ML20148K746

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Insp Repts 50-259/88-04,50-260/88-04 & 50-296/88-04. Violations Noted.Major Areas Inspected:Operational Safety, Maint Observation,Surveillance Testing Observation, Ros,Previous Enforcement Action & Restart Test Program
ML20148K746
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 03/22/1988
From: Bearden W, Brooks C, Christnot E, Ignatonis A, Andrea Johnson, Paulk G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20148K733 List:
References
50-259-88-04, 50-259-88-4, 50-260-88-04, 50-260-88-4, 50-296-88-04, 50-296-88-4, NUDOCS 8803310292
Download: ML20148K746 (23)


See also: IR 05000259/1988004

Text

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                                                                                                                         UNITED STATES
                                                                                                            NUCLEAR REGULATORY COMMISSION
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                                        Report Nos.            50-259/88-04, 50-260/88-04, 50-296/88-04
                                        Licensee: Tennessee Valley Authority
                                                    6N 38A Lookout Place
                                                    1101 Market Street
                                                    Chattanooga, TN 37402-2801
                                        Docket Nos.             50-259, 50-260, and 50-296
                                        License Nos. OPR-33, DPR-52, and DPR-68
                                        Facility Name:                           Browns Ferry Nuclear Plent
                                        Inspection Conducted:                                               February 1-29, 1988
                                        Inspectors:                         Of[dh
                                                               G. L. Pfulk, Senior R(s'iderip Inspector
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                                                                                                                                                                                                                                                   Date Signed
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                                                                                                                                                                                                                                                   Date /$igned
                                                               C.R. Bro 6k.s,ResidehtIngector
                                                                                 6 -/d C o- b _ _ S                                .O n                                                                                                      3//             <//P9_
                                                                                                                                                                                                                                                   Date Signed
                                                                E. F. Chrthtnot, Resipent [nspector
                                                                       hbi er
                                                               W. C. Bepirden, Resid(nt In{pectbr
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                                                                                                                                                                                                                                                   Date Signed
                                                                                          AhE A-wo-t                                                                                                                                             5//fbY    ~
                                                                                                                                                                                                                                                   D' ate Signed
                                                               A. H. Johtison, Project Engipeer
                                        Approved by:                                          $ b . ,~)h,4hdm                         ~
                                                                                                                                                                                                                                                     3A             '
                                                                     A. J. Itifatchis'f 5ection                        7          Chief,                                                                                                            Da e Si       e
                                                                       Inspection Programs
                                                                      TVA Projects Division

l SUMMARY

                                        Scope: This routine inspection was in the areas of operational safety,
                                        maintenance               observation,                                   surveillance           testing            observation,                                                                                  reportable

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                                        occurrences, previous enforcement action, restart test program, employee

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                                        concerns, design controls and quality surveillance report reviews.
                                        Results:     Two violations were identified: (1) two examples of inadequate
                                        procedures or failure to follow procedures for QA records preparation and
                                        workplan control, (2) failure to correctly translate the design basis into
                                        specifications and drawings.
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                                                           REPORT DETAILS
       1.    Licensee Employees Contacted:
             C. C. Mason, Senior Manager, Operations Center
            H. G. Pomrehn, Site Director
          *J. G. Walker, Plant Manager
             P. J. Speidel, Project Engineer
          *J. D. Martin, Assistant to the Plant Manager
          *R. M. McKeon, Operations Superintendent
             J. S. Olsen, Superintendent - Units 1 and 3
             T. F. Ziegler, Superintendent - Maintenance
          *0. C. Mims, Manager - Technical Services Supervisor
             J. G. Turner, Manager - Site Quality Assurance
             M. J. May, Manager - Site Licensing
          "J. A. Savage, Compliance Supervisor
             A. W. Sorrell, Site Radiological Control Superintendent
             R. M. Tuttle, Site Security Manager
          *L. E. Retzer, Fire Protection Supervisor
          *H.            J. Kuhnert, Of fice of Nuclear Power, Site Representative
             Other licensee employees contacted included licensed reactor operators,
             auxiliary operators, craftsmen, technicians, public safety officers,
             quality assurance, design and engineering personnel.
          * Attended exit interview
       2.    Exit Interview (30703)
             The inspection scope and findings were summarized on February 26 and
             March 4, 1988 with the Plant Manager and Superintendents, and other
             members of his staff. New items identified:
             a.                      Violation (259.260,296/88-04-02) Two examples for failure to follow
                                     procedures for QA records preparation and work plan control,
                                     paragraphs 5.a and 11.
             b.                      Violation (259,260,296/88-04-03) Failure to correctly                         translate
                                     design requirements into drawings, paragraph 11.
             c.                      Unresolved Item *(259,260,296/88-04-01)       A problem with security
                                     administrative controls and documentation for out of service
                                     equipment, paragraph 5.a.
              d.                     Inspector Followup Item (259,260,296/88-04-04) Single failure
                                     criteria involving emergency core cooling systems. Identified as
                                     part of restart test program.
           *An Unresolved Item is a matter about which more information is
              required to determine whether it is acceptable or may involve a
              violation or deviation.
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          e.         Inspector Followup Item (259,260,296/88-04-05) Diesel Generator
                     field breaker sizing and excessive heat in DG panel. Identified as
                    part of restart test program,
           f.         Inspector Followup Item (259,260,296/88-04-06)                         Filter capacitors
                    missing from battery charger B.
           The itcensee acknowledged the findings and took no exceptions. The
           licensee did not identify as proprietary any of the materials provided to
           or reviewed by the inspectors during this inspection.
           Commissioners Carr and Bernthal made visits to the site during this

l report period. General discussions were held with TVA management and NRC l staff.

       3.   Licensee Action on Previous Enforcement Matters (92702)
            (CLOSED) Violation (259,260,296/84-15-08) This violatior resulted from
            inspector review of plant drawings. The violation stated that Revision 2
            to TVA drawing 47W847-10 was found in the Technical Support Center (TSC).
            However, the current revision at that time should have been Revision 3.
            The out-of-date drawing was removed and the current revision of drawing
            r7W847-10 placed in the TSC. All Drawing Control Center issue clerks have
            been cautioned concerning the need for absolute accuracy in the drawing
            fi'ing process.              Additionally, the licensee is involved in an ongoing
            prote",s of review and improvement of plant drawings including replacement
            of r.xisting drawings with Configuration Control Drawings (CCDs).
            The licensee has addressed the inspectors concern as stated in the
            original inspection report and corrective action should be adequate to
            preclude recurrence. This violation is closed.
       4.   Followup of Open Inspection Items (92701)
            (CLOSED) Inspector Follow-Up Item (259/87-14-01) This item resulted from
            an inspector followup of an event which occurred during the performance of
            the monthly surveillance test on the 3 ED Diesel Generaict (DG). Failure
            of the C phase fuse conta:ts in the DG exciter potential transformer
            circuitry resulted in initiation of Standby Gas Treatment, refutling zone
             isolation, control room emergency ventilation, Unit 3 half-sc am, and
            primary containment isolation.             The cause of the failure was the line
             side of the fuse stab for the C phase becoming worn making little or
             rio contact.      This condition resulted in arcing across the contacts,
             subsequent cable damage and phase-to-phase fault. Numerous components,
            wiring and cabinet structures were damaged and the DG was secured and
             made inoperable.
             The licensee subsequently issued LER 87-08 which identified this failure
             and outlined the following corrective action:
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                            Inspection of Control Cabinets of remaining 7 DGs
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                       All 4160 volt potential transformer fuse contacts in plant to be
                       inspected
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                       Maintenance procedures to be revised to require inspection and
                       maintenance of all 4160 volt fuse contacts on regular basis
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                       Based on the results of an engineering evaluation which deter-
                       mined that these fuses were unnecessary, the fuse and spring
                       finger contacts will be bypassed on all 8 DGs
          The licensee's failure evaluation and assessment of generic ramifications
          associated with this event are adequate,         This item is being closed and
          the implementation of the above correc;1ve action will be tracked as part
          of the followup on LER 87-03. This item is closed.
          (CLOSED) Unresolved Item (259,260,296/87-30-02) CREV Inoperable Due To
          Excessive Flow. This item was opened when the inspector noted that the
           licensee's original LER 87-14 was not adequate i .e. , did not explain
           the problem with Control Room Emergency Ventilation or discuss safety
          consequences.         Also missing were dates and times the equipment was
            inoperable.
           Subsequent to this finding LER 259/87-14 Rev. I was issued. The inspector
           reviewed the newer revision to the LER and found it adequate, addressing
           the inspector concerns.          Additionally, the inspector reviewed the
            licensee's evaluation of effects on 10 CFR 50 Appendix A, accident
          exposure limits which would have resulted from reduced filter efficiency.
          The LER will remain open pending further review by the staff; however, the
            inspector determined that the licensees evaluation was adequate for the
           purpose of closing this item. This item is closed.
       5. Operational Safety (71707, 71710)
          The inspectors were kept informed of the overall plant status and any
            significant safety matters related to plant operations. Daily discussions
          were held with plant management and various members of the plant operating
            staff.         ,
           The inspectors made routine visits to the control rooms when an inspector
           was on site.         Observations included instrument readings, setpoints and
            recordings; status of operating systems; status and alignments of
            emergency standby systems; onsite and of f site emergency power sources
            available for automatic operation; purpose of temporary tags on equipment
            controls and switches; annunciator alarm status; adherence to procedures;
            adherence to limiting conditions for operations; nuclear instruments
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     operable; temporary alter &tions in effect; daily journals and logs; stack
     monitor recorder traces; and control room manning. This inspection
     activity also included numerous informal discussions with operators and
     their supervisors.
     Generai plant tours were conducted on at least a weekly basis. Portions
     of the turbine building, each reactor building and outside areas were
     visited.    Observations included valve positions and system alignment;
     snubber and hanger conditions; containment isolation alignments;
     instrument readings; housekeeping; proper power supply and breaker;
     alignments; radiation area controls; tag controls on equipment; work
     activities in progress; and radiation protection controls.           Informal
     discussions were held with selected plant personnel in their functional
     areas during these tours.
     In the course of the monthly activities, the inspectors included a review
     of the licensee's physical security program. The performance of various
     shifts of the security force was observed in the conduct of daily activi-
     ties to include; protected and vital areas access controls, searching of
     personnel, packages and vehicles, badge issuance and ret rieval, escorting
     of visitors, patrols and compensatory posts.       In addition, the inspectors
     observed protected area lighting, protected and vital areas barrier
     integrity.
     a.    Security Concerns
           During a routine tour on February 15, 1988, the inspector inter-
           viewed the secondary alarm station (SAS) watchstander regarding the
           operability of his closed-circuit television (CCTV) display screens.
           The screen for a certain can.e ra was blank but no maintenance
           request (MR) sticker or deficiency tag was hung.       The watchstander
           was unable to determine why the camera was out of service so he
           contacted the Central Alarm System (CAS). CAS personnel knew that
           the camera was out of service but they did not know which program
           controlled the work activity or when the camera could be expected to
           be available. The inspector was able to trace the work to Engineer-
            ing Change Notice (ECN) 286 and Workplan 0017-86. Work started in
           July 1987, and the camera had been out of service since December 1987.
           The workplan had been bogged down with problems for some time and had
           recently been put on complete hold until a coordinating activity was
           completed. This was expected to keep the camera out of service until
           about June 1988.      The inspector learned from the modification
           engineer that the camera could be restored to an operable status by
            simple tasks requiring only a few man-hours of work. After being
           asked for a re-evaluation of the situation, the licensee immediately
            implemented the necessary work and returned the camera to service on
            February 19, 1988. In following up on this activity the inspector
           categorized and reported his concerns to plant management as follows:

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   (1) There was a lack of aggressive action to restore security
        equipment to service.    Equipment out of service necessitates
        some compensatory action,    The number of compensatory measures
        on-site are excessive and each additional one adds to the
        overall vulnerability of the facility. This was a finding by
        the Regulatory Effectiveness Review (RER).
   (2) There was a lack of understanding by some on shif t security
        personnel of the status of security equipment.          Although
        appropriate compensatory measures were in effect for the camera,
        at least one individual thought the camera was in service, one
        individual thought the camera could be turned on if needed and
        others didn't know the status of the camera at ell.
   (3) There was a lack of attention to detail in completing the
        programmatic paperwork associatecl with removal of security
        equipment from service.      Individuals requesting removal of
        security equipment from se'"ice or degradation of a security
        barrier are required to 4:i out Form BF-117 as described in
        Standard Practice 11.5, Removal of Security Equipment From
        Service,   A portion of this form is used to document any
        applicable compensatory measures and an approval signature is
        required from the security shif t supervisor along with the time
        and date approval is given. The BF-117 form for removal of a
        certain camera did not have the required compensatory measures
        indicated nor was any signature obtained.     This was also the
        case for approximately half of the active BF-117 forms reviewed.
        Another abuse of the form was the expected duration block. This
        block was listed as indefinite for the camera re-wiring work and
        several other jobs in progress as well.
   (4) There was a lack of feedback to the security shift supervisor
        when jobs were completed which required removal of 'a security    '
        device from service or partial degradation of a security
        feature. This resulted in several 8F-117 forms being maintained
        in an active status long after completion of the job. As an
        example, the BF-117 form for the opening of a vital area was
        initiated by the project engineer for the recirculation system
        safe-end replacement job. Authorization was requested for the
        duration of the safe-end replacement; however, this job had been
        finished for about nine months.
   (5) An attitude existed among security shif t personnel such that
        they "lived with" a recurring equipment deficiency as opposed to
        pursuing a permanent repair. There was an additional attitude
        among the maintenance personnel responsible for security
        equipment such that they f ailed to believe a problem existed.
        The inspector witnessed such a problem on a camera on
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               February 15, 1988. The picture gradually lost focus until the
               picture was lost and replaced by a pattern of bars for a brief
               period of time and then the picture returned.    This cycle repeated
               itself several times while the inspector was interviewing the
               SAS watchstander. The SAS watch was completely unaware of why
               the camera performed in that manner. Watchstanders in the CAS;
               however, were very familiar with the problem and indicated
               that it was a common problem among some specific cameras not
               restricted to just a certain camera.      It was termed "crow-
               barring" and was apparently caused by a problem with the
               automatic iris adjustment. Maintenance personnel were initially
               unfamiliar with a description of the problem and af ter a short
               period of evaluation concluded that the problem only exhibited
               itself during certain times of the day. This explanation was
               rejected by the inspector since the problem was witnessed on an
               overcast day in the morning. The inspector requested a further
               evaluation of the problem.
   It should be noted that throughout this review, appropriate compensatory
   measures were being maintained when required. The problem was with the
   administrative controls and documentation which were established in order
   to assure appropriate control was maintained.       The number and character-
   ization of findings in this area indicate a definite potential for an
   actual breakdown in compensatory measures to occur. These findings will
   be tracked as an Unresolved Item (259,260,296/88-04-01) for failure to
   adhere to security procedures pending a followup inspection by Region II
   Security Inspectors.
   One additional problem outside the security organizations responsibility
   was noted during this review. The workplan control form (Form BF-62) for
   workplan WP0017-86, Cable Pull and Camera Support for Permanent Power
   Installation, was not properly completed.       Step IV.B required a check on
   whether any plant equipment is to be removed from service by the workplan
   and Step XI required the Shif t Engineer to give permission to take any
   equipment out of service. The workplan did not specify that the security
   CCTV's would be taken out of service nor was the shift engineer's
   permission obtained. This deficiency was discussed with the plant
   management and modifications representatives as an example cf a violation
   for f ailure to adhere to procedures (259,260,296/88-04-02).
   b.    Operator Logs
         The quality of Reactor Operator logs was dis:ussed with plant
         nanagement personnel on February 19, 1988. The need for continuing
         oversight by operations supervisor > was stressed. Some logs continue
         to have legibility problems and even logs that are legible are
         sometimes unintrepretable even by personnel with a good understanding

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     of plant equipment, programs, and procedures. Entries are made which
     identify a procedure in progress by number without stating the title
     of the procedure so that proper documentation of the activity is
     made. Many abbr 2viations, acror.yms and initialisms are used without
     a list of such a;. proved shortcuts. Carbon copies are maintained in
     the control room logbook while original sheets are routed for review.
     All of these factors make it difficult to interpret activities
     performed during the shift without asking for a line-by-line
     interpretation by the operator on-shift.              Another recurring
     deficiency was the use of a temporary "scratch pads" by the unit
     operators.     Contemporaneous log entries are not made at the time of
     an occurrence. Operators make entries on a temporary scratch pad
     during the shift and then at some point prior to shif t turnover
     transfer these entries into the official log.          This process lends
     itself to potential abuse in that a temptation exists that embarras-
     sing or sensitive entries may not be transferred to the legal
     logbook. Guidance as contained in Standard Practice 12.24, Conduct
     of Operations, was found to be confusing.            In one portion the
     Standard Practice reads:
            "Lags are legal records and shall be kept in a neat, legible
            manner. All entries shall be made at the time indicated on the
            log. If any log readings are missed, the reason shall be stated
            on the log. Write-overs, white-out, or erasures shall not be
            allowed on any station logs. Mistakes shall be crossed out with
            a single line, initialed and dated by the person maintaining the
            log.    All log entries, as well as other documentation,
            signatures and initials shall be made in black ink only. All
            log entries (Shif t Engineer, Unit Operator or Radwaste Logs)
            must be written clearly, precisely and completely.          The log
            books are an official record and as such all entries should be
            thought out as to understanding of an event and future reada-
            bility by others.      The records of events must be documented to
            the fullest extent".
     Another section of the Standard Practice; however, reads:
            "Log Books, Charts, Turnover Sheets, etc. are official records
            and mirror the conduct of the operations at Browns Ferry. They
            must be maintained in a professional manner. Continuity of log
            entries, specifically systems logged out of service and entries
            identifying problems, must be maintained.            To this end,
            operators are encouraged to maintain "scratch pads" to maintain
            records of out-of-service equipment and        eturn to service for
            subsequent entry into the logs.         The scratch pads may be
            destroyed after use. Formal logs are to be maintained as up to
            date as practical during the shift."
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                            Section 4.1 of the Nuclear Quality Assurance Manual, Part III
                            contains the licensee's requirements for permanent QA records.           l
                            Paragraph 6.1 states that written instructions that cover QA records     l
                            preparation shall include requirements to ensure that QA records are     ;
                            complete, legible, and in black ink or other permanent medium. An
                            exception is allowed to the permanent medium requirement which allows
                            some documents to be prepared in a nonpermanent medium. The document
                            must be converted to a p?rmanent medium prior to final approval and
                            the nonpermanent document must remain under the control and
                            responsibility of the supervisor who gives final approval of the
                            document.    Standard Practice 12.24 does not contain any control        ,
                            measures over the nonpermanent scratch pad. This is a violation of
                            10 CFR 50 Appendix B, Criterion V for failure to have an adequate
                            procedure for preparation of operating logs (259,260,296/88-04-02).
                         c. Posting of Notices and Information to Workers
                            The inspector verified posting of information as required by the
                            Nuclear Regulatory Commission was met in accordance with 10 CFR 19,
                            10 CFR 20 and 10 CFR 21. The Browns Ferry Site Director Standard
                            Practice 2.3 delineates posting requirements as specified in the Code
                            of Federal Regulations.
                            The following deficiencies were noted:
                                 (1) The Notice to Employees (Attachment 1) of SDSP 2.3
                                       references employees to use of the Nuclear Safety Review
                                       Staff (NSRS) for employee concerns not able to be handled
                                       through line management. This attachment should be updated
                                       since the NSRS no longer exists.
                                 (2) The annual summary of work injuries and illnesses was not
                                       posted by February 1 as required by SDSP 2.3.    Additionally
                                       errors exist on the location where posted column of SDSP
                                       2.3 in that new areas for posting have been selected
                                       without updating the procedure.
                                 (3) Documents required for pnsting by the 10 CFR 19, 20, and 21
                                       cannot be examined at the location given in SDSP 2.3.
                                       Corrections to the procedure should be made to correct
                                       these location errors.
                            Upon notification by the inspector the licensee took corrective
                            action to address these deficiencies.                                    I
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                         d. The inspectors audited a training course conducted by Westinghouse
                            for Operations Department personnel entitled "Conduct of Operations".
                            The goal of the class was to increase awareness of the importance of

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                                                                                   conducting Browns Ferry Station operations in an attentive, diligent
                                                                                   and conscientious manner. The concept of professionalism was
                                                                                   discussed throughout the session.             Events in other industries      l
                                                                                   including airlines, railroads, shipping and chemical plants were              1
                                                                                   assessed and operator errors which contributed to those events were
                                                                                   discussed. The Chernobyl event was discussed in detail. Barrier
                                                                                   analysis was used to analyze these events with emphasis on operator
                                                                                   performance in event mitigation. The course was very well received
                                                                                   by the attendees and was considered to be outstanding.
                    6.                                                Maintenance Observation (62703)
                                                                       Plant maintenance activities of selected safety-related systems and
                                                                       components were observed / reviewed to ascertain that they were conducted in
                                                                       accordance with requirements. The following items were considered during
                                                                        this review: the limiting conditions for operations were met; activities                 !
                                                                       were accomplished using approved procedures; functional testing and/or
                                                                       calibrations were performed prior to returning components or system to
                                                                         service;        quality control records were maintained; activities were
                                                                        accomplished by qualified personnel; parts and materials used were
                                                                        properly certified; proper tagout clearance procedures were adhered to;
                                                                        Technical Specification adherence; and radiological controls were
                                                                         implemented as required.

l Maintenance requests were reviewed to determine status of outstanding jobs ,

                                                                        and to assure that priority was assigned to safety-relat1d equipment                    t
                                                                       maintenance which might affect plant safety. The inspectors observed the                 l
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                                                                        below listed maintenance activities during this report period:
                                                                                   a.    RHRSW Coupling Replacements                                            -

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                                                                                   b.    3A Diesel Generator Yearly Inspection
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j In response to an inspector concern raised at an NRC daily management

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                                                                        meeting on February 7, 1986, the licensee has completed an inspection and
                                                                         evaluation of a structural crack noted in the plant off gas stack, TVA
                                                                         engineers conducted a physical / visual survey of the off-gas stack's

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                                                                         exterior and all accessible interior surfaces. The survey of the exterior
i                                                                          surf aces (f rom the base to the first platform, first platform to the
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                                                                           second platform and se on), was conducted or December 11, 1987, and the
                                                                         accessible interior surfaces on December 14, 1987.               The results/ findings
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                                                                         of this survey are documented in BFEPC1 Calculation No. CD-Q0066-871856,               '

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                                                                           showing all turface cracks visually identified and located in plans and
                                                                         developed elevations of the stack.                                                     ;
                                                                         TVA's conclusion was that the cracks are not evidence of a structural
                                                                         defect.        The cracks are minimum (mostly hairline) ir, size, no concrete
                                                                           spalling ar.d no Stain found in cracks to signify rusting of rebars.              It
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      was TVA's judgement that the most probable cause of these surface cracks
      would be the temperature variation that the stack has been exposed to
      since construction.      Browns Ferry Engineering Project considers this
      effort complete and the subject closed /dispositioned.
      No violations or deviations were observed in this area.
   7. Surveillance Testing Observation (61726)
      The inspectors observed and/or reviewed the below listed surveillance
      procedures. The inspection consisted of a review of the procedures for
      technical adequacy, conformance to technical specifications, verification
      of test instrument calibration, observation on the conduct of the test,
      removal from service and return to service of the system, a review of te>t
      data, limiting condition for operation met, testing accomplished by
      qualified personnel, and that the surveillance was completed at the
      required frequency.
      During a review of Surveillance Instruction 4.7 F.3 for the SI upgrade
      program, the licensee noticed that the corresponding technical specifica-
      tion (4.7.F.2.6) required cold DOP for in-place leak testing of HEPA
      filters.   It was thought that the test method in use since 1976 was a hot
      DOP test.    As a result the licensee declared the Standby Gas Treatment
      System inoperable as well as the Primary Containment Purge and Control
      Room Emergency Ventilation Systems which have similar testing require-
      ments. After further review the licensee now considers its test method to
      comply with the cold D0P test requirement but no explicit definition of a
      hot versus cold DOP test can be found. System operability was reinstated.
      To avoid a future misunderstanding, the licensee intends to submit a
      technical specification change to clarify the required testing method.
   8. Quality Surveillance Report Reviews (40704)
      The licensee program of quality surveillance survey results was reviewed
      by the inspector to assure proper review adequacy, quality assurance
      program satisfactorily implemented, and quality control program surveys
      conducted in accordance with procedures.       The following quality surveil-
      lance section results were reviewed:
             a.   Restart Test Program - QBF-S-SS-0074
             b.   Poner Stores Package Searches - QBF-5-SS-0057
             c.   Qaality Requirements for 1/4 inch and smaller OD tubing -
                  Q3F-5-SS-0032
             d.   Purchase Orders / Specifications-QBF-5-SS-0086
             e.   Grouting and Dry - Packing of Base Plate and Joints - QBF-S-
                  -99-0063
                                         _ ____ ____________________-___________________                                     ___     ____       -    . _ _ _ _ _
  .   ..
               '
         .                                                                                          11
                        f. Radiological Emergency Plan Training: Operations Support Center
                           Staff - QBF-S-88-0063
                        g. NRC Commitment Verification - QBF-S-88-0067
                        h. NRC Bulletin 79-14 Phase II Walkdown-QBF-S-88-0076
                        1. Condenser Tube Pullout - (BF-S-88-0058
               The surveys reviewed were thorough and noted significant deficiencies that
;              required correction.                                                      The surveys adequately addressed the QA and
               programmatic requirements.                                                     No concerns were noted,
'
          9.   Reportable Occurrences (90712,92700)
               The below listed licensee events reports (LERs) were reviewed to determine
               if the information provided met NRC requirements, The determination
               included: adequacy of event description, verification of compliance with
               technical specifications and regulatory requirements, corrective action
               taken, existence of potential generic problems, reporting requirements
                                                                                                                                                                 '
               satisfied, and the relative safety significance of each event.                                                                 The
               following licensee event reports are closed:
               LER No.                                                                   Date                Event
               259/84-23 Rev. 1                                                          5/18/84             Primary Containment
                                                                                                              Isolation System                                   ;
                                                                                                              Initiation                                         ,

'

               259/85-49 and Rev. I                                                      6/23/85              Inoperability of Diesel
                                                                                                             Generators Because of                               i
                                                                                                              Seismically Unqualified
                                                                                                             Battery Racks

>

               259/87-01 and Rev. 1                                                      1/28/87              Personnel Errors Cause
                                                                                                              Fire Watch Violations
               259/87-12 and Rev. 1                                                      5/6/87               Inadequate Maintenance
                                                                                                              Procedure Cause Breaker
                                                                                                              Failure to Close and
                                                                                                              Enginected Safety
                                                                                                              Actuation
               259/87-23                                                                 8/26/87              Personnel Error Results
                                                                                                              in Unrepresentative
                                                                                                              Radiological Release
                                                                                                              Assessment Data
                                                                                                                                                                 l
    . .      -   - _. _      .
                                  _ _ - . _-                                                      _  __            . _ .  _      . -      - -     __ -
   _ _ _ _ _ _ _ _       _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                                                            _____ _-__     __
                     .
                       .          .
                                                                                                               *
                                                       ,                                                                                                                                                                       12
                                                                                                         LER No.                                                                                            Date                  Event
                                                                                                        259/87-29                                                                                        11/5/87                  Personnel Error in
                                                                                                                                                                                                                                  Writing Equipment Tag-Out
                                                                                                                                                                                                                                  Clearance Results in
                                                                                                                                                                                                                                  Actuations of Engineered
                                                                                                                                                                                                                                  Safety Features
                                                                                                        296/87-04                                                                                         10/13/87                Diesel Generator 3EB
                                                                                                                                                                                                                                  Start Due to Personnel
                                                                                                                                                                                                                                  Error During Maintenance

4

 '
                                                                                                         296/87-05                                                                                        10/19/87                Unplanned Diesel
                                                                                                                                                                                                                                  Generator Start Due to
                                                                                                                                                                                                                                  Relay Failure
                                                                                                         296/87-06                                                                                        11/24/87                Unplanned Engineering
                                                                                                                                                                                                                                  Safety Features
                                                                                                                                                                                                                                  Actuations Due to Relay
                                                                                                                                                                                                                                  Failure and Personnel
                                                                                                                                                                                                                                  Error During Corrective
                                                                                                                                                                                                                                  Maintenance
                                                                                                         During replacement of a failed relay (LER 259/84-23) an adjacent wire came
                                                                                                          loose and caused primary containment isolation system i solations on
                                                                                                         Unit 2. The wire had been incorrectly terminated. The wiring on Units 2
                                                                                                          and 3 were inspected and Unit 3 was found to have similar problems,                                                                                      The

, incorrect termination on Unit 3 was determir.ed to be the result of two

                                                                                                           field changes. The wiring was corrected through engineering change notice
                                                                                                          P5135 and workplan 3048-84.

'

                                                                                                         Ouring a post maintenance review of a maintenance request to repair the
                                                                                                         diesel generator battery rack studs (LER 259/85-49) it was determined the
                                                                                                         wrong stud material was used during the 1976 and 1980 installation of
                                                                                                           studs for the new battery racks. All the diesel generator battery rack
                                                                                                           studs were replaced with certified studs and seismic qualification was
                                                                                                          restored by workplan 1224-85 and 3054-85.
                                                                                                         A fire watch was not posted (LER 259/87-01) in the area of the diesel
                                                                                                          generator building when portions of a fire protection system was isolated
                                                                                                          and an individual (fire watch) reported to the wrong cable spreading room.
                                                                                                          The plant fire protection unit de/ eloped a listing of areas requiring fire
                                                                                                         watches and the reasons for them. The listing will be routinely updated
                                                                                                          and maintained in the shift engineer's office. A fire protection engineer
                                                                                                           his been placed on the call out list.
                                                                                                          Rring transfer of a shutdown bus to its alternate power supply, the
                                                                                                           alternate power supply failed to close the breaker, causing the engineered
                                                                                                           safety feature actuation (LER 259/87-12). An inspection of the breaker

.;

                                                                                                           found grease and dirt buildup on the control cell lintage which prevented

! i I

                   _                                    .                                               _ _ _ _ . _ _ _ _ _ ,                                                                _ _ ~ _ _ _ . _ _ _ . _ _ _ _ _ _               _s
              .   -               -  -           .     .-

. ..

     '
                                          13
                                                                                  ,
    proper breaker operation. The control cell linkages on the four kilovolt
    plant breakers were inspected and cleaned. Procedure BF EMI-7, Mainte-
    nance of Medium and Low Voltage Switchgear was revised to include cleaning
    of suspect parts.
    The composite portion for the month of August 1987, was inadvertently
    disposed of which resulted in an unrepresentative quarterly sample for
    radiological release assessment data for the third quarter of 1987 (LER
    259/87-23).     The surveillance instruction was revised to emphasize
    labelling and storage of samples.
                                                                                  ,
    A fuse was removed from a panel in order to deenergize a primary contain-     '
    ment isolation valve modifications activities which resulted in engineered
    safety features actuations (LER 259/87-29). The switching necessary to
    electrically isolate the valve was inadequate during preparation of the
    clearance. The individuals involved were cautioned      and a critique of the
    incident was reviewed by operations personnel.
    On November 24, 19o7, control room personnel observed the B train of the
    CREV system to be running from an auto start signal (LER 259/87-30).
    Investigation by electrical maintenance personnel revealed that a burned
    electrical relay caused the auto start. The relay coil was assessed as
    an end-of-life failure failure and was replaced.
    During the performance of maintenance on the 3EB diesel generator an
    electrician accidently shorted the auto start relay, while connecting an
    oscilloscope, which caused an auto start (LER 296/87-04). The personnel
    involved were critiqued on the event and all electrical technicians
    reviewed and signed the critique on November 30, 1987.
    After completing a degraded logic test on a 4160 volt shutdown board the
    3D diesel generator received an auto start signal (LER 296/87-05) an
    investigation revealed two failed voltage relays that caused the auto
    start signal which were monitoring the shutdown board. The failed relays      l
    were replaced and the logic test was rerun.                                   '
    On November 22, 1987, the Unit 3 inboard containment isolation valves were
    automatically closed due to a failed relay coil in the primary containment
    isolation system. On November 24, 1987, during replacement of the fsiled
    relay coil the electrical jumper used was inadvertently dislodged by
    maintenance personnel (LER 296/87-06). Corrective maintenance was
    completed and the systems were returned to normal.
    The following licensee event reports were reviewed and remain open pending    ;
    further review:                                                               I
    LER No.                       DATE                    EVENT
    259/85-51                     9/25/85          Deteriorated Cable
                                                    in Reactor                    1
                                                   Protection System              '
                                                                                  i
                                                                                  I
                                                                                  I
                                                                                  l
  .-__-_ _______ ___ ___ ______________________ ___ _________________ _ __-_ _ ___________-_______ ___________________ _ _________________
                            .                                                    .
                                                                                                                                            '
                                                                                                        .                                                                      14
                                                                                                                                           LER No.                     DATE                    EVENT
                                                                                                                                           296/83-47 and Rev. 1        7/30/83           Seal Flow Through RHR
                                                                                                                                                                                         Seal Cooler Less Than
                                                                                                                                                                                         Required Minimum Flow Rate
                                                                                                                                           296/86-08                   9/5/86            Shorted Generator Coil
                                                                                                                                                                                         Reduces RHR Capability
                                                                                                                                           No violations or deviations were observed in this area.
                                                                                                         10.                               Employee Concerns ( Allegation)                                           '
                                                                                                                                           The inspector reviewed an employee concern involving soldering identified
,
                                                                                                                                           as employee concern ECP-87-BF-897-01. This concern was initially
                                                                                                                                           identified by a TVA instrument technician assigned to the Browns Ferry
                                                                                                                                           (BFN) Instrument Shop and a copy of the concern was sent to the Region II
                                                                                                                                           office in June 1987. The specific concern involved soldering performed by
                                                                                                                                           a vendor on solid state electronic cards used in the neutron monitoring
                                                                                                                                           system which initiates scrams and rod blocks. The inspector was informed
                                                                                                                                           by BFN personnel that the electronic cards were received from General
                                                                                                                                           Electric (GE) on site for a modification (mod) and the mod was installed
                                                                                                                                           in 1983. Under a seven (7) power microscope the inspector observed an
                                                                                                                                           electronic card similar to the cards used for the mod. The soldering
                                                                                                                                           contacts on the pins of chips and operation amplifiers (0p Amps) appeared
                                                                                                                                           contaminated,   i.e. poor pre-soldering clearing and/or post soldering
                                                                                                                                           cleaning, and discontinuing, i.e. sometimes referred to as "cold solder
                                                                                                                                           joints", where there are gaps between the pins and the solder.        The
                                                                                                                                           technician informed the inspector that these problems were identified on
                                                                                                                                           nine of eleven Tnermo Trip Cards and on nine of nine Direct Currect (DC)
                                                                                                                                           amplifier cards, all used in Unit 2. The technician also stated that the
I&C shop personnel were making repairs to the Thermo Trip Cards and DC
                                                                                                                                           amplifier cards in the I&C shop until they were instructed to return all
                                                                                                                                           cards to power stores.    The employee concerns representative indicated
                                                                                                                                           that the soldering specification may or may not have been stipulated in
                                                                                                                                           the procurement process used for the modification. The employee refer-
                                                                                                                                           enced several military specifications as possible soldering standards,

j This item will remain open and tracked as an allegation.

                                                                                                                                                                                                                     P
                                                                                                          11.                              Design Control (37702)
                                                                                                                                           On January 27, 1988, the licensee made a non-emergency report per 10 CFR
                                                                                                                                           50.72 for an unanalyzed condition outside the design basis of the plant.
                                                                                                                                           The finding concerned the seismic qualification of Emergency Equipment
                                                                                                                                           Cooling Water (EECW) and Residual Heat Removal Service Water (RHRSW)
                                                                                                                                           buried piping where the piping exits and enters building structures.
                                                                                                                                           Appendix C, Section C.2.1 of the FSAR describes this feature as follows.
                                                                                                                                           Class I buried piping, at penetrations into secondary containment and at
                                                                                                                                           entry points into the intake structure, is protected from dif ferential
                                                                                                                                                                                                                     l
                                                                                                                                                                                                                                                                                     _ _ . .
  .                                          .
                                                                                                                                                                                                                                                                                                                        l
                                                                                                                                                                                                                                                                                                                       I
                                                                                                                                                                                                                                                                                15
                                                                                                                    movement of the soil and structure by a guard box and flexible joints.
                                                                                                                     The guard box is supporteu by, and moves with, the soil. One open end
                                                                                                                    butts against, but is n7t connected to, the building. Large pipes which
                                                                                                                    may be overstressed by the differential movement of the structure and the
                                                                                                                      soil-bearing end of the guard box are provided with two flexible
                                                                                                                     couplings. One coupling is located near the structure and one near the
                                                                                                                      soil-bearing end of the guard box. The guard pipe provides adequate
                                                                                                                     clearance to permit one joint to move with the structure and one with the

,

                                                                                                                      soil, without contacting the pipe.
                                                                                                                    Analyses of seismically-induced soil motions on Class I buried piping were
                                                                                                                    made, and the seismic stresses were determined to be small.                                                                                                                            Therefore,
                                                                                                                     differential movement at support points, at containment penetrations, and
                                                                                                                     at entry points into other structures is the primary concern in designing
                                                                                                                     buried piping at the Browns Ferry Nuclear Plant.
                                                                                                                       In October 1986, the licensee discovered that the function of some of the
                                                                                                                      flexible (Dresser) couplings had been defeated at some time in the past.
                                                                                                                     Tie-rod harnesses were installed across the couplings on the B RHRSW and                                                                                                                         ,
                                                                                                                      FECW piping at the intake structure. These htenesses were apparently
j                                                                                                                       installed in order to provide additional axial support for the coupling.

9 Since no drawings could be found which showed the harnesses, +.he Division  ;

                                                                                                                     of Nuclear Engineering (DNE) was asked to evaluate the as-found condition                                                                                                                        ,
                                                                                                                      and provide the necessary design information in order to repair some of

< the tie-rods which were found damaged. DNE responded that the harnesses

;                                                                                                                    were not required and could either be repaired or removed at the option of
                                                                                                                      the plant maintenance organi:ation.
                                                                                                                     About a year later, during preparation for a hydrostatic test in
                                                                                                                    June 1987, similar damage was found on tie-rods and lugs on harnesses on
                                                                                                                       the A RHRSW couplings. The tie-rods were removed f rom these couplings

'

                                                                                                                      prior to the hydrostatic test. Later, while the system was being brought

>

                                                                                                                      up to hydrostatic test pressure, the coupling failed due to the excessive
                                                                                                                      axial load at about normal system pressure. This failure was aided by the
                                                                                                                       fact that a hanger (M-30) near the coupling had been previously removed.
                                                                                                                       It was later determined that this M-30 hanger was underdesigned for the
                                                                                                                      expected axial loading during a seismic event.
                                                                                                                       In December 1937, a Cono. tion Adverse to Quality Report (CAQR-871126) was
                                                                                                                      written which concluded that the original design intent as stated in the
                                                                                                                       FSAR had been defeated by the use of harnesses which did not preserve the
                                                                                                                       required flexibility of the Dresser coupling.                                                                                                                         As a result of the rigid
                                                                                                                      connection, relative movement between the building and buried piping as
                                                                                                                     would occur during a seismic event, would produce loads far greater than
                                                                                                                       the components were designed to withstand. A loss of both the EECW and

4

                                                                                                                       RHRSW systems could occur during a seismic event. One problem with this

4

                                                                                                                      CAQR noted by the inspector was that the check on potential af fect on                                                                                                                          l

) operability of the nuclear plant was marked "no" Justification for this

!
                                                                                                                                                                                                                                                                                                                      ,
                                                                                                                                                                                                                                                                                                                      '

!

i
    _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ . _ _ _ . _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _
                 -             - - _ _ _ _ _ _ _ .

s .

    '
                                                   16
   conclusion was contained on the CAQR continuation sheet which simply
   stated that it hao been determined that the adverse condition would not
   prevent EECW/RHRSW from performing as designed; therefore, operability was
   not affected. This was contradictory with the CAQR paragraphs.
   The subsequent red phone report was prompted by maintenance and technical
   support personnel review of the preliminary design change to the Dresser
   coupling.       The design was so radically different from the previous design
   that a question of operability of the original design and as-found condi_
   tion was raised. A high level management review team was assembled to
   evaluate the ramifications of the findings and immediate work was started
   to cut out eight of the Dresser couplings and replace them with rigid
   welds. Although an in-depth analysis is still underway by the licensee,
   the following deficiencies are currently known:
   (1) Hanger M-30 which provides the only axial restraint for the couplings
           in question was significantly underdesigned and could not withstand
           the thrust load. An analysis determined that the hanger would bend
           and deflect out of position during a seismic event. This would allow
           the coupling (without the tie-rod harness) to spring apart and fail
           the pressure boundary of the coupling.
   (2) The original design function of the Dresser coupling was defeated at
           some point by the installation of tie-rod harnesses.        No design
           analysis was performed to justify this modification.      The harnesses
           were probably installed in 1973 time frame in order to maintain the
           coupling integrity during water hammer events which were common at
           that time.     A recent analysis showed that the harnesses were
           underdesigned for the required load.
    (3) The design evaluation of the as-found condition of the couplings in
           October 1986 was erroneous. This evaluation, contained in a
           memorandum from S. R. Lawson to R. H. Wall dated 10/30/86, concluded
           that the M-30 hanger provided the necessary axial restraint that the
           Dresser coupling lacked and therefore the tie-rod harnesses could be
           eliminated.
    The safety significance of these findings are still under evaluation by
    the licensee. At a minimum, a seismic event would have resulted in a
    degradation of the RHRSW and EECW available due to a loss of the coupling
      integrity. At the most, a complete loss of the Ultimate Heat Sink (VHS)
    would have resulted. This is a violation of the Design Control require-
    ments of 10 CFR 50, Apper.di x B (259,260,296/88-04-03), Although the
     problem was identified by the licensee it is considered a self-disclosing
     violation in that a failure of the coupling had to occur during a
     hydrostatic test to force full reconciliation of the deficiency. The
     opportunity existed in October of 1986 to fully evaluate the problem
     but a perfunctory analysis failed to correct the design deficiency.
                                                      _ _ _ _
   _ _ - - - -         _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _              _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___    _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                  _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
               .
                 '                                                                                          17
                     During a review of the documentation associated with this problem the
                     inspector noted that delinquent reviews were performed on the hydrostatic
                     test data on the RHRSW system. SI 3.3,13.A.2, ASME Section XI Hydrostatic
                     Pressure Testing of the RHRSW System Buried Piping, which was performed on
                     July 30,1987, did not pass the acceptance criteria due to the failed
                     Dresser coupling. The Shift Engineer did not review the data to determine
                     if an LCO was violated until November 25, 1987. The results were not
                     reviewed by the Mechanical Engineer until November 30, 1987, and the
                     Cognizant Engineer did not review the data until February 18, 1988. For
                     the next trial of SI 3.3.13.A.2 performed on October 31, 1987, most of the
                     reviews were more timely; however, the data sheet did not specify that the
                     acceptance crii.eria was not satisfied nor was the Shitt Engineer's
                     signature obtained to document that a review for an LCO violation had
                     occurred.                                        These deficiencies were discussed with plant management as
                     further problems with attention to cetail and meticulous compliance with
                     procedures. Similar examples of nine delinquent reviews had been identi-
                     fied by the licensee and documented in CAQR 880102.

,

                 12. Restart Test Pregram
                     a.                                        Restart Testing Status
                                                               The inspector attended RTP status meetings, reviewed RTP test
                                                               procedures, observed RTP tests and associated tests performances, and
                                                               reviewed selected RTP test results.                                                             The following specific RTP
                                                               activities and associated activities were monitored during this
                                                               reporting period:
                                                               (1) RTP-002, Condensate, The system was released for testing by
                                                                    the Joint Test Group on February 23. A special test (ST-99
                                                                    Condensate Demineralizer) is in progress which involves the
                                                                    condensate polishers clean and precoat sequence and is being
,
'
                                                                    conducted under the chemistry departments responsibility.
                                                               (2) RTP-023, Residual Heat Removal Service Water (RHRSW), The system
'
                                                                    is being impacted by the header outages due to the Dresser
                                                                    couplings. Several Maintenance Requests, Hold Orders and Design
                                                                    Change Notices are outstanding as well as hydrostatic tests
                                                                    completions.
I                                                              (3) RTP-024, Raw Cooling Water (RCW), The system is being restrained
                                                                    somewhat by repairs required to 2A and 2B RCW pumps, time delay
                                                                    relays and various system valves. The system is also impacted
                                                                    by the Emergency Equipment Cooling Water (System 067) header
                                                                    outages.
I                                                              (4) RTP-030, Diesel Generator and Reactor Building Ventilation (DG &
1                                                                   RX BLDG VENT.), Section 5.1, DG Building Ventilation Flow
 l

. .

     '
   .                                                   18
             Verification Units 1,2, & 3 was performed during this reporting
             period; however, initial review of data indicates a possible
             retest of some of the twenty-six fans involved in this section
             of the test may be required.
        (5) RTP-031,     Control Building Heating Ventilation and Air
             Conditioning (Cont. Bldg HVAC), The actual restart test
             procedure is still in the draft stage. However, primary
             activities are in process which includes repairs to a tear in
             ductwork and the installation of ductwork, conduit and cable
             seals. Both of these are being worked partly under Engineering
             Change Notices 0031A and P0647 respectively. Restart test
             procedure performance is scheduled to start on March 29.
        (6) RTP-057-4, 480 Volt Distribution System (480 V Dist.),                                 The
             system is closely related to system 82 standby Diesel Generators
             (DG) in that load shedding verification is performed in
             conjunction with OG load acceptance test. Logic function tests
             are performed to plant procedures such as SMI-1-48SD.
        (7) RTP-057-5 4.16 KV Distribution System (4 KV DIST.), The system
             is also cicsely related to the DGs and has been identified as
             system necessary to support Loss of Power / Loss of Coolant
             Accident (LOP /LOCA).                    A schedule for the performance of
             procedures (Logic functions, etc.) indicates th4t the 4.16 KV
             shutdown boards till be completed prior to the associated DG Low
             Acceptance test.                     Plans are in place to perform a battery
             discharge (ampere hour) test when the 4.16 KV Shutdown Board 3EB
              is out of service for functional testing anC neintenance.
        (8) RTP-057-7, 250 VOLT OC Shutdown Board Battery Chargers (250 VOC
             S/0 Batt.), The system has received upper management attention
             through the Restart Operations Center (War Room) and every
             effcet is being made to complete the RTP r.o later than March 6.
             The major hold ups for the test has been a lack of material
             (filter capacitors) and craft support.
        (9) RTP-065, Standby Gas Treatment (SGTS), The system is under test
             not only to support LOP /LOCA, but also to establish secondary
             containment for the fuel reconstitution.                              Several dampers have
             not satisfied the time to close test specification, but also
              some dampers have been disabled by linkages and motors removed
             and did not function when initiation signals were present.
       (10) RTP-067, Emergency Equipment Cooling Water (EECW), The system is
             affected by the Dresser coupling issue due to header outages to
              remove selected couplings. Preparations were being made to
             hydrostatic test the system once the couplings were removed and
              replaced by welds.
                  ,-        _ _ _ _ - - - _ , _ -             __    _ . _ _ . - - - - . .             -__
                                                                                                          _
  - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                          .                 .
                                                                                                                                                                              !
                                                                            *
                                                                .                                                              19
                                                                               (11) RTP-070, Reactor Building Closed Cooling Water (RBCCW), The
                                                                                     system is in the pre-test stage with ASME Section 11,
                                                                                     Hydrostatic tests in progress and Mechanical Testing group is
                                                                                     performing 10 CFR 50, Appendix "J" tests, i.e, local leak rate                           '
                                                                                     tests.         The system is scheduled for restart test release the
                                                                                     first week of March,1988.
                                                                               (12) RTP-075, Core Spray (CS), The system has successfully tested
                                                                                     section 5.7, local Operation of 2A, 2B, 2C and 20 core spray
                                                                                                                                                                              "
                                                                                     pumps. Several ECNs, MRs and Surveillance Instruction updates

( are being processed to support completion of the test. ,

                                                                               (13) RTP-082, Standby Diesel Generators (STDBY DG), Several load
                                                                                     acceptance tests on the eight (8) DGs have been performed. Two
                                     ,                                               of Unit 3 DGs require degraded voltage tests and are scheduled
                                                                                     to be performed during the monthly sis.           Additional special
                                                                                     testing involving the DGs speed governors and voltage regulators
                                                                                     are scheduled for March, 1988. This special test will involve
                                                                                     direct vendor input with DNE supplying the test methodology.
                                                                                     The RTP will be revised to reflect this test.
                                                                            b.  Design Deficiencies Identified By RTP                                                         !

,

                                                                                (1) Systems 57-3, 250 Volt DC Distribution and 57-4, 480 Volt AC
                                                                                     Distribution
                                                                                     During a review of subsystem 280, Battery Boards and subsystem
                                                                                     231, 480 Volt AC shutdown boards by a system engineer in January                         +
                                                                                     of 1987, in preparation for the restart test the following was
                                                                                     discovered:
(a) The loss of 250 Volt DC Battery Board #1 would cause a loss '
                                                                                           of 4S0 V toad shed logic signals to 480 V shutdown boards
                                                                                           1A & 18.
                                                                                     (b) The loss of Battery Board #1 would cause a loss of Safety

i Divison II core spray logic.

                                                                                     The above condition was determined by the licensee as a breach
                                                                                     in single failure criterta and documented by CAQR's. This item
                                                                                     is identified as an Inspector Followup Item (259,250,296/88-                             '
                                                                                     04-04).

i (2) System 82 Diesel Generators (DGs)

l
                                                                                     The DGs are designec for 3050 KW for 1/2 hour, 2950 KW for seven
                                                                                     (7) days and 2850 KW indefinite. The RTP calls for a 24 hour

j fuel consumption run with the first 2 hours 0 2950 KW and the

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                                                              -. ___ _ ._ _                _ _ . . _ _ _ _ _ _ . _ _ . . _ _ .       _           _        _ _ _ _ _ _ _ _ _ _
  --__ _ _ _ _ _ _ _ _ _ _ _ __. _ _ _ _ _ _ _                             _-_
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4 next 22 hours 0 2850 KW. During the fuel consumption run the

                                                                               field breaker for the generator tripped shortly af ter the test
                                                                               was started while the DG was 0 2950 KW. This has been
                                                                               attributed to the following:
                                                                               (a) The field an.perage is undersized 0100 amps and a DCN No.                                                 l
                                                                                      3532 has been issued to upgrade the capacity to 125 amps.                                              '
                                                                               (b) The control cabinets where the breakers are located have
                                                                                      too high of an internal temperature and a DCN No. 3531 has
                                                                                      been issued to add ventilation louvers to the cabinets.

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                                                                                      This item is identified as an Inspector Followup Item
                                                                                      (259,260,296/88-04-05).
                                           .                             (3) System 32, Control Air System
                                                                               During the test of drywell control air suction valves FCV-32-62
                                                                               & 63, the cylinder operated valves failed to close on loss of
                                                                               power to the solenoid valve and upon loss of control air as
,
                                                                               required by the Safety Design Basis contained in the F3AR. This
                                                                               item was previously identified in NRC Report (259,260,296/87-
                                                                               -33).

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                                                                         (4) System 57-7, 250 Volt DC Shutdown Batteries
                                                                               The filter capacitors in the battery charges did not pass the
                                                                               ripple voltage tests. All capacitors are being changed and
                                                                               as of the end of this reporting period, Charger A has new
,
                                                                               capacitors, successfully passed the ripple voltage test and

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                                                                               is back in service. The restart test and 5ystem engineering
                                                                               personnel shifted to Charger B for the next ripple test.

1 Hewever, when maintenance removed the cov6r of the B Charger

                                                                               the filter capacitors wert                                          issine. This item is identified
:                                                                              as an Inspector Followup Item ( ..,26. . 296/88-04-06).                                                       ;
                                                                   c.    Deficiencies Identified By RTP That Are Under Review

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                                                                         (1)   System 82, Diesel Generators (DCs)                                                                            ,
                                                                                                                                                                                             t
                                                                               The RTP requirement is that a seven (7) day supply of diesel
                                                                               fuel oil be available for three (3) DGs. The fuel oil transfer
                                                                               pump that may be called upon is supplied from a IE source;                                                    i
                                                                               however, it must be primed from service air, which is not a
                                                                               systera important to safety.
                                                                         (2)   System 82 Diesel Generators (DG)                                                                              i
,
                                                                               During the paralleling of the Unit 1/2 DGs with the Unit 3 DGs                                                l
                                                                               the KVAR snaring was not present. It was initially determined                                                 i
                                                                               that this may be a wiring error; however, further evaluation is
                                                                               ongoing,
                                                                                                                                                                                             ,
                                                  _. ,_- - . _ . . _ - ,            -- . ,_,_ . ___ -._ _ - ,. _ -_.___ _ - _ ._ - __ . _ , _                        _ - _ . _ .     - - _ _
       m-

. s

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          (3) System 65, Standby Gas Treatment (SBGT)
               During the performance of an ANSI required test the phase to
                phase current readings for the relative humidity heater were
                greater than the 5 percent relationship required by the ANSI
                Standard. N510-1975, Section 14.2,3.
          (4)   System 23, Sump Level Switches
                The RHR service water building sump level switches cannot be
                adjusted to meet the high level pump st .*t requirement and the
                requirement has no band.

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