ML17261A450: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
 
(4 intermediate revisions by the same user not shown)
Line 3: Line 3:
| issue date = 04/05/1987
| issue date = 04/05/1987
| title = LER 87-002-00:on 870306,RCS Oxygen Analysis Indicated That Steady State Requirements of Tech Spec 3.1.6.2 Had Been Exceeded.Caused by Personnel Error & Procedural Inadequacy. Procedural Guidance Being developed.W/870405 Ltr
| title = LER 87-002-00:on 870306,RCS Oxygen Analysis Indicated That Steady State Requirements of Tech Spec 3.1.6.2 Had Been Exceeded.Caused by Personnel Error & Procedural Inadequacy. Procedural Guidance Being developed.W/870405 Ltr
| author name = FILKINS D L, KOBER R W
| author name = Filkins D, Kober R
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:REGULATORYFORMATIONDISTRIBUTIONSYM(RIDS)ACCESSIONNBR:8704130520DOC.DATE:87/04/05NOTARIZED:NOFACIL:50-244RobertEmmetQinnaNuclearPlant>Unit1>RochesterGAUTH.NAMEAUTHORAFFILIATIONFILKINSsD.L.-RochesterQas5ElectricCorp.KOBERiR.W.RochesterGasScElectricCorp.RECIP.NAME.RECIPIENTAFFILIATIONDOCKET005000244
{{#Wiki_filter:REGULATORY    FORMATION DISTR IBUTION SY      M (R IDS)
ACCESSION NBR: 8704130520          DOC. DATE: 87/04/05    NOTARIZED: NO            DOCKET 0 FACIL: 50-244 Robert Emmet Qinna Nuclear Plant> Unit 1> Rochester                G 05000244 AUTH. NAME            AUTHOR AFFILIATION FILKINSs D. L.       -
Roch ester Qas 5 El ectr i c Corp.
KOBERi R. W.           Rochester Gas Sc Electric Corp.
RECIP. NAME       . RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER87-002-00:on87030&iRCSoxygenanalysisindicatedth"tsteadystaterequirementsowTechSpec3.i.h.2hadbeenexceeded.CausedbypersonnelerrorZcproceduralinadequacy.Proceduralguidancebeingdeveloped.W/870405ltr.DISTRIBUTIONCODE:IE22DCOPIESRECEIVED:LTRENCLSIZE:TITLE:50.73LicenseeEventReport(LER)iIncidentRpt>etc.NOTES:LicenseExpdateinaccordancewith10CFR2>2.109<9/19/72).05000244RECIPIENTIDCODE/NAMEPD1-3LASTAHLEiCINTERNAL:ACRSMICHELSONACRSNYLIEAEOD/DSP/ROABNRR/ADTNRR/DEST/ADSNRR/DEST/ELBNRR/DEST/MEBNRR/DEBT/PSBNRR/DEST/SQBNRR/DLPG/GABNRR/DREP/EPBi/PMASRBEQ02RQN1FILE01EXTERNAL:EQRQQROH>MLPDRNSICHARRISJCOPIESLTTRENCL1111112211101111111111111111551111RECIPIENTIDCODE/NAMEPD1-3PDACRSMOELLERAEOD/DOAAEOD/DSP/TAPBNRR/DEST/ADENRR/DEST/CEBNRR/DEST/ICSBNRR/DEST/MTBNRR/DEST/RSBNRR/DLPG/HFBNRR/DOEA/EABNRR/DREP/RABNRR/PMAS/PTSBRESSPEISiTHSTLOBBYNARDNRCPDRNSICMAYSiGCOPIESLTTRENCL1'111111011111-11111111111111TOTALNUMBEROFCOPIESREQUIRED:LTTR41ENCL39 HrICForm$OO10421LICENSEEEVENTREPORTILERIU.S.NUCLEARREOVLATORYCOMMISSIONAFFROUEOOMSHO.$190W10aKXFIRKS:Sn)ISSFACILITYNAME(Il'.E.GinnaNuclearPowerPlantoocxtTIavMsthl21osoo,o244>o(:07RtFORTOATS(1)LthHUMSKR(I)OOCXKTHVMSKRISIps000EVENTOATSIS)MONTHOAYYEARFACII,ITVH*MOSOTHERFACILIT)ttIHVOLYEO(SIYEARrravraaarrrrvMo~ROAYaa0varraIALy?gHVMOSRMONTHYEARReactorCoolantSystemOxygenConcentrationExceedsTechnical'pecificationLimitsDue-ToPersonnelErrorandProceduralInadea'.;.0306878700200040587O500()OFSRATIHOMOOS(Sl~OIYKRppp110120.402(SI20.OCS(a)(11(020a004)(ll(tl20.409(al(litt)I20A004)ill~()el20.400(al(Illa)20.a00(alSOM(al(I)90.$9(~)(2)90.2$4)al(0SO.T$41121(~I90.22(a)12)(SOLICENSEtCONTACTFORTHISLthlit)SO,2$4I(2)IIv)SO.2$4)(2)(el90.2241(21(et)SO.T$4)121(aOI)IAI90.2$(~I(21(rat)(S)90.2$la)12)(a)THISREFORTISSUSMITTEOFURSUANTTOTHEREOUlhtlatNTSOF10CFR$r(CooersorrorNmorooIraraIotorerrrgl(11TS.TIW2$.7((a)OTHKRItooaloyMAoroeataaronarroIoI'aat,NhcFomr$SMINAMErDuaneL.Filkins,Manager,HealthPhysicsandChemistryTELKFHOHKNUMSERAREACOOK315524-4446COMFLSTSONKLINKI'OREACHCOMFOHKNTFAILUREOtSCRISKOIHTHISRtFORTl12)CAUSESYS'EMCOMFOHKNTMANUFACTUNEREFORTASLETONFROSR~%''A'FCAVSESYSTEMCOMFONENTMAHVFAGTUNERKFORTASLTOHOROS%VISUFFLKMKNTALRtFORTtXFKCTtOI)alYESIllFar,oomo)eriEXPECTEDSVSMI$$IONOATETHOAKKTRAcT(LamiaIof400a)racer.l.o.ooororarrateryhtrearrarroroeoeaoryarerrrrnNrlkroal(19)EXFECT'EOSUSMISSIONOATSIISIMONTHOAYYEAR.DuringstartupfromarefuelingoutageonMarch6,1987,at0009EST,areactorcoolantsystem(RCS)oxygenanalysisindicatedthatt:hesteadystaterequirementsofTechnicalSpecification(TS)3.1.6.2hadbeenexceeded.Areviewofthepreviousdaysanalyticalresultsindicateda-previousanalysisonMarch5,1987,hadindicatedasimilarresultwhichviolatedthe24hourlimitingconditionforoperationinTS3.1.6.4.Areactorcoolantsystemcooldownwasinitiatedtoloversystemtemperatureandtoallowadditionofhydrazinetoscavengeoxygenfromthesystem.ThecauseforexceedingtheTSrequirementswaspersonnelerrorandproceduralinadequacy.TherewasnoproceduralguidanceintheoperatingprocedureswhichcorrelatesrequiredchemistrysamplingtoRCStempera-ture.ThetechniciandidnotinitiallyrecognizethatTSrequirementshadbeenexceeded.ToprecluderecurrencebetterproceduralguidanceisbeingdevelopedandtechniciantrainingwillbeperformedbasedonthisLER.Therewerenosignificantsafetyconsequencesofthisincident.87041305205000244087040>PgRAgoC'KpgRS~HRC'Fern$90~~*~.c~(9021wi NACPererSSSA(9891LICENSEEEVENTREPORT(LERITEXTCONTINUATIONU.S,NUCLEAAAEOULATOAYCOMMISSIONAPPROVEOOMSNO.SISOW(04EX~INES:8(SI(85I'ACILITYNAME(llR.E.GinnaNuclearPowerPlantTEXT(IfrrrereNreceIrreeeeee,wecere(lre(Hr(CferrrrJSSAYl(IllOOCXETNUMSEI((SIosooo244LEIINUMEEI(ISIYEAN.p)8SSOUSNTIALPr&#xc3;eeyrSIONNUMTrlrerrrUMee7-002-0~AOE(SI2oF07I.PRE-EVENTPLANTCONDITIONSOnMarch4,1987,theunitwasstartingupfromtheannualrefuelingandmaintenanceoutage.Onthisdatetheplantleftthecoldshutdownconditionandheateduptoapproximately315F,350psigreactorcoolantsystem(RCS)temperatureandpressure,respectively,toperformsteamgenerator(S/G)crevicecleaningperoperatingprocedure.0-10.TheTSrequirementsforRCSoxygenoflessthan0.1ppmhadbeenachievedpriortoincreasingRCStemperatureabove200oF.II.DESCRIPTIONOFEVENTA.EVENTOnMarch6,1987,at0009ESTwithS/Gcrevicecleaninginprogress,aRCSsamplewastakenasrequiredbyAttachmentIofprocedurePC-1.1(PrimarySystemAnalysisScheduleandLimits).ThisprocedureoutlinestherequiredanalysisandlimitsforRCSchemistryduringhotshutdownandnormaloperation.Theresultoftheoxygenanalysisoftheabovesamplewas0.5ppm.Theplanttechnicianperformingtheanalysisrecognizedthisresulta6anumbergreaterthanallowedbyTSfortheexistingplantconditions.Asisroutine,aconfirmingsamplewastakenandanoxygenanalysisperformedat0130ESTwiththesameresult.AreviewoftheplanttechnicianslaboratorynotebookrevealedthatonMarch5,1987at0030EST,anothersampleandanalysishadbeenperformedwhichalsoindicatedoxygenconcentrationintheRCSgreaterthan0.1ppm.TheGinnaStationTS,Section3.1.6.2,requiresthatcorrectiveactionbetakenimmediatelywhenthenormalsteadystateRCSoxygenconcentrationlimitof0.1ppmisexceeded.AlsoTSSection3.1.6.4requiresthatifthenormalsteadystatelimitsforRCSoxygenareexceeded-andcannotbereturnedtowithinthelimitswithin24hours,thereactorshallbebroughttothecoldshutdowncondition.Because,from0030ESTonMarch5,1987,until0235ESTonMarch6,1987,(alapsedtimeofapproximately26hours),theRCSoxygenconcen-trationexceededitsnormalsteadystatelimitwithnocorrectiveactiontaken,bothsectionsofTS,3.1.6.2and3.1.6.4wereexceeded.B.INOPERABLESTRUCTURES,COMPONENTSORSYSTEMSTHATCONTRIBUTEDTOTHEEVENT:Nonerr(981I NRCFmwJTSAl9SJILICENSEEEVENTREPORT(LER)TEXTCONTINUATIONV.S.NVCLKARRSOVLATORYCOMMISSIONAPPROY500MSNO,JI50&IdiSXPIRTSS/JI/95FACILITYNAMSIllR.E.GinnaNuclearPowerPlant:TTJTIITraceepoCPIIleeAwd.Pae~NIICfOneJTSAJI0T)OOCKKTNVMJSRIJIooooo44LTRNVMJSRISIYSAR~X,STCUTNTIAL:NATY>SUNNMTTR.'i~FNUMTR870020~AOIIJI03ap07C.DATESANDAPPROXIMATETIMESFORMAJOROCCURRENCES:-oMarch4,1987,0900EST:Unitleavescoldshutdown,RCS.oxygenconcentrationlessthan0.1ppm.oMarch5,1987,0030EST:Eventdate.oMarch6,1987,0009EST:Discoverydate.oMarch6,1987,0130EST:Confirmatory.sampletaken.oMarch6,1987,0235EST:Plantcooldowninitiated.NoMarch6,1987,0800EST:RCSaveragetemperaturelessthan250oF.oMarch6,1987,1030EST:RCSoxygenconcentrationwithinTSrequirements.D.OTHERSYSTEMSORSECONDARYFUNCTIONSAFFECTED:NoneE.METHODOFDISCOVERY:Theeventwasmadeapparentduringtheforeman'sreviewoftheplanttechnicianslaboratorynotebook.F.OPERATORACTION:TheplanttechnicianreportedtheeventtotheControlRoom.TheControlRoomoperatorsinitiatedaplantcooldownperTSrequirementsat0235ESTonMarch6,1987.By0800ESTtheRCSaveragetemperaturewaslessthan250F.At0935ahydrazineadditionwasmadetotheRCSwhichbroughttheoxygenconcentrationwithinTSrequirementsby1030EST.SAFETYSYSTEMRESPONSES:Nonek'f7DlAelll95JI NRCSarraSSSA(985)LICENSEEEVENTREPORTILER)TEXTCONTINUATIONU.S.NUCLEARREOULAIORYCOMMISSIONAP/rROVEOOMSNO.5150&l0eEXelRES.8/Sl/85aACILITYNAME(IIR.E.GinnaNuclearPowerPlantTEXT///mareeaece/e/rr/rerLeeee~AlRC/rarm8(/SA'e/IITIIII.CAUSEOpEVENTOOCKETNUMSER(llosooo244LERNUMSER(SISEQUENT/*Ll),)IYIS0Nvv8I~~r/UMSKA70200eACE(sI04pFO7A.IMMEDIATECAUSE:RCSoxygenconcentrationwasgreaterthanthenormalsteadystateTSlimitformorethan24hourswithnoimmediatecorrectiveactiontaken.ThiswasduepartiallytoacognitiveerrorsincethetechnicianfailedtorecognizethattheanalyticalresultsexceededtheTSrequirementsfortheRCStemperaturewhichexistedatthetime.ItwasalsopartiallytheresultofaproceduralinadequacysincetherewasnoproceduralguidanceintheoperatingprocedurewhichcorrelatedrequiredchemistrysamplingtoRCStemperature.B.ROOTCAUSE:Theresultsofarootcauseinvestigationdeterminedthatthereweretwomajor.rootcausesthatcontributedtotheevent.Theseareasfollows:TheHealthPhysicsandChemistrysectionfailedtorecognizetheRCSoxygenconcentrationwasexceedingTSrequirementsforapproximately24hours.Thisoccurredbecauseofthefollowingreasonsandactions:oThecrevicecleaningoperatingprocedureholdstheRCStemperaturebetweencoldshutdownandhotshutdownforextendedperiodsoftime.0Theplantchemistryprocedure,PC-1.1,onlyprovidedascheduleforanalysisforthefollowingplantconditions:0a.Hotshutdownornormaloperation,AttachmentIb.Coldshutdown,AttachmentIIc.Refuelingshutdown,AttachmentIIIOnMarch5,1987,AttachmentIIwasinuse,whichdidnotrequireaRCSoxygenanalysisbetaken.ThetechnicianwhoperformedtheoxygenanalysisonthisdatehadreceivedaverbalrequestfromanothertechniciantoruntheRCSoxygenanalysiswithnoapparentreasongiven.Sincetheanalysiswasnotrequired,hedidnot,recognizethesignificanceoftheresults.NRCeORM888*t985I NRClorna844AI98SILICENSEEEVENTREPORTILER)TEXTCONTINUATIONV.S.NUCLEARREOULATORYCOMMISSIONATPROYEOOM8NO.SISOMI04EXPIRES:8ISII8$tACILITYNAMEIIIR.E.GinnaNuclearPowerPlantOOCKETNUMEERISILERNUMEERl4lYEAR,'8@slQUENTIALgPntvataonNUMttll..rNUMttnTACEISITEXTlitmoroNaoco*rotarooe'.ooooOtrnrnaMHRCrranrn848A'rIIITIosooo2487,0020'0'5QF07.0TheanalyticalresultsforRCSchemistryarenormally.enteredintothePrimarySystemChemistryLogandalsoontheDailyChemistryAnalysisResultsFormwhichisforwardedtoOperationsdaily.ThechemistryresultsobtainedonMarch5,1987,werenotenteredoneitheroftheserecords.SupervisoryreviewLofthechemistrylogdidnotrecognizethelackofresultsforMarch.5,1987,untilMarch6,1987,andOperationsalsodidnotrecognizethelackofresultsforMarch5,1987.AlthoughthereviewoftheselogswouldnothaveprecludedexceedingtherequiremegtsofTS3.1.6.2,itislikelythatcorrectiveactionwouldhayebeentakenpriortoexceeding24hoursiftheresultshadbeenproperlylogged.2.TheunanticipatedoxygenconcentrationincreaseintheRCS.Thishappenedbecauseofthefollowingreasonsandactions:oTheinvestigationofthecauseoftheoxygenincreaseintheRCSrevealedthatthestep.inprocedure0-10whichrequiresburpingofthevolumecontroltank(VCT)withhydrogenhadbeenmarkednon-applicable'(N/A);Thisisallowed-procedurally.andOperationshadbeendirectedbytheoutageplanninggrouptoproceedwithonlyanitrogenoverpressureontheVCT.Thishadbeendoneinthe1985and1986outageswithoutoxygenexcursions,sothiswasnotwithoutprecedent.Thereasonfornotintroducinghydrogenistoallowamorerapidturnaroundifsystemleaksshoulddevelopduringperformanceoftheprimarysystemhydro.IfthehydrogenconcentrationisincreasedintheRCS,operatingproceduresrequireremovalpriortosystemdraindowntoprecludepossibleexplosivemixturesinprimarycomponents.Thisisatimeconsumingprocess.0Withouthydrogentocontroloxygen,anysourceofoxygenwouldcauseincreasesintheRCSoxygenconcentration.ThreesourcesthatcouldhavecontributedtotheoxygeningresstotheRCSwere:a.ThevolumecontroltankwasnotburpedsoanyoxygeninthetankwouldhavebeenallowedtocomeintoequilibriumwiththeRCS.aa'aI98SI NRCiona$48A19881LICENSEEEVENTREPORT{LER)TEXTCONTINUATIONV.S,NUCLEARREOVLATORYCOMMISSIONAPPROVEDOMENO.S($0&(08EXPIRES:8/SI/8$PACILIEYNAMElllR.E.GinnaNuclearPowerPlantDOCKET'VMEER(EILERNVMEER(81YEAR@'80vENT/AL$8)aov/SionNUMPEN~aNVMoaSEXY///naaoNN(o/o~,oooo////oao/HRCAN/a80848I(11(osooo2448700006ov0'7b.c~Normalintroductionofreactormake-upwaterwouldintroduceoxygenintotheRCS.Someoxygenwouldhavebeenformedbyradiolysisofwaterwhilepassingthroughthecore.IV.ANYSISOFEVENTIThiheventisreportableinaccordancewith10CFR50.73,LicenseeEventReportSystem,Item(a)(2)(i)(B),whichrequiresreportingof"anyoperationprohibitedbytheplant'sTechnicalSpecifi-cations>>inthattheplantwasinadegradedmodeavowed'bytheTechnicalSpecificationsforaperiodoftimelongerthanthatpermittedbytheTechnicalSpecifications.Anassessmentwasperformedofthesafetyconsequencesandimpli-cationsoftheeventwiththefollowingresultsandconclusions:oThebasisforcontrolofoxygenintheRCSistominimizegeneralcorrosionandtopreventlocalizedstresscorrosioninthepresenceofchlorideandfluorideions.Duringtheperiodoftimethattheoxygenconcentrationwasoutsidetheoperatingband,.boththechlorideandfluorideconcentrationswerewellbelowthenormaloperatingrequirements.oSincetheoxygenconcentrationsneverexceededtheTStransientlimits(always0.5ppmorless)andthechlorideandfluorideconcentrationswerewithinrequirements,therewouldhavebeennoanticipateddegradationofRCSsystemcomponentsand,therefore,nosafetyconsequencesorimplicationsfromthisevent.V.CORRECTIVEACTIONA.ACTIONSTAKENTORETURNTHERCSOXYGENCONCENTRATIONTONORMALSTEADYSTATEOPERATINGVALUES:oTheRCSwascooleddowntolessthan250oFtoallowtheadditionofhydrazinetoscavengetheoxygen.oHydrazine'asaddedtotheRCSandoxygenwasbroughtwithinTSlimits.B.ACTIONSTAKENORPLANNEDTOPREVENTRECURRENCE:nlRaila(84$10CorrectiveactioncurrentlyinprogresswillprovidebetterproceduralguidancetoassuretheHealthPhysicsandChemistrysectionisawarewhentheRCStemperature-hasbeenincreasedandchemistryrequirementshavechanged.
LER  87-002-00: on 87030&i RCS oxygen analysis indicated th "t steady state requirements ow Tech Spec 3. i. h. 2 had been exceeded. Caused by personnel error Zc procedural inadequacy.
NIICPena588A19831LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLTAIIIITOULATOIIYCOMMISSIONAPPAOY8OOM8NO.31$0WI058XPIA85"8ITI/8$PACILITYNAM8lllR.E.GinnaNuclearPowerPlant-OOCK8TNUM88IILTILKIINUM88II181YTAAj>pI55QUCNTIAL&Aileayl5%n,c,.?NUM8P4'UMTePA48151TtxTIII<<eeaapacela>>aakaf,a>>aaAveavlryilcPane888A81Illlosooo24487-002-007DF07oTheHealthPhysicsandChemistrytechniciansinvolvedwithprimarysystemchemistryhaveallbeenmadeawareoftheerrorswhichcontributedtotheevent.oAcopyofthisLERwillbeforwardedtotheTrainingsectionandwillbe.includedinthetrainingprogramfortheHealthPhysicsandChemistrysection.VI.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:Therewerenocomponentfailuresthatcontribgtedtothisevent.B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththefoilowingresults:nodocumentationofsimilarLEReventscouldbeidentified.Nc019851
Procedural guidance being developed. W/870405 ltr.
.=?Cl"HEIE"arl~,r55r57aN.OE,'87,<Veau@Ronl~B>w,Av.>va~g-oco>a'C.5April5,1987U.S.NuclearRegulatoryCommissionDocumentControlDeskWashington,DC30555
DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR              ENCL      SIZE:
TITLE: 50. 73 Licensee Event Report (LER) i Incident Rpt> etc.
NOTES: License Exp date in accordance        with  10CFR2> 2. 109<9/19/72).       05000244 RECIPIENT          COPIES            RECIPIENT          COPIES ID CODE/NAME        LTTR ENCL        ID CODE/NAME      LTTR ENCL PD1-3 LA                      1      PD1-3 PD              1      '1 STAHLEi C                1    1 INTERNAL: ACRS MICHELSON                  1      ACRS MOELLER          1 ACRS  NYLIE            1    1      AEOD/DOA                      1 AEOD/DSP/ROAB            2    2      AEOD/DSP/TAPB          1      1 NRR/ADT                  1    1      NRR/DEST/ADE          1      0 NRR/DEST/ADS            1    0      NRR/DEST/CEB                  1 NRR/DEST/ELB            1    1      NRR/DEST/ ICSB                1 NRR/DEST/MEB            1    1      NRR/DEST/MTB          1      1 NRR/DEBT/PSB            1    1      NRR/DEST/RSB          1-NRR/DEST/SQB            1    1      NRR/DLPG/HFB          1      1 NRR/DLPG/GAB            1    1      NRR/DOEA/EAB                  1 NRR/DREP/EPB            1    1      NRR/DREP/RAB          1      1 i/PMAS     RB        1    1      NRR/PMAS/PTSB          1      1 EQ              02          1      RES  SPEISi T          1      1 RQN1    FILE    01          1 EXTERNAL: EQRQ QROH>      M          5    5      H ST LOBBY NARD        1      1 LPDR                    1    1      NRC PDR                1      1 NSIC HARRIS    J        1    1      NSIC MAYSi G          1 TOTAL NUMBER OF COPIES REQUIRED: LTTR            41  ENCL    39
 
HrIC Form $ OO                                                                                                                                                        U.S. NUCLEAR REOVLATORY COMMISSION 10421                                                                                                                                                                          AFFROU EO OMS HO. $ 190W10a KXFIRKS: Sn) ISS LICENSEE EVENT REPORT ILERI FACILITY NAME                                                                                                                                            oocxtT IavMsth        l21 Ginna Nuclear Power Plant                                                                                                                o s o o,o 244                                >o(:07 (Il'.E.
Reactor Coolant System Oxygen Concentration Exceeds Technical'pecification Limits Due- To Personnel Error and Procedural Inade a '.;.
EVENT OATS IS)                              Lth HUMSKR (I)                                RtFORT OATS (1)                               OTHER    FACILIT)tt IHVOLYEO (SI YEAR            aa0  v a rr a I AL  rravraaarr                  OAY      YEAR                FACII,ITV H*MOS                          OOCXKT HVMSKRISI MONTH        OAY            YEAR                y?g        HVMOSR            rrvMo ~ R MONTH p  s    0    0    0 0      306 87                        8 7                002                0      0 0 4              0 5      8 7 O  50        0    ()
ill THIS REFORT IS SUSMITTEO FURSUANT T O THE REOUlhtlatNTS OF 10 CFR $ r                    (Cooers orro  rN moro  oI rara Iotorerrrgl (11 OFSRATIHO MOOS (Sl                             20.402(S I                                      20.a00(al                              SO,2  $4 I(2)I Iv)                                TS.TIW
    ~ OIYKR                                  20.OCS(a)(11(0                                  SOM(al (I )                             SO.2 $ 4) (2)(el                                  2$ .7((a) p p p                      20 a004)(ll(tl                                  90.$ 9( ~ )(2)                         90.2241(21 (et)                                  OTHKR Itooaloy M Aoroeat 1101 aaron arro Io I'aat, Nhc Fomr 20.409(a   l(litt)I                            90.2$ 4)al(0                            SO.T $ 4)121(aOI)  IAI                            $ SMI 20A00 4)       ()el                            SO.T $ 41121( ~ I                      90.2$ ( ~ I(21(rat)(S) 20.400(al    (Illa)                            90.22(a) 12)(SO                        90.2$ la) 12) (a)
LICENSE    t CONTACT FOR THIS Lth lit)
NAME                                                                                                                                                                            TELKFHOHK NUMSER r
AREA COOK Duane        L. Filkins, Manager, Health Physics and Chemistry                                                                                                                              44 46 31 55 24 COMFLSTS ONK LINK I'OR EACH COMFOH KNT FAILURE OtSCRISKO IH THIS RtFORT l12)
SYS'EM                                    MANUFAC                EFORTASLE                                                                          MAHVFAG            KFORTASL CAUSE                        COMFOHKNT                  TUNER              TO NFROS                                CAVSE SYSTEM      COMFONENT                  TUNER              TO HOROS
                                                                                                                                                                                                                    %VI R~%
                                                                                            ''A '
F SUFFLKMKNTALRtFORT tXFKCTtO I)al                                                                                              MONTH      OAY    YEAR.
EXFECT'EO SUSMISSION OATS IISI YES  IllFar,       oomo)eri EXPECTED SVSMI$$ ION OA TET                                              HO AKKTRAcT(Lamia Io f400 a)racer. l.o. ooororarratery htrearr arroroeoeao ryarerrrrnNr lkroal                (1 9)
During startup from a refueling outage on Marchindicated                                                                                6, 1987, at 0009 EST, a reactor coolant system (RCS)                                                               oxygen            analysis                                          that t:he steady state requirements                                                of    Technical                      Specification                      (TS)           3.1.6.2                had been exceeded.                         A    review                  of  the        previous                days    analytical                      results                indicated                a-previous analysis on March 5, 1987, had indicated a similar                                                                                                                result          which violated the 24 hour limiting condition                                                                            for operation in TS 3.1.6.4. A reactor coolant system cooldown was initiated to lover system                                                                                                              temperature the      system.
and to allow addition of hydrazine to scavenge oxygen                                                                                                      from The cause for exceeding the TS requirements was personnel                                                                                                                      error and procedural inadequacy. There                                                              was          no  procedural              guidance                  in      the      operating procedures which correlates                                                          required              chemistry              sampling                    to      RCS      tempera-ture. The technician did not initially recognize that TS                                                                                                                  requirements had been exceeded.
To      preclude recurrence better procedural based                                                                      guidance is being developed and        technician training will be performed                                                                                        on this LER.
There were no significant safety consequences of this incident.
870413052              0 87040>
~ HRC'Fern $ 90 (9021
                                ~           ~ *~       . c   ~
PgR S
AgoC'K 05000244                pgR wi
 
NAC Perer SSSA (9 891                                                                                                                  U.S, NUCLEAA AEOULATOAYCOMMISSION LICENSEE EVENT REPORT (LERI TEXT CONTINUATION                                        APPROVEO OMS NO. SI SOW(04 EX ~ INES: 8(SI(85 I'ACILITYNAME (ll                                                            OOCXET NUMSEI( (SI LEII NUMEEI( ISI                      ~ AOE (SI
                                                                                                              .p)8 SSOUSNTIAL Pr&#xc3;     eeyrSION R.E. Ginna Nuclear Power Plant                                                                      YEAN        NUM Trl    rer rrUM ee o  s  o  o    o  244      7  002                       0       2oF      07 TEXT (If rrrere Nrece Ir reeeeee, we cere(lre( Hr(C ferrrr JSSA Yl (Ill I.             PRE-EVENT PLANT CONDITIONS On      March 4, 1987, the unit was starting up from the annual refueling and maintenance outage.                                     On this date the plant left the cold shutdown condition and                              heated      up to approximately 315 F, 350 psig reactor            coolant                system (RCS)     temperature      and pressure, respectively, to perform steam generator (S/G) crevice cleaning per operating procedure .0-10. The TS requirements for RCS oxygen of less than 0.1 ppm had been achieved prior to increasing RCS temperature above 200oF.
II.           DESCRIPTION OF EVENT A.           EVENT On      March 6, 1987, at 0009 EST with S/G crevice cleaning in progress, a RCS sample was taken as required by Attachment I of procedure PC-1. 1 (Primary System Analysis Schedule and Limits). This procedure outlines the required analysis                                                                  and limits for                        RCS chemistry during hot shutdown and normal operation.
The        result of the oxygen analysis of the above sample was 0.5 ppm. The plant technician performing the analysis recognized this result a6 a number greater than allowed by TS for the existing plant conditions. As is routine, a confirming sample was taken and an oxygen analysis performed at 0130 EST with the same result. A review of the plant technicians laboratory notebook revealed that on March 5, 1987 at 0030 EST, another sample and analysis had been performed which also indicated oxygen concentration in the RCS greater than 0.1 ppm.
The Ginna Station TS, Section 3.1.6.2, requires that                                                    corrective action be taken immediately when the normal steady                                                        state RCS concentration            limit        of  0.1          is    exceeded.                     Also TS oxygen Section 3.1.6.4 requires that limits for RCS oxygen are exceeded -and cannot be returned to ifppm the normal steady state within the limits within 24 hours, the reactor shall be brought to the cold shutdown condition. Because, from 0030 EST on March 5, 1987, until 0235 EST on March 6, 1987, (a lapsed time of approximately 26 hours), the RCS oxygen concen-tration exceeded its normal                                    steady state limit with no corrective action taken, both sections of TS, 3. 1. 6. 2 and 3.1.6.4 were exceeded.
B.           INOPERABLE STRUCTURES,                         COMPONENTS OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None rr (9 81 I
 
NRC Fmw JTSA                                                                                                      V.S. NVCLKAR RSOVLATORY COMMISSION l9 SJI LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                                      APP  ROY 5 0 0 MS NO, J I 50 &I di SXPIRTSS/JI/95 FACILITY NAMS      Ill                                              OOCKKT NVMJSR IJI                  LTR NVMJSR ISI                        ~ AOI  IJI YSAR  ~X, STCUTNTIAL:   N ATY>SUN
                                                                                                                      .'i~F N MTTR          NUM TR R.E. Ginna Nuclear Power Plant:
TTJT IIT race epoCP II leeAwd.
C.
Pae ~     NIIC fOne JTSAJI 0T) o  o  o  o DATES AND APPROXIMATE TIMES FOR MAJOR OCCURRENCES:
o      4 4 87          002              0          03 ap07 o        March 4, 1987, 0900 EST: Unit leaves cold shutdown,                                                           RCS
                                        . oxygen concentration less than 0.1 ppm.
o        March 5, 1987, 0030 EST:                       Event date.
o        March 6, 1987, 0009 EST:                       Discovery date.
o        March 6, 1987, 0130 EST:                       Confirmatory. sample taken.
o        March 6, 1987, 0235 EST:                       Plant cooldown initiated.
N o      March 6, 1987,             0800 EST:             RCS    average temperature                              less than 250oF.
o      March 6, 1987,                 1030 EST:             RCS    oxygen concentration within            TS requirements.
D.           OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None E.           METHOD OF DISCOVERY:
The event was made apparent                            during the foreman's review of the plant technicians                  laboratory        notebook.
F.           OPERATOR ACTION:
The    plant technician reported the event                              to the Control Room.
The    Control Room operators initiated                            a  plant        cooldown per TS 0800 EST the requirements at 0235 EST on                          March    6,   1987.         By At 0935 a RCS average temperature                        was      less    than      250        F.
hydrazine addition                  was    made      to  the    RCS      which            brought                the oxygen concentration                within        TS  requirements          by        1030        EST.
SAFETY SYSTEM RESPONSES:
None k 'f7D    lAell l95JI
 
NRC Sarra SSSA (9 85)                                                                                                           U.S. NUCLEAR REOULAIORY COMMISSION LICENSEE EVENT REPORT ILER) TEXT CONTINUATION                                  AP/rROV EO OMS NO. 5150&l0e EXelRES. 8/Sl/85 aACILITY NAME (II                                                          OOCKET NUMSER (ll          LER NUMSER (SI                    eACE (sI SEQUENT/*L l),) IYIS 0 Nvv 8 I r/UMSKA R.E. Ginna Nuclear Power Plant
                                                                                                                          ~ ~
244    7    0      2        0  0    04    pFO    7
        /// mare                      e~EVENT                              o  s  o  o  o III. CAUSE T EXT          eaece /e /rr/rerL eee      AlRC /rarm 8(/SA'e/ I ITI Op A.             IMMEDIATE CAUSE:
RCS    oxygen concentration                      was    greater than the normal steady state TS limit for more than 24 hours with no immediate corrective action taken. This was due partially to a cognitive error since the technician failed to recognize that the analytical results exceeded the TS requirements for the RCS temperature which existed at the time. It was also partially the result of a procedural inadequacy since there was no procedural guidance in the operating procedure which correlated required chemistry sampling to RCS temperature.
B.             ROOT CAUSE:
The    results of                  a root cause investigation determined that there were two                      maj or .root causes          that contributed to the event.           These are as follows:
The Health Physics and Chemistry section failed to recognize the RCS oxygen concentration was exceeding TS requirements for approximately 24 hours. This occurred because of the following reasons and actions:
o              The      crevice cleaning operating procedure holds the RCS        temperature between cold shutdown and hot shutdown for extended periods of time.
0              The plant chemistry procedure, PC-1.1, only provided a schedule for analysis for the following plant conditions:
: a. Hot shutdown or normal operation, Attachment I
: b.         Cold shutdown, Attachment          II
: c.         Refueling shutdown, Attachment              III 0            On March 5, 1987, Attachment II was in use, which did not require a RCS oxygen analysis be taken. The technician who performed the oxygen analysis on this date had received a verbal request from another technician to run the RCS oxygen analysis with no apparent reason given. Since the analysis was not required, he did not, recognize the significance of the results.
NRC eORM 888*
t9 85 I
 
NRC lorna 844A I9 8SI                                                                                                              V.S. NUCLEAR REOULATORY COMMISSION LICENSEE EVENT REPORT ILER) TEXT CONTINUATION                                  ATPROYEO OM8 NO. SISOMI04 EXPIRES: 8ISII8$
tACILITYNAME III                                                            OOCKET NUMEER ISI LER NUMEER l4l                    TACE ISI R.E. Ginna Nuclear Power Plant                                                                YEAR,'8@ slQUENTIAL NUMttll gP..r ntvataon NUMttn o  s  o  o  o  2 4 8 7,      0 0 2          0'0'        5  QF    0 7.
TEXT lit moro Naoco *rotarooe'. ooo oOtrnrnaM HRC rranrn 848A'rI IITI 0           The      analytical results for RCS chemistryare normally.
entered into the Primary System Chemistry Log and also on the Daily Chemistry Analysis Results Form which is forwarded to Operations daily. The chemistry results obtained on March 5, 1987, were not entered on either of these records. Supervisory reviewL of the chemistry log did not recognize the lack of results for March .5, 1987, until March 6, 1987, and Operations also did not recognize the lack of results for March 5, 1987. Although the review of these logs would not have precluded exceeding the requiremegts o f TS 3. 1. 6. 2, likely that corrective action would haye been taken it      is prior to exceeding 24 hours properly logged.
if  the results had been
: 2.           The unanticipated oxygen concentration increase in the RCS.             This happened because of the following reasons and actions:
o            The investigation of the cause of the oxygen increase in the RCS revealed that the step .in procedure 0-10 which requires burping of the volume control tank (VCT) with hydrogen had been marked non-applicable'(N/A); This is allowed- procedurally.
and Operations had been directed by the outage planning group to proceed with only a nitrogen overpressure on the VCT. This had been done in the 1985 and 1986 outages without oxygen excursions, so this was not without precedent. The reason for not introducing hydrogen is to allow a more rapid turnaround          if    system leaks should develop during performance of the primary system hydro. If the hydrogen concentration is increased in the RCS, operating procedures require removal prior to system drain down to preclude possible explosive mixtures in primary components. This is a time consuming process.
0            Without hydrogen to control oxygen, any source of oxygen would cause increases in the RCS oxygen concentration. Three sources that could have contributed to the oxygen ingress to the RCS were:
: a.         The volume control tank was not burped so any oxygen in the tank would have been allowed to come into equilibrium with the RCS.
a  a'a I9 8SI
 
NRC    iona $ 48A                                                                                      V.S, NUCLEAR REOVLATORY COMMISSION 19 881 LICENSEE EVENT REPORT {LER) TEXT CONTINUATION                              APPROVED OME NO. S($ 0&(08 EXPIRES: 8/SI/8$
PACILIEY NAME    lll                                              DOCKET'VMEER (EI          LER NVMEER (81 YEAR @'80vENT/AL $a8) aov/Sion NVM oa R.E. Ginna Nuclear Power Plant                                                            NUMPEN    ~
24487      00                          0 6 ov 0 '7 SEXY /// naao NN(o /o ~, ooo o////oao/HRC AN/a 80848 I (11(
b.
o  s  o  o  o Normal introduction of reactor make-up water 0
would introduce oxygen into the RCS.
c   ~     Some oxygen would have been formed by radiolysis of water while passing through the core.
IV.       AN    YSIS OF EVENT I
Thih event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, Item (a)(2)(i)(B), which requires reporting of "any operation prohibited by the plant's Technical Specifi-cations>> in that the plant was in a degraded mode avowed 'by the Technical Specifications for a period of time longer than that permitted by the Technical Specifications.
An assessment                  was performed of the safety consequences and impli-cations of the event with the following results and conclusions:
o      The basis for control of oxygen in the RCS is to minimize general corrosion and to prevent localized stress corrosion in the presence of chloride and fluoride ions. During the period of time that the oxygen concentration was outside the operating band,.both the chloride and fluoride concentrations were well below the normal operating requirements.
o      Since the oxygen concentrations never exceeded the TS transient limits (always 0.5 ppm or less) and the chloride and fluoride concentrations were within requirements, there would have been no anticipated degradation of RCS system components and, therefore, no safety consequences or implications from this event.
V.         CORRECTIVE ACTION A.     ACTIONS TAKEN TO RETURN THE RCS OXYGEN CONCENTRATION TO NORMAL STEADY STATE OPERATING VALUES:
o            The      RCS        was  cooled down to less than 250oF to allow the addition of hydrazine to scavenge the oxygen.
o            Hydrazine'as added to the RCS and oxygen was brought within            TS  limits.
B. ACTIONS TAKEN OR PLANNED TO PREVENT RECURRENCE:
0            Corrective action currently in progress will provide better procedural guidance to assure the Health Physics and Chemistry section is aware when the RCS temperature-has been increased and chemistry requirements have changed.
nl Rail a (8 4$ 1
 
NIIC Pena 588A                                                                                            U.S. NUCLTAII IITOULATOIIYCOMMISSION 19 831 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                                APPAOY8O OM8 NO. 31$ 0WI05 8XPIA85" 8ITI/8$
PACILITY NAM8    lll                                          OOCK8T NUM88II LTI              LKII NUM88II 181                  PA48  151 YTAA j>pI  55QUCNTIAL &Ail eayl5%n R.E. Ginna Nuclear Power Plant-                                                     ,c,.?   NUM 8      P4'UM Te o  s  o o    o  24 487 002 0                              07 DF07 TtxT III<<eea apace la>>aakaf, a>> aaAveavl ryilc Pane 888A81 Illl o          The Health Physics and Chemistry technicians involved with primary system chemistry have all been made aware of the errors which contributed to the event.
o          A      copy of this LER will be forwarded to the Training section and will be .included in the training program for the Health Physics and Chemistry section.
VI.         ADDITIONAL INFORMATION A.         FAILED COMPONENTS:
There were no component                      failures    that contribgted to this event.
B.         PREVIOUS LERs ON SIMILAR EVENTS:
A    similar LER event historical search was conducted with the foilowing results:                   no documentation of similar LER events could be identified.
N c      0 19 851
 
arl  ~, r 5 r5 57 aN
.=? Cl"HEI E"                               .O E,'87,<Veau@ Ronl~B >w, A v. >va~g-oco>
a'C .5 April 5,   1987 U.S. Nuclear Regulatory Commission Document        Control Desk Washington,         DC    30555


==Subject:==
==Subject:==
LER87-002,ReactorCoolantSystemOxygenConcentrationExceedsTechnicalSpecificationLimitsDuetoPersonnelErrorandProceduralInadequacyR.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordancewith10CFR50.73,LicenseeEventReportSystem/Item(a)(2)(i)(B)whichrequiresareportof"anyoperationprohibitedbytheplantTechnicalSpecifications",theattachedLicenseeEventReportLER87-002isherebysubmitted.~~Vtrulyyours,xc:U.S.NuclearRegulatoryCommissionRegionI631ParkAvenueKingofPrussia,PA19406GinnaUSNRCResidentInspectorRogerW.Kober
LER  87-002, Reactor Coolant System Oxygen Concentration Exceeds Technical Specification Limits Due to Personnel Error and Procedural Inadequacy R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System/
}}
Item (a)(2)(i)(B) which requires a report of "any operation prohibited by the plant Technical Specifications", the attached Licensee Event Report LER 87-002 is hereby submitted.
                                        ~ ~
V      truly yours, Roger  W. Kober xc:         U.S. Nuclear Regulatory Commission Region  I 631 Park Avenue King of Prussia, PA    19406 Ginna  USNRC  Resident Inspector}}

Latest revision as of 17:58, 29 October 2019

LER 87-002-00:on 870306,RCS Oxygen Analysis Indicated That Steady State Requirements of Tech Spec 3.1.6.2 Had Been Exceeded.Caused by Personnel Error & Procedural Inadequacy. Procedural Guidance Being developed.W/870405 Ltr
ML17261A450
Person / Time
Site: Ginna Constellation icon.png
Issue date: 04/05/1987
From: Filkins D, Kober R
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-87-002, LER-87-2, NUDOCS 8704130520
Download: ML17261A450 (9)


Text

REGULATORY FORMATION DISTR IBUTION SY M (R IDS)

ACCESSION NBR: 8704130520 DOC. DATE: 87/04/05 NOTARIZED: NO DOCKET 0 FACIL: 50-244 Robert Emmet Qinna Nuclear Plant> Unit 1> Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION FILKINSs D. L. -

Roch ester Qas 5 El ectr i c Corp.

KOBERi R. W. Rochester Gas Sc Electric Corp.

RECIP. NAME . RECIPIENT AFFILIATION

SUBJECT:

LER 87-002-00: on 87030&i RCS oxygen analysis indicated th "t steady state requirements ow Tech Spec 3. i. h. 2 had been exceeded. Caused by personnel error Zc procedural inadequacy.

Procedural guidance being developed. W/870405 ltr.

DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR ENCL SIZE:

TITLE: 50. 73 Licensee Event Report (LER) i Incident Rpt> etc.

NOTES: License Exp date in accordance with 10CFR2> 2. 109<9/19/72). 05000244 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 PD1-3 PD 1 '1 STAHLEi C 1 1 INTERNAL: ACRS MICHELSON 1 ACRS MOELLER 1 ACRS NYLIE 1 1 AEOD/DOA 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TAPB 1 1 NRR/ADT 1 1 NRR/DEST/ADE 1 0 NRR/DEST/ADS 1 0 NRR/DEST/CEB 1 NRR/DEST/ELB 1 1 NRR/DEST/ ICSB 1 NRR/DEST/MEB 1 1 NRR/DEST/MTB 1 1 NRR/DEBT/PSB 1 1 NRR/DEST/RSB 1-NRR/DEST/SQB 1 1 NRR/DLPG/HFB 1 1 NRR/DLPG/GAB 1 1 NRR/DOEA/EAB 1 NRR/DREP/EPB 1 1 NRR/DREP/RAB 1 1 i/PMAS RB 1 1 NRR/PMAS/PTSB 1 1 EQ 02 1 RES SPEISi T 1 1 RQN1 FILE 01 1 EXTERNAL: EQRQ QROH> M 5 5 H ST LOBBY NARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS J 1 1 NSIC MAYSi G 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 41 ENCL 39

HrIC Form $ OO U.S. NUCLEAR REOVLATORY COMMISSION 10421 AFFROU EO OMS HO. $ 190W10a KXFIRKS: Sn) ISS LICENSEE EVENT REPORT ILERI FACILITY NAME oocxtT IavMsth l21 Ginna Nuclear Power Plant o s o o,o 244 >o(:07 (Il'.E.

Reactor Coolant System Oxygen Concentration Exceeds Technical'pecification Limits Due- To Personnel Error and Procedural Inade a '.;.

EVENT OATS IS) Lth HUMSKR (I) RtFORT OATS (1) OTHER FACILIT)tt IHVOLYEO (SI YEAR aa0 v a rr a I AL rravraaarr OAY YEAR FACII,ITV H*MOS OOCXKT HVMSKRISI MONTH OAY YEAR y?g HVMOSR rrvMo ~ R MONTH p s 0 0 0 0 306 87 8 7 002 0 0 0 4 0 5 8 7 O 50 0 ()

ill THIS REFORT IS SUSMITTEO FURSUANT T O THE REOUlhtlatNTS OF 10 CFR $ r (Cooers orro rN moro oI rara Iotorerrrgl (11 OFSRATIHO MOOS (Sl 20.402(S I 20.a00(al SO,2 $4 I(2)I Iv) TS.TIW

~ OIYKR 20.OCS(a)(11(0 SOM(al (I ) SO.2 $ 4) (2)(el 2$ .7((a) p p p 20 a004)(ll(tl 90.$ 9( ~ )(2) 90.2241(21 (et) OTHKR Itooaloy M Aoroeat 1101 aaron arro Io I'aat, Nhc Fomr 20.409(a l(litt)I 90.2$ 4)al(0 SO.T $ 4)121(aOI) IAI $ SMI 20A00 4) ()el SO.T $ 41121( ~ I 90.2$ ( ~ I(21(rat)(S) 20.400(al (Illa) 90.22(a) 12)(SO 90.2$ la) 12) (a)

LICENSE t CONTACT FOR THIS Lth lit)

NAME TELKFHOHK NUMSER r

AREA COOK Duane L. Filkins, Manager, Health Physics and Chemistry 44 46 31 55 24 COMFLSTS ONK LINK I'OR EACH COMFOH KNT FAILURE OtSCRISKO IH THIS RtFORT l12)

SYS'EM MANUFAC EFORTASLE MAHVFAG KFORTASL CAUSE COMFOHKNT TUNER TO NFROS CAVSE SYSTEM COMFONENT TUNER TO HOROS

%VI R~%

A '

F SUFFLKMKNTALRtFORT tXFKCTtO I)al MONTH OAY YEAR.

EXFECT'EO SUSMISSION OATS IISI YES IllFar, oomo)eri EXPECTED SVSMI$$ ION OA TET HO AKKTRAcT(Lamia Io f400 a)racer. l.o. ooororarratery htrearr arroroeoeao ryarerrrrnNr lkroal (1 9)

During startup from a refueling outage on Marchindicated 6, 1987, at 0009 EST, a reactor coolant system (RCS) oxygen analysis that t:he steady state requirements of Technical Specification (TS) 3.1.6.2 had been exceeded. A review of the previous days analytical results indicated a-previous analysis on March 5, 1987, had indicated a similar result which violated the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> limiting condition for operation in TS 3.1.6.4. A reactor coolant system cooldown was initiated to lover system temperature the system.

and to allow addition of hydrazine to scavenge oxygen from The cause for exceeding the TS requirements was personnel error and procedural inadequacy. There was no procedural guidance in the operating procedures which correlates required chemistry sampling to RCS tempera-ture. The technician did not initially recognize that TS requirements had been exceeded.

To preclude recurrence better procedural based guidance is being developed and technician training will be performed on this LER.

There were no significant safety consequences of this incident.

870413052 0 87040>

~ HRC'Fern $ 90 (9021

~ ~ *~ . c ~

PgR S

AgoC'K 05000244 pgR wi

NAC Perer SSSA (9 891 U.S, NUCLEAA AEOULATOAYCOMMISSION LICENSEE EVENT REPORT (LERI TEXT CONTINUATION APPROVEO OMS NO. SI SOW(04 EX ~ INES: 8(SI(85 I'ACILITYNAME (ll OOCXET NUMSEI( (SI LEII NUMEEI( ISI ~ AOE (SI

.p)8 SSOUSNTIAL Prà eeyrSION R.E. Ginna Nuclear Power Plant YEAN NUM Trl rer rrUM ee o s o o o 244 7 002 0 2oF 07 TEXT (If rrrere Nrece Ir reeeeee, we cere(lre( Hr(C ferrrr JSSA Yl (Ill I. PRE-EVENT PLANT CONDITIONS On March 4, 1987, the unit was starting up from the annual refueling and maintenance outage. On this date the plant left the cold shutdown condition and heated up to approximately 315 F, 350 psig reactor coolant system (RCS) temperature and pressure, respectively, to perform steam generator (S/G) crevice cleaning per operating procedure .0-10. The TS requirements for RCS oxygen of less than 0.1 ppm had been achieved prior to increasing RCS temperature above 200oF.

II. DESCRIPTION OF EVENT A. EVENT On March 6, 1987, at 0009 EST with S/G crevice cleaning in progress, a RCS sample was taken as required by Attachment I of procedure PC-1. 1 (Primary System Analysis Schedule and Limits). This procedure outlines the required analysis and limits for RCS chemistry during hot shutdown and normal operation.

The result of the oxygen analysis of the above sample was 0.5 ppm. The plant technician performing the analysis recognized this result a6 a number greater than allowed by TS for the existing plant conditions. As is routine, a confirming sample was taken and an oxygen analysis performed at 0130 EST with the same result. A review of the plant technicians laboratory notebook revealed that on March 5, 1987 at 0030 EST, another sample and analysis had been performed which also indicated oxygen concentration in the RCS greater than 0.1 ppm.

The Ginna Station TS, Section 3.1.6.2, requires that corrective action be taken immediately when the normal steady state RCS concentration limit of 0.1 is exceeded. Also TS oxygen Section 3.1.6.4 requires that limits for RCS oxygen are exceeded -and cannot be returned to ifppm the normal steady state within the limits within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, the reactor shall be brought to the cold shutdown condition. Because, from 0030 EST on March 5, 1987, until 0235 EST on March 6, 1987, (a lapsed time of approximately 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />), the RCS oxygen concen-tration exceeded its normal steady state limit with no corrective action taken, both sections of TS, 3. 1. 6. 2 and 3.1.6.4 were exceeded.

B. INOPERABLE STRUCTURES, COMPONENTS OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:

None rr (9 81 I

NRC Fmw JTSA V.S. NVCLKAR RSOVLATORY COMMISSION l9 SJI LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APP ROY 5 0 0 MS NO, J I 50 &I di SXPIRTSS/JI/95 FACILITY NAMS Ill OOCKKT NVMJSR IJI LTR NVMJSR ISI ~ AOI IJI YSAR ~X, STCUTNTIAL: N ATY>SUN

.'i~F N MTTR NUM TR R.E. Ginna Nuclear Power Plant:

TTJT IIT race epoCP II leeAwd.

C.

Pae ~ NIIC fOne JTSAJI 0T) o o o o DATES AND APPROXIMATE TIMES FOR MAJOR OCCURRENCES:

o 4 4 87 002 0 03 ap07 o March 4, 1987, 0900 EST: Unit leaves cold shutdown, RCS

. oxygen concentration less than 0.1 ppm.

o March 5, 1987, 0030 EST: Event date.

o March 6, 1987, 0009 EST: Discovery date.

o March 6, 1987, 0130 EST: Confirmatory. sample taken.

o March 6, 1987, 0235 EST: Plant cooldown initiated.

N o March 6, 1987, 0800 EST: RCS average temperature less than 250oF.

o March 6, 1987, 1030 EST: RCS oxygen concentration within TS requirements.

D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:

None E. METHOD OF DISCOVERY:

The event was made apparent during the foreman's review of the plant technicians laboratory notebook.

F. OPERATOR ACTION:

The plant technician reported the event to the Control Room.

The Control Room operators initiated a plant cooldown per TS 0800 EST the requirements at 0235 EST on March 6, 1987. By At 0935 a RCS average temperature was less than 250 F.

hydrazine addition was made to the RCS which brought the oxygen concentration within TS requirements by 1030 EST.

SAFETY SYSTEM RESPONSES:

None k 'f7D lAell l95JI

NRC Sarra SSSA (9 85) U.S. NUCLEAR REOULAIORY COMMISSION LICENSEE EVENT REPORT ILER) TEXT CONTINUATION AP/rROV EO OMS NO. 5150&l0e EXelRES. 8/Sl/85 aACILITY NAME (II OOCKET NUMSER (ll LER NUMSER (SI eACE (sI SEQUENT/*L l),) IYIS 0 Nvv 8 I r/UMSKA R.E. Ginna Nuclear Power Plant

~ ~

244 7 0 2 0 0 04 pFO 7

/// mare e~EVENT o s o o o III. CAUSE T EXT eaece /e /rr/rerL eee AlRC /rarm 8(/SA'e/ I ITI Op A. IMMEDIATE CAUSE:

RCS oxygen concentration was greater than the normal steady state TS limit for more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> with no immediate corrective action taken. This was due partially to a cognitive error since the technician failed to recognize that the analytical results exceeded the TS requirements for the RCS temperature which existed at the time. It was also partially the result of a procedural inadequacy since there was no procedural guidance in the operating procedure which correlated required chemistry sampling to RCS temperature.

B. ROOT CAUSE:

The results of a root cause investigation determined that there were two maj or .root causes that contributed to the event. These are as follows:

The Health Physics and Chemistry section failed to recognize the RCS oxygen concentration was exceeding TS requirements for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. This occurred because of the following reasons and actions:

o The crevice cleaning operating procedure holds the RCS temperature between cold shutdown and hot shutdown for extended periods of time.

0 The plant chemistry procedure, PC-1.1, only provided a schedule for analysis for the following plant conditions:

a. Hot shutdown or normal operation, Attachment I
b. Cold shutdown, Attachment II
c. Refueling shutdown, Attachment III 0 On March 5, 1987, Attachment II was in use, which did not require a RCS oxygen analysis be taken. The technician who performed the oxygen analysis on this date had received a verbal request from another technician to run the RCS oxygen analysis with no apparent reason given. Since the analysis was not required, he did not, recognize the significance of the results.

NRC eORM 888*

t9 85 I

NRC lorna 844A I9 8SI V.S. NUCLEAR REOULATORY COMMISSION LICENSEE EVENT REPORT ILER) TEXT CONTINUATION ATPROYEO OM8 NO. SISOMI04 EXPIRES: 8ISII8$

tACILITYNAME III OOCKET NUMEER ISI LER NUMEER l4l TACE ISI R.E. Ginna Nuclear Power Plant YEAR,'8@ slQUENTIAL NUMttll gP..r ntvataon NUMttn o s o o o 2 4 8 7, 0 0 2 0'0' 5 QF 0 7.

TEXT lit moro Naoco *rotarooe'. ooo oOtrnrnaM HRC rranrn 848A'rI IITI 0 The analytical results for RCS chemistryare normally.

entered into the Primary System Chemistry Log and also on the Daily Chemistry Analysis Results Form which is forwarded to Operations daily. The chemistry results obtained on March 5, 1987, were not entered on either of these records. Supervisory reviewL of the chemistry log did not recognize the lack of results for March .5, 1987, until March 6, 1987, and Operations also did not recognize the lack of results for March 5, 1987. Although the review of these logs would not have precluded exceeding the requiremegts o f TS 3. 1. 6. 2, likely that corrective action would haye been taken it is prior to exceeding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> properly logged.

if the results had been

2. The unanticipated oxygen concentration increase in the RCS. This happened because of the following reasons and actions:

o The investigation of the cause of the oxygen increase in the RCS revealed that the step .in procedure 0-10 which requires burping of the volume control tank (VCT) with hydrogen had been marked non-applicable'(N/A); This is allowed- procedurally.

and Operations had been directed by the outage planning group to proceed with only a nitrogen overpressure on the VCT. This had been done in the 1985 and 1986 outages without oxygen excursions, so this was not without precedent. The reason for not introducing hydrogen is to allow a more rapid turnaround if system leaks should develop during performance of the primary system hydro. If the hydrogen concentration is increased in the RCS, operating procedures require removal prior to system drain down to preclude possible explosive mixtures in primary components. This is a time consuming process.

0 Without hydrogen to control oxygen, any source of oxygen would cause increases in the RCS oxygen concentration. Three sources that could have contributed to the oxygen ingress to the RCS were:

a. The volume control tank was not burped so any oxygen in the tank would have been allowed to come into equilibrium with the RCS.

a a'a I9 8SI

NRC iona $ 48A V.S, NUCLEAR REOVLATORY COMMISSION 19 881 LICENSEE EVENT REPORT {LER) TEXT CONTINUATION APPROVED OME NO. S($ 0&(08 EXPIRES: 8/SI/8$

PACILIEY NAME lll DOCKET'VMEER (EI LER NVMEER (81 YEAR @'80vENT/AL $a8) aov/Sion NVM oa R.E. Ginna Nuclear Power Plant NUMPEN ~

24487 00 0 6 ov 0 '7 SEXY /// naao NN(o /o ~, ooo o////oao/HRC AN/a 80848 I (11(

b.

o s o o o Normal introduction of reactor make-up water 0

would introduce oxygen into the RCS.

c ~ Some oxygen would have been formed by radiolysis of water while passing through the core.

IV. AN YSIS OF EVENT I

Thih event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, Item (a)(2)(i)(B), which requires reporting of "any operation prohibited by the plant's Technical Specifi-cations>> in that the plant was in a degraded mode avowed 'by the Technical Specifications for a period of time longer than that permitted by the Technical Specifications.

An assessment was performed of the safety consequences and impli-cations of the event with the following results and conclusions:

o The basis for control of oxygen in the RCS is to minimize general corrosion and to prevent localized stress corrosion in the presence of chloride and fluoride ions. During the period of time that the oxygen concentration was outside the operating band,.both the chloride and fluoride concentrations were well below the normal operating requirements.

o Since the oxygen concentrations never exceeded the TS transient limits (always 0.5 ppm or less) and the chloride and fluoride concentrations were within requirements, there would have been no anticipated degradation of RCS system components and, therefore, no safety consequences or implications from this event.

V. CORRECTIVE ACTION A. ACTIONS TAKEN TO RETURN THE RCS OXYGEN CONCENTRATION TO NORMAL STEADY STATE OPERATING VALUES:

o The RCS was cooled down to less than 250oF to allow the addition of hydrazine to scavenge the oxygen.

o Hydrazine'as added to the RCS and oxygen was brought within TS limits.

B. ACTIONS TAKEN OR PLANNED TO PREVENT RECURRENCE:

0 Corrective action currently in progress will provide better procedural guidance to assure the Health Physics and Chemistry section is aware when the RCS temperature-has been increased and chemistry requirements have changed.

nl Rail a (8 4$ 1

NIIC Pena 588A U.S. NUCLTAII IITOULATOIIYCOMMISSION 19 831 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPAOY8O OM8 NO. 31$ 0WI05 8XPIA85" 8ITI/8$

PACILITY NAM8 lll OOCK8T NUM88II LTI LKII NUM88II 181 PA48 151 YTAA j>pI 55QUCNTIAL &Ail eayl5%n R.E. Ginna Nuclear Power Plant- ,c,.? NUM 8 P4'UM Te o s o o o 24 487 002 0 07 DF07 TtxT III<<eea apace la>>aakaf, a>> aaAveavl ryilc Pane 888A81 Illl o The Health Physics and Chemistry technicians involved with primary system chemistry have all been made aware of the errors which contributed to the event.

o A copy of this LER will be forwarded to the Training section and will be .included in the training program for the Health Physics and Chemistry section.

VI. ADDITIONAL INFORMATION A. FAILED COMPONENTS:

There were no component failures that contribgted to this event.

B. PREVIOUS LERs ON SIMILAR EVENTS:

A similar LER event historical search was conducted with the foilowing results: no documentation of similar LER events could be identified.

N c 0 19 851

arl ~, r 5 r5 57 aN

.=? Cl"HEI E" .O E,'87,<Veau@ Ronl~B >w, A v. >va~g-oco>

a'C .5 April 5, 1987 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 30555

Subject:

LER 87-002, Reactor Coolant System Oxygen Concentration Exceeds Technical Specification Limits Due to Personnel Error and Procedural Inadequacy R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System/

Item (a)(2)(i)(B) which requires a report of "any operation prohibited by the plant Technical Specifications", the attached Licensee Event Report LER 87-002 is hereby submitted.

~ ~

V truly yours, Roger W. Kober xc: U.S. Nuclear Regulatory Commission Region I 631 Park Avenue King of Prussia, PA 19406 Ginna USNRC Resident Inspector