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 Start dateReporting criterionEvent description
05000311/LER-2017-00113 June 2017

On April 14, 2017 at 13:57 while attempting to transfer the 2C 4 Kilovolt (kV) vital bus from 24 Station Power Transformer (SPT) to 23 SPT, the 24 SPT infeed breaker opened properly but 23 SPT infeed breaker failed to close.

The 23 SPT infeed breaker failing to close as expected resulted in de-energization of the 2C 4kV vital bus and subsequent start and loading of the 2C Emergency Diesel Generator (EDG) to power the bus.

This report is being made in accordance with 10CFR50.73 (a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," for this event actuation of the 2C EDG.

Notification of this event was provided via ENS report 52681 NS'C, FORM 366 I04-20

  • 17:1
05000311/LER-2016-00631 August 2016
31 October 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation

At approximately 1500 hours on August 31, 2016, the 21 Reactor Coolant Pump (RCP) tripped resulting in an automatic reactor trip on low flow in one reactor coolant loop above the P-8 permissive (36% power permissive). As expected, the 21, 22 and 23 Auxiliary Feedwater (AFW) pumps started on low steam generator level following the unit trip. Unit 2 was stabilized in Mode 3 at normal operating temperature and pressure with the 22, 23 and 24 RCPs in-service.

The trip of the 21 RCP was caused by a Service Water (SW) leak that developed on the 22 Containment Fan Coil Unit (CFCU) motor cooler. The SW leaked on to the 21 RCP motor lead containment penetration and the motor leads in the termination box. This caused the A and C phase instantaneous overload relays to actuate causing the trip of the RCP and the subsequent reactor trip on low flow in one reactor coolant loop.

This report is being made in accordance with 10CFR50.73 (a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," for this event actuation of the Reactor Protection System (RPS) and the Auxiliary Feedwater System (AF).

05000311/LER-2016-00528 June 2016
29 August 2016

On 6/28/16 at 04:22 Salem Unit 2 automatically tripped from 100% power on Generator Protection. The reactor trip was initiated due to a Main Turbine (MT) trip caused by a Main Generator ProtectiOn signal.

All emergency core cooling systems and emergency safeguards feature systems functioned as expected.

The motor driven and steam driven auxiliary feedwater pumps started as expected on steam generator low level. Operators stabilized the plant in Mode 3 with decay heat removal via the main steam dump valves and auxiliary feedwater system.

Investigation identified that a broken current transformer core ground wire internal to the A Main Power Transformer (MPT) was intermittently touching the X1 and X2 low voltage connections inside the transformer bushing compartment causing a ground fault. This caused the turbine generator trip.

This report is being made in accordance with 10CFR50.73 (a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," for this event actuation of the Reactor Protection System (RPS) and the Auxiliary Feedwater System (AF).

05000311/LER-2016-004

On 2/16/16 at 0827 22 Steam Generator Feed Pump (SGFP) tripped while operators were transferring the steam supply to the pump from heating steam to main steam. Trip of 22 SGFP initiated emergency safeguard feature (ESF) actuation for start of the 21 and 22 Auxiliary Feedwater (AFW) Pumps. This event occurred during Unit 2 start-up following a unit trip from generator protection.

This report is being made in accordance with 10CFR50.73 (a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," for this event actuation of the Auxiliary Feedwater System. Notification of this event was provided via ENS report 51738.

TO EPIX

the Desk Officer, Office of Information and Regulatory Affairs, NEOB-1 0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

1. FACIUTY NAME 2. DOCKET 6. LER NUMBER 3. PAGE Salem Generating Station — Unit 2 05000311

PLANT AND SYSTEM IDENTIFICATION

Westinghouse-Pressurized Water Reactor (PWR/4) Feedwater / Digital Control System (SJ/DCC) *Energy Industry Identification System (EllS) codes and component function identifier codes appear as (SS/CCC).

IDENTIFICATION OF OCCURRENCE

Event Date: 02/16/2016 Discovery Date: 02/16/2016

CONDITIONS PRIOR TO OCCURRENCE

Salem Unit 2 was in Mode 2 (Startup) at 4 percent rated thermal power (RTP).

DESCRIPTION OF OCCURRRENCE

On 2/16/16 at 0827 22 Steam Generator Feed Pump (SGFP) tripped while operators were transferring the steam supply to the pump from heating steam to main steam. Trip of 22 SGFP initiated emergency safeguard feature (ESF) actuation for start of the 21 and 22 Auxiliary Feedwater (AFW) Pumps. This event occurred during Unit 2 start-up following a unit trip from generator protection.

The digital feedwater control system (DFCS) (SJ/DCC) indicated a trip on overspeed. Review of the Plant Computer and the Control Console did not indicate an overspeed trip.

SGFP speed lowered during the swap from heating steam to main steam. SGFP condensate flow momentarily decreased, causing an increase in steam demand to 22 SGFP. At 08:27:17 22 SGFP speed rapidly increased from 2170 to 2450 RPM. The sudden increase in SGFP speed appears to be coincident with opening of the poppet valve, allowing a sudden increase in steam supply to 22 SGFP. Data downloaded from the digital feedwater control system showed a 400 RPM speed increase occurred in 300 milliseconds with all three speed pick up relays indicating a overspeed rate change trip (SGFP acceleration rate trip). 22 SGFP speed slows from 2450 to feedwater control system. No other spikes in SGFP speed were observed in the digital feedwater control system, the Plant Computer or on the associated Control Console during this event.

the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

Salem Generating Station - Unit 2 05000311 The DFCS design change package (DCP) was implemented during the Fall 2015 refueling outage. The rate trip is a new trip added during the DFCS DCP. The SGFP acceleration rate trip is incorporated as standard protection as part of the DFCS speed detection module. The setting is currently at maximum value allowed by the module. This trip is anticipatory to an overspeed condition.

This report is being made in accordance with 10CFR50.73 (a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," for this event actuation of the Auxiliary Feedwater System. Notification of this event was provided via ENS report 51738.

CAUSE OF EVENT

The 22 SGFP trip was a rate trip (-400 RPM increase in 300milliseconds) caused when the main steam poppet valve opened. A root cause evaluation was conducted for this event.

The evaluation determined that one root cause was that the specification agreed upon by PSEG and the DFCS vendor did not identify the acceleration rate trip that was incorporated into the digital feed modification. An independent Critical Digital Review (CDR) was performed by an experienced independent vendor. The CDR did not identify the installation of the trip. The vendor was involved in the process throughout the entire lifecycle, from requirements definition to factory acceptance testing. The design requirements/specifications as defined by PSEG for the implementation of the modification did not identify the acceleration rate trip. The DFCS vendor was contacted and requested to validate that the acceleration rate trip was not discussed in the Functional requirements document.

The response to the inquiry was 'The Trip on acceleration is NOT required; therefore it is not contained in the Functional Requirements Document" The trip function was installed without knowledge by engineering and the vendor had documentation identifying function/trip did exist, but did not specifically communicate the existence or functionality of the specific trip function. The acceleration rate trip will be removed from the system in accordance with the design change process.

A second root cause identified was that the instructions for swapping from low pressure steam to high pressure steam provided in the procedure utilized did not include a conservative description/method for implementing a change in steam supply source to minimize speed perturbation. A review of data collected from the event was performed. The speed and demand signals specific to this event indicated a delta from previous start ups and a speed perturbation was experienced. The feed pump operation was performed within the requirements of the procedure and the review performed by this evaluation indicates that this was not the conservative method to operate/perform the transition from heating steam (HS) to main steam (MS).

Additional guidance is required to prevent further speed perturbations.

the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the Information collection.

Salem Generating Station — Unit 2 05000311

SAFETY CONSEQUENCES AND IMPLICATIONS

There were no safety consequences as a result of this event.

The operating crew responded correctly to the event. The applicable abnormal operating procedure was properly entered and documentation met expectations.

The DFCS and the AFW systems operated as designed. There were no nuclear safety implications associated with this event.

SAFETY SYSTEM FUNCTIONAL FAILURE

This condition did not result a safety system functional failure as defined in NEI 99-02, Regulatory Assessment Performance Indicator Guidelines.

PREVIOUS EVENTS

A review of the previous three years identified no similar events:

CORRECTIVE ACTIONS

  • Revise the Material, Equipment and Service Specification governing procedure to require any exceptions or additional features from PSEG detailed specifications be identified by supplier in writing and evaluated by PSEG to determine suitability for use.
  • Revise procedure for swapping the SGFPs from low pressure steam to high pressure steam to include guidance for conservative operation during swap from Heating Steam to Main Steam of the SGFP.

COMMITMENTS

There are no regulatory commitments contained in this LER.

05000311/LER-2016-00314 February 2016
14 April 2016

On 2/14/16 at 20:58 Salem Unit 2 automatically tripped from 100% power on Generator Protection.

The trip was initiated due to a Main Turbine trip caused by a Main Generator Protection signal. All emergency core cooling systems and emergency safeguards feature systems functioned as expected. The motor driven and steam driven auxiliary feed pumps started as expected on steam generator low level. Operators stabilized the plant in Mode 3 with decay heat removal via the main steam dump valves and auxiliary feed water system. Condenser vacuum remained available for the duration of the event. Operators also ensured a normal offsite electrical power lineup. Investigation identified a Stator Water Cooling valve leak dripping onto a relay, shorting the relay wiring terminations. This caused the turbine generator trip.

This report is being made in accordance with 10CFR50.73 (a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," for this event actuation of the Reactor Protection System and the Auxiliary Feedwater System.

05000311/LER-2016-0024 February 2016
7 September 2017
10 CFR 50.73(a)(2)(iv)(A), System Actuation

On 2/4/16 at 11:21, Salem Unit 2 automatically tripped from approximately 74% power. Power had been reduced at the beginning of dayshift to support a 500 KV transmission line outage. The reactor trip was due to a Main Turbine trip caused by a Main Generator Protection signal initiated by a main generator automatic voltage regulator (AVR) volts/hertz over excitation protection relay. All emergency core cooling systems and emergency safeguards feature systems functioned as expected. As found calibration data for the generator protection logic relay were found out of specification low. An evaluation determined the cause of the generator protection relay trip was poor manufacturing quality and/or shipping damage to an adjusting rheostat.

This report is being made in accordance with 10 CFR 50.73 (aX2Xiv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," specifically automatic actuation of the Reactor Protection System and the Auxiliary Feedwater System for this event.

05000311/LER-2016-00120 April 2015
21 March 2016

On January 19, 2016, while reviewing outage data, plant staff recognized that anomalous data collected in October 2015, for the 21 Auxiliary Feed Pump time response loop resulted in failure to meet a surveillance, rendering that channel of Auxiliary Feedwater automatic actuation inoperable. In November 2015, the isolation valve for the pressure override defeat pressure transmitter was found closed. The pressure transmitter provides an input into the 21 AFW Pump run-out protection circuit. With the isolation valve closed, it would take longer to sense pump discharge head and consequently the opening of the auxiliary feed pump flow control valves would be slower than normal. This condition resulted in 21 Auxiliary Feedwater Pump loop time response greater than Technical Specification (TS) acceptance criteria. The failed channel was not recognized and the TS action was not taken, resulting in a condition prohibited by TS. The investigation revealed that the condition most likely existed since April 20, 2015, when maintenance activities were performed on the auxiliary feedwater pump discharge pressure transmitter. The isolation valve was opened and the surveillance was performed satisfactorily.

This report is being made in accordance with 10CFR50.73 (a)(2)(i)(B), "Any operation or condition which was prohibited by the plant's Technical Specifications.

05000311/LER-2015-00323 November 2015
22 January 2016
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

At 2136 on November 23, 2015, the Boron Injection Tank (BIT) relief valve 2SJ10 exhibited increased seat leakage during the performance of troubleshooting to determine the cause of low BIT pressure. The increased seat leakage from 2SJ10 initiated a Reactor Coolant System (RCS) leak greater than 10 gallons per minute (gpm). Technical Specification (TS) 3.4.7.2.b action b was entered for RCS unidentified leakage greater than 1 gpm.

The BIT was isolated at 2137 and the leakage was stopped. Isolation of the BIT resulted in loss of the high head safety injection flow path for both trains of high head safety injection, requiring entry into TS 3.0.3.

This event was caused by ineffective use of internal operating experience in the decision making process to reuse the 2CV141, which had been installed on the discharge of the 23 positive displacement charging pump, as a suitable replacement for the 2SJ10 during 2R21.

This report is being made in accordance with 10CFR50.73 (a)(2)(v)(D) "Any event or condition that could have prevented the fulfillment of the safety functions of structures or systems that are needed to mitigate the consequences of an accident"

05000311/LER-2015-0025 August 2015
7 September 2017
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(iv), System Actuation

On 8/05/15, at 1539, Salem Unit 2 experienced an automatic reactor trip. The cause of the reactor trip was due to a trip of the 21 Reactor Coolant Pump (RCP) causing a 21 Reactor Coolant Loop low flow condition.

The 21 RCP breaker tripped as designed when the 2B Auxiliary Power Transformer (APT) infeed breaker to the 2H 4 kilovolt (kV) Non-Vital Bus opened. The root cause evaluation did not identify a definitive cause.

However the most probable cause of the 2H 4 kV Non-Vital Bus trip was due to a ground fault on the 21 Heater Drain Pump (HDP) motor that was not isolated by its associated neutral overcurrent relay. An automatic start of the Auxiliary Feedwater (AFW) system occurred as expected following the reactor trip due to low steam generator water levels.

Corrective actions include replacement of the 21 HDP motor and its neutral overcurrent relay.

This event is reportable under 10 CFR 50.73 (a)(2)(iv)(A) as an event that resulted in an automatic actuation of the reactor protection system and actuation of the AFW system.

05000311/LER-2015-00120 January 2015

On 1/20/15, a step change occurred on the high differential band indicator of the Axial Flux Difference recorder. Subsequent troubleshooting of the recorder on 1/26/15 identified a failed isolator that provides input to Channel 4 of Overtemperature Delta -T logic circuitry. This failure rendered Channel 4 of the Overtemperature Delta-T protection circuit inoperable for a period of approximately five and a half days without being placed in a tripped condition. The isolator was replaced and the Overtemperature Delta-T Channel was returned to service.

This report is made in accordance with 10 CFR 50.73 (a)(2)(i)(B), "Any operation or condition which was prohibited by the plant's Technical Specifications...

05000311/LER-2012-00110 CFR 50.73(a)(2)(iv)(A), System Actuation

On March 23, 2012, at approximately 1428 hrs. Salem Unit 2 experienced an automatic reactor trip due to a turbine trip. The cause of the turbine trip was the spurious, simultaneous spiking of all three 103% overspeed inputs to the turbine Digital Electro Hydraulic Controller.

At the time of the trip, the 22 Station Power Transformer was tagged out of service for maintenance.

Upon unit trip and non-vital bus transfer from the Auxiliary to the Station Power Transformers, power to the F and G group buses was lost due to unavailability of the 22 Station Power Transformer. The 23 and 24 Reactor Coolant Pumps tripped as a result of the F and G busses being de-energized.

This report is being made in accordance with 10CFR 50.73(a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)...

05000311/LER-2011-005

This report is being made in accordance with 10CFR50.73 (a)(2)(i)(A) "The completion of any nuclear plant shutdown required by the plant's Technical Specification.

At 2038 on July 14, 2011, during the performance of the Salem Unit 2 Emergency Core Cooling System (ECCS) fill and vent monthly surveillance test, a leakage path was identified from the Boron Injection Tank (BIT) relief valve 2SJ10 piping. Investigation determined that the leakage was approximately 15 gpm due to lifting of the 2SJ10 relief valve. Upon closure of the BIT inlet valve 2SJ4 to isolate the flow through the relief valve, a through wall socket weld crack developed on the 2SJ10 relief valve inlet piping. The BIT is part of the flow path of the high head safety injection system. Without the high head safety injection flow path operable, Technical Specification (TS) 3.0.3 was entered.

The 2SJ10 relief valve lifting was the result of missed opportunities to correct a component design application deficiency. The socket weld cracking was determined by laboratory analysis to be caused by a combination of fatigue and transgranular stress corrosion cracking. The affected 2SJ10 piping has been replaced with a new straight run of pipe and the relief valve internals were replaced. Design changes will be performed to resolve 1/2SJ10 operating margin, eliminate unnecessary non-isolatable socket welds in the BIT system and replace the remaining non-isolatable socket welds in the BIT system with low carbon weld filler and install a stiffener on the 2SJ10 relief valve piping.

Salem Generating Station Unit 2 05000311

05000311/LER-2011-00310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

This report is being made in accordance with 10CFR50.73(a)(2)(i)(B), "any operation or condition which was prohibited by the plant's Technical Specifications." At approximately 0100 hours on April 8, 2011, a test of the Unit 2 Fuel Handling Building Ventilation System (FHV) was performed following the replacement of the high efficiency particulate air (HEPA) filter on the 21 FHV filtration train. The fuel handling building exhaust flow was measured at 24,627 cfm with the 21 FHV filtration train in service. Technical Specification (TS) 4.9.12.c requires a system flow rate of 19,490 cfm +/- 10% during system operation. Movement of irradiated fuel in the Fuel Handling Building (FHB) is to be suspended in accordance with TS 3.9.12 Action 'a' when the FHB ventilation system is inoperable. The measured flow rate was approximately 26% above the TS flow rate of 19,490 cfm. On April 5, 2011, irradiated fuel was moved in the Unit 2 FHB with the air flow rate exceeding the requirements of TS 3.9.12.

The cause of the high air flow rate in the Unit 2 FHB is attributed to the air supply balancing damper being out of position; the air pressure regulator on the FHB roll up door was incorrectly set not allowing the door seal to inflate and the FHB exhaust fan inlet guide vanes operating in a degraded condition. Corrective actions consisted of setting the supply damper in the correct position, restoring the FHB roll up door air regulator to the proper setting, repairing the FHB exhaust fans, and revising the procedure for control of fuel movement in the fuel handling building.

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Salem Generating Station Unit 2 05000311

05000311/LER-2011-00210 CFR 50.73(a)(2)(iv)(A), System Actuation

This report is being made in accordance with 10CFR50.73 (a)(2)(i)(B), "any operation or condition which was prohibited by the plant's Technical Specifications...

On April 11, 2011, at 11: 51 control room personnel entered TS 3.4.10.3 Act b to support testing of the Pressurizer Overpressure Protection System (POPS) channel 1 (2PR1) in accordance with procedure S2.OP- ST.PZR-0003 "Inservice Testing Pressurizer and Reactor Head Vent Valves." When the 2PR1 valve was demanded to open as the test key switch was turned to the test position, the channel 1 test light illuminated, but the valve did not respond as expected. 2PR1 was restored to its pretest position; however, 2PR1 remained inoperable and OFF. Following satisfactorily testing of 2PR2, control room personnel attempted to open 2PR1 from normal control room bezel, but 2PR1 failed to open again. At this point it was determined that 2PR1 had been inoperable since the entry into Mode 5 on April 10 at 02:21, and that Salem Unit 2 had operated in a condition prohibited by Technical Specifications. The troubleshooting and the as-found condition of the valve plug OD & cage ID confirmed that foreign material was the most likely cause of the failure of the valve to open upon initial demand. A new trim set was installed into the valve, and the valve was tested satisfactorily.

Salem Generating Station Unit 2 05000311

05000311/LER-2011-001

This report is being made in accordance with 10CFR50.73 (a)(2)(i)(B), "any operation ... prohibited by the plant's Technical Specification" for the containment integrity function of valve 21SW122 being inoperable for greater than one-hour, contrary to the requirements of TS 3.6.1.1. On May 17, 2010 at 0116 hours, while performing a high flow flush of the No. 21 Component Cooling Heat Exchanger (CCHX), the required Service Water (SW) flow range of 9000-10000 gpm could not be achieved. Technical Specification Action Statement (TSAS) 3.7.3 was entered.

Containment integrity was not at issue as the 21SW122 valve appeared to have stroked closed. A team established to investigate the CCHX low SW flow issue determined that the 21SW122 valve was not controlling flow. The valve was declared inoperable on May 17 at 1005 hours and Containment Integrity TSAS 3.6.1.1 was entered. The No. 21 CCHX was isolated on May 17 at 1053 hours and TSAS 3.6.1.1 was exited.

Troubleshooting activities identified that the shaft of the No. 21 CCHX inlet air operated valve 21SW122 had corroded to the point of complete severing at the stem to body interface. The valve stem was replaced and the valve returned to OPERABLE status on May 18, 2010. A past operability evaluation was completed on May 28, 2010. This evaluation concluded that the valve was INOPERABLE for the closed (Containment Integrity) direction. On February 16, 2011, during an NRC inspection of the 21SW122 repair and extent of condition reviews, it was discovered that the 21SW122 being inoperable greater than the TS allowed action time had not been reported in accordance with 10CFR50.73 (a)(2)(i)(B). The cause of the 21SW122 valve shaft failure was severe localized microbiologically influenced corrosion attack. Actions taken included replacement of all SW122 valve stems, identification of susceptible valves, procedure revisions and preventive maintenance task changes to remove the shaft for inspection.

05000311/LER-2010-002

On January 21, 2010, at 1818 hours, the 21 Steam Generator Feedwater Pump (SGFP) tripped. A turbine .

runback automatically initiated as expected and steam generator level in all four Steam Generators (SG) continued to lower. The 22 SG reached the SG low level reactor trip setpoint at 1820 hours resulting in an automatic reactor trip. All control rods fully inserted on the trip. All three Auxiliary Feedwater (AFW) pumps started in response to the low SG water level and decay heat was removed by the steam dumps to the main condenser. Operators entered the emergency procedures for the plant trip and stabilized the plant in Mode 3 (HOT STANDBY).

The cause of the 21 SGFP trip was an internal wiring short in the SGFP trip control circuit that resulted in a false low suction pressure trip signal. The cause for the wiring short was the result of poor work practices. The reactor tripped on low water level in the 22 SG as designed. Corrective actions consist of lug inspections, document changes, training analysis, and evaluation of the integrated plant response to a SGFP trip from full power and implementing changes as appropriate.

This report is made in accordance with 10CFR50.73 (a)(2)(iv)(A), "any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B).

05000311/LER-2004-0032 January 200410 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

On April 12, 2004, at approximately 10:33, the Control Room Emergency Air Conditioning System was placed in a condition where it did not comply with its design basis for post LOCA mitigation. During maintenance of the Salem Unit 1 Solid State Protection System, a safety injection signal was generated.

As a result of the invalid safety injection signal on Unit 1, the Control Room Emergency Air Conditioning System actuated to its accident pressurized mode alignment, in which the Salem Unit 1 emergency intake air dampers were isolated and the Salem Unit 2 dampers opened. In this configuration, Salem Unit 2 was in a condition where it did not comply with its design basis for post LOCA mitigation. The Salem dose analysis performed to meet the requirements of the General Design Criterion (GDC) 19 states that with only one train of the Control Room Emergency Air Conditioning System available at the start of a design basis LOCA, the make up air supply to pressurize the control room envelope must be supplied by the non accident Unit's emergency outside air intake. The apparent cause of this event was a defective universal logic card in the Solid State Protection System (SSPS). When this card was moved from one position to another in the SSPS cabinet, a safety injection signal from Unit 1 Train 'B' occurred. Corrective actions taken were: (1) The defective card was replaced, and (2) A full functional test procedure on Train B was performed satisfactory. This condition is reportable under 10 CFR 50.73(a)(2)(v)(D).

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (1.2001r� 1 DOCKET (2)FACILITY NAME (1) LER NUMBER 6) PAGE (3)

05000311/LER-1990-03024 July 1990
05000311/LER-1990-02717 July 1990
05000311/LER-1990-0269 July 1990
05000311/LER-1984-010, Corrected LER 84-010-00:on 840423,during Startup Operations, Turbine Trip & Reactor Trip Occurred.Caused by hi-hi Level in Steam Generator 23.Feedwater Flow Nozzle Replaced & All Sys Performed as Designed23 May 1984
05000311/LER-1983-083, Forwards Supplemental LER 83-083/03X-1.Detailed Event Analysis Encl26 April 1983
05000311/LER-1983-023, Corrected LER 83-023/03L-0:on 830117-0418,seven Containment Isolation Valves Experienced Leakage Rates Greater than Max Range of Test Equipment.Total Containment Type B & C Leakage Could Not Be Demonstrated.Valves Repaired8 June 1983
05000311/LER-1983-017, Supplemental LER 83-017/03X-1:on 810515,during Startup & Cycle 1 Operations,Leakage Past Pressurizer PORVs & Pressurizer Overpressure Protection Sys Values Observed. Cause Not Stated.Porvs Modified16 September 1983
05000311/LER-1983-015, Forwards LER 83-015/03L-0.Detailed Event Analysis Encl5 May 1983
05000311/LER-1983-013, Forwards LER 83-013/03L-0.Detailed Event Analysis Encl6 May 1983
05000311/LER-1983-012, Forwards LER 83-012/03L-0.Detailed Event Analysis Encl28 April 1983
05000311/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analysis Encl29 April 1983
05000311/LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl4 March 1983
05000311/LER-1983-009, Forwards LER 83-009/03L-0.Detailed Event Analysis Encl4 March 1983
05000311/LER-1983-008, Forwards LER 83-008/99X-0.Detailed Event Anaysis Encl24 February 1983
05000311/LER-1983-007, Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days18 February 1983
05000311/LER-1983-004, Forwards LER 83-004/04L-0.Detailed Event Analysis Encl13 April 1983
05000311/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl9 February 1983
05000311/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Encl6 April 1983
05000311/LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Encl27 January 1983
05000311/LER-1982-153, Forwards LER 82-153/03L-0.Detailed Event Analysis Encl3 January 1983
05000311/LER-1982-152, Forwards LER 82-152/03L-0.Detailed Event Analysis Encl5 January 1983
05000311/LER-1982-150, Forwards LER 82-150/03L-0.Detailed Event Analysis Encl30 December 1982
05000311/LER-1982-148, Forwards LER 82-148/03L-0.Detailed Event Analysis Encl30 December 1982
05000311/LER-1982-147, Forwards LER 82-147/03L-0.Detailed Event Analysis Encl22 December 1982
05000311/LER-1982-146, Forwards LER 82-146/03L-0.Detailed Event Analysis Encl30 December 1982
05000311/LER-1982-145, Forwards Corrected LER 82-145/03X-1.Detailed Event Analysis Encl11 January 1983
05000311/LER-1982-144, Forwards LER 82-144/03L-0.Detailed Event Analysis Encl15 December 1982
05000311/LER-1982-143, Forwards LER 82-143/03L-0.Detailed Event Analysis Encl8 December 1982
05000311/LER-1982-142, Forwards LER 82-142/03L-0.Detailed Event Analysis Encl8 December 1982
05000311/LER-1982-141, Updated LER 82-141/03X-1:on 821121 & 1204,P-250 Computer Inoperable Due to Parity Error.Caused by Periodic Increases in Ambient Temp Due to Insufficient Ventilation.Computer Reprogrammed & Action Statement Terminated16 December 1983
05000311/LER-1982-140, Forwards LER 82-140/03L-0.Detailed Event Analysis Encl15 December 1982
05000311/LER-1982-139, Forwards LER 82-139/03L-0.Detailed Event Analysis Encl8 December 1982
05000311/LER-1982-138, Forwards LER 82-138/03L-0.Detailed Event Analysis Encl8 December 1982