ML20211N266

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Evaluation of Licensee Response to Insp Rept 50-302/86-12. Procedure AI-401 Found to Be Inadequate & Resulted in Restatement of Violation 2.Design Error Could Cause Loss of RHR Ability
ML20211N266
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 02/19/1987
From:
NRC
To:
Shared Package
ML20211N244 List:
References
RTR-REGGD-01.033, RTR-REGGD-1.033 GL-85-01, GL-85-1, GL-86-10, NUDOCS 8703020030
Download: ML20211N266 (7)


See also: IR 05000302/1986012

Text

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ENCLOSURE

STAFF EVALUATION OF LICENSEE RESPONSE

INSPECTION REPORT 86-12

Restatement of Violation 2 (86-12-06)

Technical Specification 6.8.2.b requires that certain procedural changes receive

intradepartmental and interdisciplinary reviews by qualified reviewers prior to

approval by the responsible superintendent or manager. The Plant Review

Comittee (PRC) shall then review the 10 CFR 50.59 evaluation within 14 days of

approval.

Technical Specification 6.8.1.a requires that written procedures be established

to cover those activities recomended in Regulatory Guide 1.33, November 1972.

Regulatory Guide 1.33, Section A, recomends that administrative procedures be

established to provide the method for changing procedures.

-Contrary to the above, procedure AI-401, Origination of and Revisions to P0QAM

Procedures, which implements TS 6.8.2.b., was found to be inadequate in that it

allows Housekeeping Changes (HKCs) to be made to procedures and implemented

following approval by the responsible superintendent or manager. These HKCs do

not receive the required review by appropriate intradepartmental and

interdisciplinary qualified reviewers nor are the associated safety evaluations

reviewed within 14 days by the PRC.

As a result, several curves in the OP-103 series, Plant Curve Book, have been

changed using HKCs. These include curves for radiation monitors for the Reactor

Building air and Auxiliary Building liquid release paths and the reactor plant

heatup/cooldown curves.

Additionally, on March 20, 1986, a HKC was used to add a quality control (QC)

hold point to a maintenance procedure (MP-174) without receiving the reviews

required by TS 6.8.2.b.

This is a Severity Level IV violation (Supplement I).

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Sumary of Licensee's Response

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! Florida Power Corporation agrees that Housekeeping Changes (HKCs) should not have

been used to include curves for radiation monitors for the reactor building air

and auxiliary building liquid release paths and the reactor plant heatup/cooldown

l curves. FPC takes exception to the example that a HKC was incorrectly used to

add a QC hold point to MP-174.

Relative to the observation during the performance of MP-174 on March 20, 1986,

,

no new QC inspection / verification requirements were added. The signature blanks

l added to steps 7.2.19 and 7.2.21 were redundant to information already included

in Enclosure 6, which is referenced by steps 7.2.19 and 7.2.21. These signature

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l 8703020030 070219 2

PDH ADOCK 0500

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Enclosure 2

blanks were added for clarity and consistency with other procedures to remind the

person performing the procedure to notify QC prior to proceeding. The addition

of the signature blank and words " Hold Point" to step 7.2.31 was a poor choice of

words, but was not an unapproved change to MP-174 since that step referred the

user to Enclosure 3 which already contained QC inspector verification signature

blank. Again, the signatures were added to the applicable procedure step to

ensure the requirement to notify QC was not missed. These Housekeeping Changes

were made in accordance with the instructions in AI-401, and in FPC's opinion did

not circumvent the procedure review and approval process required by TS 6.8.2.

NRC Evaluation

The NRC Staff has carefully reviewed the licensee's response and notes the

licensee's position that a Housekeeping Change was appropriate in the addition

of a QC Hold Point to procedure MP-174.

.

The staff concurs with the position that the signature block additions to steps

7.2.19 and 7.2.21 were redundant to information included in Enclosure 6 and that

no new inspection / verification requirements were added. The staff does not

concur that the addition of the signature blank and the words " Hold Point" added

in step 7.2.31 were the same as the signature required on Enclosure 3.

The QC signature required on Enclosure 3 is to ensure that a QC inspector has

verified that the new materials to be used have received proper inspection

through the issuance of Quality Control Inspection (QCI) documentation. The

notes on this Enclosure state: "QCI documentation for new materials must be

attached to the work package." and "QC Inspector verify QCI's

Date "

. This inspection could be performed before or after the snubber is

rebuiTt and would not stop personnel from proceeding with subsequent steps in the

procedure. The " Hold Point" added to step 7.2.31, however, requires Enclosure 3

to be completed Crior to proceeding on in the procedure. Therefore, the signature

addition to step 7.2.31 does not have the same meaning as the signature required

on Enclosure 3.

The staff has also reviewed your position on the HKC's. The NRC position on such

procedure changes is that only changes due to typographical errors can be made

without the review required by Technical Specification 6.8.2. All other changes

must be reviewed and approved as required by the Technical Specifications.

NRC Conclusion

For the above reasons, the violation occurred as stated.

Restatement of Violation 3 (86-12-04)

10 CFR 50.73 (a)(2)(v)(B) requires the subnittal of a Licensee Event Report (LER)

within 30 days of the event for any condition that could result in a loss of the

plant's ability to remove residual reactor heat.

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Enclosure 3 I

Contrary to the above, on December 19, 1985, it was determined that a design

error could cause a loss of residual reactor heat removal ability and no LER was

issued.

Summary of Licensee's Response

FPC disagrees with this violation. This design problem was identified and

evaluated by FPC personnel according to established procedures and determined not

to be reportable under 10 CFR 50.73(a)(2)(v)(B). That part of the rule requires

licensees to report, "(v) anj event or condition that alone could have

prevented the fulfillment of the safety function of structures or systems that

are needed to:...(B) remove residual heat;." The design problem (failure to

protect the bearing flush water supply to the Nuclear Services seawater pumps and

the decay heat seawater pumps from fire damage) would not alone have prevented

the function of systems required to remove residual heat. It shoald be noted

that upon uin.overi of liis inisuiiuersi.oiidien) ui Ris v=:iidur- i riiviiiis i.iuie , FFC

performed an analysis, as suggested by Generic Letter 85-01 (superseded by

Generic Letter 86-10), and voluntarily submitted this information to the

appropriate NRC office for review and concurrence. Thus, FPC notified the NRC

even though we chose not to report it via a particular means (an LER). Our

normal practice to carbon copy the NRC Regional Office was not followed due to

administrative oversight. However, the NRC Senior Resident Inspector was, in

accordance with normal practices, copied via FPC's internal distribution.

If fire damaged the systems providing the bearing flush water supply to the plant

during normal power operation, the turbine driven emergency feedwater pump would

have remained available to remove residual heat. To continue to cool down, or

for fire damage occurring at cold shutdown, one train of decay heat removal

equipment including one of the decay heat seawater pumps will remain operable.

If fire damages all sources of bearing flush water (redundant A and B domestic

water pumps plus Nuclear Service closed cycle cooling water supplied through

redundant motor operated valves) only one operating decay heat seawater pump

would be damaged. The non-operating decay heat seawater pump would not be

affected. The non-operating pump would only autostart on an ES signal and

therefore would remain unaffected, since other plant accidents need not be

considered concurrent with a fire (See Branch Technical Position APCSB 9.5-1

l AppendixA,ItemA-4).

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The loss of bearing flush water supplies could disable both Nuclear Service

seawater systems and eliminate the Nuclear Services closed cycle cooling water

heat sink. However, the Nuclear Services closed cycle cooling pumps would remain

operable for the purpose of supplying bearing flush water for the decay heat

r seawater pumps through either of the two redundant motor operated valves. Manual

l action may be required to open one of the motor operated flush water supply

valves depending on specific fire damage. Sufficient time for manual action

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would be available before the decay heat system was required, and access to the

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area following a fire would not be a problem since the duration of an

unsuppressed fire from the combustion of all material in the area has been

conservatively evaluated to be approximately 12 minutes. This fire duration

estimate takes no credit for sprinklers or fire barriers around cable trays that

now exist in this area.

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Enclosure 4

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The Inspection Report fails to note that this entire area would not meet literal

Appendix R requirements and thus a Technical Exemption for this fire area was

sought and granted. The primary technical basis for this exemption is detection,

suppression, amount of combustible materials, and room geometry (high ceiling

with hot gas traps inherently present). These continued to exist and supported a

reduced level of concern with regard to the identified error. FPC continues to

maintain that this design error did not create a reportable condition under

10 CFR 50.73(a)(2)(v)(B).

NRC Evaluation

The licensee stated, that the design problem, of failure to protect the bearing

flush water supply to the Nuclear Services Seawater Pumps (RWP) and the Decay

Heat Seawater Pumps (DCP) wcid not alone have prevented the function of systems

required to remove residual heat. On December 19, 1985, in a letter to the

Licensing Project Manager (LPM), NRR, the licensee provided their fire protection

evaluation of the Domestic Water Supply to Nuclear Services Seawater Pumps and

decay heat seawater pumps bearings. In this evaluation FPC identified that the

RWPs are considered hot shutdown equipment and the DCPs are considered cold

snutdown equipment. The licensee's evaluation states that, "... without either A

or B domestic water pump, or without opening of either redundant back-up supply

valve from the Nuclear Service Closed Cycle Cooling Water System, the seawater

pumps would fail."

The staff's review of the MAR Package included review of the licensee's

Nonconformance Operations Report (NCOR), No.85-209. This NCOR also identified

the cause of the event as a design error in that the analysis of the domestic

water supply was not included in the Appendix R design. The evaluation and NCOR

clearly identify this condition was a result of design and analysis inadequacies

of the original Fire Hazards Analysis in that none of the redundant bearing

Flushwater Systems for the safe shutdown equipment were analyzed for the effect

of fire within fire area AB-95-3T.

10 CFR 50.73(a)(2)(vi) states that events covered in paragraph (a)(2)(v) of this

section may include discovery of design and analysis inadequacies.

As stated in the violation 10 CFR 50.73(a)(2)(v)(B) the licensee shall submit a

LER for any event of the type in this paragraph.

It appears that the NCOR, however, in Parts 2, 3, and 4 does not indicate any

reference to a review of this event against the reporting requirements of 10 CFR

50.73. The licensee's response appears to justify their action of voluntarily

submitting their evaluation information to the NRC/NRR office on December 19,

1985, in lieu of a LER as a means suggested by Generic Letter (GL) 86-10. This

item was addressed by paragraph "C" of the GL as related to Fire Area Boundaries.

Also in the Generic Letter, paragraph E, the licensees are reminded of their

obligation to notify the NRC of Fire Protection deficiencies which meet the

criteria of 10 CFR 50.72 or 10 CFR 50.73. In fact, several comments within the

evaluation columns of Part 2 and 3 of Enclosure 1 to Procedure CP-111, Rev. 32,

indicate that the event was considered significant, but further guidance was

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-Enclosure 5

required to determine the-safety significance, yet the event was not identified

as reportable.

Paragraph 2 and '3 of the licensee's response appear to discuss the plant's

operational and-technical aspects of its non-compliance with the requirement of

Appendix R and FPC's evaluations to justify the corrective actions taken. These

aspects discussed, however, are not gemain to the issue of the reportability of

a design and Fire Hazards Analysis . inadequacy as described in the proceeding

paragraphs. Also, the licensee stated that the Ins

that a Technical Exemption for Fire Area (AB-95-32)pection

was sought Report failedThe

and granted. to note

licensee should be reminded that this Technical Exemption applied specifically to -

the separations-of the RWP and SWP where the protection of redundant pump power

circuits in one hour fire enclosure / wraps was provided. At the time of the

inspection, this ~ same level of fire protection was not provided for the circuits

of the domestic water pumps (D0P-2A, 2B) or the redundant Motor Operated Valves

(D0V-210,238) which are located within the same fire zone, AB-95-3T.

NRC Conclusion

Based upon the NRC staff's review as outlined above, we conclude that FPC's

discovery of the _ design and analysis inadequacies in the plant Fire Hazards

Analysis as related to loss of the bearing flush water supplies to safe shutdown

equipment did in fact constitute an event as defined by 10 CFR 50.73(a)(2)(vi)

and that these deficiencies were not properly reported in accordance with the

requirements of 10 CFR 50.73(a)(2)(v)(B). For the above reasons, the violation

occurred as stated.

Restatement of Deviation (86-12-05)

In a letter to the Nuclear Regulatory Commission from Florida Power Corporation

dated December 19, 1985, the licensee identified a design error that could result

in a loss of the Nuclear Services Seawater and the Decay Heat Seawater pumps in

the event of a fire. In the corrective actions for this design error, the

licensee committed to continue 20-minute roving fire watches until such time that

plant modifications to prevent this loss of pumps were completed.

Contrary to the above, at 2:00 p.m., on March 14, 1986, the roving fire watch was

secured even though the plant modification for these pumps was not completed.

Summary of Licensee's Response

FPC disagrees with this deviation. FPC maintained a level of protection for the

functions at risk that was appropriate to the hazard that existed. This

protection included periodic surveillance by roving security officers and plant

operators. Their normal duties include observation of abnomal conditions,

including fire, and response to those conditions. The FPC letter of December 19,

1985, referenced in the Notice of Deviation, was a fire protection evaluation

-forwarded under the guidance of draft Generic Letter 85-01 as reaffirmed by

Generic Letter 86-10. FPC chose this approach in a proactive effort to keep the

.NRC staff aware of our fire protection activities. The alternate approach

offered by draft Generic Letter 85-01 was simply retaining this evaluation in our

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Enclosure- 6

files available for review. Since the second alternative existed FPC felt

justified in adjusting our compensation to the hazard at the time.

FPC's letter noted the 20-minute roving fire watch was in place at that time. In

addition, it stated " Roving fire watches will continue in.the areas containing

components necessary for maintenance of the current bearing flush water supply l

until modifications are complete." This commitment does not state the 20-minute l

frequency would be maintained without regard to plant status- '

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At the time the evaluation was written, Crystal River Unit-3 (CR-3) was in power

operations and 20-minute roving fire watches were being used as compensation in l

the auxiliary building for uncompleted fire barrier construction around cable

trays and conduits. At the time of the alleged deviation CR-3 had been shutdown

for approximately two and one half months and all cable and conduit fire barrier

construction had been completed. FPC believes the fire protection provided in

the area, which included operable automatic sprinklers, operable automatic fire

detection, and roving patrols by security and operations personnel, was adequate

for the hazard.

Prior to discontinuing the 20-minute roving fire watches -which had been

established as part of Appendix R Schedular Exemption, FPC Licensing contacted

both the NRR Fire Protection Reviewer and the NRC Senior Resident Inspector for

CR-3. FPC contacted the NRR Fire Protection Reviewer regarding the Appendix R

requirements when the plant is in cold shutdown. Based on discussion regarding

the fact that Appendix R requirements are not clearly defined when the plant is

in cold shutdown, FPC was justified in modifying the protection to more closely

match the hazard. On March 13, 1986, one day prior to discontinuing the fire

watches, FPC Licensing informed the Senior Resident Inspector for CR-3 that the

20-minute roving fire watches were being discontinued. FPC informed the Senior

Resident this was because the schedular exemption modifications were complete and

because we were not aware of any specific Appendix R guidelines applicable to

cold shutdown. The Senior Resident was also informed the seawater pumps bearing

flush water modification was not complete. There was no discussion with the

Senior Resident Inspector specifically addressing the commitments in FPC's

December 19 letter, but there was no objection voiced to the discontinuance of

the 20-minute roving fire watches.

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It is FPC's position that sound fire protection was maintained for the seawater

pumps, that our actions were taken after careful consideration of the guidance

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that exists, and after consultation with NRC staff. Based on the foregoing, FPC

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requests this Deviation be withdrawn.

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j NRC Evaluation

In a letter to the NRC licensing project manager (LPM) from Florida Power

Corporation dated December 19, 1985, the licensee identified an inadequacy of

their Fire Hazards Analysis of failure to identify and to protect the bearing

flush water supply to the Nuclear Services Seawater and Decay Heat Seawater pumps

which are considered hot shutdown and cold shutdown equipment, respectively. In

the corrective actions, FPC in lieu of providing fire protection features in

accordance with Appendix R,Section III.G.2.a, b or c, elected to perform a plant

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Enclosure 7

modification which would provide bearing flush water to both the Nuclear Services

and Decay Heat Seawater pumps from the pumpage of the seawater pumps themselves.

FPC in their December 19, 1985 letter indicated that these modifications would be

completed by March 31, 1986, and that the compensatory 20 minute roving fire

watches, which were required and approved by the NRC in order to provide FPC

scheduled relief to complete Appendix R modifications, would be continued in the

areas containing components necessary for maintenance of the current bearing

flush water supply until the flush water modifications were complete.

Based on NRC Region II's review of FPC's December 19, 1985 submittal, the region

concluded no additional compensatory measures were required of FPC and that the

existing 20 minute roving fire watches would provide sufficient assurance that,

during all modes of plant operation, a fire would be detected and suppressed

prior to causing fire damage to redundant seawater pump bearing flush water

systems.

Although, the Senior Resident Inspector was notified that the 20-minute roving

fire watches were being discontinued, he was not informed that this action was

being taken contrary to the commitments made in the December 19, 1985 letter. In

addition, it is our policy that relief from commitments made to the NRC cannot be

verbally granted by the Senior Resident Inspector. It is the licensee's

l responsibility to comply with all commitments made unless granted relief through

proper channels.

NRC Conclusion

For the reasons stated above, we conclude that on March 14, 1986, FPC deviated

from their December 19, 1985 fire watch commitments.

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