ML20128D249

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Insp Rept 50-298/93-01 on 930104-08.Design Mod Activities Performed within Licensee Organization W/Limited Outside Contractor Augmentation.Major Areas Inspected:Engineering & Technical Support at Station
ML20128D249
Person / Time
Site: Cooper Entergy icon.png
Issue date: 01/29/1993
From: Collins S, Mullikin R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20128D229 List:
References
50-298-93-01, 50-298-93-1, NUDOCS 9302100093
Download: ML20128D249 (28)


See also: IR 05000298/1993001

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U.S. NUCLEAR REGULATORY COMISSION-

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REGION IV

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l NRC Inspection Report: 50-298/93-01

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Operating License: DPR-46

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Licensee: Nebraska Public Power District- (NPPD)

, P.O. Box 499

Columbus, Nebraska 68702-0499

j Facility llame: Cooper Nuclear Station

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Inspection At: Brownville, Nebraska

l Inspection Conducted: January 4-8, 1993

l Acting Team Leader: 7 1Z M /-2 f- f3

R. P. Mullikin, Acting. Tea 6 Leader -Date

Technical Support Section-

Division of Reactor Projects

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leam Members: T. F. Westerman, Chief, Engineering-Section

Division of Reactor Safety-

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R. K. Frahe, Jr., Vendor Inspector (Rotational Assignment)

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Engineering'Section, Division of Reactor Safety

l P. A. Goldoerg, Reactor Inspector, Engineering Section

Division of Reactor Safety

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M.'F. Runyan, Reactor Inspector, Engineering Section

Division of Reactor safety.

l R.-B. Vickrey, Reactor Inspector, Engineering Section-

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Division of Reactor Safety.

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Accompanying Personnel: H. Rood, Project Manager, Office _.of Nuclear Reactor

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Approved: IN% i ~4 *t- 9~5

Date

y Samuel J. Collins, Director, Division of Reactor

Safety

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TABLE OF CONTENT 4

EASA -

EXECUTIVE SUMMARY . . . . . . . . . . . . . . . . . . . . . . . . . . iii

DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . I

1. ENGINEERING AND TECilNICAL SUPPORT ACTIVITIES . .-. . . . . . . 1

1.1 Design Chenges_and Modifications ............. -

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1.1.1 Permanent Design Changes and Modifications .-. . . I

1.1.2 Temporary Modifications .............

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1.1.3 Conclusions ...,............... 8-

1.2 Offsite Support Staff . . . . . . . . . . . . . . . . . . . -

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1.2.1- Nuclear Power Group . . . . . . . . . . . . ._. . . 8

1.2.2 Nuclear Engineering and Construction Divisinn . . . 9

1.2.3 Nuclear Configuration Management Department . . . . 9

1.2.4 Nuclear Engineering Department .......... 10

1.2.5 Nuclear Projects and Construction Department- ... 13

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1.2.6 Nuclear Fuels Department ............. 13

1.2.7 Cooper Nuclear Statf an Engineering Department . . . 13

1.2.8 Configuration Management ............. 15

1.2.9 Design Basis Program ............... 16

1.2.10 Engineering Disposition of Nonconformance Reports . 16

1.2.11 Audits and Assessments .............. 19

1.2.12 -Engineering Initiatives . . . . . . . . . . . . . .- 19

1.2.13 General Observations-Related to Engineering . . . . 19

1.2.14 Conclusions . . . . . . ............. 19

ATTACHKENT 1 - EXIT MEETING AND ATTENDEE 5

ATTACHMENT 2 - ENGINEERING STAFF GROWTH

ATTACHMENT 3 - ENGINEERING INITIATIVES

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EXECUTIVE SUMMARY

A team of NRC staff members conducted an inspection of engineering and

technical support at the Cooper Nuclear Station. The inspection was conducted

from January 4-3, 1993.

The NRC team utilized the guidance provided in NRC Inspection Procedures

37700, " Design Changes and Modifications," 37702, " Design Changes and

Modifications Program," and 40703, "Offsite Support Staff."

The inspection team reviewed the engineering organization for organizational

structure and interfaces, manpower and work backlogs, scheduling and

prioritization of work activities, support of plant operations, and

qualifications of personnel. The quality of engineering performance was

evaluated by reviewing completed station modification, design change work

packages, temporary modifications, and engineering disposition of

nonconformance reports. -The quality assurance audits and assessments of the

engineering and technical support organization, and the actions taken with

respect to the assessments and audit findings were reviewed.

The inspection team observed the following:

  • The engineering organization (onsite and corporate) had grown from

approximately 27 engineers in 1980 to 154 engineers by 1993.

  • In general, all design modification activities are performed

.within the licensee's organization with limited outside contractor

augmentation.

  • The overall process to control projects and design modification

activities appeared to be very effective. The backlog of work was

sina11.

  • Procedures for design changes and modifications were found to be

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comprehensive and well written.

  • The plant modification packages were found to be well written with good

safety evaluations.

  • A great deal of engineering effort was incorporated into the

modification process. Conservative engineering practices were observed.

strengths were noted in the weekly audit performed by senior licensed

operators and the use and control of permanent temporary modification

tags. The use of temporary modifications was limited and were not left

in place over 6 months.

  • The interface between corporate-engineering and site engineering-

appeared effective.

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  • There was a very stable engineering staff with a low turnover

rate.

  • Engineering personnel were qualified, trained, and their

responsibilities defined. Good morale was observed.

  • Staff levels appeared consistent with the workload.
  • Of particular note, with regard to qualification, was the emphasis

on shift technical advisor certification for system engineers.

  • The development of the program engineering department was seen as

an enhancement to the Cooper Nuclear Station engineering

department (onsite engineering.)

  • Engineering appeared to have good credibility and working

relationships within the licensee's organization.

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  • Configuration management was found to be effective.

In response to team observations, the licensee made the following comitments:

1. The licensee committed to annotate control room drawings and procedures

to indicate that an open temporary modifications affects those

documents. Inspection Followup Item 298/9301-01 was opened.

2. The licensee comitted to review the open temporary design changes

to determine if any could be rettaved or made permanent plant

reodifications. Inspection Followup Item 298/9301-02 was opened.

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DETAILS

1 ENGINEERING AND TECHNICAL SUPPORT ACTIVITIES

1.1 Quian Ch1D90_IDitiodifications (37700 and 37702)

1.1.1 Permanent Design Changes and Modifications

The team examined six design modifications to verify that the design

modifications were in conformance with the requirements of the Technical

Specifications,10 CFR Part E0.59, the updated safety analysis report (USAR),

and applicable codes and standards. The design change packages reviewed were:

  • DC 89-252B, " Trim Hodification to RHR-H0V-H034A"
  • DC 90-283, "CS-HOV-H026A&B and SW-HOV-H089A&B Rerate Due to Insufficient

Wall Thickness"

  • DC 90-292, "No Break Power Panel Static Inverters"
  • DC 90-302, "ASCO Transfer Switch Hodifications"
  • DC 92-141B " Independence of DC LPCI Valves from 125 VDC System"

The team reviewed the licensee's process associated with plant modifications.

The governing procedure for all permanent modifications to structures,

systems, components or equipment located at Cooper Nuclear Station (CNS) was

CNS Operations Manual Engineering Procedure 3.4, " Station Modifications,"

Revision 14. This procedure described the station modification process and

provided an overview on the use of the subset of procedures required to

process a design change. In addition, the team reviewed Engineering

Procedure 3.4.3, " Design Change," Revision 3, and Instruction Number NED-24,

"DC Writer's Guide," Revision 5. Procedure 3.4.3 specified the method for

preparing a permanent design change at CNS, and the instruction provided

information concerning the format and items which should be addressed when

preparing a design change. The team found the procedures to be comprehensive

and well written.

The team found that the development of a design modification package and the

assignment to a design engineer formally began after an engineering work

request was approved. Prior to the preparation of the package, a scoping

meeting was held at the site with participants from design engineering and

various site eganizations. As the package was developed, a conceptual design

meeting was held with the site organizations to review the design criteria,

proposed design fix, and perform walkdowns. The design change package

prepared by the design engineer consisted of a description of the change,

design analysis, safety evaluation, installation procedure, and acceptance

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testing. Once the package was complete, a General Office disciplinary review

and CNS site review were performed. In addition, selective reviews would be

performed as determined necessary. The package was approved by engineering

and the station operations review committee prior to implementation.

1.1.1.1 Design Change DC 89-2528

The team reviewed DC 89-252B, " Trim Modification to RHR-H0V-M034A," which

installed anticavitation trim into essential Valve RHR-H0V-H034A. The valve

is an 18-inch globe valve manufactured by Anchcr/ Darling Valve Company. This

valve is the res11ual heat removal Loop A suppression pool cooling throttle

valve. During the 1990 refueling vutage, the same trim was installed in the

Loop B equivalent valve and was found to be performing in a satisfactory

manner.

The plant previously had determined that the wall thickness of

Valve RHR-H0V-M034A was being gradually reduced due to cavitation / erosion

taking place. The modification was developed to arevent further

cavitation / erosion of the valve walls to insure tlat the minimum allowable

wall thickness was not violated.

The valve tria design change was completed in October 1991. The modification

consisted of replacing the original disc and seat ring, which required

complete disassembly of the valve. The original seat ring was machined out

and the new design welded in place. Welding and nondestructive examination

were performed in accordance with the ASME Boiler and Pressure Vessel Code,

Section III, 1986 Edition. The new trim utilized stellite as the hardfacing

material. Acceptance testing was performed in November 1991, which consisted

of a residual heat removai Loop A flow test and an inservice leak test.

The team reviewed the evaluation performed in accordance with the provisions

of 10 CFR Part 50.59, as well as the ALARA review and the impact on the USAR

and Technical Specifications. The team found that the safety evaluation was

complete and weli written. The team noted that a great deal of engineering

effort had been incorporated into the modification and conservative

engineering practices had been utilized.

1.1.1.2 Design Change DC 90-1748

The team reviewed DC 90-174B, " Service Water Pump Bearing and Shaft

Modification," which was prepared to modify the bronze bearings, shaft

sleeves, and shafts in the four Byron Jackson service water pumps. This

modification consisted of replacing the original bronze bearings with rubber

bearings housed in stainless steel casings. This bearing replacement was done

since the rubber bearings were designed to allow debris up to 1/8 inch in

diameter to be flushed through the bearing without affecting its performance.

Since the rubber bearings were larger in annular area than the bronze bearings

f9r strength purposes, it was necessarv to remove the stainless steel shaft

sleeves at the bearing locations and hard face the shafts to minimize shaft

wear.

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This modification was developed due to the difficulty of operation and the

high raintenance costs associated with maintaining the original service water

pump essential gland water injection system. The original dand water system

used cyclone separators to remove suspended solids. Because the components of ,

the essential gland water injection system were not no.mally operated,  !

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accumulation of particles in the components led to increased maintenance and

cleanup requirements. By using the rubber bearings which allowed debris to be

flushed through, this modification would allow the essential gland water

system to be simpitfied to delete the cyclone separators and allow the direct

use of the Missouri River water. This design change package only covered the

service water pumps' bearing and shaft modifications. The essential gland

seal modification was the subject of another design change package.

The rubber bearings and hardfaced shaft were initially installed on Service

Water Pump B and then tested for ar.ceptable performatice prior to modifying

Service Water Pumps A, C, and D. The licensee stated that, prior to the 1993

refueling outage, the remaining three service water pumps will have the

modification completed. The team performed an inspection of the physical

installation of the modification and found that the modification was installed

in accordance with the approved design.

The team found that a considerable effort had been made to address issues of

safety significance created by this modification. The team considered the

10 CFR Part 50.59 safety evaluation to be thorough-and well written. The team

also noted that the design change package reflected conservative engineering

practices.

1.1.1.3 Design Change DC 90-283

The team reviewed DC 90-283, "CS-MOV-M026A&B and SW-MOV-M089A&B Rerate Due to

Insufficialit hil Thickness." This design change rerated the core spray and

service water valves from the original purchased ratings to ratings which

l corresponded to the design temperatures and pressures of the valves. This

modification was a paper change only ard did not physically modify the valves

or-their systems.

The licensee had previously determined that the valves were below their

minimum wall thickness based on the ANSI Class they were purchased to. In

response to NRC Information Notice 89-01 concerning erosion in valves used for

throttling, the licensee had performed ultrasonic testing inspections and

found that the two service water valves and one of the core spray valves had

wall thicknesses below the minimum required for their ANSI Class. As a

result, nonconformance reports (NCRs) were generated to document the wall

thicknesses. The root causes for the insufficient wall thicknesses were

documented in the NCRs. The core spray valve was determined to have been

l originally supplied with a reduced wall thickness and was not subject to

erosion. However, the service water valves were determined to be susceptible

to erosion. .To prevent further erosion of the service water valves, the

licensee had applied an epoxy coating to the internals of the valves which was

documented in Special Test Procedure STP 89-173, " Application of Abrasion

l Control Putty on SW-MOV-M089A/M0898." The licensee is monitoring the epoxy

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coating in accordance with Preventive Maintenance Procedure 06821.

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This design change rerated the core spray valves (CS-MOV-M26A&B) from ANSI

Class 300 to ANSI Class 250, and rerated the service water valves

(SW-MOV-M089A&B) from ANSI Class 300 to ANSI Class 180. This was accomplished

in accordance with ANSI B16.34, 1977 Edition. The design pressures and

temperatures of the valves were used to determine the intermediate ANSI Class

ratings and minimum wall thicknesses. The minimum ANSI Class ratings were

documented in Calculation NEDC 89-1908.

The team found that the safety evaluation and checklists were thorough and

well written. The team also noted that the assertions and assumptions were

documented and reflected conservative engineering practices.

1.1.1.4 Design Change DC 90-292

The team reviewed DC 90-292 which modified the 120/240-Vac power supply to the

no break power panel (NBPP) by replacing the Static Inverter IA, static

switch, and manual bypass switch. This design change also modified the power

supply to four reactor core isolation cooling system control components by

installing a separate static inverter to provide essential 120-Vac power.

CNS initiated this modification because they felt the existing inverters and

associated components, which were original plant equipment, had an increased

likelihood of failure as the equipment continued to age. Failure of a

component in the inverter would likely cause a plant trip because a

significant number of instruments and controls derive their power from the

NBPP. The design change would minimize the likelihood of static inverter

failure and hence provide a more reliable power source to the NBPP.

The design basis for the inverter and NBPP was to provide a uninterruptible

power source for nonessential components that are critical for plant operation

and was unaffected by this modification. Performance of this design change

necessitated a change to the USAR to reflect the NBPP in its final

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The modification was reviewed and approved by the appropriate technical

disciplines prior to installation. The team reviewed the safety evaluation

' and 10 CFR Part 50.59 reportability analysis and considered them to have been

very detailed and well researched. All of the additional detailed evaluations

were made as part of the design change package, and the listing of affected

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document changes including drawings, procedures, vendor manuals, calculations,

and the USAR appeared complete. A license change request form was completed

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to assure a description of the change would be included in the annual report

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because a USAR change is reportable under 10 CFR Part 50.59(b).

Installation and acceptance testing of this design change was completed during

the 1991 refueling outage. The team walked down portions of the physical

osta11ation of the modification and found no problems. The team viewed that

..iis modification thoroughly addressed safety considerations and was well

prepared and installed,

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1.1.1.5 Design Change DC 90-302

The team reviewed DC 90-302 which removed the automatic transfer function from

the ASCO Model 935-307 transfer switches by physically removing the

unnecessary circuitry and components. The modification also added isolation

fuses in each of the transfer switches to allow local (manual) de-energizing

of the control circuit and provide electrical isolation of the nonessential

control power from the essential busses. Transformers were also installed to

lower the control circuitry voltage to 120 Vac to reduce potential safety

hazards during maintenance activities.

This design change was initiated to close out Temporary Design Change

TDC 90-300 which electrically removed the automatic transfer function from

Transfer Switch EE-MCC-X(IA) and exchanged the normal and emergency feedere to

provide a more appropriately distributed diesel loading. This design chm;;c

removed the disconnected components from that switch and performed a similar

modification on several other ASCO transfer switches. The control logic in

these transfer switches had been defeated procedurally by de-energizing the "

emergency feeders to the switches.

The design basis for the transfer switches, which was to provide a continuous

source of power, was maintained. This design change required a minor

modification to two figures in the USAR, but did not require any changes in

the Technical Specifications. The modification was reviewed and approved by

the appropriate technical areas prior to insti.llation. The safety evaluation

and 10 CFR Part 50.59 reportability analysis were completed and analyzed. All

of the additional detailed evaluations were ?ade as part of the design change

package, and the listing of affected document changes including drawings,

procedures, vendor manuals, calculations, and the USAR appeared complete. A

license change request form was completed to assure a description of the

change would be included in the annual report because a USAR change is

reportable under 10 CFR Part 50.59(b).

Installation and acceptance testing of the modification was completed during

the 1991 refueling outage. The team inspected the physical installation of

the modification for several of the transfer switches and found that they were

installed in accordance with the approved design change. The team concluded

that this design change package was clearly documented and implemented with a

great deal of engineering consideration of safety concerns.

1.1.1.6 Design Change DC 92-141B

The team reviewed DC 92-141B which modified the control power circuit for the

low pressure coolant injection (LPCI) and reactor recirculation pump discharge

valves. The contro~l power supplied to the starters was from a 125-Vdc source,

and this modification changed the source to the 250-Vdc motive power which was

already in each starter. The modification involved replacement of the starter

contact coils and control circuit fuses with components rated at a nominal

250-Vdc. It also included removal of starting resistors and associated

relays, installation of contactor coil surge suppression resistors and relays,

and miscellaneous wiring changes.

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This design change permitted control of LPCI injection and reactor

recirculation discharge valves to be independent of the 125-Vdc system. The

need for this modification was discovered during CNS's design basis review

efforts, when a failure moda was identi?ied in the 125-Vdc system which would

be more limiting than the previously analyzed LPCI injection valve failure.

Completion of the modification resolved the concerns related to the LPCI

single failure vulnerabilities and returned CNS to its original @ sign bases.

The loss of one division of 250-Vdc power is similar to the loss of one LPCI

valve and had already been aalyzed and documented in the USAR, so the

determination was made that this design change did not require a change to the

USAR or Technical Specifications. The modification was reviewed and approved

by several technical areas including systems, operations, maintenance,

radiation )rotectirtn, and quality assurance prior to installation. The team

reviewed tie safety evaluation and 10 CFR Part 50.59 reportability analysis

and considered then to have been quite thorough and well written. Additional

detailed evaluations were made as part of the design change package to

determine effects on ALARA, fire protection / Appendix R, inservice

inspection / testing, human factors, environmental qualification, Regulatory

Guide 1.97, emergency operating procedules, motor operated valves, and others.

The packaga also included a detailed listing of affected document changes

including drawings, procedures, vendor manuals, and calculations.

Installation and acceptance testing of the modification was completed in

September 1992, while the plant was in cold shutdown. Five changes were made

to the original modification package and were documented by on-the-spot change

sheets as detailed in Engineering Procedure 3.4.10. " Revisions, Amendments,

and On-The-Spot Changes," Revision 2. The team concluded that this design

change package was well prepared and reviewed by CNS to identify and address

all potential issues of safety significance created by the modification.

1.1.2 Temporary Modifications

fhe team reviewed six ,,lant temporary modifications. The temporary

modifications reviewed were:

  • PTM-92-05 Leak Repair Clamp on HPCI Steam Line Dripleg

Drain Line to Main Cendenser

  • PTM-92-06 Pipe Cap on B-5 Heater Inlet Drain Valve MC-V-524
  • PTM-92-09 Lifted Leads on MS-LS-101 and 102 Due to Grounds
  • PTM-92-12 Pipe Cap on Drain Valve DGD0-V-44

Setpoint Change

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The team reviewed Conduct of Operations Procedure 2.0.7, " Plant Temporary

Modifications Control," Revision 14, and Engineering Procedure 3.4.4,

" Temporary Design Change." Revision 4. The team concluded that the procedures

properly provided for the control of temporary modifications to safety-related

plant systems as required by the Technical Specifications and

10 CFR Part 50.59. These procedures applied to both safety-related and

nonsafety-related temporary modifications. The licensee attempted to limit

the number of temporary modifications by utilizing the permanent design change

process for major scope temporary modifications. There were relatively few

temporary modifications installed during the past 2 years (17 in 1992 and 22

in 1991). However, the licensee utilizes temporary design changes, which are

temporary modifications installed greater than 6 months. The use of temporary

design changes had the benefit of drawing and procedure updates. There were

19 temporary design changes still open during the time of the inspection, of

which 3 were installed in 1986. The team reviewed these temporary design

changes and found, although minor in significance, that several could possibly

be removed or made permanent plant modifications. The licensee committed to

review the open temporary design changes to determine which could be removed

or made permanent. The review of the licensee's review of temporary design

changes is an inspection followup item. (50-298/9301-01)

The team reviewed the six temt irary modifications and found the

10 CFR Part 50.59 evaluations to be good. The modifications had proper review

and approval by the licensee. The team noted that control room drawings

affected by temporary modifications were not procedurally required to be

annotated in any manner to indicate an outstanding temporary modification.

This created the possibility of an operator making a decision using a drawing

that was not indicative of the actual plant configuration. However, the

temporary modifications installed that afi'ected control room drawings would

have very little safety significance. In addition, there were a small number

of open temporary modifications and the shift supervisors interviewed were

aware of the temporary modifications. The licensee committed to enhance the

temporary modification process by requiring that control room drawings end

! procedures be annotated to reflect that a temporary modification affected that

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document. The team's review of the licensee's enhancements to the temporary

modification program is an inspection followup item. (50-298/9301-02)

The licensee performs various audits of the teroorary modification process.

The operations supervisor or designee performed a monthly administrative audit

of the control room temporary modification log. This audit mainly determined

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i which modifiestions were no longer needed and which ones were to be made

temporary design changes. A weekly audit was performed by the shift

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supervisor or a . senior reactor operator. This audit was a physical walkdown

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to verify that the installation is as described by the temporary modification

package. The team accompanied the shift supervisor on his weekly audit and

found no discrepancies with the field installation. The team noted two

strengths from this audit. The verification was very detailed and would

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provide excellent assurance of proper plcnt configuration of the temporary

modification. Secondly, the licensee utilizes permanent plastic temporary

modification tags which were visibly attached near the modification. These

tags were noted by number in the control room log and must be returned to the

control room efter the temporary modification is removed. The tags were

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audited to verify that all tags are accounted for. This provided for added

assurance that closed temporary modifications are actually removed.

The team also rufewed the results of recent quality assurance surveillances

of the temporary modification and temporary design change processes, and found

that a good review was parformed by the-licensee. The team also reviewed a

computer printout describing all the safety-related maintenance work requests

generated in 1992. The team found no instances where a maintenance work-

request was used in lieu of a temporary modification, temporary design change,

or a perwanent plant design change.

1.1.3 Conclusiong

  • Procedures for design changes and modifications were found to be

comprehensive and well written.

  • The plant modification packages were found to be well written with good

safety evaluations.

  • A great deal of engineering effort was apparently incorporated into the

modification process. Conservative engineering practices were apparent.

strengths ware noted in the weekly audit performed by senior licensed

operators ar.d the use and control of permanent temporary modification

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j changes process were noted. The licensee committed to annotate

, control room drawings and procedures to indicate the existence of

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an open temporary modification. Also committed to was the review

of open tusporary design changes-to determine if any could be

removed or made permanent plant modifications.

1.2 Offsite Suonort Staff (40703)

1.2.1 Nuclear Power Group (NPG)

The engineering and technical support functions for CNS were an integral part

of NPG,-located both in the NPPD General Office in Columbus, Nebraska and

onsite. All functions of NPG reported via the NPG Manager, located in the

NPPD General Office, to the Vice President - Production. Reporting to the NPG

Manager were the CNS Site Manager - Nuclear Operations Division, the Division

Manager of Nuclear Engineering & Construction, the Division Manager of Quality

Assurance, and the Division' Manager of Nuclear Support. The specific

responsibilities of each manager were outlined in functional job descriptions.

NPG Directive 1.2 stated that within NPG a single integrated organization is

provided for the safe and efficient operation, maintenance, modification, and

support of CNS. The inspection team observed that the-staff within NPG has

evolved from around 280 in 1985 to a present allocated staff of 569 with

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around 10 vacancies. This number did not include a contract security force of

around 85, general office personnel of around 100, and outside contractors.

The use of contractors was observed by the inspection team to be generally

limited (indicated presently to be 13). Engineering (onsite and corporate)

had evolved from approximately 27 engineers in 1980 to 154 engineers by 1993.

Attachment 2 is a giaphical chart of engineering staff growth from 13 NPPD

deneral Office and 14 CNS engineers in 1980 to 97 NPPD General Office and 57

CNS engineers in 1993. The overall organization appeared stable with a very

low turnover rate.

Engineering functions within NPG were principally performed by the nuclear

engineering and construction (NE&C) division in the General Offices of NPPD

and onsite by the CNS engineering group. The NE&C division has established a

site engineering group to improve their interface and support of the site.

The CNS engineering group reported to the CNS Site Manager.

The hierarchy of procedures observed by the inspectors consisted of NPG

directives (establishing corporate policy and direction), CNS policy

. directives (site), NE&C division procedures, and HE&C division guidelines.

1.2.2 NE&C Division

The NE&C division consisted of the nuclear configuration management

department, the nuclear enginewring department, the nuclear projects and

construction department, and the nuclear fuels department. The inspection

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team found that there were 102 engineers and technicians allocated to this

division with five vacancies.

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The inspection team found that major activities and planning were set forth in

, a 5-year business plan that is updated annually. Goals and objectives are

also assigned to each division. The implementation of the goals and

objectives are reviewed quarterly and a status issued by each division. The

inspectors observed that the goals and objectives established for the NE&C

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division provided for continued enhancements to the NESC division. Goals

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established included the completion of all modification packages and

procurement 30 days prior to a planned refueling outage and 90 days prior to

work that does not require an outage. An outage scope list was established by

the work planning and ianagement committee (composed of corporate and site

managers) for each refueling cycle. The outage scope list established the

engineering activities to be accomplished during each cycle. Licensee

management indicated that the outage scope list for the next fuel cycle was

near completion. The inspectors found that a monthly NED status of activities

l for NED was maintained. There was also a NE&C division programs book for

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setting priorities and tracking engineering initiatives and programs. Project

managers issued a monthly report. The overall scheduling and prioritization

of work was computer tracked by the nuclear item tracking (NAIT) or the CNS

action and comitment tracking (ACT) systems. Licensee management has '

indicated that changing the CNS fuel cycle to 18 months over the last two - 4

cycles has provided engineering with more time to plan and complete their

engineering activities. Work backlogs have essentially been eliminated.

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1.2.3 Nuclear Configuration Management Department  !

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The nuclear configuration manaDement department had three major groups. These

consisted of the configuration management group, the PRA and engineering

review group, and the design basis group. There were 12 personnel allocated

with no vacancies.

The configuration management group was a special group that had been verifying

the as-built configuration of the 245 safety-related drawings utilized by the

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o>erators in the control room and the 1300 related drawings. Supervision in

t11s group indicated that approximately 98.2 percent of control room drawings

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have been upgraded. ,

The PRA engineering review group had responsibility for the. site PRA related

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activities and engineering reviews. The status of the individual plant

examination (IPE) program was reviewed by the team. The program was also

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supported by NED personnel, the CNS operation support group, and CNS system

engineers. Science Applications international Corporation (SAIC) has been the

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primary contractor. Engineering & Research, Inc.-(ERIN) has been contracted

and was providing prog am advice and third party review. The licensee stated

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that preliminary results indicate that there was-no significant vulnerability.

The core damage frequency for CNS is 7.9/ E-5. The licensee indicated that

the core damage frequency was dominated by station blackout (35 percent) and .

transient induced LOCA (30 percent). Their IPE (PRA Level I and II) submittal

in response to Generic Letter OL 88-20, " Individual Plant Examination of

Severe Accident Vulnerabilities," was scheduled for March 1993. This group

will continue to have the responsiFility to maintain the PRA. The utilization

of PRA was indicated to have been limited due to the concentration of effort

to complete the IPE. The future uttiization of PRA within the licensee's

, activities was under development. The IPEEE (PRA Level III) was being

. developed by the project management group and was sr.heduled for submittal in

i June 1994.

The design basis group has responsibility for the design basis program. This

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program was observed by the team to have been through a significant

evolutionary process. The NPPD first pilot program began in 1987. There were

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several starts and stops in the program. All work was stopped as late as

September 1992 following issuance of the August 10, 1992, NRC Polic' Statement

which was issued in conjunction with SECY 91-364 (November 12, 199.j and

. SECY 92-193 (May 26, 1992). The scope of the program was to complete 21

system design criteria documents and five topical design criteria documents.

. The diesel generator design criteria document (one of three documents

completed) was reviewed by the team and appeared to be of good quality. The

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scheduled completion was in 1997. The licensee planned to complete the

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program in house and maintain the expertise within NPPD. The licensee has

indicated that the plant design appears to be " robust." The identification of

the recent control wiring routing in a non-Class IE area which could have

rendered both emergency diesel generators inoperable was observed by the team

to be indicative of the present level of review.

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1.2.4 Nuclear Er,gineering Department (NED)

The NED was responsible for the dest n of the plant, maintaining the plant

designbasis,andprovidingengineer$ngsupporttotheplantonanas-needed i

basis. The NED organization included instrumentation and control (!&C),

electrical, civil / structural, mechanical, aid technical support disciplines

based in the NPPD General Office, as well as a site engineering group based at

the CNS site. The technical support group focused on regulatory issues so

that the other engineering disciplines could concentrate on plant

modifications. NED was composed of 69 people including 46 degreed engineers,

21 technicians, and 2 secretaries.

The first four groups identified above performed all design modification

activities for NPPD in each of the identified engineering disciplines. The

inspectors found that the licensee performed all design work with in-house

personnel, with limited utilization of outside contractors t3 provide staff

augmentation when necessary. When assigned the lead, a design package would

be completely developed by the assigned engineer with the assistance of the

other discipline groups as required. This same engineer would go to the site

for full coverage of the modification during installation as part of the site

engineering group. An engineer may be assigned to work as a part of a

projects group, but is technically responsible for his work to the supervisor

for his discipline. The inspectors observed that there were some safety-

related software programs used by the civil / structural groups in performing

Class I seismic analysis and some within the electrical engineering group. In

discussions with the supervisors in NED, the inspectors found that the

licensee has been able to hire quality angineers with high grade point

averages. Most successful hires have been from engineers coming back to the

area. In accordance with the NPPD training program description, technical

training was provided as )osition required, task required, and optional. In <

addition, most engineers 1 ave Ld system training. Additional general

training was recently completed for all engineers in response to a third party

audit. All engineers were encouraged to obtain their professional engineer's

license. A monthly salary bonus is provided to all engineers with a

professional engineer's license.

The technical support group performed special studies, responded to some NRC

requests such as generic letters, was responsible for fire protection long-

term compitance, performed engineering reviews, coordinated procurement for

modifications, and was responsible for the development of engineering

directives, policies, and procedures.

The site engineering group provided the onsite interface with NED and

coordinated all onsite NED engineering activities (particularly during

refueling or other outages). There was also a dedicated group of onsite

draftsmen that assisted with walkdowns and drawing upgradas.

The team interviewed 20 NED engineers assigned to the I&C, electrical,

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civil / structural, mechanical, and technical support disciplines to evaluate

the functionality of the NED staff. The engineers were knowledgeable of their

res)onsibilities and interfaces as well as the availability and use of

tec1nical information. Those interviered appeared very pleased with the

current operation of NED and many emphasized that recent improvements were

effective, including the addition of the NED site manager and the increased

availability of computers.

The team determined that staffing levels of each discipline appeared to be

consistent with the workload. Between outages, the design engineers worked

little or no overtime. During outager., however, the design engineers

typically worked six 12-hour days, e ,secially if they were the responsible

engineer for any of the modifications being installed. NED developed the  !

large majority of their own modifications, and the small portion delegated to

contractors were reviewed by NED engineers. l

4

The team found that the NED staff's average nuc1'.c experience was 6 years,

and 19 of the NED engineers had obtained their pwfessional certification.

The staff also had available tuition assistance for job-related education, but  !

few engineers participated due to the lack of local opportunities. The NED l

had a low attrition rate which could indicate that the engineers had a great

deal of job satisfaction.

The team noted that the design engineers were respensible for their assigned

modifications from conception to completion. The design engtheers stated that

they were not involved in day-to-day site activities and that those activities

were the responsibility of the plant systems engineers. There appeared to be

little if any duplication of effort within the NED or with plant systems

engineering.

The team observed that interfaces between the NED and site personnel appeared

effective despite the fact that the NED design engineers were stationed at the

General Office. The NED design engineers stated that they made frequent

visits to the site as necessary when preparing their design change packages,

perhaps once or twice a month, and were predominately at the site during

outages when their :nodifications were being installed. Management encouraged

the design engineers to spend time at the site, and made available two

airplanes and numerous company cars for transportation. The scoping and

conce)tual design meetings in the early stages of the design change process

also 1elped to improve communications with plant systems engineering,

operations, maintenance, and other site groups. The addition of the NED site

manager and his staff also greatly increased the effectiveness of

communications between the NED and site personnel.

The training program for NED employees appeared to be effective. Subject

matter included root cause analysis,10 TR Part 50.59 reviews, a boiling

water reactor system overview, industry codes and standards, the CNS Technical

Specifications, the USAR, and numerous others. Some of the engineers lacked

training in operability determinations and regulatory requirements, but were

not directly responsible for these activities and were cognizant of how to

find the requirements if necessary.

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The team discovered that there were several tools available to the design

engineers. Most of the engineers had personal computers on their desks with

word processing and other capabilities. They also had access to a main frame

computer which provided information on component data, action item tracking,

nonconformance report (NCR) tracking, drawing numbers, purchase orders, spare

parts inventory, microfilm record addresses and others. There were

controlled sets of vendor manuals, applicable procedures, Technical

Spacifications, and the USAR readily available. There were only a few design

basis documents issued to date, but the engineers felt they would be a useful

tool in the future.

The team concluded that employee morale was high and management support was

strong. NED personnel were qualified, trained, and their responsibilities

defined. The team considered the staffing levels to be consistent with the

work load and interfaces between NED and site personnel to be sufficient.

Overall, the team viewed NPPD as having an effective design engineering

program.

1.2.5 Nuclear Projects and Construction Department

Within this department was the nuclear projects group and construction group.

There were four project managers and a construction manager. A total 14

allocated positions, including two secretaries formed this department. The

team found that the )rojects group operated as a matrix organization with a

project manager in c1arge. Each project manager normally had several projects

assigned. Normally, the more major projects assigned can draw from all of NPG

for personnel to perform within the project. The design, procurement,

installation and testing of the hard vent was one of the projects assigned to

this group.

The construction group was responsible for providing onsite craft personnel to

accomplish both outage and nonoutage activities.

1.2.6 Nuclear Fuels Department

Within this department were three allocated positions, all associated with

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nuclear fuels procurement. The manager position was vacant. The team fou~i

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that all engineering and reload analysis was performed by General Electric

(GE). This department provided oversight of GE. As a part of this oversight,

staff members participated in an annual audit of GE in the fuels area.

1.2.7 CNS Engineering Department

The CNS engineering department was the )rimry onsite engineering resource,

consisting of three departments. The t1ree departments were operations,

plant, and programs engineering, with each reporting to a department

supervisor. Also, three senior engineers reported to an assistant engineering

manager. The supervisors and the assistant manager reported to the

engineering manager, who reported to the plant manager. Additionally, smaller

staffs of engineers were assigned to the maintenance department, the technical

staff department, the quality assurance department, and the onsite design

engineering department.

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The system engineers were divided into two departments. The operations

engineering department consisted of 10 budgeted engineers with no vacancies.

This department was responsible for power production systems including the

reactor, turbine, and associated support systems. The engineers were divided

into three groups; reactor, operations, and performance engineering. Each

group reported via a lead engineer to the operations department supervisor.

The plant engineering department consisted of 13 budgeted engineers with no

vacancies. This department was responsible for safety systems incit ding

reactor protection, containment isolation, em^rgency power, and emergency core

cooling. The engineers were divided into two groups; electrical /I&C and

mechanical engineering. Each group reported via a lead engineer to the plant

engineering supervisor.

The main functions of the system engineers were:

  • Observing surveillance tests
  • Monitoring equipment performance
  • Reviewing maintenance work req 1tsts ato postmaintenance testing
  • Generating maintenance work request special instructions

Of the 70 systems in the plant, all were assigned to system engineers in the

system engineering departments.

The team found that systems engineers were given extensive systems training,

and received a detailed system checkout on their assigned systems as a part of

their qualification arocess. The team also found th'it, in addition to other

rsquired training, w11ch included root cause and safety evaluation tra,ining,

system engineers were allnwed the opportunity to attend other scheduled

courses such as maintenance training and career enhancement courses. Of

particular note was the licensee's efforts to strengthen system engineering

with shift technical advisor certification of system engineers. The team

observed that the system engineering staff had experienced a very low turnover

rate. The licensee appeared to have a goed development program for system

engineers.

'

The licensee had developed an extensive trending program. This program was

under the administration of the assistant engineering manager. The program

tracked over 2000 individual tr# nds. System re) orts were updated quarterly

and a quarterly adverse trend rsport was publisied. The system was readily

j available to individual system engineers through the local area network

l system.

The programs engineering department consisted of eight budgeted engineers,

with one vacancy. This department was responsible for the tuhnical direction

of 21 progr!.ms. The department was composed of mechanical and electrical

l engineers who were respon;ible for the various programs under engineering such

l as ASME, Ap)endix J, environmental qualification, procurement, etc. This

department 1ad been initiated to focus engineering programs into one

department. Since its inception, a large portion of the resources in this

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department have been devoted to upgrading these programs. The department

responsibilities included: direct technical su> port of maintenance, project

management / program development, independent tecinical overview / review, and

specialized technical expertise.

The CNS engineering action items were tracked, scheduled, and prioritized

through a computerized database (ACT). Regulatory compliance actions items

were also independently tracked by a separate database (NAIT). The status of

critical items was discussed daily in manager and supervisor staff meetings.

These mechanisms were used to ensure that action items were identified and

completed in a timely manner and that management was aware of action item

status and emerging issues. 1he team concluded that these mechanisms had been

effective in reducing previous backlogs and maintaining subsequent bachlogs at

a reasonably low lavnl.

The taam concluded that the CNS engineering department training program was a

strength in development of an effective engineering program. Of particular

note was the licensee's emphasis on shift technical advisor certification of

system engineers. The team viewed the engineering department's coordination

of related activities as superior. The licensee's initiative in the

development of the program engineering department wa: seen as an enhancement

to the CNS engineering departoeat. The team found the engineering department

engineers had developed very good credibility and working relationships

throughout the licensee's organization. The team found a strong sense of

ownership of systems by the system engineers.

1.2.8 Configuration Management

The team reviewed the NPPD 1rocess for controlling CNS design changes to

determine the adequacy of t1eir configuration management program. The nuclear

power group directive tiefining and describing the program was documented in

" Configuration Management," Operations Section 4.4, Revision 1. CNS

criginated drawing changes were documented on the drawing change notice (DCN)

form and forwarded to the record; administration section (RAS) as described in

Engineering Procedure 3.7, " Drawing Change Notico," Revision 7. RAS verified

duplication of the change, assigned DCN control numbers, issu'ed DCN

transmittals to all drawing custodians in accordance with the distribution

list, and tracked the status of the DCNs to assure timeliness of

incorporation. The team noted that NPPD seemed to incorporate design changes

in a tirrely manner with a minimal backlog.

The team reviewed the controlled drawings that )rovide the control room

operators the necessary information to assure tie plant raaintains safe

operation. Control room drawings (CRDs) were maintained by the CRD custodian

in accordance with Operations Instruction Number 3 " Control Room Orawings,"

Revition 3. When a modification was approved which would affect a CRD, the

CRD custodian stamped the affected drawing to inform the operators that the

drawing was subject to revision. When the modification was installed, the CRD

custodian would receive a status report wi'.h a marked-up interim drawing

attached as detailed in Engineering Procedure 3.4.11, " Status Reports,"

Revision 3. The CRD custodian then filed the interim drawings and highlighted

the stamp on the affected drawing to signify the design change installation

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and the availability of interim drawings. Once the DCN was issued, the CRD

custodian stamped the affected drawings to reference the DCN number, filed the

DCN, and discarded the interim drawings. U)on receipt of the revised drawing

transmittals, the CRD custodian discarded tie old drawing revision and

replaced it with the new revision. Tne CRD custodian also performed a

quarterly audit of the CRD drawings and drawing files to assure accuracy. The

team spot checked several drawings to verify proper revision and status and

found no discrepancies. The team concluded that control room drawings were

controlled.

The team also reviewed the program for ensuring the accuracy of vendor

manuals. The engineering programs department (EPD) maintained the vendor

manual control system as described in Engineering Procedure 3.11 " Vendor

Contact for Verification of Manuals," Revision 4. The EPD contacted

applicable vendors yearly for essential components, and every two years for

nonessential components, to assure the CNS controlled vendor manuals were the

latest revision pertinent to equipment installed at CNS. CNS utilized a

vendor manual change form to assure manuals were evaluated and updated as

necessary based on information originating either within or outside NPPD. The

program requirements for this activity were contained in Engineering

Procedures 3.11.1, " Generating and Dispositioning Vendor Manual Change Forms,"

Revision 2, and 3.11.2 " Vendor Manual Update Control," Revision 1. The team

viewed CNS's program for updating vendor manuals as very good, but did not

verify the implementation of the program,

1.2.9 Design Basis Program

CNS's " Design Basis Program Description," dated November 30, 1992, documented

the )regram and assigned responsibility for its develo) ment and implementation

to tie nuclear configuration management department. T1e purpose of the

program was to document the design basis in design criteria documents (DCDs)

for the identified safety systems, to ensure that the physical plant and

design documents avset the design basis. CNS identified several uses for the

DCDs including serving as a reference to support operability and reportability

evaluations, safety reviews, Technical Specification reviews, and

design /setpoint reviews.

The current procedure to control the process for preparatlon, review, and

maintenance of the DCDs was Procedure NECDP-03 " Design Criteria Document

Production," Revision 1. Design basis teams were developed with

representatives from NED, licensing, operations, and system engineering to

coordinate the review and approval of the DCDs within their departments. The

procedure included an extensive listing of design documents which should be

reviewed for applicebility when preparing DCDs. A logic diagram would then be

produced which identified the system safety objective, design criteria, design

requirements, and critical components to serve as a template for the system

design basis development.

Individuals which identified design basis information that deviated from, or

should be included in the DCD, were instructed to complete a change request'

form to assure incorporation into the DCDs. Procedure NECDP-09, " Evaluation

of Open Items Identified during DCD Production," Revision 2, provided controls

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for processing and resolving open items and discrepr.ncies identified during

the production and maintenance of DCDs. The team concluded that the use of

DCDs is clearly defined and measures have been implemented to maintain the

documents current to accurately reflect plant modifications.

1.2.10 Engineering Disposition of Nonconformance Reports (NCRs)

in addition to developing design modification packages. HED provided support

to the plant by evaluating a small percentage of NCRs that are specifically

directed to them for disposition. The team reviewed the following NCRs that

fell into this category:

  • 91-045 Loss of Voltage Relay Setting
  • 91-055 Diesel Generator Fan Coil Unit Supports not Seismically

Qualified

  • 91-077 Loss of 161 kV Power Due to Operator Error
  • 91-099 Diesel Generator Manual Start Problems

Nonessential HVAC

  • 92-078 Unqualified Terminal Block in EQ Circuit

Each of the NCRs that were reviewed showed extensive effort and conservative

judgement. Of special note, a root cause analysis was performed for each NCR

and was used in conjunction with a study of previous similar NCRs to develop

an effective preventive action plan. The team determined that the actions

taken for each of the NCRs and the level of documentation provided in the

finished document were appropriate. The team interviewed several of the

engineers responsible for the disposition of the reviewed NCRs and determined

that a high degree of professionalism and expertise was evident. Overall, the

effort provided by the NED engineers to address the reviewed NCRs was

exemplary.

To assess the quality of support provided by the site engineering group for

plant operations, the team selected for review several NCRs and deficiency

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reports that had been directed to site engineering for disposition. The NCRs

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that were selected are listed below:

o 91-074 Indications on Reactor Pressure Vessel Head Studs

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  • 91-093 Use of a Nonessential Mechanical Seal

i * 91-103 Safety Relief Valve Lift Pressures Out of Tolerance

  • 91-118 Motor Operator loosened and Rotated on a Yalve
  • 92-016 Temperature Switch Setpoint Out Of Tolerance
  • 92-070 Olesel Generator Fuel Oil flash Puint less Than Minimum

Specified ,

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  • 92-102 Suppression Chamber Air Temperature Detector failure

Similar to the NCRs performed by NED, the above NCRs dispositioned by the site

engineering group showed extensive effort and conservative judgement. A

detailed and well-conceived root cause analysis was provided for each NCR

along with a review of previous NCRs to detect potential repetitive problems.

In all cases, the immediate corrective and long-term preventive actions

, a)peared appropriate. .To gather additional information on some of the NCRs, ,

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tie team interviewed the responsible engineers. Two observations were

discussed with the licensee. NCR 92-102 documented a failure of a suppression

chamber air temperature detector due to a power supply failure. The detectors

and associated power supplies were manufactured by Honeywell. The power

supply failed due to a failed diode and capacitor, apparently an.end-of-life

consideration. At least one previous Honeywell power supply failure was due

to a similar cause. The licensee had considered the failure rate to be too

. sporadic to justify generic action (i.e., replacement), but the team was

sensitive to the potential for an increasing failure rate due to a shared end-

of-life (20 years since installation) condition. The team did not expect the

licensee to take imediate action on this observation but to be aware of the

potential implications. The other observation concerned NCR 91-103 which

documented the fact that all eight of the main steam safety relief valves had

been found to lift at pressures ranging from 1.7 to 13.3 percent above the

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Technical Specification setpoint. The allowed toler;nce was only

+/- 1 percent. The licensee detennined the root cause to be corrosion bonding

and labyrinth seal friction. An analysis had been perforo d showing that the

as-found lift pressures would not have compromised the safety of the plant.

Corrective action on this problem was being held in abeyance pending future

initiatives anticipated from the boiling water reactors owners group. The

team did not identify a concern with the proposed corrective action plan, but

did note that the licensee had considered the reporting of this event to be

voluntary.

The team reviewed the following deficiency reports that had been directed to

the site engineering group for dispositioning:

  • 92-025 Small Boric Piping Does Not Meet Code Allowable Stress

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  • 92-029 Battery Cell Voltage Low ,

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The team considered the corrective and preventive actions taken for the above

deficiencies to be proper. Additionally, none of the reviewed deficiency

reports appeared to be of sufficient severity to be more appropriately

categorized as an NCR. The deficiency report process was implemented in

October 1992,

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1.2.11 Audits and Assessments l

The overviev function of engineering activities was the responsibility of the

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Division Manager of Quality Assurance. This organization performed audits,  ;

surveillances, safety system functional inspections (SSrls), and self

assessments.

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i The inspector observed that an audit of design control was performed annually.

The inspector reviewed the findings of the audits performed in 1991 and 1992.

i The 1992 audit report iridicated that 236 surveillances and in-line reviews

were performed. The report indicated that 69 were )erformance bued. Only

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one finding was issued. The 1992 audit concluded t1at the functional area of

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design control was being effectively implemented. The licensee indicated that

job task training was being given to the auditors. More performance Leased

i audits and surveillances were being planned and conducted. One SSFI was

performed of the core spray system. The use of SSF!s has been limited. In

accordance with the NPG self-assessment program, c self assessment of

electrical distribution system was performed in 1991 which concluded'that tha

electrical distribution system and related support systems at CNS met its

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intended design functions. More self-assessment activities were being

planned. A self assessment of shutdown risk activities was just being

completed. A self assessment of the service water system was being scheduled.

The licensee was encouraged by the team to consider conducting a self

.ssessment of engineering. .

i 1.2.12 Engineering Initiatives

The licensee provided the team with a list of 35 NPG engineering initiatives ,

(Attachment 3). The team observed that the initiatives were being implemented ,

in a number of different projects throughout the organization.-

1.2.13 General Observations Related to Engineering

The team observed that the licensee has established a program in response'to

the NRC program for systematic asse:ssment of licensee performance (SALP). The

program provided for a quarterly status of the enhancement and actions taken

in response to the SALP identified issues. The program document stated that

nuclear safety is of paramount importance, that rising standards of

performance are necessary to achieve and maintain excellence of performance,

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and the importance to develop and sustain a self critical, questioning

attitude among all employees. The team reviewed the engineering and technical

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, support section of the quarterly status report and found that each of the

l issues identified in the previous NRC SALP report have or were being responded

l to.

1.2.14 Conclusions l

  • There was a very stable engineering staff (onsite and corporate) with a

low tiirnover rate, which had evolved from approximately 27 engineers in

1980 to 154 engineers by 1993. q

  • In general all design modification activities are performed within

the itcensco's organization with limited outside contractor

augmentation.

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  • -The overall process to control projects and design modification

activities appears to be very effective. The backlog cf work is i

small.

  • The design basis program has been through a significant evolution.

The recent identification of design basis issues was indicative of

the effectiveness of the program.

  • The individual clant examination for PRA Levels I and II was t

. scheduled to be'sutaitted in March 1993. The licensee indicated

that no significant vulnerabilities have been identified.

  • The interface between corporate engineering'and site engineering

appeared effective. .

  • Employee morale was high and management support was strong.

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  • Engineering personnel were qualified, trained,- ar.d their

responsibilities defined.

  • Staff levels appeared consistent with the workload.
  • Of particular note, with regard to qualification, was the emphasis ,

en shift technical advisor certification-for system engineers.

  • iLe development of the program engineering-department was seen as -

u enhancement to the CNS engineering department.

  • .12gineering had good credibility and working relationships within -

m e licensee's organization.

  • fanfiguration management was found to be effective.

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ATTACHMENT 1

1 PERSONS CONTACTED

1.1 Licensee Personnel

R. Augspurger, Lead Civil / Structural Civil Engineer

A. Boesch, I&C Engineering Supervisor l

M. Borce, Design Basis Superviser

J. Branch, PRA and Engineering Review Supervisor

  • L. Bray, Regulatory Compliance Specialist  !

D. Busan, Lead Electrical Engineer

R. Bussard, I&C Electrical Engineer

K. Curry, Mechanical Engineer

J. Dewyke, Mechanical Engineer

K. Done, Mechanical Engineering Supervisor

T. Duren, Civil / Structural Engineer

  • J. Dutton, Nuclear Training Manager

W. Fisher, Electrical Engineering Supervisor

  • J. Flaherty, Cooper NJClear Station Engineering Manager
  • R. Foust, Assistant Engineering Mar,ager
  • S. Freborg, Plant Engineering Supervisor
  • R. Gardner, Plant Manager

M. H111strom. Technical Support Supervisor

  1. G. Horn, Nuclear Power Group Manager

M. Kennedy, Electrical Engineer

S. Kochanowicz, Mechanical Engineer

L. Kohles, Nuclear Projects and Construction Manager

E. Lanning, Acting Nuclear Fuels Manager

  • E. Hace, Senior Manager, Site Support

M. Mager, Senior Mechanical Engineer

  1. G. McClure, Nuclear Engineering Department Manager

T. McC1'Jre, Hechanical Engineer

D. McManaman, Electrical Engineer

B. McMillen, Lead I&C Electrical Engineer

  • J. Neacham, Site Manager
  • C. Moeller, Technical Staff Manager

J. Murphy, Acting Nuclear Projects and Construction Manager

M. Parr, Lead I&C Specialist

  • S. Peterson, Senior Manager of Operations

R. Rexroad, Electrical Engineer

  1. D. Robinson, Quality Assurance Manager

M. Siedlik, Civil / Structural Supervisor

  1. G. Smith, Licensing Manager
  • M. Spencer, Engineering Programs Supervisor
  • W. Swantz, Project Manager

S. Thompson, Lead Electrical Enginaer

G. Tillotson, Civil / Structural Engineer

J. Ullmann, Configuration Management Supervisor

K. Walden, Nuclear Configuration Management Department Manager

  • R. Wenzl, Muclear Engineering Department Site Manager

A. Wiese, lead Mechanical Engineer

1

-

. ' <* ,

,

4

  1. R. Wilbur, Nuclear Engineering and Construction Division Manager

B. Wilcox, Lead Mechanical Engineer

J. Wright, Mechanical Engineer

B. Vants, IAC Electrical Engineer

1.2 NRC Periknn.tl

  • S. Collins, Division Director, Division of Reactor Safety, Region IV I
  • J. Gagliardo, Chief, Reactor Projects Section C, Region IV
  • W. Walker, Resident Inspector

in addition to the personnel listed above, the inspectors enntacted other

personnel during this inspection period.

  • Denotes personnel that attended the exit meeting.

4 # Denotes personnel that attended the exit meeting via telephone-from Corporate

Headquarters ,

l

2 EXII REETING l

i

An exit meeting was conducted on January 8,1993. - During this meeting, the

team reviewed the scope and~ findings of the report. The licensoe did not

identify, as proprietary, any information provided to or reviewed by the

inspector.

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O ek 4

ATTACHMENT 3

1

NPG ENGINIiERING INITIATIVES

'

  • Electrical Calculation Updates
  • Dapper Program Voltage Drop Study
  • Instrumentation Setpoints Program
  • Appendix "R" Cable Sepamtion Database
  • Pire Protection Program
  • Individual Plant Evaluation
  • Source Term Resolution
  • Steady State Core hWel ,
  • Spare Parts Bar Coding Program
  • Diesel Generator Owner's Group
  • Motor Operated Valve Program
  • Erosion / Corrosion Program Upgrade
  • Procurement Engineering
  • As Building Program
  • Design Change Writer's Guide
  • Technical Support Training
  • Vibration Monitoring
  • Vendor Mt.nual Program Upgrade
  • Equipment Spare Pstts List
  • ISI Program Upgrade
  • Turbine Six Year Plan
  • Core Plate Plug Lifetime Evaluation
  • Trending Program Development
  • Non-Essential Instrument Air Project
  • IST Program Upgrade
  • Fuse Control Program
  • CGI Dedication Program Upgrade
  • DG Spare Parts Upgrade
  • ILRT/LLRT Program Upgrade
  • SNM Inventory Program Upgrade
  • Design Basis Document Program

!

l

l arnt.epsi

, -. , , -. , -. ,