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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 ML20195J9401999-06-15015 June 1999 Safety Evaluation Supporting Amend 211 to License DPR-50 ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20153A9941998-09-16016 September 1998 Safety Evaluation Denying Request to Remove Missile Shields from Plant Design ML20151U8821998-09-0808 September 1998 SER on Revised Emergency Action Levels for Gpu Nuclear,Inc, Three Mile Island Nuclear Plant Units 1 & 2 ML20237A8331998-08-12012 August 1998 Safety Evaluation Accepting USI A-46 Program Implementation at Plant,Unit 1 ML20217K4851998-04-24024 April 1998 Safety Evaluation Supporting Amend 207 to License DPR-50 ML20199G8371998-01-22022 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Three Mile Island Nuclear Station,Unit 1 ML20198K2281997-10-16016 October 1997 Safety Evaluation Supporting Amend 206 to License DPR-50 ML20211G8561997-10-0202 October 1997 Safety Evaluation Supporting Amend 204 to License DPR-50 ML20210Q9991997-08-28028 August 1997 Safety Evaluation Concluding That Since 25th Tendon Surveillance on Few Yrs Away,Adequacy of Remaining Prestressing Force Will Be Critical to Verify ML20217Q7341997-08-27027 August 1997 Safety Evaluation Supporting Amend 203 to License DPR-50 ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20149D2671997-07-11011 July 1997 SER Concluding That Exemption from Listed Fire Areas Should Be Granted & Exemption from Fire Area FH-FZ-5 Should Be Denied ML20141L9571997-05-27027 May 1997 Safety Evaluation Supporting Amend 201 to License DPR-50 ML20138H6671996-12-19019 December 1996 Safety Evaluation Accepting Util IPE Submittal in Response to GL 88-20 ML20134D7811996-10-24024 October 1996 Safety Evaluation Supporting Amend 51 to License DPR-73 ML20128L6741996-10-11011 October 1996 Safety Evaluation Accepting Third ten-year Interval for Pump & Valve Inservice Testing Program for Facility ML20128K1981996-10-0808 October 1996 Safety Evaluation Supporting Amend 50 to License DPR-73 ML20094Q0301995-11-24024 November 1995 Safety Evaluation Supporting Amend 199 to License DPR-50 ML20092N2551995-10-0202 October 1995 Safety Evaluation Supporting Amend 197 to License DPR-50 ML20092J1861995-09-19019 September 1995 Safety Evaluation Supporting Amend 196 to License DPR-50 ML20087G5771995-08-14014 August 1995 Safety Evaluation Supporting Amend 195 to License DPR-50 ML20086R7421995-07-24024 July 1995 Safety Evaluation Supporting Amend 194 to License DPR-50 ML20078H3961995-01-31031 January 1995 Safety Evaluation Supporting Amend 193 to License DPR-50 ML20077C2901994-11-28028 November 1994 Safety Evaluation Supporting Amend 192 to License DPR-50 ML20071N3991994-08-0101 August 1994 Safety Evaluation Supporting Amend 191 to License DPR-50 ML20071K8741994-07-25025 July 1994 Safety Evaluation Supporting Amend 190 to License DPR-50 ML20071L2381994-07-25025 July 1994 Safety Evaluation Supporting Amend 189 to License DPR-50 ML20071K8921994-07-25025 July 1994 Safety Evaluation Supporting Amend 188 to License DPR-50 ML20070H2851994-07-14014 July 1994 Safety Evaluation Supporting Amend 187 to License DPR-50 ML20070D2741994-06-30030 June 1994 Safety Evaluation Supporting Amend 186 to License DPR-50 ML20069K5401994-06-10010 June 1994 Safety Evaluation Supporting Amend 185 to License DPR-50 ML20073S3941994-05-23023 May 1994 Safety Evaluation Supporting Amend 184 to License DPR-50 ML20067B3191994-02-10010 February 1994 Safety Evaluation Supporting Amend 182 to License DPR-50 ML20059D1771993-12-28028 December 1993 Safety Evaluation Supporting Amend 48 to License DPR-73 ML20062L5081993-12-22022 December 1993 Safety Evaluation Supporting Amend 181 to License DPR-50 ML20062M2481993-12-21021 December 1993 Safety Evaluation Supporting Amend 180 to License DPR-50 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 05000289/LER-1999-010, :on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With1999-09-21021 September 1999
- on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With
ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With 05000289/LER-1999-009, :on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced1999-07-22022 July 1999
- on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced
ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 05000289/LER-1999-007, :on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed1999-06-18018 June 1999
- on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed
ML20195J9401999-06-15015 June 1999 Safety Evaluation Supporting Amend 211 to License DPR-50 05000289/LER-1999-005, :on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With1999-06-14014 June 1999
- on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With
ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 05000289/LER-1999-003-01, :on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open1999-05-0707 May 1999
- on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open
ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With 05000289/LER-1999-002, :on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With1999-03-14014 March 1999
- on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With
ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With 05000289/LER-1999-001-01, :on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys1999-02-19019 February 1999
- on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys
ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits 05000289/LER-1998-014-01, :on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With1999-01-11011 January 1999
- on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With
ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt 05000289/LER-1998-013, :on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance1998-10-15015 October 1998
- on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance
ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing 05000289/LER-1998-010-01, :on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued1998-10-0909 October 1998
- on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued
ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With 05000289/LER-1998-011, :on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge1998-09-23023 September 1998
- on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge
1999-09-30
[Table view] |
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P c-ENCLOSURE
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THREE MILE ISLAND, UNIT 1, NUCLEAR POWER PLANT INDIVIDUAL PLANT EXAMINATION STAFF EVALUATION REPORT i
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I.
INTRODUCTION On May 23, 1993, the General Public Utility Co. (GPU) submitted the Three Mile Island, Unit 1, (TMI) Nuclear Power Plant Individual Plant Evaluation (IPE) submittal in response to Generic Letter 88-20 and associated supplements. On August 3,1995, the staff sent questions to the licensee requesting additional information.
The licensee responded in a letter dated December 6, 1995.
A " Step 1" review of the TMI IPE submittal was performed and involved the efforts of Brookhaven National Laboratory in the front-end, back-end, and j
human reliability analysis (HRA). The Step 1 review focused on whether the
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licensee's method was capable of identifying vulnerabilities.
Therefore, the review considered:
(1) the completeness of the information, and (2) the j
reasonableness of the results given the TMI, design, operation, and history. A more detailed review, a " Step 2" review, was not performed for this IPE submittal. Details of the contractors' findings are in the attached technical evaluation report of this staff evaluation report (SER).
In accordance with Generic Letter 88-20, TMI proposed to resolve Unresolved Safety Issue (USI) A-45, " Shutdown Decay Heat Removal Requirements."
(See a discussion of this isSection II). The-licensee also proposed, and the staff agrees to consider resolved, USI A-17, " Systems Interactions in Nuclear Power Plants," with the submission of the internal flood portion of the submittal.
In addition, the licensee listed GSI-23, " Reactor Coolant Pump (RCP) Seal J
Failures," in the IPE. The Commission has decided not to take additional rulemaking action at this time and plans to issue a generic letter on this issue at a later date.
The submittal does not state whether the licensee intends to maintain a "living" probabilistic risk assessment, although the staff strongly recommends they do so, particularly in light of the fact that the licensee indicated they plan to use the IPE models for on-going risk management activities.
II.
EVALUATION TMI is
%cox bd Wilcox PWR with a large, dry containment. The TMI IPE has of 4.2E-05 per reactor-year from estimated a core damage frequency (CDF) floods are not included in the above internally initiated events.
Internal total and they add another 3E-6 per reactor year to the CDF. The TMI CDF compares reasonably with that of other Babcock & Wilcox PWR plants.
Transients contributed 60 percent to the total CDF, loss of coolant accidents, 38 percent, interfacing system LOCA, 2 percent, and steam generator tube rupture (SGTR), 0.4 percent. The important system / equipment contributors to the estimated CDF that appear in the top sequences are:
1.
Failure of the High Pressure Injection (HPI) system, 2.
Failure of the Decay Heat River Water and Closed Cooling Water system, and 3.
Failure of recirculation from the reactor building sump. )
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i-i The licensee's Level 1 analysis appears to have examined the significant initiating events and dominant accident sequences.
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Based on the licensee's IPE process used to search for decay heat removal l
(DHR) vulnerabilities, and review of TMI plant-specific features, the staff j
finds the licensee's DHR evaluation ' consistent with the intent of the USI A-45 i
l (DHR Reliability) resolution and is, therefore, acceptable.
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The licensee performed an HRA to document and quantify-potential failures in human-system interactions and to quantify human-initiated recovery of failure 4
events. The licensee identified the following operator actions as important l
in the estimate of the CDF:
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Failure to switch over to reactor building sump recirculation following l
a large loss of coolant accident.
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Failure to refill the borated water storage tank (BWST) given a SGTR or
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very small LOCA.
3.
Failure to throttle HPI flow after engineering safeguards actuation.
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i The licensee evaluated and quantified the results of the severe accident progression through the use of a containment event tree but did not examine uncertainties in containment response through the use of. sensitivity analyses, j
The licensee's back-end analysis appeared to have considered important severe accident phenomena. The licensee identified the following conditional containment failure probabilities:
Early containment failure is 3 percent with hydrogen overpressure (with both high and low vessel pressure sequences) l the primary contributor; late containment failure is 63 percent with basemat meltthrough and overpressurization due to steam and non-condensible gas being the primary contributors; and bypass is 4 percent with interfacing systems LOCA and SGTR the primary contributors. According to the licensee, the containment remains intact 30 percent of the time. Early radiological releases are dominated by bypass and most late releases are due to benign, rather than catastrophic containment failure. The licensee's response to containment performance improvement program recommendations is consistent with the intent of Generic Letter 88-20 and associated Supplement 3.
The licensee based the majority of their containment response analysis on work done for the Oconee nuclear plant co..'ainment. While the staff finds this approach acceptable as a search for vulnerabilities, based on the similarities i
of these large, dry containments, the submittal makes it difficult to determine what new TMI-specific information regarding accident progression the licensee learned. We also note that the submittal did not include a containment phenomena sensitivity analysis as requested by Generic Letter 88-20. This represents a weakness in the IPE submittal, especially in light of the fact that the " template" approach was used. Although the template approach is an acceptable method for Generic Letter 88-20 compliance (which relies on existing analyses of similar containments in other nuclear plant *:e the staff believes that the licensee could have gained more of an understanding of the range of accident progression outcomes, and therefore the TM1 containment performance, had sensitivity analysis been performed. M
D Some insights and unique plant safety features identified by the licensee at TMI are:
1.
The turbine driven main feedwater pumps will continue to run for most transients, with puiap flow output automatically matched to the decay heat level.
2.
The turbine driven emergency feedwater pump has a mechanical linkage for control and is, therefore, not dependent on DC power for long term control in station blackout scenarios.
(The IPE did not take credit for this feature.)
3.
The czergency feedwater system pumps (two motor driven and one turbine driven) have been shown by licensee testing to not need bearing cooling for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
4.
One pressurizer power operated relief valve (PORV) and two safety valves can be used for feed and bleed. The PORV block is usually open and it depends only on DC power, not on nitrogen supply or instrument air.
5.
The RCP seals use new high temperature 0-rings which, according to the licensee, show a reduced leakage potential following a loss of all seal cooling.
6.
Recirculation switchover is accomplished manually.
The licensee defined.a front-end vulnerability as any core damage sequence i
exceeding IE-04 per reactor year. They defined a back-end vulnerability as any containment bypass or large early containment failure that exceeds IE-06 per reactor year.
Based on these definitions the licensee did not identify any vulnerabilities.
Plant improvements, however, were identified. These procedural improvements (none hardware-based) are listed below. They have not yet been implemented, however, their contribution to the reduction to CDF was assessed by the licensee to be smail:
1.
Operator action to isolate the steam generator experiencing a tube rupture and cooling down the reactor coolant system via the intact steam generator in cases where HPI is lost (CDF reduction approximately 1 percent).
2.
Operator action to refill the borated water storage tank during SGTR and very small break LOCA sequences (CDF reduction 4 percent).
Procedures are in place for refilling the BWST for small break LOCAs and the BWST level is monitored by numerous groups during emergency drills.
3.
Operator action to verify the closure of stop-check valve MUV-14 when aligning for piggyback recirculation from the reactor building sump (CDF reduction " negligible" but the risk achievement worth is high due to the potential bypass path to the environment.) _.
I Even though the licensee assessed the CDF reductions from these plant im.irovements as being small, we recommend that the licensee be encouraged to make these procedural changes and advise the staff upon their completion.
III.
CONCLUSION Based on the above findings, the staff notes that: (1) the licensee's IPE is complete with regard to the information requested by Generic Letter 88-20 (and associated guidance in NUREG-1335), and (2) the IPE results are reasonable given the TMI design, operation, and history. As a result, the. staff concludes that the licensee's IPE process is capable of identifying the most likely severe accidents and severe accident vulnerabilities, and therefore, that the TMI IPE has met the intent of Generic Letter 88-20.
i It should be noted that the staff's review primarily focused on the licensee's ability to examine TMI for severe accident vulnerabilities. Although certain aspects of the IPE were explored in more detail than others, the review is not intended to validate ',he accuracy of the licensee's detailed findings (or i
quantification estimates) that stemmed from the examination. Therefore, this SER does not constitute NRC approval or endorsement of any IPE material for purposes other than those associated with meeting the intent of Generic Letter 88-20.
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