fire Watch Patrols Will Be posted.W/970711 Ltr ML17229A3871997-06-19019 June 1997 LER 97-003-00:on 970521,determined Required Post Maint Open Stroke Test for Valve V3245,2B2 SIT Discharge Check Valve, Had Not Been Performed.Caused by Personnel Error.Procedure revised.W/970619 Ltr ML17229A3841997-06-17017 June 1997 LER 97-002-00:on 970518,containment Sump Debris Screen Was Not IAW Design Due to Gaps in Screen Encl.Performed SER to Document Containment Sump Design requirements.W/970617 Ltr ML17229A3751997-06-0202 June 1997 LER 97-006-00:on 970501,operation Was Prohibited by TS Due to Inadequately Tested Degraded Voltage Sys.Revised Unit 1 ESFAS Surveillance Test procedure.W/970602 Ltr ML17229A3611997-05-29029 May 1997 LER 97-007-00:on 970502,reactor Coolant Pump Oil Collection Sys Was Outside App R Design Bases.Identified Leak Sites Were Repaired & Mods to RCP Oil Collection Sys to Capture Any Future Leakage from areas.W/970529 Ltr ML17229A3491997-05-21021 May 1997 LER 97-001-00:on 970423,containment Isolation Actuation Occurred.Caused by Increased Radiation Levels During Removal of Upper Guide Structure.Proper Actuation of Containment Isolation Components Was verified.W/970521 Ltr ML17229A3441997-05-13013 May 1997 LER 97-005-00:on 970419,reactor Was Shutdown Due to Reactor Coolant Pressure Boundary Leakage.Hot Cracking Was Caused by Weld Contamination.Repairs to RCPB Were Completed & 1A SDC Train Was Restored to Svc ML17229A3141997-04-30030 April 1997 LER 97-004-00:on 970402,refueling Machine Was Operating in Manner Prohibited by TS Due to Original Design of Refueling Machine Bypass Feature Conflicting W/Ts Requirements. Eliminated Overload Cut Off Limit bypass.W/970430 Ltr ML17229A2951997-03-31031 March 1997 LER 97-003-00:on 970304,automatic Rt Resulted from Loss of Electrical Power to 1A2 Rc Pump.Rcp Breaker Was Replaced & Pump Was Returned to svc.W/970331 Ltr ML17229A2721997-03-21021 March 1997 LER 97-002-00:on 970221,operation in Excess of Max Rated Thermal Power Occurred Due to Digital Data Processing Sys (Ddps) Calorimetric Error.Verified Acceptable Performance of Ddps Functions & Reviewed Software mods.W/970321 Ltr 1999-07-06
[Table view] Category:RO)
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr ML17229A7381998-05-21021 May 1998 LER 98-006-00:on 980421,missed EDG Fuel Oil Sample Surveillance Was Noted.Caused by Personnel Error.Revised Fuel Oil Sampling Service Purchase Order & Revised Site procedure.W/980521 Ltr ML17229A7011998-04-27027 April 1998 LER 98-003-00:on 980326,discovered Containment Pressure Instrumentation Design Single Failure Vulnerability.Caused by Inadequate Design by Personnel Error.Removed RPS & ESFAS Containment Pressure Bypass Keys immediately.W/980427 Ltr ML17229A6761998-04-0202 April 1998 LER 98-005-00:on 980305,identified Two Conditions That Were Outside App R Design Bases.Caused by Design Oversight During Development of Original App R Safe SD Design.Established 30 Minute Roving Fire Watches & Provided training.W/980402 Ltr ML17229A6731998-03-26026 March 1998 LER 98-002-00:on 980224,radiation Monitor Surveillance Inadequacies Led to Operating of Facility Prohibited by Tss. Caused by Congnitive Personnel Error.Permanent Procedure Changes Were implemented.W/980326 Ltr ML17229A6551998-03-0505 March 1998 LER 98-001-00:on 980206,high/low Pressure Shutdown Cooling Interface Was Noted Outside App R Design Bases.Caused by Personnel Error.Addl Guidance Was Provided to Engineering Dept personnel.W/980305 Ltr ML17229A6281998-02-19019 February 1998 LER 98-004-00:on 980121,emergency Lighting Outside App R Design Bases Occurred.Caused by Congnitive Personnel Error During Translation of App R Section Iii.Procedures Onop 1 & 2 ONP-100.01 Were Issued for Use on 980206.W/980219 Ltr ML17229A6211998-02-0909 February 1998 LER 98-003-00:on 980110,manual Rt Due to DEH Leak at Turbine Test Block Was Noted.Caused by o-ring Extrusion.Shortened Bolts by About 0.125 & Reinstalled at Correct Torque values.W/980209 Ltr ML17229A6191998-02-0404 February 1998 LER 98-002-00:on 980105,CIS Bistable in Bypass Resulted in Condition Prohibited by Tss.Caused by Personnel Error. Radiation Monitor Was Restored to service.W/980204 Ltr ML17229A6161998-02-0303 February 1998 LER 98-001-00:on 980104,inadvertent RPS Actuation Occurred Due to Personnel Error.Caused by Procedural Inadequacies & Inadequate self-checking by Licensed Utility Personnel. Placards Have Been Placed in CRs.W/980203 Ltr ML17229A6051998-01-27027 January 1998 LER 97-010-01:on 971027,inadvertent Core Alteration Prohibited by TSs Were Noted Due to Stuck Cea.Caused by Personnel Error.Cea #24 Was Dislodged & Transferred to Spent Pool for insp.W/980127 Ltr ML17229A5501997-12-0505 December 1997 LER 97-008-00:on 971107,inadequate CR Ventilation Surveillance Resulted in Condition Prohibited by Ts.Caused by non-cognitive Personnel Error.Operating Procedure 2-1900050 Was revised.W/971205 Ltr ML17309A9091997-12-0202 December 1997 LER 97-011-00:on 971102,non-conservative RAS Set Point Resulted in Operation Prohibited by Ts.Caused by Inadequate Set Point & Instrument Loop Scaling Process.Revised ESFAS Functional Tp W/Proper Set point.W/971202 Ltr ML17229A5391997-11-26026 November 1997 LER 97-010-00:on 971027,inadvertant Core Alteration Prohibited by TS Occurred.Caused by CEA Failure to Detach from Ugs.Safety Evaluation Was Performed & Procedural Rev Made to Continue Upper Guide Structure move.W/971126 Ltr ML17229A5151997-11-0707 November 1997 LER 97-007-00:on 971008,inoperable Containment Cooling Fan Resulted in Operation of Facility Outside Design Basis. Caused by non-cognitive Personnel Error.Ccs Operation Was Revised & Issued on 971013.W/971107 Ltr ML17229A4991997-10-17017 October 1997 LER 97-009-00:on 970917,inoperable PORV Block Valve Resulted in Operation Prohibited by Tech Specs Occurred.Caused by Plant GL 89-10 Program Plan to Review Plant Manager Action Item Sys.Porv Block Valve V-1403 restored.W/971017 Ltr ML17309A9011997-08-27027 August 1997 LER 97-008-00:on 970728,mechanical Fire Penetrations Were Inoperable & Outside App R Design Bases.Caused by Seal Mfg Not Providing Formal Documentation for Installed Seals. Modified Inoperable Fire penetrations.W/970827 Ltr ML17229A4311997-07-29029 July 1997 LER 97-006-00:on 970630,discovered Inadequate Testing of Engineered Safety Features Subgroup Relays.Caused by Inadequacy in Implementing TS Requirements in Surveillance Procedures.Revised Surveillance procedures.W/970729 Ltr ML17229A4241997-07-25025 July 1997 LER 97-005-00:on 970625,discovered That Hot Shutdown Control Panel Shutdown Cooling Flow indicator,FI-3306 Inoperable. Caused by Weakness in Work Order & Procedure Used to Repair FI-3306.Section Meeting W/I&C Planners held.W/970725 Ltr ML17229A3971997-07-11011 July 1997 LER 97-004-00:on 970611,discovered Incorrect Original Cable Tray Fire Stop Assembly Installation Was Outside App R Design Basis.Caused by Personnel Error.Hourly Fire Watch Patrols Will Be posted.W/970711 Ltr ML17229A3871997-06-19019 June 1997 LER 97-003-00:on 970521,determined Required Post Maint Open Stroke Test for Valve V3245,2B2 SIT Discharge Check Valve, Had Not Been Performed.Caused by Personnel Error.Procedure revised.W/970619 Ltr ML17229A3841997-06-17017 June 1997 LER 97-002-00:on 970518,containment Sump Debris Screen Was Not IAW Design Due to Gaps in Screen Encl.Performed SER to Document Containment Sump Design requirements.W/970617 Ltr ML17229A3751997-06-0202 June 1997 LER 97-006-00:on 970501,operation Was Prohibited by TS Due to Inadequately Tested Degraded Voltage Sys.Revised Unit 1 ESFAS Surveillance Test procedure.W/970602 Ltr ML17229A3611997-05-29029 May 1997 LER 97-007-00:on 970502,reactor Coolant Pump Oil Collection Sys Was Outside App R Design Bases.Identified Leak Sites Were Repaired & Mods to RCP Oil Collection Sys to Capture Any Future Leakage from areas.W/970529 Ltr ML17229A3491997-05-21021 May 1997 LER 97-001-00:on 970423,containment Isolation Actuation Occurred.Caused by Increased Radiation Levels During Removal of Upper Guide Structure.Proper Actuation of Containment Isolation Components Was verified.W/970521 Ltr ML17229A3441997-05-13013 May 1997 LER 97-005-00:on 970419,reactor Was Shutdown Due to Reactor Coolant Pressure Boundary Leakage.Hot Cracking Was Caused by Weld Contamination.Repairs to RCPB Were Completed & 1A SDC Train Was Restored to Svc ML17229A3141997-04-30030 April 1997 LER 97-004-00:on 970402,refueling Machine Was Operating in Manner Prohibited by TS Due to Original Design of Refueling Machine Bypass Feature Conflicting W/Ts Requirements. Eliminated Overload Cut Off Limit bypass.W/970430 Ltr ML17229A2951997-03-31031 March 1997 LER 97-003-00:on 970304,automatic Rt Resulted from Loss of Electrical Power to 1A2 Rc Pump.Rcp Breaker Was Replaced & Pump Was Returned to svc.W/970331 Ltr ML17229A2721997-03-21021 March 1997 LER 97-002-00:on 970221,operation in Excess of Max Rated Thermal Power Occurred Due to Digital Data Processing Sys (Ddps) Calorimetric Error.Verified Acceptable Performance of Ddps Functions & Reviewed Software mods.W/970321 Ltr 1999-07-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for St Lucie,Units 1 & 2.With 991014 Ltr ML17241A4741999-08-31031 August 1999 Rev 1 to PCM 99016, St Lucie Unit 1,Cycle 16 Colr. ML17241A4591999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for St Lucie,Units 1 & 2.With 990913 Ltr ML17241A4301999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for St Lucie Units 1 & 2.With 990805 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A4091999-06-30030 June 1999 Monthly Operating Repts for June 1999 for St Lucie,Units 1 & 2.With 990712 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3631999-05-31031 May 1999 Monthly Operating Repts for May 1999 for St Lucie Units 1 & 2.With 990610 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17241A3331999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for St Lucie,Units 1 & 2.With 990517 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0841999-04-0707 April 1999 Rev 2 to PSL-ENG-SEMS-98-102, Engineering Evaluation of ECCS Suction Lines. ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0961999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for St Lucie,Units 1 & 2.With 990408 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229B0461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for St Lucie,Units 1 & 2.With 990310 Ltr ML17229B0051999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for St Lucie,Units 1 & 2.With 990211 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9961999-01-14014 January 1999 SG Tube Inservice Insp Special Rept. ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9831998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for St Lucie,Units 1 & 2.With 990111 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17241A3581998-12-0909 December 1998 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period of 970526-981209. ML17229A9421998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for St Lucie,Units 1 & 2.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17241A4931998-11-0101 November 1998 Statement of Account for Period of 981101-990930 for Suntrust Bank,As Trustee for Florida Municipal Power Agency Nuclear Decommissioning Trust (St Lucie Project). ML17229A9051998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for St Lucie,Units 1 & 2.With 981110 Ltr ML17229A8871998-10-19019 October 1998 Part 21 Rept Re Potential Defect in Swagelok Stainless Steel Front Ferrule,Part Number SS-503-1 Which Was Machined with Improper Length.C/A Includes Insp Equipment That Will 100% Identify Short Length ML17229A8781998-10-19019 October 1998 Part 21 Rept Re Potential Defect in Swagelok Stainless Steel Front Ferrule,Part Number SS-503-1,which Was Machined with Improper Length.Insp Equipment That Will 100% Identify Short Length ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8721998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for St Lucie Units 1 & 2.With 981009 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8611998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for St Lucie,Units 1 & 2.With 980911 Ltr ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17229A8481998-08-0707 August 1998 Rev 1 to PSL-ENG-SEFJ-98-013, St Lucie Unit 2,Cycle 10 Colr. ML17229A9461998-08-0707 August 1998 Rev 0 to PCM 98016, St Lucie Unit 2,Cycle 11 Colr. ML17229A8301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for St Lucie,Units 1 & 2.W/980814 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7981998-06-30030 June 1998 Monthly Operating Repts for June 1998 for St Lucie,Units 1 & 2.W/980713 Ltr ML17229A7701998-05-31031 May 1998 Monthly Operating Repts for May 1998 for St Lucie,Units 1 & 2.W/980612 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr 1999-09-30
[Table view] |
Text
CATEGORY j.
REGULATO INFORMATION DISTRIBUTION TEM (RIDS)
AGCESSION NBR:9706100099 DOC.DATE:. 97/06/02 NOTARIZED: NO DOCKET FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power a Light Co. 05000335 AUTH:NAME'UTHOR AFFILIATION FREHAFER,K.W. Florida Power 6 Light Co.
STALL,J.A. Florida Power & Light Co.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 97-006-00:on 970501,operation was prohibited by TS due to inadequately tested degraded'oltage sys.Revised Unit 1 ESFAS surveillance test procedure.W/970607 ltr. .
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ! ENCL .( SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME'D2-3 LTTR ENCL ID CODE/NAME LTTR ENCL PD 1 1. WIENS,L. 1 1 INTERNAL: ACRS 1 AEGD/PSQQ/RAB 2 2 AEOD/SPD/RRAB I FILE CENTERRI 1 1 NRR/DE/ECGB 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 RGN2 FILE 01 1 '1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 1 1 NOAC POOREFW. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN 5D-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25
Florida Power & Light Company, 6501 South Ocean Drive, Jensen Beach, FL 34957 June 2, 1997 APL L-97-145%
10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: St. Lucie Units 1 and 2 Docket No. 50-335 Reportable Event: 97-006 Date of Event: May 1, 1997 Operation Prohibited by Technical Specifications The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.
Very truly yours, J. A. Stall Vice President St. Lucie Plant JAS/KWF Attachment cc: Regional Administrator, USNRC Region II P igeyjqqgesident Inspector, USNRC, St. Lucie Plant 9706100099 970602
'PDR ADOCK 05000335 l S PDR II!IIII!fllllllllllllllllllflllllffllffl an FPL Group company
NRC FORM 466 u. CLEAR REGULATORY COMMISSION APPROVED SY OINI No. S 1604104 (4.06) EXPSIES 04130ISS ESllMATEO BURDEN PER RESPONSE TO COMPLY WITH THIS MANOATO INFORMATION COLLECTION REQUEST: 60.0 HRS. REPORTED LESSON LEARNED ARE INCORPORATED INTO THE UCENSINO PROCESS ANO F LXCENSEE EVENT REPORT (LER) SACK TO seOUSTIIY. FORWARD COMMENTS REOAROINO BURDEN ESllMAT TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH IT% F331
'I UB. NUCLEAR REGIAATORY COMMISSION, WASHINGTON, DC 206664001 AND TO THE PAPERWORK REDUCTION PROJECT (316041041, OFRCE 0 (See reverse for required number of
~
MANAOEMENTANO SUDOET, WASHINOTON, DC 20603.
digits/characters for each block)
FACIUTYNAME ul DOCKET NIEVSER 12) PAOE Isl ST. LUCIE UNIT 1 05000335 1 OF7 IE ial Operation Prohibited by Technical Specifications Due to Inadequately Tested Degraded Voltage System SEQUENTIAL FACIUTYNAME DOCKET NUMBER MONTH DAY YEAR REVISION NUMBER NUMBER MONTH DAY YEAR St. Lucle Unit 2 05000389 FACIUTY NAME 5 1 97 97 006 0 6 2 97 DOCKET NUMBER 05000 OPERATINQ MODE (6) 20.2201(b) 20.2203(a)(2) (v) 60.73(e) (2) (i) 50.73(a)(2)(viii)
POWER LEVEL (10) 20.2203(0)(2)(g 20.2203(a) (3) (ii) 50.73(a) (2)(iii) 73.71 OTHER 20.2203(a)(2) (Hi) S0.36(o) (1) 50.73(a) (2)(v) Specify In Abstract below 20.2203(a)(2)(iv) or In NRC Form SBBA S0.36(c)(2) S0.73(a) (2) (v(i)
NAME TELEPHONE'UMBER OncMe Area Code)
K. W. Frehafer, Lincenslng Engineer (561) 468%284 CAUSE SYSTEM COMPONENT MANUFACTURER To NPRDS 'AUSE SYSTEM MANUFACTURER REPORTABLE To NPRDS MONTH DAY YEAR EXPECTED YES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). X No DATE (16)
ABSTRACT (Umit 40 1400 spaces, I.e., approximately 16 s)ngie-spaced typewritten lines) (16)
On May 1, 1997, Unit 1 was in Mode 1 at 100 percent power and Unit 2 was in Mode 6 and defueled for a refueling outage. As a result of the on-going review of the Unit 2 Engineered Safety Features Actuation System (ESFAS) Test Procedure for compliance with NRC Generic Letter 96-01, it was discovered that the Safety Injection Actuation Signal (SIAS) permissive contact for degraded voltage protection was not adequately tested as required by the Technical Specifications.
The cause of the event was inadequate surveillance test procedures which did not test the degraded voltag protection system SIAS permissive contact. This contact provides an ESFAS function which initiates load shed and Emergency Diesel Generator (EDG) start for a sustained degraded voltage condition.
The Unit 1 A EDG was declared inoperable, due to a missed surveillance, at approximately 0900 on 5/1/97.
Testing of the degraded voltage system SIAS permissive was successfully performed at approximately 1630 on 5/1/97, and the 1A EDG was subsequently declared operable. Operability of the Unit 1 B EDG was demonstrated via a previous event where the degraded voltape permissive signal was provided by a Containment Isolation Actuation Signal (CIAS) contact. Testing of the Unit 2 degraded voltage system ESFAS permissives was satisfactorily completed May 9, 1997.
The Unit 2 ESFAS surveillance test procedure was revised to ensure the degraded voltage system SIAS permissive contact is tested. The Unit 1 ESFAS surveillance test procedure will be revised to ensure the degraded voltage system ESFAS permissive contacts are tested.
NRC FORM 366 (4-96)
4RC FORM 366A U.S. NUCLEAR REGULATORY COMMLSSIO I4-96)
LZCENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 2 .OF 7 97 006 0 TEXT llfmore opooo io rerlulrod, uoo odditlonol oopko of HRC f'orm 3MAJ I17I On May 1, 1997, Unit 1 was in Mode 1 at 100 percent power and Unit 2 IH~as in Mode 6 and defueled for a refueling outage. While performing a review of the Unit 2 Engineered Safety Features Actuation System (ESFAS) fEIIS:JE] Test Procedure, 2-0400050, Rev. 22, for compliance with NRC Generic Letter (GL) 96-01, it was.discovered that the Safety Injection Actuation Signal (SIAS) permissive contact for degraded voltage protection may not have been*adequately tested in accordance with Technical Specifications.
Failure of the contact would not allow the degraded voltage system to initiate load shed and Emergency Diesel Generator (EDG) start within the time specified in the Technical Specifications.
At the time of discovery, Unit 2 was in a mode where degraded voltage protection was not required.
Engineering determined that the Unit 1 B train degraded voltage system was functional based on a previous event that demonstrated operability. However, the Unit 1 A EDG was declared inoperable and the ACTION statement for Technical Specification 3.8.1.1 was entered. The Unit 1 A train degraded voltage SIAS permissive contact was successfully tested and the 1A EDG was returned to service.
The degraded voltage protection system consists of a set of undervoltage relays, set to a higher voltage level than the loss of voltage relays, and two time. delays. The first time delay is of a length of time sufficient to establish the existence of a degraded voltage condition. At the end of this delay, an alarm in the control room alerts operators to the degraded voltage condition. An interlock with the SIAS is included such that a subsequent SIAS will immediately separate the Class 1E power distribution system from the offsite power system and the EDGs are started and loaded. The second time delay is of a limited duration such that the permanently connected Class 1E loads will not be damaged by operation at reduced voltage for that time period. Following this delay, if not corrected, the Class 1E power distribution system is separated from the offsite power system and the EDGs are started and loaded.
The St. Lucie Unit 1 and 2 Technical Specifications include limiting conditions for operation, surveillance requirements, trip setpoints,'nd allowable values for the degraded voltage relays and associated time delay relays. Since the degraded voltage protection system is. considered part of the loss of power protection system, it has been determined that the surveillance test requirements for the degraded voltage protection system should consist of functional verification every 18 months, during refueling.
The load shed and EDG start ESFAS function is tested by initiating a complete loss of power to the busses, which results in the first level of protection, the loss of voltage relays, initiating load shed and EDG start.
Functioning of load shed is thus verified only for a complete loss of power. It was determined that the SIAS permissive contact that initiates load shed and EDG start for a sustained degraded voltage condition was not verified by test, which is contrary to the Technical Specifications requirements.
There are differences between the St. Lucie Units 1 and 2 degraded voltage protection systems. These differences and the identified test deficiencies are described below:
NAG FORM 388A I4-96I
4RC FORM SSSA U.S. NUCLEAR REGULATORY COMMISSIO (4-95)
LLCENSEE EVENT REPORT (LER)
TEXT CONTINUA1 ION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 3 OF 7 97 006 0 TEXT /ifmore space is required, use additional copies of NRC Form 366A/ I17)
Unit 1 description:
The degraded voltage system for St. Lucie Unit 1 consists of 2 undervoltage relays (27-1 and 27-4),
connected in a 2 out of 2 logic, with permissives for SIAS, Containment Isolation Actuation Signal (CIAS),
and Main Steam Isolation Signal (MSIS). When both relays detect a degraded voltage condition with a coincident or subsequent SIAS, CIAS or IVISIS, relay 27X4 is actuated, which initiates load shed and EDG starting. See Figure 1 for a simplified drawing:
Procedure 1-0970027 calibrates and tests the undervoltage relays. Both the degraded voltage relays are actuated together but the SIAS, CIAS, or MSIS permissive contacts are jumpered out and therefore not included in the testing. The Unit 1 ESFAS procedure 1-0400050 does not test the degraded voltage ESFAS permissives; during Loss Of Offsite Power (LOOP) and LOOP/ESFAS testing, a loss of voltage is initiated by opening the startup transformer circuit breakers, producing an immediate and total loss of voltage which is detected by other undervoltage relays.
Unit 2 description:
The 4160V bus degraded voltage system for St. Lucie Unit 2 consists of 3 undervoltage relays (27M-A, 27N-B, and 27N-C), connected in a 2 out of 3 logic, with a SIAS permissive contact. When 2 of the 3 relays detect a degraded voltage condition and time out, without a coincident SIAS, an annunciator alarms in the control room to alert the operators to the degraded voltage condition. A subsequent SIAS will initiate an immediate load shed, EDG start, and load sequencing. See Figure 2 for a simplified drawing.
Procedure 2-0920020 calibrates and tests the undervoltage relays. This includes using the trip test pushbuttons for two relays at a time and observing a test light to indicate energization of the load shed bus, isolated during testing, to verify the logic. The SIAS contact is bypassed by a jumper and is not included in the testing. Procedure 2-0400053 tests the safeguards relays; however, the relays associated with the SIAS Group 7, which includes the degraded voltage permissive, are stated as being tested in accordance with OP 2-0400050, "Periodic'Test of the Engineered Safety Features." Therefore, the interlo k is not tested in this procedure. However, procedure 2-0400050, up to revision 22, did not test the degraded voltage interlock since during Loss Of Offsite Power (LOOP) and LOOP/ESFAS testing a loss of voltage is initiated by opening the startup transformer circuit breakers, producing an immediate and total loss of voltage which is detected by other undervoltage relays.
The cause of the event was inadequate ESFAS surveillance test procedures in that the SIAS permissive contact that initiates load shed and EDG start for a sustained degraded voltage condition was not verified by test. This latest issue was found as part of the continuing review of St. Lucie test and surveillance procedures against the plant Technical Specifications requirements as committed to in response to GL 9-
- 01. St. Lucie has reported previous discoveries in the past. GL 96-01 recognized that surveillance NRC FORM 388A I4-951
SRC FORM SSSA (4-95)'ICENSEE EVENT REPORT (LER)
U.S. NUCLEAR REGULATORY COMMISSIO TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 4 OF 7 97 006 0 TEXT /ifmore space is rerluired, use addilionel copies of NRC Farm 366A/ '17I procedures may not adequately test all required logic paths, and the industry as a whole has identified and reported problems found as a result of th'ese reviews.
his event is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B), as any operation prohibited by the plant's Technical Specifications.
Degraded voltage protection is a requirement instituted as a result of incidents at the Millstone and Arkansas Nuclear One plants. These events disclosed the possibility of degraded voltage conditions that co uld exist on plant emergency busses undetected by the loss of offsite power relays. Sustained operation at lower voltages could cause damage to safety related components. Branch Technical Position PSB-1 re quired the installation of a degraded voltage protection system that would prevent this occurrence, in ad dition to the loss of voltage relays.
PSB-1 also imposed requirements that the plant Technical Specifications be revised to include limiting conditions for operation, surveillance requirements, trip setpoints, and allowable values for the degraded voltage relays and associated time delay relays. The Technical Specifications for St. Lucie Units 1 and 2 incorporated the requirements for degraded voltage protection in accordance with PSB-1. Since the degraded voltage protection system is considered part of the loss of power protection system, it has been determined that the surveillance test requirements for the degraded voltage protection system should consist of functional verification every 18 months, during refueling.
0 perability of 'tlie Unit 1 B train degraded voltage system was demonstrated via the event described in LER 33 5 96-007, where the degraded voltage permissive signal was provided by a CIAS contact. This resulted in load shed of the B train emergency busses and start of the 1B EDG. This constituted an acceptable test SI nce performance of the Integrated Safeguards procedure demonstrates that a SIAS signaI will initiate a C IAS signal. Therefore, credit was taken for an operable degraded voltage permissive signal.
S ince surveillance testing had not been performed for the Unit 1 A train, the 1A EDG was declared in operable, due to a missed surveillance, at approximately 0900 on 5/1/97. A Letter of Instruction was P repared to perform testing to verify the functioning of the SIAS permissive contact (LOI ¹1-LOI-l&C-18 ).
The scope of-the I Ol test procedure was limited to verification of the SIAS permissive contact used in the d egraded voltage actuation logic (as opposed to SIAS, CIAS and MSIS). Based upon review of the design b sis for the degraded voltage circuit, the presence of the CIAS and MSIS permissive contacts is considered to be a conservative design feature, not required by the Technical Specifications; therefore, surveillance te sting of the CIAS and MSIS permissive contacts is not required. Testing was successfully performed at ap proximately 1630 on 5/1/97, functioning of the SIAS permissive was verified, and the 1A EDG was d clared operable.
Testing was successfully performed on both A and B trains of the Unit 2 degraded voltage system SIAS P ermissive contacts as of May 9, 1997. This completes the GL 96-01 reviews for Unit 2. The Unit 1 re views will be completed by the end of the Fall 1997 Unit 1 Cycle 15 refueling outage.
l
%RC FORM SSSA U.S. NUCLEAR REGULATORY COMMISSIO (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 5 'OF 7 97 006 0 TEXT (/fmore speceis required, use edditionel copies of NRC Form 3MAi I17I In general, surveillance procedures for St. Lucie Units 1 and 2 provide for calibratioh and test of the degraded voltage'etection relays, time delay relays, and the relay logic. Although the degraded voltage protection ESFAS permissive contacts had not been specifically tested during past ESFAS test surveillances, testing has been satisfactorily performed that verifies the operability of these conta'cts.
Therefore, this condition had no adverse affect on the protection of the health and safety of the public.
Testing of the Unit 1 A train degraded voltage protective system ESFAS functions was successfully demonstrated on May 1, 1997.
- 2. The Unit 2 ESFAS Test Procedure (2-0400050) was revised to incorporate testing of the SIAS interlock with degraded voltage protection. Testing of the degraded voltage protection SIAS interlock for both Unit 2 trains was completed on May 9, 1997.
- 3. The Unit 1 ESFAS Test Procedure (1-0400050) will be revised to incorporate testing of the SIAS degraded voltage protection permissive contacts.
LER 389 96-007 describes the discovery of a failure to adequately test the MSIS Actuation Logic during GL 96-01 reviews.
LER 389 96-006-0 describes the discovery of a failure to adequately test Auxiliary Feedwater Actuation Logic during GL 96%1 reviews.
y LER 389 96-005-0 describes the discovery of a failure to adequately test the Reactor Trip Breakers during GL 96-01 reviews.
LER 335 96-007 describes the incident where the degraded voltage permissive signal was provided by a CIAS contact.
NRr,'RAM sRRd (d 4fil
NRc FORM 366A U.S. NUCLEAR RMULATORYCOMMISSIO 14-95)
L1CENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION ST. LUCIE UNIT 1 05000335 6 OF 7 1 97 006 0 TEXT Iifmore spece is reqvired, use edditionel copies of NRC Form 366AI I 17) 27~ I 27<
CIS SIAS MSIS 27x4 A CONTACT FROM 27X4 INITIATES 4.16KV LOAD SHED AND EDG START I
Figure 1 Unit 1 Degraded Voltage Protection Scheme UPI cll410 lRRh M,OCl
0 10 NRC FCRM 366A U.S. NUCLEAR REGULATORY COMMISSIO
$ 4 95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION YEAR SEQUENTIAL REVISION St. Lucie Unit 1 05000335 7 OF 7 97 006 0 TEXT llfmore space i's required, use additional copies of NRC Form 388Al I17I
(+)
27N-A 27N-C 27N-C 2l3 COINCIDENT LOGIC 27N-B 27N-A 27DX
(+)
27DX'RIP SIAS (GROUP 7)
BUS 0 0 ENERGIZING THIS BUS INITIATES LOAD SHED AND EDG START Figure 2 Unit 2 Degraded Voltage Protection Scheme NAc FORM 388A I4-95)