ML20214N215

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SALP Rept 50-334/85-98 for 851001-870315
ML20214N215
Person / Time
Site: Beaver Valley
Issue date: 05/20/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20214N201 List:
References
50-334-85-98, NUDOCS 8706020101
Download: ML20214N215 (56)


See also: IR 05000334/1985098

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ENCLOSURE 1

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

REPORT 50-334/85-98

DUQUESNE LIGHT COMPANY

BEAVER VALLEY POWER STATION, UNIT 1

ASSESSMENT PERIOD: OCTOBER 1, 1985 - MARCH 15, 1987

BOARD MEETING DATES: APRIL 23-24, 1987

?DR * 870520

0 U$000K05000334

PDR.

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TABLE OF CONTENTS

P,a!Le

I. INTRODUCTION......................................................... 1

A. Purpose and 0verview............................................ 1

B. SALP Board and Attendees........................................ 1

II. CRITERIA............................................. ............... -2

III. SUMMARY OF RESULTS................................................... 4

A. Overall Summary................................................. 3

B. Background...................................................... 3

C. Facili ty. Performance Analysis Summary. . . . . . . . . . . . . . . . . . . . . . . . . . . 6

D. Plant Shutdowns and Trips................... ................... 7

IV. PERFORMANCE ANALYSIS................................................. 8

A. Plant 0perations................................................ 8

B. '

Radiological Controls........................................... 11

C. Maintenance..................................................... 15

D. Surveillance.................................................... 18

E. Fire Protection and Housekeeping................................ 22

F. Emergency Preparedness.......................................... 25

G. Security and Safeguards......................................... 27

H. Refueling and Outage Management................................. 30

I. Licensing Activities............................................ 33

J. Training and Qualification Effectiveness........................ 35

K. Engineering Support............................................. 37

L. Assurance of Quality............................................ 39

V. SUPPORTING DATA AND SUMMARIES........................................ 42

A. Investigation and Allegation Review............................. 4E

B. Escalated Enforcement Action.................................... 42

C. Licensee Conferences Held During Appraisal Period............... 42

D. Confirmatory Action Letters..................................... 42

E. Review of Licensee Event Reports (LERs)......................... 42

F. Licensing Activities............................................ 43

TABLES

Table 1 - Inspection Report Activities

Table 2 - Inspection Hours Summary

Table 3 - Enforcement Activities

! Table 4 - Tabular _ Listing of LERs by Functional Area

Table 5 - LER Summary

ATTACHfiENT

Attachment 1 - Total Number of Shutdowns and Trir,s Per Year Since Startup

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I. INTRODUCTION

A. Purpose and Overview

The Systematic Assessment of Licensee Performance (SALP) is an integrated

NRC staff effort to collect the-available observations and data on a

periodic basis and to evaluate licensee performance based upon this in-

formation. The SALP program is supplemental to normal regulatory pro-

cesses used to ensure compliance with NRC rules and regulations. The

SALP program is intended to be sufficiently diagnostic to provide a

rational basis for allocating NRC resources and to provide meaningful

guidance to the licensee management to promote quality and safety of

plant operation.

An NRC SALP Board, composed of the staff members listed below, met on

April 23, 1987, to review the collection of performance observations and

data to assess the licensee performance in accoroance with the guidance

in NRC Manual Chapter 0516, " Systematic Assessment of Licensee Perform-

ance". A summary of the guidance and-evaluation criteria is provided

in Section II of this report.

This report is the SALP Board's assessment of the licensee's safety per-

formance at Beaver Valley Power Station, Unit 1 for the period October

1, 1985 through March 15, 1987.

B. SALP Board and Attendees

Chairman

W. Kane, Director, Division of Reactor Projects (DRP)

Members

W. Johnston, Director, Division of Reactor Safety (DRS)

S. Collins, Deputy Director, DRP (Part Time)

L. Bettenhausen, Deputy Director, DRS (Part Time)

J. Stolz, Director, Directorate I-4, NRR (Part Time)

E. Wenzinger, Chief, Projects Branch No. 3, DRP

M. Shanbaky, Acting Chief, Emergency Preparedness and Radir b g cal

Protection Branch, Division of Radiation Safety and Safeg.rards (DRSS)

(Part Time)

L. Tripp, Chief, Reactor Projects Section 3A, DRP

P. Tam, Licensing Project Manager, NRR (Part Time)

W. Troskoski, Senior Resident Inspector

Other Attendees (non-voting)

J. Beall, Senior Resident Inspector, Beaver Valley Unit 2

S. Pindale, Resident Inspector, Beaver Valley Unit 1 (Part Time)

W. Lazarus, Chief, Emergency Preparedness Section, DRSS (Part Time)

G. Smith, Safeguards Specialist, QRSS (Part Time)

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Beaver Valley Unit 1 2

II. CRITERIA

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Licensee performance is assessed in-selected functional areas, depending on

whether the facility is in a construction, preoperational or operating phase.

Each functional area normally represents areas significant to nuclear safety

and the environment, and are normal programmatic areas. Special areas may

be added to highlight significant observations.

One or more of the following evaluation criteria were used to assess each

functional area.

1. Management involvement and control in assuring quality.

2. Approach to resolution of technical issues from a safety standpoint.

3. Responsiveness to NRC initiatives.

4. Enforcement history.

5. Operational events (including response to, analysis of, and corrective

actions for).

6. Staffing (including management).

Based upon the SALP Board assessment, each functional area evaluated is clas-

sified into one of three performance categories. The definitions of these

performance categories are:

Category 1. Licensee management attention and involvement are aggressive and

oriented toward nuclear safety; licensee resources are ample and effectively

used so that a high level of performance with respect to operational safety

is being achieved. Reduced NRC attention may be appropriate.

Category 2. Licensee management attention and involvement are evident and

are concerned with nuclear safety; licensee resources are adequate and rea-

sonably effective so that satisfactory performance with respect to operational

safety is being achieved. NRC attention should be maintained at normal levels.

Category 3. Licensee management attention or involvement is acceptable and

considers nuclear safety, but weaknesses are evident; licensee resources ap-

peer to be strained or not effectively used so that minimally satisfactory

performance with respect to operational safety is being achieved. Both NRC

and licensee attention should be increased.

The SALP Board may have determined to include an appraisal of the performance

trend of a functional area. Normally, this performance trend is only used

where both a definite trend of performance is discernible to the Board and

the Board believes that continuation of the trend may result in a change of

performance level. Improving (declining) trend is defined as: Licensee per-

formance was determined to be improving (declining) near the close of the

assessment period.

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III. SU R RY'AND RESULTS

A. -Overall Summary

As with all facilities in the status of Beaver Valley 1 and 2, the main

focus of management attention has been on the unit in the final stages

of construction and preoperational testing. Despite the drain on licen-

see resources, good performance was generally maintained for the operat-

ing unit. Of particular significance was the small number of personnel

errors which demonstrated good attitudes and proper attention to detail

by workers and first line supervisors. Continued strong performance was

observed in the. Security and Emergency. Preparedness functional areas with-

some improvements noted in recovery from refueling outages.

This assessment noted lingering problems with components such as feedwater

control valves, the inverter for Vital Bus No. 3, and balance of' plant

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equipment which had'not previously received appropriate corporate man-

agement attention and engineering support. By the end of the. assessment

period, more comprehensive actions appeared to be planned in each of.

these cases. It was concluded that although the quality assurance pro-

gram was in compliance with regulatory requirements, it was not being

effecti.vely.used as a management tool to identify potential problems be-

fore they occur, improve overall performance, and provide added assurance

that-quality is being achieved. Significant slippage was noted in the

licensing area; it appeared to be due to reassignment of key personnel

to Unit 2 startup activities and decreased licensee attention to this

activity for Unit 1.

B. Background l

1. Licensee Activities

This assessment period started with Beaver Valley Unit 1 operating

mid-way through the fifth fuel cycle. From October 1, 1985, until

the start of the Fifth Refueling Outage on May 16, 1986, the station

operated at power except for three reactor trips, one manual shut-

down and five instances of power reductions or holds due to equip-

ment problems. Two of the reactor trips (October 4, 1985 and

February 10, 1986) involved the failure of Vital Bus III which

caused a malfunction in the feedwater control system that led to

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a steam generator level trip. The third reactor trip occurred on

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October 25, 1985, during performance of a reactor protection system

(RPS) instrumentation surveillance test and was due to a combination

of procedure deficiency and technician error. The manual reactor

shutdown of November 1,1985, and all power reductions or holds were

! due to balance of plant feedwater component problems; most notably

i the feedwater control .alves.

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Beaver Valley Unit 1 4

The Fifth Refueling Outage lasted about 14 weeks and included major

maintenance, modification and test activities such as: reactor

vessel 10 year in-service inspection (ISI), containment integrated

leak rate test (CILRT), steam generator tube inspection and plugging,

main turbine maintenance, snubber and valve testing. Refueling

activities confirmed the first instance of fuel damage at BV-1 due

to baffle jetting (6 fuel rods in one assembly). A spare assembly

was reconstituted with seven stainless steel rods and placed m the

damaged assembly's location as an interim fix. Results of the

multi-frequency eddy-current testing identified the existence of

steam generator cold leg tube thinning. About 50 tubes were

hydraulically expanded against the lower support plates as a joint

experiment with Westinghouse, the NSSS vendor, in an attempt to

arrest the thinning phenomena.

Plant startup from the outage was delayed several days as the reac-

tor coolant system (RCS) had to be cooled down from Mode 3 due to

a leaking pressurizer safety valve flange and to effect an emergency

modification to the containment hydrogen recombiner (HR) system.

The HR blowers had been replaced during the outage with new envi-

ronmentally upgraded models that did not have the reserve capacity

to overcome line resistances offered by the swing check valves.

Additional manual valves were installed outside containment to pro-

vide equivalent protection.

From the Fifth Refueling Outage startup through the end of this

assessment period, the station experienced four additional trips.

The first occurred with the plant in Mode 2 during initial startup

after a failure in the rod control system dropped four rod cluster

control assemblies (RCCAs) and operators manually tripped the reac-

tor in accordance with emergency procedures. The other three trips

occurred from full power and were due to: an instrument technician

error and procedure human factors deficiency during performance of

a reactor trip breaker (RTB) surveillance test on September 3, 1986;

operator error and procedure deficiency during performance of a

turbine pedestal test on January 11, 1987; and, a malfunction in

the turbine overspeed control system due to random component failure

on February 7, 1987. The plant was also manually shut down two

other times and power reduced to 25% for feedwater system problems

that included feedwater control valve (FCV) repair and rewelding

of 3/4" vent and drain lines adjacent to the high vibration area

of the FCVs.

During the last several months of this period, the station was in

the final stages of preparation for integrating operation of Units

1 and 2. Major activities included plans for expanding the site's

security boundaries, removing the walls separating the two control

rooms and integrating the various support groups.

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Beaver Valley Unit 1 5

2. Inspection Activities

One NRC senior resident inspector was assigned to Beaver Valley

Power Station, Unit 1 for the entire assessment period and a resi-

dent inspector (trainee) was assigned for 12 months. The total NRC

inspection effort for the period was 3445 hours0.0399 days <br />0.957 hours <br />0.0057 weeks <br />0.00131 months <br /> (2362 annualized

resident and region-based) with a distribution in the various func-

tional areas as shown in Table 2.

An NRC Emergency Preparedness Inspection Team observed the annual

emergency exercise on November 20, 1986, in which Region I partici-

pated.

Other NRC team inspections were conducted for Equipment Qualifica-

tion, 10 CFR Part 50 Appendix R, Fire Protection, actions relative

to the Salem ATWS generic requirements (NRC Generic Letter 83-28)

and added coverage of the station's Fifth Refueling Outage recovery.

This report also discusses " Training and Qualification Effectiveness"

and " Assurance of Quality" as separate functional areas. Although

these topics, in themselves, are assessed in the other functional

areas through their use as criteria, the two areas provide _a synop-

sis. For example, quality assurance effectiveness has been assessed

on a day-to-day basis by resident inspectors and as an integral

aspect of specialist inspections. Although quality work is the

responsibility of every employee, one of the management tools to

mea,ure this effectiveness is reliance on quality assurance inspec-

tions and audits. Other major factors that influence quality, such

as' involvement of first-line supervision, safety committees, and

work attitudes, are discussed in each area.

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Beaver Valley Unit 1 6

C. Facility Performance Analysis Summary

FUNCTIONAL AREA LAST THIS RECENT

PERIOD PERIOD TREND

1. Plant Operations 2 2

2. Radiological Controls 2 2

3. Maintenance 1 2

4. Surveillance 2 2

5. Fire Protection and

Housekeeping 1 2

6. Emergency Preparedness 1 1

7. Security & Safeguards 1 1

8. Refueling and Outage

Management 3 2

9. Licensing Activities 1 2 Declining

10. Training and Qualifi-

cation Effectiveness *

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11. Engineering Support *

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12. Assurance of Quality *

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  • These are functional areas which were not assessed in previous assessments, but

are treated as separate functional areas in this assessment.

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D. Unplanned Shutdowns, Plant Trips and Forced Outages i

Date/ Functional

Power Level Description Root Cause Area

10/14/85 Feedwater control system malfunc- Repetitive Assurance

45% tion upon loss of Vital Bus III component failure, of Quality

10/25/85 RCS flow transmitter spike during Technician error Maintenance

100% post-maintenance testing compounded by an

error in a procedure.

11/2/85 Manual shutdown to repair feed- Design Engineering

100% water control valves due to

damage resulting from high

vibration.

2/10/86 Feedwater control system malfunc- Repetitive Assurance

100% tion upon loss of Vital Bus III component failure of Quality

8/26/86 Manual trip in response to 4 Random component

below 5% dropped control rods. failure.

9/3/86 Reactor Trip Breaker Shunt Trip Technician error Surveillance

100% during surveillance testing. compounded by

inadequate switch

labeling.

9/12/86 Manual shutdown to repair two Design Engineering

100% feedwater water control valves

due to damage resulting from

high vibration.

l 10/27/86 Manual shutdown to repair leaking Design Engineering

i 100% weld on 3/4" feedwater vent line

l located near the high vibration

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area of the feedwater control

valves.

1/11/87 Reactor trip - turbine trip ini- Inadequate proce- Surveillance

100% tiated by " low auto-stop oil procedure.

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pressure" during surveillance

test.

2/7/87 Reactor trip - turbine trip due Random component

i 100% to =purious actuation of the tur- failure.

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Beaver Valley' Unit 1 '8

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IV. PERFORMANCE ANALYSES

A. . Plant Operations (1029 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.915345e-4 months <br />, 29.7%)

1. Analysis

The previous assessment noted that the overall conduct of operations

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during non-outage. conditions was considered satisfactory; a Category

2 rating was assigned. Problems occurred during the recovery period

j of major refueling outages as management and personnel resources

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were being directed toward support of Unit 2 startup. .The overall

staff experience level at BV-1 was considered relatively low due

to the need to ensure an adequate staff of licensed operators with

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commercial experience for BV-2. \

). This assessment is based on routine inspections performed by'the-

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resident. inspectors and a team inspection of operations during the

last refueling outage.

The past concerns either were not repeated or had minimal impact s

during this current assessment. However, the success of station

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management in assuring quality and resolving technical issues aris-

ing from operational events has been mixed, though adequate re-

sources were generally allotted. During the previous assessment,

.there were three reactor. trips from low power due to steam' generator

.(SG) level control problems during.startup. Because of control

system modifications, improved procedures and operator _ training,

there were no low power trips due to SG level _ control problems for

, the last 18 months. The previous assessment saw one SI-reactor trip

c due to the failure of Vital Bus No. 3. -This assessment saw two full

). power reactor trips due to the recurrent failure of this same busi

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and operator action prevented trips for two other failures. The

majority of the manual shutdowns and major power. reductions'has

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continued to be due to. problems on the secondary side. .Previously,

these problems were mostly related to condenser tube';eakage (the

condensers were retubed) and balance of plant (B0P) pumps'for the

! last assessment period, totalling:about 12 separate events. This

i cu'rrent' period saw improvement with about 9 such events relating

to B0P pumps and the feedwater control valves (FCV). Though the

FCVs have undergone several modifications, an effective engineering

i solution is still pending as discussed in Section K, Engineering

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Experience with the primary side was much better. Corporate and

. station management have not hesitated to take whatever actions

necessary, including ordering plant shutdown, to ensure that safety

issues are addressed in a timely and technically conservative manner.

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Startup from the Fifth Refueling Outage was delayed several days

as the plant was cooled down to investigate and repair the source

of a primary system leak that was within technical specification

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Beaver Valley Unit 1 9

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limits. Extensive. measures were taken to retrieve secondary system

loose parts that could subsequently degrade steam generator tubes.

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When SG cold leg tube thinning was found, the station joined with

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the NSSS vendor to investigate this phenomena and conduct a tube

, expansion experiment to arrest the thinning. After one fuel assem-

(: bly experienced baffle jetting damage and a near-term fix imple-

i ;s mented (stainless steel rods), plans were developed to perform an

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upflow cooling modification, scheduled for the Sixth Refueling

Outage. >

The various station safety committies continue to function well.

The Offsite Review Committee (0RC), composed of the more senior

corporate personnel, and its varic'ps subcomcittees is an effective

and aggressive organization. The'0RC has served as a management

tool in upgrading plant performance through assignment of tasks to

, resolve selected safety issues that require extensive, allocation

of resources and coordination among station groups. It has been

,s able to provide the study oversight of plant problems and' activities

s because all of the Nuclear Group personnel, including senior man-

agement, are located on site. . Special meetings are often held.

The Onsite Safety Committee (OSC) is staffed by more junior person-

nel to limit the time ~ de.nards on the senior staff. Despite this

lower level of, emphasis, there have been no problems readily attri-

butable to it.

The Station's problem identificatioh system is generally sound.

The Unit Off Normal Reports (U0NRs) were deliberately set up with

a low thres' hold for identifying a wide range of problems and anoma-

lies. It can provide an effective method for trending events and

ensuring an appropriate level of review and corrective action.

Though significant events;are evaluated and reported when necessary

and within the regulatory 3time constraints, the lower tier UONRs

were often backlogged for several months before completion. This

indicates that overview of this system has not been aggressively

coordinated and managed. Hpwever, final root cause analysis and

long term corrective actions have been sound and technically ade-

quate with two notable exceptions. Problems with the_FCVs and Vital

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7 Bus No. 3 inverter have persisted; they are discussed in more detail

in' Section L, As'turance of Quality.

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Within the last year, the station has set up a trip reduction pro-

( g gram in conjunction with other Westinghouse NSSS plants. Advisory

in nature, its full' poteipial is still unknown. The Operations

i Assessment Group is assigned oversight responsibilities.

Preparation of ' operator candidates for taking the NRC administered

exams was a problem in 1986 in that 9 of 16 Senior Reactor Operators

(SR0s)'and 5 of 17 Reactor Operators (R0s) candidates failed various

portions of tbt exams. This is discussed in more detail in Section

J, Training ard Qualification Effectiveness.

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Beaver Valley Unit 1 10

Staffing levels remained stable and operator performance showed an

improving trend over the last assessment period. No trips were due

to inadequate operator performance. Several automatic trips were

avoided due to operator knowledge of recent events or the specific

field location of components. Over this 18 month period, there were

several problems associated with personnel failing to pay attention

to detail: cycling a safety injection valve and leaving it out of

position during reactor shutdown; startup of both low head safety

injection (LHSI) pumps with the suction valves closed for about 10

seconds (another operator immediately identified it) during its

annual test; an unlocked Nuclear Shift Supervisor (NSS) key cabinet;

and failure to act in a more aggressive manner when a power operated

relief valve (PORV) was leaking 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after it lifted as evi-

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denced by elevated tail pipe temperatures. Once identified, post-

tive corrective actions were taken, consistent with station policy.

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No major vio?ations occurred. The attitude of the operators, first

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line supervision and station managerrent toward safety remained

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positive. A notable strength has been the number of licensed per-

sonnel found in the management organization and various support

groups. However, although there currently is a large number of

licensed personnel within the organization, it is not clear what

long term plans are being made to bring new candidates into the

training pipeline.

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Plant operations performance has been sound and generally consistent.

Current licensed personnel are well trained in an INP0-accredited

program and use of a plant-specific simulator. The overall level

of professionalism is good and appears to be improving. First line

supervision is active in planning and controlling significant plant

evolutions. Though several plant configuration control problems

occurred, the overall program is sound and receives additional

management attention. Despite the increased demands of the Unit

2 project, management involvement is evident. Improved performance

was observed in this area during this assessment period. No sig-

nificant problem areas are evident.

2. Conclusions

Category 2.

3. Board Recommendations

None.

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Beaver Valley Unit 1 11

B. Radiological Controls (384 hours0.00444 days <br />0.107 hours <br />6.349206e-4 weeks <br />1.46112e-4 months <br />, 11.1%)

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1. Analysis

The previous Category 2 rating in this area was based principally I

on a decline in the radiological controls program due to uncertain-

ties as to the functions and responsibilities resulting from or-

ganizational changes during the period. Although no major program-

matic weaknesses were identified, minor problems were identified

that were indicative of a need for improvements in two program areas:

(1) the evalaution/ corrective action system, and (2) management

oversight of radiological control activities,

a. Radiation Protection

During this assessment period, there were indications of in-

creased management attention in the program. Adequate controls

over individual external and internal exposures were exercised.

Organizational changes caused problems during the last assess-

ment period. During the current period, the radiological con-

trols organization remained stable, and radiological control

personnel seemed more confident in their functions and re-

sponsibilities. Late in the assessment period, the upward

reporting channel for the radiological control organization

was changed from Nuclear Services to Operations. In light of

the past problems when organizational changes were made, the

licensee should closely monitor the impact of this latest

change.

Indications of increased plant management attention and con-

trols included a short-term requirement that line supervisors

perform radiological protection surveillances. Radiological

protection management instituted a new system to allow tracking

the status of daily surveillance items. Although the new sys-

tem constituted a good initiative to increase management over-

sight, it was not formalized to achieve its full potential as

an effective management tool in that it did not provide for

trending, evaluation, and correction of radiological deficien-

cies. It also did not allow for direct input by organizations

other than the radiological controls group.

In the ALARA area, the licensee's three year running average

for collective person-rem continued to decline through the end

of calendar year 1986 (398 person-rem). This performance is

fairly close to the three year running averige for all PWRs

(444; a 10 percent difference). However, the licensce's three-

year running average is heavily weighed by the atypically low

60 person-rem in 1985, a non-outage year. The annual person-

rem total for 1986 (627, an outage year) slightly exceeded the

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Beaver Valley Unit 1 12

goal of 570. This was apparently due to the fact that it was

a 10 year ISI outage and that unforeseen outage work had to i

be performed. This overall performance was close to the in-  !

dustry average. Concerns in this area included no aggressive

oversight and coordination of ALARA activities, due to the fact

that there was no assigned full-time staff in charge of imple-

mentation of the program and that there was low attendance at

the Nuclear Group ALARA Review Committee meetings. (This com-

mittee has the responsibility to review the status of program l

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implementation.)

Adequate controls over individual external and internal ex-

posures were exercised resulting in individual exposures being

maintained below the applicable administrative limits. For

the outage during this assessment period, a computerized indi-

vidual and RWP-dose tracking program was implemented and up-

dated daily. This represented a significant improvement in

the personnel exposure tracking area over the previous manual

methods. Numerous other microcomputer-run programs are now

used in the respiratory protection, radwaste shipping, instru-

ment status, and procedure maintenance areas. Heightened em-

phasis on work to increase the degree of computerization in

the area of personnel exposure records contributed to increased

efficiency and improved record retrieval and accuracy. These

findings indicated that the licensee has made progress in

automating the cumbersome manual system of records and reports.

Minor and infrequent violations were identified. One of the

two violations in this area involved failures to issue termina-

tion exposure records to contractor personnel within the pre-

scribed time limits and was a repeat violation. The other

violation concerned an instance in which administrative control

of keys to high radiation areas was lacking. The NRC had pre-

viously expressed concern about the administrative control of

these keys and the lack of a procedure for key issuance, in-

l ventory, and accounting. This weakness continued during this

SALP period. There were also inadequacies in the air sampling

program during the outage, which caused the loss of airborne

survey information for some significant radiological operations.

The licensee has initiated significant steps to upgrade radio-

logical control equipment and instrumentation f e combined Unit

1 and 2 operations. Four automatic whole-body friskers, two

high-throughput whole-body counters and two new gamma spectro-

meters, with one dedicated to radiological control purposes,

have been ordered. Four new portal monitors are in place at

the proposed common site security access point but are not yet

operational.

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Beaver Valley Unit 1 13

b. Radioactive Waste Management and Effluent Controls

There was one inspection of the licensee's transportation ac-

tivities during this assessment period. Several problems were

identified resulting from inadequate quality assurance and

quality control activities. The licensee had changed their

Process Control Program (PCP) which established operating and

test parameters to ensure a stabilized waste product. The

revised PCP was implemented prior to review and approval by

appropriate management levels as required. Second, the licen-

see had used a vendor procedure for dewatering which had not

been reviewed since 1983. The maximum allowed review period

is two years. Third, a shipment of two drums of radwaste was

sent offsite with puncture holes, and represented a situation

where the licensee failed to perform appropriate inspection

of the shipment. During the last assessment period, an NRC

inspection determined that quality assurance activities related

to verifying waste characterization in transportation activi-

ties needed improvement. While the licensee has responded in

a timely manner to all the specific NRC identified problems,

the number of problems indicate there had been inadequate

self-identification of problems and weaknesses in this area.

There were no inspections in the Effluent Controls area during

this assessment period. However, the licensee submitted the

results of their ventilation line loss study initiated in 1983

as a result of an NRC unresolved item. Preliminary review in-

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dicated a comprehensive study which received ongoing management

support. NRC's evaluation of the licensee's analysis of the

data showed some incongruities concerning application of cor-

rection factors. The licensee provided additional information

at NRC's request near the end of this period. In addition,

there was an unplanned minor release of radioactive liquid

effluent as a result of improper operation of an isolation

valve. This release was significant enough to constitute a

violation of Technical Specifications. A citation was written

in the operations area for improper valve operation.

In summary, the licensee has initiated increased management atten-

tion to certain areas while other areas need improvement. Instru-

mentation and equipment are being upgraded. The radiological con-

trols program and ALARA continue to be adequate. Quality assurance

and quality control in the area of transportation require increased

management oversight.

.

- , . - . . - ,..-...e w -- - . , ,

- . . - - - _ _ _ _ - _ _ _ - _ _ ---_

.

..

Beaver Valley Unit 1 14

2. Conclusions

Category 2

3. Board Recommendations

None.

_ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ .

_ . - . _ - -- . -

...

I

.

Beaver Valley. Unit 1 15

,

'

C. -Maintenance and Modification (400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br />, 11.5%)

1. Analysis

.

  • ~

No major programmatic problems were evident during the last SALP

and the licensee's performance was-judged to be relatively consist-

ent. . A Category 1' rating was assigned. One weakness.noted was the

~

E

'

number of secondary side component problems that were responsible ,

'for 8 of-the 15 reactor shutdowns and 13 major power reductions.

,

'

'There'were also indications that corporate support should be

_ directed toward both parts procurement and improving coordination

between multiple plant groups to shorten the length of time compon-

ents were out of service' for corrective maintenance or modification.

v . .

!~ This assessment is based on specialist inspections of the' mechanical

, and maintenance areas, a maintenance program review, a team inspec-

'

-tion of actions impleniented in response to Generic Letter 83-28, .

and observations of ongoing activities by the resident-inspectors.

A general improvement trend was evident-throughout this assessment

-

period concerning the impact of secondary side mechanical problems

on the reactor protection system, though two causally linked event.

chains remained active since the last SALP. The first involved

-

repetitive failures of the Vital Bus No. 3 inverter and the second-

,

concerned continued high vibration problems due to the -feedwater

!- control valve design. This adverse trend was considered to primar-

'

ily be the result of ineffective engineering resolution of long

! standing problems and is further discussed in Section.K, Engineering

Support.-

r

Together, the above problems, cach persisting for several years,

l demonstrate a management determination to make existing plant

equipment function despite an adverse impact on plant reliability

and unnecessary safety system challenges. However, for other prob-

lems where a root-cause could be identified, sound solutions were

implemented in a timely manner. Many of the power reductions during

the previous assessment period were due to main condensor tube leaks.

A retubing modification and addition of an increased capacity steam

generator blowdown system (during the Fourth Refueling Outage)

enhanced secondary chemistry and eliminated this' major source of

down time. ,

Procedures and policies were rarely violated by maintenance person-

nel. Fcr the two reactor trips that occurred due to technician-

error, procedure human factors deficiencies were a contributing

l

cause. The 18 month calibration procedure for low RCS loop flow

I is not normally performed at power and consequently, did not contain

appropriate caution steps for the transmitter post-maintenance test.

- . - , . - . , - - - . . - - - , - . , - a ..... - - . - , - . . . . . - - . - - . . . . - -

.

.

9

-Beaver Valley Unit 1 16

The other trip that occurred during the.RTB shunt test was partially

due to the lack of distinctive labeling. Each event was promptly

addressed through the station's corrective action system.

Two region-based specialist inspections identified a weakness in

complying with administrative requirements for complete Maintenance

Work Request documentation. Examples were found where some MWRs

were not completely filled out with all the desired information.

Also, the required post-maintenance testing or reasons for not per-

forming a test were not always clearly identified on the MWR. Once

these concerns were raised, the station was responsive to re-evalu-

ating the MWR system and revising it to better serve their needs,

including trending component failures between systems.

Staffing levels were maintained fairly constant, despite Unit 2

mobilization efforts and the reassignment of a number of mechanics

outside their original positions and the introduction of personnel

from outside the station due to a company-wide reorganization re-

sulting from the shutdown of a fossil fuel plant.

Portions of the maintenance tri.ining program have already been

accredited by INPO, and the remaining areas are awaiting the INP0

site visit. Though the program implements a minimum job training

concept, neither the training nor maintenance departments maintain

a list of personnel qualified to perform certain jobs, although this

is a long term goal. Instead, personnel-are chosen on an as-avail-

able basis by supervisors familiar with the individuals' qualifica-

tions. Though this practice is generally satisfactory (especially

in I&C where a first class and second class technician often work

together with well-written and proven procedures), there have been

some historical problems in the mechanical area. For example, since

1976, the two main feedwater pumps have experienced 22 separate

problems for which the corrective action included replacing or re-

building the pump seals (an evolution that requires that reactor

power be limited to 65% with one pump out of service). A balance

of plant trending program could have more quickly focused management

attention in this area.

The day to day corrective and preventive maintenance of safety re-

lated components was consistently observed to have received adequate

pre planning and supervisory oversight. Plan of the day meetings

in the morning proviJe a strong coordinating tool for controlling

plant maintenance activities and ensuring adequate support from all

station groups. A Plant Managers meeting with representatives of

the various departments is routinely held at the end of each day

to review the status of the major maintenance items.

Use of proper procedures, clearances and interface with the Radcon

and QC Departments was routinely noted in the field. No program-

matic problems were evident in the conduct of work.

1

.

..

Beaver' Valley Unit 1 17

In summary, licensee and contractor activities associated with pre-

ventive and corrective maintenance have generally been well con-

trolled. Procedures used during routine evolutions were generally

well written although one trip was due to a defective procedure.

Training appears adequate as the station just completed a self-

evaluation of.the mechanical and electrical areas which is required

by INP0 accreditation. There has been increased attention in the

balance of. plant components although the maintenance program is

basically informal and based on past plant experience. Program

strengths included good adherence to procedures and equipment

clearances, job pre planning, and QC involvement. Improvements in

documentation MWR completeness and post-maintenance testing speci-

ficity were noted during this assessment.

2. Conclusions

Category 2.

. 3. Board Recommendations

None.

,

---.v. - , ..--._,-.,-,c. ,,-e, . , , - - , . , , . - - - - . .

.

.

Beaver Valley Unit 1 18

D. Surveillance (610 hours0.00706 days <br />0.169 hours <br />0.00101 weeks <br />2.32105e-4 months <br />, 17.6%)

1. Analysis

The licensee's performance during the last half of the previous

assessment period was excellent, with no new significant problems

identified. For the whole period, a Category 2 rating was assigned.

Programs controlling test scheduling, procedure development, data

review and approval appeared to be functioning well. Conduct of

testing was generally sound across all departments involved with

the BV surveillance program. Areas where the licensee's performance

was generally satisfactory, but could be improved, included better

control over
(1) contractor groups performing ISI and IST work,

and (2) conduct of 18 month Operational Surveillance Tests (OSTs)

performed during each refueling outage by the Operations Department.

This assessment is based on four specialist inspections of the ISI

program, containment integrity, and core physics testing. The

resident inspectors and an inspection team provided input regarding

routine and outage-related testing.

In general terms, the various test programs that management had

previously set up to administratively control surveillance testing

continued to function well. Test scheduling and performance showed

consistent evidence of prior planning by all groups involved. The

individual procedures were found to be explicit and generally pro-

vide for good control of activities.

One programmatic area still requiring further plant management r -

tention is the set up of system alignments for performance of th(

18 month OSTs. The NRC team inspection of the recovery period of

the Fifth Refueling Outage found that this previously identified

weakness had not yet been fully corrected because of the continued

reliance on adherence to plant configuration control procedures

during high activity periods and the number of deviations from those

control procedures identified by the team. Conversely, the 18 month

Beaver Valley Tests (BVTs) (performed by the Plant Performance and

Testing Group) and Maintenance Surveillance Procedures (MSPs) (per-

, forfm. by various maintenance and support groups) were found to ex-

plicitly control alignments for both pre-test and as-left conditions.

Two NRC inspections of the BV 10-Year ISI Program found stronger

evidence of the licensee's efforts to update and control the program.

Department coordinators were directly involved in the oversight of

contractor activities. Their efforts resulted in adequate control

over ISI program documents and inspection acti v ities.

Management commitment toward addressing safety issues from a tech-

nically sound safety standpoint was also evident in the use of

advanced equipment and concepts during the refueling outage inspec- ,

!

.

Beaver Valley Unit 1 19

tion activities. These included application of the B&W Automated

Reactor Inspection System for contact ultrasonic examination of the

reactor vessel, and the Automated Data Acquisition System for data

analysis. Also, the MIZ 18 multi-frequency eddy-current system was

utilized for steam generator tube inspections. The licensee also

took the initiative in implementing an experimental steam generator

tube modification in an attempt to arrest the cold leg tube thinning

phenomena.

A special inspection to assess the BV-1 containment. integrity found

good management controls over station programs to assure the func-

tion and availability of appropriate systems. A subsequent inspec-

tion of the in progress Type A Containment Integrated Leak Rate Test

found it technically adequate and well controlled. The station has

dedicated ample resources to assure the operability of this import-

ant fission product barrier.

Strong oversight of the startup physics testing program was apparent.

The Cycle 6 startup physics tests were performed in accordance with

approved test procedures by highly qualified personnel. Test re-

sults were properly evaluated and documented. Also, the safety

evaluations performed to support the Cycle 6 startup (such as Cycle

6 core reload, steam generator tube plugging, and insertion of re-

constituted fuel assemblies) were well prepared and technically

sound.

The Test and Plant Performance Group's staffing was found ample.

Interviews with cognizant personnel determined reactor engineers

were very knowledgeable in their assigned areas. Quality Control

personnel were observed providing surveillance coverage during Cycle

6 startup testing and zero power physics testing. Additional man-

agement control in this area was evidenced by the completion of an

administrative plant procedure audit by Quality Assurance prior to

the Cycle 6 startup.

The first level review of tests has not always taken a critical look

at the test results. Data needs to be analyzed not only for meeting

specified acceptance criteria, but also reasonableness early in the

review process to determine whether or not the surveillance test

intent has been successfully accomplished. For example, the BVT

measuring total RCS flow for DNB parameters was signed off as being

acceptable despite the fact that two loops indicated individual flow

rates less than that assumed in the core design. Aggressive resolu-

, tion of the apparent anomaly was not pursued until questioning by

the NRC. Also, the 18 month OST measuring accumulator check valve

leakage was considered satisfactory despite the fact that data were

contradictory in that measured back leakage was greater through two

check valves in sories as opposed to the single check valve align-

t

!

r 1

a

Beaver Valley Unit 1 20

ment. Another example included the routine review and acceptance

of an erroneous remote shutdown panel instrument indication that

had failed low.

Greater engineering technical assistance is needed during the modi-

fication process to assure adequate development of surveillance test

acceptance criteria. Examples include the use of Rosemount RTDs

as replacement components in the reactor protection system without

considering possible efforts on the time delay constants specified

in the TSs. Also, the PORV stroke time for use in the low-tempera-

ture overpressure protection system was not defined in the test

program, resulting in one valve being outside the limit assumed in

the SER.

Plant experience indicates that greater consideration and caution

needs to be exercised during the initial performance of new tests

and the conduct of tests in other than normal conditions. During

this assessment period, two reactor trips from full power occurred

partially due to technician error and partially due to procedure

human factors inadequacies during an RCS loop flow calibration not

normally run while operating, and the reactor trip breaker shunt

relay tests on components which had just been modified. Unusual

alignments also contributed to a safety injection while in cold

shutdown during performance of an 18 month emergency diesel genera-

tor test in coincidence with an off-normal solid state protection

system setup.

Operator error during surveillance testing was responsible for two

events during the Fifth Refueling Outage. A motor operated safety

injection valve was left open after stroking for a surveillance test

resulting in reactor vessel overfill. Also, both low head safety

injection pumps suction valves were inadvertently left closed for

a short period of time during performance of the full flow SI test.

The two surveillance tests that were missed during this assessment

period had no programmatic link. The fuel pool cooling pump test

requirement was misinterpreted during the outage and the missed low

setpoint power range monitor trip channel check was due to an in-

adequate startup check list that was not revised to reflect a tech-

nical specification amendment issued about two years ago.

Early in this assessment period, a general weakness in the fire

protection surveillance area was identified. Four LERs and two

Level IV Violations were generated due to inoperable smoke detectors,

filter bank spray nozzles and detection system, and inadequate post-

modification testing of the Backup Indicating Panel (BIP). This

area is discussed in greater detail in Section E, Fire Protection.

_ _ _ _ - - _ - _ - _ - _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _

__ _

.

.

Beaver Valley Unit 1 21

The various surveillance programs previously established continued

to function well. Routine monthly surveillance tests were effective

in identifying equipment problems. Improved controls were found

in the ISI program and strong programs were found in all physics

testing and integrated leak rate testing. Test acceptance criteria

were generally well defined with the exception of the DNB reactor

coolant loop flow measurement and the absence of the low temperature 1

overpressure protection PORV stroke time assumed in the safety

evaluation report. The plant staff was responsive to these concerns,

once raised. One remaining weakness is the area of pre-test system

alignment for the 18-month operational surveillance tests.

To summarize, the surveillance programs generally functioned well.

owever, the potential high level of performance was not obtained

due to concerns related to review of test data for reasonableness,

several missed surveillance tests and the continued need to

strengthen th 18 month OST system alignment methodology. Though

good programs are in place, better implementation at the line

supervisor level and a strong technical involvement in developing

new test acceptance criteria is necessary to realize further im-

provements and prevent recurrences of past problems.

2. Conclusions

Category 2.

,

3. Board Recommendations

None.

!

l

'

t

.

_ - _ - - _ - _ _ _ - _ _ _ _ _ - - - _ _ _ - _ - - . - . - _ _ _ - - - _ _ - .

o

a

Beaver Valley Unit 1 22

E. Fire Protection and Housekeeping (231 hours0.00267 days <br />0.0642 hours <br />3.819444e-4 weeks <br />8.78955e-5 months <br />, 6.7%)

1. Analysis

In the last assessment, it was concluded that the licensee's fire

prevention program had been effective in minimizing fire hazards

and maintaining a high state of readiness to handle challenges

through a well trained and equipped staff. Housekeeping was con-

sidered satisfactory. A Category 1 rating was assigned.

This section assesses the licensee's overall performance in fire

protection, including: prevention, detection, ability to respond

to any fire with appropriate onsite and supplemental offsite forces,

engineering and hardware features to limit its spread, and the

ability of the station to deal with its operational consequences

(safe shutdown). This assessment is based on a team inspection of

Appendix R commitments, and review of onsite activities by the

resident inspector.

Management involvement is strongly evident in the areas of preven-

tion (there were no fires), and ensuring adequate resources to re-

spond to any fire. The onsite fire brigade is well staffed; each

shift drills once per month. Additionally, offsite forces are

readily available through the Mutual Fire Assistance Program. Ex-

tensive pre planning is demonstrated during the yearly drills with

offsite agencies. Onsite fire fighting equipment is modern and

maintained in good working order through inclusion in the plant's

surveillance program.

A team inspection of Appendix R requirements found excellent review

of the issues, prior planning and management involvement at all

levels. The station analysis to show compliance with the cost-fire

safe shutdown requirements was noteworthy, particularly in the areas

of associated circuit analysis. An alternate safe shutdown proce-

dure for use in the event of a control room or other design basis

fire, were found to be very thorough, detailed, and practical. A

satisfactory walk-through of these procedure exhibited the effec-

tiveness of operator training and a good working knowledge in this

area. Human factors considerations were generally good; only minor

concerns were identified regarding the adequacy of emergency light-

ing in some areas. Previous actions taken to address the oil col-

lection system for the reactor coolant pumps and the safe shutdown

capability issues were found adequate.

Several hardware and instrumentation deficiencies became evident

in this assessment period. Some had existed for several years and

were due in part to inadequate engineering support to the fire pro-

tection issue addressed by Generic Letter 81-12 and 10 CFR 50, Ap-

pendix R. QA audits were ineffective in early identification of

this weakness.

- - -.

.-

.

Beaver Valley Unit 1 23

A 1985 QA audit, performed in response to IE Information Notice 83-69

found several missing fire dampers that isolated various ventilation

ducts that traversed adjacent fire zones. Inspections of other fire

dampers, resulting from a deficiency identified prior to this as-

sessment period, found that the automatic closure feature for 6

dampers in the cable spreading room were not reconnected after a

1981 modification. No post-modification test had been performed.

Expanded damper testing subsequently identified an operability

problem due to inadequate lubrication after initial installation.

Together, these hardware problems demonstrate an apparent insensi-

tivity to the fire protection issue earlier in the Beaver Valley

project history, at a time when resources were severely stressed

due to the TMI action item modifications. After completion of the

work, the statiun failed to adequately look back at the issues to

self identify deficiencies in a more timely manner.

Analysis of LER 86-05 found that the initial root cause investiga-

tion and corrective actions for the blocked main filter bank spray

nozzles, to be inadequate. Appropriate attention was focused on

this issue after the NRC identified the concern. This indicates

that the plant problem identification systems still lack a strong

sensitivity toward fire protection.

Instrumentation problems included inoperability of a portion of the

' Backup Indicati:g Panel (BIP) due to inadequate post modification

testing. Keys necessary to operate BIP functions were found not

to fit the locks after the system had been installed for one full

fuel cycle (although master keys were available). The NRC Appendix

R inspection also found that emergency lighting in safe shutdown

access routes required additional work. Together, these problems

would have hindered, but not prevented, the operators efforts to

bring the plant to cold shutdown from outside the control room.

Other instrumentation problems included the unintentional (and un-

knowing) de-energization of the river water intake structure smoke

detectors, and an inoperable smoke detector in the emergency diesel

generator room that was not identified over an extended period of

time due to inadequate vendor performed surveillance testing.

Together, the above problems (scme of which pre-dated Appendix R) ,

show that the station lacked a comprehensive overview of this area '

, during its inception, especially engineering support to define the

post-modification test acceptance criteria. The various station

groups did not develop a cohesive overview of this area and QA

failed to identify this weakness. Though resources are adequate

and either redundant systems were available or analysis showed that

the protection function would have been met, additional management

attention is warranted to ensure that the design, modification, and

plant maintenance functions do not subsequently degrade this area.

j

l

.-

.

Beaver Valley Unit 1 24

Housekeeping has generally been satisfactory. A plant improvement

program has been underway since the last refueling outage resulting l

in a general upgrade of plant appearance. New emphasis has been

placed on maintaining the material condition of the plant by the

operations staff. '

2. Conclusions

Category 2.

3. Board Recommendations

None.

_ - - - - - - - - - - - _ - - - _ - - - - - . . - - - - - - - - - - . -

,

O

.

Beaver Valley Unit 1 25

F. Emergency Preparedness (154 hours0.00178 days <br />0.0428 hours <br />2.546296e-4 weeks <br />5.8597e-5 months <br />, 4.4%)

1. Analysis

During the previous assessment period, the licensee was rated a

Category 1. During this assessment period, there was one inspection

of emergency preparedness activities which included observation of

the annual full participation emergency exercise.

The licensee's execution and participation in the exercise demon-

strated thorough planning and a strong commitment to emergency pre-

paredness. Emergency response personnel were observed to be knowl-

edgeable in their duties and in use of plant EP Implementing Proce-

dures, a reflection of a high level of training and a strong commit-

ment to emergency preparedness. Only minor deficiencies were iden-

tified in the exercise concerning: operation of the Post Accident

Sampling System (PASS); activation of the Technical Support Center

(TSC); offsite notifications; and use of IP 4.1 "Offsite Protective

. Actions".

t

The licensee conducted a good critique of the exercise, highlighting

areas for improvement and committing to taking appropriate correc-

tive action where necessary.

The licensee has ample full-time onsite and corporate staff who are

assigned to maintain the emergency preparedness program. The Train-

ing Department staff is also actively involved in the program. It

obtains feedback from the emergency preparedness group regarding

deficient exercise performance or other programmatic areas and in-

tegrates corrections into emergency response training.

Emergency response facilities (ERF) are dedicated and have been well

maintained throughout the period. These include the Emergency

Operations Facility, Technical Support Center, Radiological Opera-

tions Center, Operations Support Center, and Emergency News Center.

An outstanding rapport is maintained with offsite officials in a

very difficult situation of coordinating with three states, several

local governments and two FEMA regions. A strong commitment by the

licensee to train and inform both offsite officials and the general

public has been made and implemented.

In summary, the licensee has maintained a high level of emergency

preparedness both onsite and offsite. Personnel have displayed an

excellent attitude toward maintaining a high level of emergency

preparedness. Overall management involvement in emergency prepared-

ness activities has been effective as evidenced by timely respon-

siveness to NRC initiatives.

_ - _ _ _ _ _ _ _ _ - _ _ - _ _ _ _ - - _ _ _ _

_ - - _ - .

.

.

Beaver Valley Unit 1 26

)

l 2. Conclusions

--

Category 1.

3. Board Recommendations

None.

3

_

.

.

Beaver Valley Unit 1 27

G. Security and Safeguards (146 hours0.00169 days <br />0.0406 hours <br />2.414021e-4 weeks <br />5.5553e-5 months <br />, 4.1%)

1. Analysis

During the last assessment period, no programmatic weaknesses were

identified. The only significant performance problem involved

access badging issues; there has been no recurrence. A Category

1 rating was assigned.

During this assessment period, the licensee's overall performance

remained essentially consistent with the previous assessment period.

Program strengths that remained apparent during this period were:

licensee oversite of the security contractor; clear and concise

program implementing procedures; effective training; adequate staff-

ing; and high morale. Toward the end of the period, preparation

for bringing the Unit 2 project (construction was about 98% complete)

under the Beaver Valley Security Program lagged sufficiently behind

schedule to place the security program and hardware installation

on critical path. This lack of progress toward completion of

various security systems has since been corrected in response to

NRC's concerns by applying significant construction and support

group resources toward completing the necessary work.

Licensee's management involvement, support and oversight of the

security program remained evident and resulted in highly successful

implementation of the program during this assessment period. Man-

agement oversight of the contract security force was adequate to

provide the licensee with necessary and current knowledge regarding

program implementation.

Program implementing procedures and instructions were updated, when

required, to provide the security force with current, clear and

concise directions. The effectiveness of the procedures and in-

structions, and also the training program,'is apparent by the small

number of personnel errors during the period. This is especially

significant since there was a change in the security force contrac-

tor about two-thirds of the way through the period.

In October 1986, the security service contractor was changed. All

the original security force supervisors and about half of the guards

and watchmen were retained by the new contractor. The remainder

of the new guard force was made up of industrial security personnel

previously employed at Beaver Valley Unit 2. The new Unit 1 secur-

ity force members were provided classroom and on-the-job training

by experienced Unit 1 personnel prior to assuming their new posts.

Although a QA audit of records prior to contractor changeout did

not occur until prompting by NRC, comprehensive planning for this

evolution took place. Licensee management, on its initiative, met

with Region I personnel to describe the plans for the changeover.

_

.

.

Beaver Valley Unit 1 ~ 28

The changeover was accomplished without any problems or decrease

in security effectiveness. This is further indication of the at-

tention management affords to the plant security program.

The turnover rate in the contractor security force remains low and

staffing appears adequate, as indicated by the limited use of over-

time. Contractor supervisory and administrative staffing appears

adequate for the current work load. The licensee's proprietary

security force staff currently consists of three full-time positions

for Units 1 and 2. The accumulated total experience of the licen-

see's staff was recently significantly reduced due to personnel

turnover. It remains to be seen whether the licensee's current

staff can effectively provide the necessary cversight and control

of the contract security force for a two unit site, especially con-

sidering the problems inherent with the startup of the new systems

and equipment.

The training program is administered by four, full-time, experienced

instructors. Lesson plans have been developed, are current, and

reflect the commitments in the NRC-approved security program plans.

Training facilities are professional and instructional aids are ex-

tensively utilized. All security related facilities, e.g. , guard

house, alarm stations and office areas, are well maintained, orderly

and clean. Licensee oversight of the training facilities and

security program is provided and is evidence of the licensee's in-

tent to maintain an effective and professional security force. Mem-

bers of the security force were found to be very knowledgeable of

their duties and responsibilities when performance tested by NRC

personnel.

The licensee submitted seven security event reports under 10 CFR

73.71(c) during this assessment period. A continuation of a series

of badging problems that started in the previous assessment period

was responsible for two reports. Management involvement in enforc-

ing station policy and a change in security procedures eliminated

further recurrence. Other reports involved strikes by craft workers

at Unit 2 that resulted in picket lines around both units (twice),

and a bomb threat received at Unit 2 but, because of its non-spect-

fic nature, a search was conducted at both si:'s with negative re-

sults. Another event involved a degraded vital area barrier due

to a lack of communications between maintenance and security. The

last event involved an electrical breaker that had been found

t + oed. A thorough investigation by the licensee disclosed that

i d been tripped by a member of the security force out of curi-

%. j. All events were properly handled and compensatory measures

were initiated when required. The event reports were clear, concise

and adequate for NRC analysis. The quality of the event reports

is indicative of proper management review.

.

. *

Beaver Valley Unit 1 29

The licensee's program and procedures for the cnntrol and accounting

-

of special nuclear material at Unit 1 were reviewed and found to

., be adequate and generally well implemented.

During the assessment period, the licensee submitted a revision to

the Security Plan and a revision to the Training and Qualification

Plan in accordance with the provisions of 10 CFR 50.54(p) and re-

sponded to the Miscellaneous Amendments to 10 CFR 73.55, codified

by NRC in August, 1986. The revisions to the Security and Training

and Qualification Plans were technically adequate. The licensee's

response to the Miscellaneous Amendments is currently under review.

In summary, the 1icensee has sustained its previous performance

level in the area of security during this assessment period. A

problem with the identification badging process carried over from

the previous assessment period but was effectively corrected early

in this period. The matter could have received closer management

attention to resolve it more expeditiously. During the next assess-

ment period, close management attention and monitoring will be re-

quired to determine if the licensee's small proprietary staff can

effectively continue to provide the necessary oversight and control

of the contract security force when the Unit 2 security program is

combined with the Unit 1 program. It is evident by the licensee's

performance during this period that efforts to maintain a high

quality security program are continuing.

2. Conclusions

Category 1.

3. Board Recommendations

None.

. - _ _ _ _ _ . _ _ _ - _

.

.

Beaver Valley Unit 1 30

H. Refueling and Outage Management (262 hours0.00303 days <br />0.0728 hours <br />4.332011e-4 weeks <br />9.9691e-5 months <br />, 7.6%)

1. Analysis

The previous assessment noted that a series of problems occurred

within a relatively short time span during recovery from the Fourth

Refueling Outage that resulted in a Category 3 rating. Though

operational in nature, they were perceived to be due to inadequate ,

management control over the system restoration and outage recovery I

activities. As similar problems occurred during the same time span  !

while recovering from the Third Refueling Outage, but were notice-

ably lacking during minor outages and routine cperations, it was

concluded that the normally effective management control system

broke down due to the station's perceived need to place the plant

l back on line to meet a scheduled deadline. Other indicators of

degraded management effectiveness included: (1) control room con-

gestion and (2) a lack of supervisory attention to major plant

evolutions. A contributing factor to some of these problems was

the cumbersome startup procedure methodology used. Within the last

SALP period, the licensee made major efforts beyon+1 those formally

committed to, to upgrade their administrative controls. These

efforts were effective in a two week outage but were not fully

'

tested during a major outage recovery.

During this assessment period, there were several reactor trips and

unplanned shutdowns, each of a relatively short duration. From mid-

May until the end of August,1986, the plant was shut down for the

Fifth Refueling Outage and received extensive attention through an

NRC team inspection. Several weaknesses identified in the previous

SALP were still apparent with the refueling outage OSTs that in-

cluded: (1) specific acceptance criteria was found to be ambiguous

in several tests, (2) pre-test requirements to have "all valves in

designated NSA positions as determined by control room logs or flow

diagrams" was an inappropriate practice as many instances were

identified where control room logs and flow diagrams contained dis-

crepancies from actual alignments. This concern is formally ad-

dressed in Section D, Surveillance.

The actual outage recovery received extensive backshift coverage

and focused on the conduct of control room activities, plant con-

figuration control and completion of startup prerequisites. The

attitude of Operations personnel was positive, cooperative and pro-

fessional. The reactor operators, for the most part, enforced the

station's policy on limiting access to the controlled area. Good

involvement by the Nuclear Shift Operations Foreman (an SRO) in both

routine evolutions and outage testing occurred. The STA was often

involved in performing calculations and tracking followup of startup

open items. The station's commitment in response to previously

expressed NRC concerns, particularly during outages, to keep control

room noise levels to a minimum was manifested by the addition of

.- _ ____ ____

_ _ _ _ _ _ _ . . _ _ _ _

..

.

Beaver Valley Unit 1 31

carpeting to muffle background noise. The equipment clearance desk

was moved outside of the control room during the outage, thus mini-

mizing personnel access. Station management was evident throughout

this entire period and unlike the last several refueling outages,

the recovery was handled in a more disciplined fashion that lessened

the " push to startup" problems previously observed.

Commitments in this area made in response to concerns expressed in

the last SALP generally led to overall success. The concept of

developing an outage logic diagram of required safety functions and

hardening those flow paths by use of equipment caution tags was

effective during the outage. Other changes which included the

development of a low level incident reporting system, a system

manager program, reactor trip reduction program, and prescriptive

requirements for review criteria relating to tagging and log reviews

were also beneficial. Though plant configuration control appeared

to have improved to the point where there were none of the signifi-

cant deficiencies previously observed, some general weaknesses still

remain. The "NSA Deviation Review Log" which is intended to ensure

that final system alignments contain no unacceptable deviations has

little value because instances were identified where the walkdown

for some systems was not completed until over 30 days after initi-

ation. Operations personnel had difficulty in maintaining the con-

trol room status boards up-to-date because valve lineups were often

changed several times through equipment clearance work and ongoing

outage testing after the initial walkdowns were started. The NRC

team inspection concluded that weaknesses still existed in that some

system lineups were started while significant work remained, control

room drawings could not be maintained current to reflect actual

system alignment, the system of deviations as currently practiced

is an administrative burden on supervisory personnel and the clear-

ance system though generally effective, is inefficient.

In summary, the previous outage recovery problems were successfully

avoided during this recovery through the intensive use of manpower

and extensive supervisory overview. The plant configuration prob-

lems that did occur had little impact on plant safety. This is in-

dicative of the high priority that DLC management has placed on the

outage recovery process that went beyond the commitments made to

the NRC. However, the fact that several minor problems still oc-

curred such as initially running both LHSI pumps with their suction

valves closed for several seconds (due to inexplicit 18 month OST

system lineup instructions and operator error) and a valve was

stroke tested and left open, indicate that further improvements

centered on refinement of the plant configuration control system

and continued emphasis on operator attention to detail are still

necessary.

_ - _ _ _ .

.

.-

Beaver Valley Unit 1 32

2. Conclusions

Category 2.

3. Board Recommendations

None.

- - --_-__ _-- -______-_ - - _ _ _ - _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ - - _ _ _ - - _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ - - _ _ _ _ - _ _ _ _ _ - - - _ _ _ _ _ _ -

.

.

Beaver Valley Unit 1 33

I. Licensing

1. Analysis

In the last assessment, it was concluded this area was staffed by

qualified technical personnel who adequately understood technical

issues with good timely handling of ongoing issues. A Category 1

rating was assigned.

The licensee's corporate management demonstrated a gradual decline

in involvement and control over licensing issues during this assess-

ment period. Corporate management chose to reassign personnel from

the licensing organization of Unit 1 to Unit 2, thus creating a

drain of talent and a marked decrease in aggressiveness to resolve

issues. For example, the need for an amendment to remove fuel rod

weight limits was identified early in 1986, but the change request

was not submitted until considerably later, requiring the staff to

take expedited action to issue an amendment. A second example in-

volves the modification of the hydrogen recombiner blowers. Ap-

parently, insufficient engineering work was done for this modifica-

tion, resulting in the need to request an emergency technical speci-

fication change. The staff took the route of " discretionary en-

forcement" and allowed the plant to restart with the stipulation

that the technical specification be expeditiously reviewed. By the

end of the assessment period and seven months after the initial

submittal, the licensee had yet to provide the revised version to

the staff for review. A third example late in the period involved

removal of the Unit 1/2 control room partition. Apparently, the

design work was not started early enough and was not substantially

complete when the first technical specification changes were re-

quested. This resulted in the staff having to review documents that

were constantly being revised. Greater discipline must be restored

to the licensing process.

Notwithstanding the above, the interaction of the licensee with NRC

staf' has usually resulted in clear understanding of safety issues.

Sour; technical approaches were usually taken by the licensee's

tech.dcal staff toward resolution of the majority of issues handled

during this assessment period. Conservatism was usually exhibited,

with sound technical judgement provided for most deviations from

staff guidance. The "no significant hazards" analysis provided by

the licensee were usually adequate.

The communications between the licensee and NRC staff have been

generally beneficial to both in the processing of licensing actions

and minimizing the need for additional information. On several

issues, multiple delays and document submittals still did not result

in resolution. The licensee lacked aggressiveness in pursuing close-

out of open issues and providing requested followup information for

_ _ _ _ _ _ _ _ _ _ _ _

. c

.

Beaver Valley Unit 1 34

i

such items as SPDS design information and the effect of Rosemount

RDTs on various reactor trip time constants. Very often the late-

ness is blamed on lack of support by other organizations.

Early in this period, the staff requested all licensees to provide

information on implementation status of generic requirements. The

licensee's response was long overdue when it finally arrived. NRR

management was most concerned about the licensee's late response.

In summary, the licensee's previous high level of performance has

slipped due to the reassignment of personnel in support of Unit 2

startup activities. Though still generally satisfactory, management

appears to have lost the initiative in the licensing area and has

adopted a reactionary mode of operation as evidenced by the submit-

tal of TS changes prior to the completion of design work and num-

erous late submittals of what should have been routinely handled

information. The staff is not aware of any systematic efforts by

the licensee to provide additional oversight of licensing issues

to preclude such problems from occurring.

2. Conclusions

Category 2, Declining.

3. Board Reconnendations

Licensee: DLC needs to independently determine why the significant

decline in performance has occurred in this functiona area.

NRC: None.

.

.

Beaver Val 1ey_ Unit 1 35

J. Training and Qualification Effectiveness

1. Analysis

This functional area was not addressed separately in prior assess-

ments. Attributes of this area have been discussed in other appro-

priate areas and here provides a synopsis of the effectiveness of

the training and qualification programs.

The licensed operator training program produced two groups of can-

didates in 1986 that were not as well prepared for the NRC license

examinations as previous classes. From both groups, 9 of 16 SR0

and 5 of 17 R0 candidates failed various portions of their written

and simulator exams. The wide variation observed in the candidate

performance on the NRC exams as well as a high number of failures

on a facility administered pre-examination (10), is indicative of

either weakened program effectiveness and/or poor candidate selec-

tion. The testing of a large number of candidates for Unit 1 in

1986, which presently has 102 licensed operators, appears to have

been driven by management desire to dual license individuals on both

units. This lack of thorough preparation and effectiveness in

screening candidates was indicative of poor corporate management

oversight.

The requalification program appears effective. Administrative con-

trols were appropriate and program management was exemplary. No

reactor trips occurred during the past 18 months due to licensed

operator error or training deficiencies. There was a notable ab-

sence of trips on steam generator level at low power due in part

to training emphasis in this area. Operator response to plant

transients during this period was considered appropriate and in-

dicative of good training and excellent plant knowledge. Also,

training pertaining to new regulatory issues, such as the require-

ments of the Appendix R for cold shutdown from outside the control

room, was strong.

A site specific simulator was in use throughout this period. It

was effectively utilized in developing and running various EPP

scenarios as well as validating the new emergency operating proce-

dures. The simulator was also used to dry run various temporary

operating procedures and to enhance operator performance prior to

special evolutions. There was a good working relationship between

the operations and training departments.

Non-licensed operator training was adequate. The general employee

retraining program provides an annual refresher course to station

personnel that is tailored to include issues of current interest.

I

__. _ - . - , . _

.

.

Beaver Valley Unit 1 36

Technician and mechanic training was sound. There were two reactor

trips due to technician error, the same number as in the last as-

sessment, but training was not considered a primary factor in either.

There were no major or repetitive problems during this assessment

period due to inadequate training.

Licensed operator, non-licensed operator, and license retraining

programs were accredited by INP0 in December 1985. INP0 also ac-

credited the STA, radiation technician, chemistry, and I&C programs

in March 1986 shortly after the end of this assessment period. The

station has completed the self-evaluation reports and is currently

awaiting an INP0 site visit to complete accreditation of the me-

chanical, electrical, test staff, and manager areas.

A strong commitment to training was evident in many other areas.

This was evident by the efforts in emergency planning that include

not only extensive training of DLC personnel, but also a strong

commitment to train and inform both offsite officials and the

general public. In the area of security, the training and qualifi-

cation program made a positive contribution to the continued good

performance despite a change in contractor organizations. An active

program was also evident in the ISI and non-destructive examination

fields. The overall good performance of radiation technicians and

lack of any significant events due to technician error also reflects

a satisfactory program.

In summary, ample resources have been devoted to training at Beaver

Valley. All groups are involved and programs are satisfactory.

Good effectiveness was achieved as evidenced by strong worker per-

formance, low personnel error rates, and in particular, a low number

of reactor trips where personnel error was a contributing factor.

The relatively poor performance of licensee candidates in 1986 was

not indicative of past performance and appears to reflect decreased

management oversight of this area.

2. Conclusion

Category 2.

3. Board Recommendation

Licensee: Review program for scrcening licensed operator candidates

before putting them up for NRC exams.

NRC: None.

,

.

.

Beaver Valley Unit 1 37

K. Engineering Support (208 hours0.00241 days <br />0.0578 hours <br />3.439153e-4 weeks <br />7.9144e-5 months <br />, 6.0%)

,

1. Analysis

This is a special section that has not been addressed as a separate

functional area in the last several assessments. It is based on

observations made during routine resident and several specialist

team inspections of areas that required significant engineering in-

put. This assessment focuses on the ability of the Nuclear Engi-

neering and Records Unit (NERU) to support the station design change

and modification process, its effective use in resolving special

station problems, and its ability to adequately address new regula-

tory initiatives.

Several strengths are apparent. Over the past several years, all

engineering services that impact the station have been brought under

the NERU. The unit is located in the Emergency Response Center,

within easy access to the station. NERU is an active participant

in o'itage planning meetings and routine plan of the day meetings.

During this assessment period, there has been increased emphasis

on providing engineering support in the field (such as during the

charging pump modifications) to investigate problems. However, the

response time required to answer station requests still appears to

be somewhat excessive. (In addition to completing design work for

the Sixth Refueling Outage modifications and working toward comple-

tion of a long overdue records update, significant efforts have been

directed toward the Unit 2 project transition program.) In response

to industry group initiative, the design change and modification

process is being upgraded in that the responsible design engineer

now performs a pre modification team walkdown to evaluate construct-

ability, maintenance and operability requirements.

NERU was not effectively used in the past to resolve long standing

problems at the station. There appears to have been a reluctance

to provide more timely assistance while the maintenance groups were

involved in protracted troubleshooting. Examples include a long

history of feedwater control valve problems that have persisted

since initial plant startup, and a number of failures of Vital Bus

No. 3 for which a root cause could not be determined. These short-

comings appear to have been recognized by management as evidenced

by the initiation of a feedwater reliability analysis program and

appropriate modifications planned for the next refueling outage.

For new regulatory requirements, such as fire protection, environ-

mental qualification of components, and motor-operated valve analy-

sis and testing (M0 VATS), the overview provided by NERU was not

vigorous. There were numerous design and installation problems

associated with fire protection early in that program that have just

been recently identified and wo'rked out. An early audit of the

environmental qualification document packages found poor record

-- _

- _ - _ _ - - . _ - - _.

-_ . _ . --_ - ._

.

.

Beaver Valley Unit 1 38

management indicative of a lack of program oversight. There has

been a tendency to place new regulatory issues such as M0 VATS on

a low priority because of other ongoing tasks.

As another example of lack of vigorous followup, a design change

to the hydrogen recombiner blowers during the last outage resulted

in its failure to meet the technical specification flow rates and

required additional modification to the piping. Yet, the capacity

of the new blowers was questioned during the design process about

one year prior to installation, but not resolved.

In total, the above items suggest that engineering support has not

always been timely. Until relatively recently, the station has not

been able to provide appropriate engineering expertise in a more

expeditious time frame due to other priorities. However, the over-

all quality of the majority of engineering work completed has been

generally satisfactory. Significant effort has been directed toward

the Unit 2 project, and is expected to continue through the next

assessment period.

2. Conclusion

Category 2.

3. Board Recommendation

Licensee: None.

NRC: Perform a team inspection of the engineering support

activity after the Units 1 and 2 engineering organizations

are combined.

.

.

Beaver Valley Unit 1 39

L. Assurance of Quality

1. Analysis

During this assessment period, management involvement and control

in assuring quality is being considered as a separate functional

area for the first time and continues to be one evaluation criterion

for each functional area. The various aspects of Quality Assurance

Program requirements have been considered and discussed as a integ-

ral part of each functional area and the respective inspection hours

are included in each one. Consequently, this discussion is a

synopsis of the assessments relating to quality work conducted in

other areas. However, it is not solely an assessment of the QA/QC

departments.

Significant resources have been dedicated to the assurance of qual-

ity, as measured by the number of personnel committed to the QA,

QA Surveillance and QC groups as well as implementation of the

double verification of alignment requirement for all station groups.

A strong commitment to this concept was evident by management ac-

tions with regard to recovery from the fifth Refueling Outage, and

conservative approaches taken to response to identified problems

(fuel baffle jetting, steam generator tube thinning, secondary side

loose parts control and containment integrity).

Throughout this assessment period, there was evidence that work in ,

the plant was being performed well at the mechanic-operator-techni- l

cian level through to first line supervision. There was a strong

QC presence at the work site. . Of particular note was the small

number of trips that occurred due to operator or mechanic error.

This was indicative of good morale, training, procedures, and

supervision.

The station has made a significant commitment to training that

appears effective. This has been partly responsible for the sus-

tained good performance in security and emergency planning as well

as the good operator performance record.

Although QA was in compliance with rules and regulations pertaining

to the QA program, it does not appear to be used as a management

tool to assure that new rules or regulations are met prior to their

required implementation date and NRC inspections. When QA was used

as such, for example the pre-inspection audit of the Environmental

Qualification Program at NRC urging, potential deficiencies and

violations were identified and corrected. Following this QA audit,

the NRC team inspection found a solid EQ program in place. Examples

where such a preventive review did not take place and would have

been helpful were implementation of the 10 CFR 61, Transportation,

.

.

Beaver Valley Unit 1 40

and various fire protection requirements. In general terms, QA has

not made a significant contribution to identifying safety or major

program problems such as discussed elsewhere in this assessment.

A second weakness until recently, has been the lack of a quality

program for balance of plant equipment which has caused a signifi-

cant fraction of plant trips and unplanned shutdowns. Within the

last two years, a substantial number of surveillance tests have been

developed to monitor component or system performance for any adverse

trends. An informal balance of plant preventive maintenance program

aimed at increasing the reliability of major components is slowly

evolving, based in large part on plant experience.

Management oversight has generally been effective, considering the

increased demands the Unit 2 project placed on limited resources.

Several major areas where it appeared that management failed to

resolve problems in a timely manner or preclude their developing

included the Vital Bus No. 3 inverter problems, continued feedwater

control valve vibration difficulties, the decline in the performance

of the Licensing Group and the failure to assure that candidates

were ready to take the NRC license examiantions. With the above

exceptions, it appears that management involvement is assuring

quality was satisfactory.

Management and the Offsite and Onsite Safety Review Committees have

provided effective reviews of the modification process safety

evaluations. A low level incident report system has been in place

for the past several years. High visibility items or significant

events quickly work their way through the system for evaluation of

reportability and significance. However, the effectiveness of this

low threshold trending system has been limited by the length of time

required to complete the review process (some items not closed out

after nine months although important issues were generally acted

upon quickly). Because both ORC subcommittees and the OSC are part

of the review chain, the inordinate amount of time some of those

items remain open is indicative of a lack of strong management over-

sight and direction.

In summary, during this assessment period, the attitude toward

quality by the workers and first line supervision was found to be

solid throughout all plant groups. Station supervision routinely

gets out into the plant and keeps well informed of major activities

and developing trends. Strong QC involvement is evident in safety

related maintenance and is increasing in the balance of plant.

However, QA was not effectively used as a management tool to provide

further assurance that quality was being achieved. Corporate man-

agement and engineering support was not timely in resolving some

complex, long-standing technical issues that adversely affected

plant operations.

,

.

.

Beaver Valley Unit 1 41

2. Conclusion

Category 2.

3. Board Recommendation

Licensee: DLC should reassess the scope and charter for the quality

assurance function to determine how QA can more effec-

tively be used as a management tool to identify potential

problems before they occur, improve overall performance,

and provide added assurance that quality is being achieved.

NRC: None.

.

.

Beaver Valley Unit 1 42

V. Supporting Data and Summaries

A. Investigations and Allegations Review

There were three allegations received during this SALP period. One was

referred to NRR for technical review and found not to be a safety concern.

A second allegation involved three separate concerns raised by a con-

tractor Health Physics technician after employment termination. A rou-

tine Radcon inspection partially substantiated some of the concerns re-

lating to weak breathing air sampling methods though no noncompliances

were identified. The last allegation concerned a lack of control of

security keys and a vague reference to drug problems with security and

contractor personnel. Each of these concerns was evaluated by NRC but

none were substantiated.

B. Escalated Enforcement Action

1. Civil Penalties. None

2. Orders. None

C. Licensee Conferences Held During Appraisal Period

An enforcement conference concerning a security issue was held on the

Region I office on December 19, 1985.

Region I management met with DLC management to discuss SALP report 85-99

on December 19, 1985.

D. Confirmation of Action Letters

,

None

E. Review of Licensing Event Reports (LERs)

1. Tabular Listing

Type of Event

a. Personnel Errors 8

b. Design / Manufacturing /Const/Insta11ation 1

c. External Cause 1

d. Defective Procedure 5

e. Component Failure 5

x. Other _1

Total 21

.- . . - - .-. - - - - . - - . - - . - .-- - - . - -

.

L

r

.*

! Beaver Valley Unit 1 43

2. Causal Analysis

The following set of common mode events were identified:

t a. LERs 85-18 and 86-01 are events caused by the failure of the

i

vital bus III inverter. This is a continuation of three pre-

vious events since January 1985.

! b. LERs 85-19, 86-03, -04, -06, -07, -10, -12, -13, -14, and 87-03

are events that were due substantially to personnel error out-

side the control room (50% of the LERs). Seven occurred during

surveillance testing.

,

c. LERs 86-03, -04, -05, and -07 were related to fire protection

deficiencies in hardware or testing.

l F. Licensing Activities

1. NRR/ Licensee Meetings

December 19, 1985 Enforcement Conference

l

!

October 16, 1986 Counterpart Meeting for Westinghouse 3-Loop

) plant Personnel

January 5, 1987 Cross-training of Unit 1/ Unit 2 Operators

i

! 2. Site Visits / Meetings by NRR Personnel

November 22, 1985 Fire Protection Audit Exit Meeting -

l October 22, 1986 Site Tour regarding fire protection exemp-

tion request

February 11-13, 1986 Detailed Control Room Design Review

'

May 6, 1986 Site Tour and discussions of licensing

status, meeting with Resident Inspectors

July 9, 1986 Site four and SALP Meeting

l

September 30, 1986 Site Tour and discussion of licensing

status, meeting with Resident Inspectors

February 18, 1987 Site Tour and Meeting on Security

3. Commission Briefing

None

,

.

O

Beaver Valley Unit 1 44

4. Exemptions Granted

One on Fire Protection (fire doors)

5. Licensee Amendments Issued / Denied

No. 97 thru 107 were issued. None were denied.

6. Emergency Technical Specifications Issues

None

7. Orders Issued

None

of

_ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ - _ _ _ . _ _ _ _ _ _ _ . .___________ _ __ __ __

.

.

Beaver Valley Unit 1

TABLE 1

INSPECTION REPORT ACTIVITIES

Report No. Inspector Hours Areas Inspected

85-22 Resident 64 Routine resident inspection.

85-23 Specialist 26 Safeguards Inspection.

85-24 Resident 117 Routine resident inspection.

85-25 Specialist 187 Special announced team inspection of 10

Team CFR 50, Appendix R. Fire Protection.

85-26 Resident- 5 Special inspection to review circumstances

Special and licensee action relative to apparent

violation of Physical Security Plan.

85-27 Resident 71 Routine resident inspection,

85-28 Specialist 75 Radiation protection program.

86-01 Resident 67 Routine resident inspection.

86-02 Examiners 0* Examination Report of Operator Licensing

Examinations.

86-03 Cancelled

86-04 Resident 141 Routine resident inspection.

86-05 Specialist 49 Transportation.

86-06 Resident 132 Routine resident inspection.

86-07 Resident 116 Routine resident inspection.

86-08 Specialist 176 Generic letter 83-28.

Team

86-09 Specialist 118 ISI Program and NDE.

86-10 Specialist 120 Radiation protection program during Refuel-

ing Outage.

86-11 Resident 175 Routine resident inspection, plus Chemistry

and Environmental Monitoring Programs.

  • No inspection hours are credited to license examinations.

T1-1

- _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

Beaver Valley Unit 1

Report No. Inspector Hours Areas Inspected

86-12 Specialist 251 10 CFR 50.49, Qualification of Electrical

Team Equipment.

86-13 Specialist 83 Containment Integrity

86-14 Specialist 20 Nuclear Material Control and Accounting.

86-15 Resident 138 Routine resident inspection,

86-16 Examiners 0 Examination Report of Operating License

Examinations.

86-17 Specialist 69 ISI Inspection During SR.

86-18 Resident & 400 Routine resident inspection and Augmented

Augmented Team Team Inspection of Outage Recovery.

86-19 Specialist 31 Security.

86-20 Resident 131 Routine resident inspection.

86-21 Specialist 36 Electrical Modifications and Testing.

86-22 Specialist 37 Cycle 6 Startup Physics Testing Program.

Precritical Tests, Zero Power Physics Tests

and Power Ascension Tests.

86-23 Specialist 32 Maintenance Program and Procedures, Licen-

see actions on LERS and QA/QC Interfaces.

86-24 Resident 119 Routine resident inspection,

86-25 Specialist 8 In-Plant Radiation Protection.

86-26

86-27 Specialist 137 Emergency Preparedness Inspection and Ob-

Team servation of Licensee's Fu11 Scale Annual

Emergency Preparedness Exercise.

86-28 Resident 146 Routine resident inspection.

87-01 Cancelled

87-02 Resident 80 Routine resident inspection.

T1-2

_ _ _ _ - _ _ _ _ _ __-____________________________ -_ _ _ _

.

.

Beaver Valley Unit 1

Report No. Inspector Hours Areas Inspected

87-03 Specialist 32 Security

87-04 Specialist 30 Radiation Protection

,

87-05 Resident 115 Routine resident inspection.

t

I

l

I

l

l

!

>

t

r

T1-3  :

i

_ _ _ - _ - _ - _ _ _ _ _ _ _ _ _ _ _

.

I

O

Beaver Valley Unit 1

TABLE 2

INSPECTION HOUR SUMMARY

Annualized

Area Hours Hours  % of Time

Operations 1029 706 29.7

Rad Protection 384 263 11.1

Maintenance 400 274 11.5

Surveillance 610 418 17.6

Fire Protection-HK 231 158 6.7

Emergency Prop. 154 106 4.4

Sec/ Safeguards 147 101 4.1

Outages 262 180 7.6

'

Licensing 0 0 0.0

Training 0 0 0.0

l Engineerin0 Support 208 143 6.0

+

Assurance of Quality 46 32 1.3

TOTALS: 3471 2381 100.0

,

,

1

i

'

'

l-

)

T2-1

_ _ _ _ _ _ _ - -

1

i

.

Beaver Valley Unit 1

'

TABLE 3

ENFORCEMENT ACTIVITY

A. Violations Versus Functional Area by Severity Level

!

Functional No. of Violations in Each Severity Level

Area V IV III II I Total

1. Plant Operations 2 2

2. Radiological Controls 2 2 4

,

3. Maintenance 1 1 2

4. Surveillance 2 2

5. Fire Protection / Housekeeping 4 4

6. Emergency Preparedness

7. Security & Safeguards 1 1

8. Refueling & Outage Management

9. Licensing

10 Training and Qualification

Effectiveness

11. Engineering Support

12 Assurance of Quality __ __ __ __ __

TOTALS 3 12 15

I

i

i

i

l

T3-1

l

- --_ -_---------- -- - - - - -

_ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.-

, .

Beaver Valley Unit 1

B. Summary

Inspection Severity

, _ Number Requirements Level Area Subject

85-22 10 CFR 20.408 V Radcon Failure to issue radworker

termination exposure reports.

Repetitive.

10 CFR 50, IV Radcon Unplanned & unauthorized

App. B release from Unit 1 to Unit

2 due to inadequate shared

system boundary isolation.

85-25 10 CFR 50, IV Fire Protec- Lack of emergency lighting

App. R, tion * units for safe shutdown

Sec. III-J access routes.

85-26 Security Plan IV Security Protected area access with-

out proper photo-identifi-

cation badge.

86-05 10 CFR 71.5 IV Radcon LSA drums shipped with holes.

(Transporta- No QC check of container

tion) integrity.

TS 6.8 V Radeon Procedure not reviewed on

l (Transporta- 2 year frequency,

tio j)

86-06 TS 4.3.3.5 IV Surveillance Shutdown Panel channel check

I failed to properly identify

l RHR temperatures as in-

operable.

TS 4.3.3.6.1 IV Fire Protec- EDG smoke detector survell-

l

'

tion lance test failed to iden-

tify inoperable channel &

control room alarm function.

l FSAR DEV N/A EDG day fuel oil tanks not

Table 8.1-1 constructed to seismic re-

quirements.

86-08 10 CFR 50.55a IV Fire Protec- R18 control wiring not

IEEE-279 tion * separated by a fire retard-

ant barrier of 6" min, air

space.

T3 2

1

L

- __. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

Beaver Valley Unit 1

Inspection Severity

Number Requirements Level Area Subject

86-08 TS 6.8.1 IV Maintenance Failure to adhere to ad-

(cont.) ministrative controls re-

garding completion of MWR

documentation,

86-11 10 CFR 50, IV Fire Protec- Failure to perform a com-

App. B and R tion * plete sensor to indicator

functional test of RCS cold

leg temp. & failure to

assure BIP transfer keys

functioned.

86-18 TS 6.12.2 IV Operations Failure to control access

to NSS key cabinet contain-

ing high rad area keys.

86-23 10 CFR 50, V Maintenance Failure to follow industrial

App. B safety practices during

battery MSP.

87-02 TS 4.3.1.1.1 IV Surveillance Missed Power Range Monitor

nuclear instrument channel

check during startup.

87/05 10 CFR 50, IV Operations Violation of plant config-

App. B uration control procedures,

resulting in minor gas

release to Primary Auxiliary

Building.

  • It is recognized that these could also be included in an Appendix R, Engineering

or Assurance of Quality section.

T3-3

, _ - _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ __ _ _ _ _ _ _ . _ _ _ _ _ _ _

O

O

Beaver Valley Unit 1

TABLE 4

TABULAR LISTING OF LERs BY FUNCTIONAL AREA

Area Number /Cause Code Total

6 g g g E 3

Plant Operations 2 1 0 0 4 0 7

Radiological Controls 0

Maintenance 1 1

Surveillance 4* 3* 1 1 9

Fire Protection / Housekeeping 1 1 2 4

Emergency Preparedness 0

Security and Safeguards 0

Refueling and Outage Control 0

Licensing

Training and Qualification

Effectiveness

Engineering Support

Assurance of Quality _ _ _ _ _ _

Total 8 1 1 5 5 1 21

  • 0ne LER contained two events that occurred during one trip - startup evolution.

Cause Codes:

A - Personnel Error

B - Design, Manufacturing, Construction or Installation Error

.

C - External Cause

D - Defective Procedures

E - Component Failure

X - Other

T4-1

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

Beaver Valley Unit 1

TABLE 5

LER SYNOPSIS

LER

Number Summary Description

85-17 Inoperable Rod Position Indication System due to computer failure.

85-18 Vital Bus III inverter input fuse failure causing reactor trip.

85-19 Reactor trip due to RCS loop flow instrumentation spikes.

85-20 Out-of-specification PRM nuclear instrumentation rate trip setting.

86-01 Vital Bus III inverter input fuse failure causing reactor trip.

86-02 MSSV left settings outside a110wable Ilmits.

86-03 Partially inoperable fire detection system in diesel Generator area.

86-04 Inadequate fire protection system surveillance test (CO2 flow through

nozzles).

86-05 Inoperable filter bank sprinkler nozzles.

86-06 Mis plu00ed steam generator U-tubes.

86-07 Inoperable fire suppression system smoke detectors.

86-08 Steam generator tube plu0ging.

86-09 failure to perform fuel pool pump survelliance test within ASME required

frequency.

86-10 Train B ESF actuation in Mode 5 due to operator error.

86-11 Hanual reactor trip when four control rods dropped.

86-12 Reactor Trip during RID shunt trip test due to personnel error.

86-13 Operation prohibited by technical specifications when emergency bus

undervoltage relay testing exceeded I hour.

87 01 Reactor trip during turbine pedestal surveillance test due to operator

error, failure to perform PRM low trip setpoint surveillance during

subsequent startup.

87-02 Reactor trip duo to EHC malfunction.

87-03 Inadvertent start of motor driven auxiliary feodwater pump.

T5-1

. _ _ - _ _ _ _ _ - _ ____-____ - ___ _ -___ - ___________ _________________ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

l'

.

Beaver Valley Unit 1  !

ATTACHMENT 1 i

'

TOTAL NUMBER OF SHUTDOWNS AND TRIPS PER YEAR SINCE STARTUP

'

No. of at Power No. of Unplanned

Year Reactor Trips Shutdowns ,

I

l

1976 43 15

'

1

i

1977 47 18

[

1978 25 7  !

1979 15 5

1980* 5 1 i

-

1981 11 1

! l

1982 9 4 i

) 1983 11 3

~

i 1984 5 5 ,

l

'-

1985 8 7

,

t 1986 3 2

'

1987** 2 0

, i

!

  • The plant was shutdown for most of 1980 for major modifications.

(

l **As of 3/15/07. f

f

i

i

!

,

i

j I

!  !

!

!  !'

i

i  !

I

i

l

f

4  :

Al-1

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.

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