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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P7171999-10-26026 October 1999 Informs That Effective 991026,SW Holmes Will Be NRC Inspector for Facility at Dow Chemical Co,Due to Retirement of Previously Assigned Inspector ML20210P9881999-08-10010 August 1999 Forwards Insp Rept 50-264/99-201 on 990712-15.No Violations Noted.Insp Consisted of Selected Exams of Procedures & Representative Records,Interview with Personnel & Observations of Activities in Progress ML20210N3311999-08-0202 August 1999 Forwards Proprietary Details Re Loss of Communication Between Dow Emergency Services & Dow Triga Research Reactor. Details of Facility Security Plan Are Withheld Under Provisions of 10CFR2.790 ML20153B5451998-09-14014 September 1998 Forwards Proposed Modified Emergency Plan,Including Version in Form of Strikethrough Format (Deletions) or Bold Format (Additions) & Explanation for Change & Version Incorporated Into Text of Plan.With One Oversize Drawing ML20151Z4391998-07-27027 July 1998 Informs NRC That Wl Rigot Has Assumed Role of Facility Director of Dow Chemical Co Triga Nuclear Reactor,Replacing SB Butts.Sb Butts Will Replace J Roeck as Level 1 Mgt within Administration as Described in 6.1 of Facility TSs ML20203L1271998-02-26026 February 1998 Forwards Request for Addl Info Re Emergency Plan Submitted on 960708,as Supplemented on 980115.Responses Requested to Be Provided within 30 Days of Date of Ltr ML20203A0561998-02-11011 February 1998 Forwards Amend 8 to License R-108.Amend Increases Amount of Time from 30 to 60 Days That Temporary Radiation Monitor May Be Used in Place of Area Monitor ML20198P7821998-01-15015 January 1998 Forwards Proposed Modified Emergency Plan for Dow Triga Reactor & Responses to NRC ML20198B4181997-12-18018 December 1997 Forwards Insp Rept 50-264/97-201 on 971202-03.No Violations or Deviations Identified.Annual Emergency Plant Drill Acceptable Demonstration of Ability to Respond & to Mitigate Consequences of Reactor Event ML20217P3201997-08-22022 August 1997 Informs That Responsibility for Non-Power Reactor Insp Program Has Been Transferred from Nrr.All Related Repts, Correspondence & Inquires W/Docket Number Specified Should Be Directed to Listed Address ML20210R0971997-08-19019 August 1997 Forwards Amend 7 to License R-108 & Safety Evaluation.Amend Deletes Requirement for Scram Function on Min Reactor Period,Changes Periodic Insp of Reactor Fuel Schedule, & Modifies Facility Organizational Structure ML20141C2931997-06-16016 June 1997 Forwards Response to 970417 Request for Addl Info Re Amend Request for FOL R-108.Encl Includes Changes Proposed for Amend 7 & Explanation for Question Raised in NRC Ltr ML20140E5471997-04-23023 April 1997 Forwards Insp Rept 50-264/97-01 on 970407-11.No Violations Noted ML20135C7251997-02-24024 February 1997 Forwards Response to NRC Request for Addl Info Re Amend Request for Facility Operating License R-108,ltr Dtd 961217.Encl Includes Changes Proposed for Amend 7 & Explanation for Question Raised in Ltr ML20132D2781996-12-17017 December 1996 Forwards Request for Addl Info Re License Triga Research Reactor ML20132D5511996-12-16016 December 1996 Ack Receipt of Ltr Dtd 961030,transmitting Changes to Physical Security Plan for Dow Triga Research Reactor Submitted,Per 10CFR50.54(p) ML20133G3151996-12-0909 December 1996 Informs That Rept Describing Review of Decommissioning Costs Re Dow Triga Research Reactor Will Be Available for NRC Review When on-site Insp Occurs ML20129B5951996-10-0808 October 1996 Forwards Response to RAI Re 960912 Amend Request for License R-108 ML20129H1331996-10-0202 October 1996 Requests Addl Info Re Dow Triga Research Reactor Emergency Plan Submitted on 960708 Before Review Can Be Complete ML20115E6671996-07-0808 July 1996 Forwards Proposed Modified Emergency Plan,Including Strikethrough Format (Deletion) or Bold Format (Additions) Version & Version W/Changes Incorporated in Text ML20113C3661996-06-18018 June 1996 Responds to Request for Addl Info Re Amend Request for FOL R-108 ML20101H6281996-03-18018 March 1996 Forwards Annual Rept for Triga Facility for 1995 ML20087E4011995-08-0707 August 1995 Forwards TSs in Response to RAI Re 950607 Application for Amend to License R-108 ML20078M1371995-02-0808 February 1995 Forwards Response to RAI Re 941221 Application for Amend to License R-108 ML20069J1651994-06-0606 June 1994 Notifies That Cw Kocher Has Retired from Dow Chemical Co Effective 940531,therefore,no Longer Needs Senior Operator License SOP-3922 ML20065B2231994-03-28028 March 1994 Informs That Effective 940322,WL Rigot Has Replaced Cw Kocher as Supervisor for Dow Triga Nuclear Reactor (R-108) ML20057D4511993-09-30030 September 1993 Informs That RA Wolcott Replaced Jj Havel as Chairman of Reactor Operations Committee for Dow Triga Research Reactor ML20072Q9111991-03-14014 March 1991 Advises That Power Level Increase to 300 Kw,Authorized by Amend 5 to License R-108,issued on 890508,implemented. Neutron Detectors Near Reactor Core Moved to Reflect Higher Max Power Level ML20062F7411990-11-19019 November 1990 Forwards Microprocessor-Based I&C Sys for Dow Triga Research Reactor, Containing Mods to 901015 Amend Request for License R-108 ML20058N4841990-08-0101 August 1990 Forwards Insp Rept 50-264/90-01 on 900709-11.No Violations or Deviations Identified ML20055F6901990-07-0101 July 1990 Advises That Vendor Has Not Received Part 55 Svcs from NRC & Requests That 900627 Invoice I1111 Be Corrected ML20247H7581989-09-0707 September 1989 Forwards Matl Control & Accountability Insp Rept 50-264/89-02 on 890829-30.No Violations Noted ML20247C9361989-09-0505 September 1989 Forwards Physical Security Insp Rept 50-264/89-01 on 890829- 30.No Violations Noted ML20246M6451989-05-0808 May 1989 Forwards Amend 5 to License R-108,renewing License for 20 Yrs from Issuance Date & Authorizing Power Increase from 100 to 300 Kws.Environ Assessment,Safety Evaluation,Notice of Renewal & Environ Consideration Also Encl ML20247M8271989-03-30030 March 1989 Discusses Licensee Requests for Changes to Requalification Program.Requests Include Extension of Max Time Period of 24 Months for Requalification Cycle to Account for Changes in Outage Schedules & Reorganization of Training Programs ML20207C7931988-06-29029 June 1988 Advises That Jj Havel Replaced Mb Gibbs as Chair of Reactor Operations Committee,Effective 880623 ML20154C2651988-04-29029 April 1988 Forwards Mods to Suppl Application for Renewal of License R-108,per a Adams Request ML20151X1821988-04-28028 April 1988 Ack Receipt of Describing Proposed Mods to Security Plan.Changes Consistent W/Provisions of 10CFR50.54(p) & Acceptable ML20150D9721988-03-18018 March 1988 Informs of NRC Relocation to Stated Address.Mailing Address Unchanged.A Adams Project Manager & TS Michaels back-up Project Manager ML20148G8991988-01-14014 January 1988 Advises That 880107 Rev to Physical Security Plan Consistent W/Provisions of 10CFR50.54(p) & Acceptable.Encl to Contains Proprietary Info & Being Protected Against Unauthorized Disclosure (Ref 10CFR2.790(d)) ML20237E1481987-12-23023 December 1987 Forwards Exam Rept 50-264/OLS-87-01 of Exam Administered on 871201-02 ML20236B0621987-10-0505 October 1987 Informs That 870925 Audit of Triga Research Reactor Showed Two Tasks Involving Surveillance Required by Tech Specs Not Done Per Scheduled Weekly Checklist for Wk of 870713.Failure to Complete Tasks Did Not Violate Tech Specs ML20238A0461987-08-14014 August 1987 Forwards Supplementary Info Re Renewal of License R-108 for Dow Triga Research Reactor ML20237L4351987-08-14014 August 1987 Forwards Licensed Operator Requalification Program for Facility.Program Reflects Changes Made Following Guidance of Hn Berkow ,Ansi/Ans 15.1-1977 & Changes in 10CFR55 Effective 870526 ML20238A3091987-08-13013 August 1987 Forwards Answers to Questions Posed Following Submittal of May 1987 Formal Answers,Including More Detailed Info Re fire-fighting Equipment in Reactor Room & Nearby Areas & Detailed Analysis of Temp Rise Expected in Fuel Element ML20237H3941987-08-11011 August 1987 Requests Ref Matl Listed in Encl 1 & Applications 60 Days Prior to Operator & Senior Operator Licensing Exams Scheduled for Wk of 871130.Requirements for Administering Exam & Rules & Guidance Also Encl ML20236P5661987-08-0505 August 1987 Requests Addl Info Re Vendor Revs to 870702 Triga Research Reactor Requalification Program,Submitted in Response to NRC .Program Does Not Satisfy Revs to 10CFR55 That Became Effective on 870526.Response Requested in 30 Days ML20236H1311987-07-28028 July 1987 Forwards Revised Security Plan,Per RA Erickson 870526 Request.Rev Withheld (Ref 10CFR2.790) ML20215B4931987-06-11011 June 1987 Informs of Recent Reorganization in Nrr.Organization Now Called Standardization & Non-Power Reactor Directorate Under Div of Reactor Projects Iii,Iv,V & Special Projects.Project Manager for Facility Is a Adams ML20214U9841987-06-0303 June 1987 Forwards Revised NRC Form 398,personal Qualifications statement-licensee & NRC Form 396,certification of Medical Exam by Facility Licensee.Forms Revised to Reflect Changes to 10CFR55 Effective on 870526.W/o Encls 1999-08-02
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20210N3311999-08-0202 August 1999 Forwards Proprietary Details Re Loss of Communication Between Dow Emergency Services & Dow Triga Research Reactor. Details of Facility Security Plan Are Withheld Under Provisions of 10CFR2.790 ML20153B5451998-09-14014 September 1998 Forwards Proposed Modified Emergency Plan,Including Version in Form of Strikethrough Format (Deletions) or Bold Format (Additions) & Explanation for Change & Version Incorporated Into Text of Plan.With One Oversize Drawing ML20151Z4391998-07-27027 July 1998 Informs NRC That Wl Rigot Has Assumed Role of Facility Director of Dow Chemical Co Triga Nuclear Reactor,Replacing SB Butts.Sb Butts Will Replace J Roeck as Level 1 Mgt within Administration as Described in 6.1 of Facility TSs ML20198P7821998-01-15015 January 1998 Forwards Proposed Modified Emergency Plan for Dow Triga Reactor & Responses to NRC ML20141C2931997-06-16016 June 1997 Forwards Response to 970417 Request for Addl Info Re Amend Request for FOL R-108.Encl Includes Changes Proposed for Amend 7 & Explanation for Question Raised in NRC Ltr ML20135C7251997-02-24024 February 1997 Forwards Response to NRC Request for Addl Info Re Amend Request for Facility Operating License R-108,ltr Dtd 961217.Encl Includes Changes Proposed for Amend 7 & Explanation for Question Raised in Ltr ML20133G3151996-12-0909 December 1996 Informs That Rept Describing Review of Decommissioning Costs Re Dow Triga Research Reactor Will Be Available for NRC Review When on-site Insp Occurs ML20129B5951996-10-0808 October 1996 Forwards Response to RAI Re 960912 Amend Request for License R-108 ML20115E6671996-07-0808 July 1996 Forwards Proposed Modified Emergency Plan,Including Strikethrough Format (Deletion) or Bold Format (Additions) Version & Version W/Changes Incorporated in Text ML20113C3661996-06-18018 June 1996 Responds to Request for Addl Info Re Amend Request for FOL R-108 ML20101H6281996-03-18018 March 1996 Forwards Annual Rept for Triga Facility for 1995 ML20087E4011995-08-0707 August 1995 Forwards TSs in Response to RAI Re 950607 Application for Amend to License R-108 ML20078M1371995-02-0808 February 1995 Forwards Response to RAI Re 941221 Application for Amend to License R-108 ML20069J1651994-06-0606 June 1994 Notifies That Cw Kocher Has Retired from Dow Chemical Co Effective 940531,therefore,no Longer Needs Senior Operator License SOP-3922 ML20065B2231994-03-28028 March 1994 Informs That Effective 940322,WL Rigot Has Replaced Cw Kocher as Supervisor for Dow Triga Nuclear Reactor (R-108) ML20057D4511993-09-30030 September 1993 Informs That RA Wolcott Replaced Jj Havel as Chairman of Reactor Operations Committee for Dow Triga Research Reactor ML20072Q9111991-03-14014 March 1991 Advises That Power Level Increase to 300 Kw,Authorized by Amend 5 to License R-108,issued on 890508,implemented. Neutron Detectors Near Reactor Core Moved to Reflect Higher Max Power Level ML20062F7411990-11-19019 November 1990 Forwards Microprocessor-Based I&C Sys for Dow Triga Research Reactor, Containing Mods to 901015 Amend Request for License R-108 ML20055F6901990-07-0101 July 1990 Advises That Vendor Has Not Received Part 55 Svcs from NRC & Requests That 900627 Invoice I1111 Be Corrected ML20207C7931988-06-29029 June 1988 Advises That Jj Havel Replaced Mb Gibbs as Chair of Reactor Operations Committee,Effective 880623 ML20154C2651988-04-29029 April 1988 Forwards Mods to Suppl Application for Renewal of License R-108,per a Adams Request ML20236B0621987-10-0505 October 1987 Informs That 870925 Audit of Triga Research Reactor Showed Two Tasks Involving Surveillance Required by Tech Specs Not Done Per Scheduled Weekly Checklist for Wk of 870713.Failure to Complete Tasks Did Not Violate Tech Specs ML20238A0461987-08-14014 August 1987 Forwards Supplementary Info Re Renewal of License R-108 for Dow Triga Research Reactor ML20237L4351987-08-14014 August 1987 Forwards Licensed Operator Requalification Program for Facility.Program Reflects Changes Made Following Guidance of Hn Berkow ,Ansi/Ans 15.1-1977 & Changes in 10CFR55 Effective 870526 ML20238A3091987-08-13013 August 1987 Forwards Answers to Questions Posed Following Submittal of May 1987 Formal Answers,Including More Detailed Info Re fire-fighting Equipment in Reactor Room & Nearby Areas & Detailed Analysis of Temp Rise Expected in Fuel Element ML20236H1311987-07-28028 July 1987 Forwards Revised Security Plan,Per RA Erickson 870526 Request.Rev Withheld (Ref 10CFR2.790) ML20214T0611987-06-0202 June 1987 Forwards ALARA Policy Statement,Revised Requalification Program & Tech Specs & Addl Info in Support of Application for Renewal of License R-108,per a Adams Request ML20213G8111987-05-13013 May 1987 Forwards Endorsement 60 to Nelia Policy NF-160 ML20210S5901987-02-0909 February 1987 Forwards Revised Licensed Operator Requalification Program for Facility,Per Hn Berkow Recommendation.Revised Program Follows Guidance of Ansi/Ans 156.4-1977 ML20214V5141986-12-0202 December 1986 Forwards Check Inadvertently Omitted from 861117 Reactor License Renewal Application ML20116H1641985-04-23023 April 1985 Forwards Endorsement 56 to Nelia Policy NF-160 ML20137G9971985-03-20020 March 1985 Advises of Mods to Physical Security Sys Resulting in Change to Security Plan ML20112E7091984-12-21021 December 1984 Responds to NRC Re Violations Noted in Insp. Corrective Actions:All Licensed Senior Reactor Operators Received Written Reminders of Notification Requirements ML20090F1521984-07-13013 July 1984 Notifies That,Effective 840711,emergency Plan for Dow Triga Research Reactor Implemented ML20081A0941984-03-0101 March 1984 Forwards Revised Emergency Plan ML20028F6771983-01-10010 January 1983 Forwards Public Version of Emergency Plan,Originally Submitted in Oct 1982 ML20079K2791982-12-20020 December 1982 Forwards Public Version of Corrected Pages to Emergency Plan ML20065G8111982-09-29029 September 1982 Forwards Endorsements 47 & 48 to Nelia Policy NF-160. Endorsement 47 Amends Description of Facility to Include Larkin Lab ML20137G9511982-07-13013 July 1982 Notifies That Cw Kocher Reinstated as Reactor Supervisor, Effective 820607 & Fj Knoll Replaced Jm Macki as Research Manager of Bldg 1602 & Chairman of Reactor Operations Committee,Effective 820624 ML20054F5261982-06-10010 June 1982 Forwards Endorsement 46 to Nelia Policy NF-160 ML20041C1611982-02-12012 February 1982 Forwards Endorsement 44 to ANI Policy NF-160 ML20136H4101982-01-26026 January 1982 Responds to NRC 820113 Insp Rept on 811207-10.Requests Rept Be Modified Before Placement in Pdr.No Matls Disposed of by Incineration Under License 21-00265-06 ML20137G9031981-12-11011 December 1981 Informs That Cw Kocher Will Replace Ou Anders as Reactor Supervisor.Cw Kocher Resume Encl ML20004B0951981-04-28028 April 1981 Forwards Endorsement 42 to Nelia Policy NF-160 ML20003G9351981-04-27027 April 1981 Forwards Endorsements 40 & 41 to Nelia Policy NF-160 ML20008E2091980-10-10010 October 1980 Forwards Advance Premium,Std Premium & Reserve Premium Endorsements,Effective 800101.Also Forwards Amend 10 to Indemnity Agreement B-34 ML19351C9701980-09-25025 September 1980 Informs of Adding H Emmel,W Kocher & E Bickel to Reactor Operations Committee,As of 800826.T Parsons Was Deleted from Committee.Forwards Resumes.W/O Encls ML19323J2511980-06-0909 June 1980 Responds to NRC 800507 Ltr Re Dow Chemical Co Triga Reactor Facility Nonpower Reactor Physical Protection Requirement. Response Not Received Re Dow Triga 781005 Security Plan. Security Plan Meets 790724 & 800325 Fr Rules & Regulations ML20137H0451980-02-22022 February 1980 Informs of Personnel Changes in Reactor Operations Committee.H Gill Replaced by J Macki as Committee Chairman, Norwood Replaced by T Prasons as Health Physicist & P North Replaced by J Simpson as Senior Reactor Operator ML19296D3441980-02-22022 February 1980 Informs of Recent Personnel Changes in Reactor Operations. Reactor Operations Committee Chairman H Gill Replaced by J Macki,Health Physicist s Norwood Replaced by J Parsons & Senior Reactor Operator P North Replaced by J Simpson 1999-08-02
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The Dow Chemical Company Mdand, Mchigan 48667
. 18 March 1996 l
Regional Adminsistrator l US Nuclear Regulatory Commission l
l Region III 801 Warrenville Road Lisle, Illinois 60532-4351 j
l DOW TRIGA RESEARCH REACTOR - DOCKET 50-264 Enclosed is the Annual Report for the Dow TRIGA facility for the year 1995.
Very truly yours, l 1
kk W. L. Rigot Reactor Supervisor 1602 Building l
I f
n 1 010001 9604010022 960318 N2I 7996 PDR ADOCK 05000264 pun R_
m- - _ _ _ . _ - . _ _ _ _ _ _ . _ _ _ _ _ _ . _ _ _ _ _ ___
l
- * ', DOW TRIGA* RESEARCH REACTOR ANNUAL REPORT - 1995 There were no major changes, maintenance problems, or down time involving the reactor during 1995.
Operation of the reactor continues to bc plagued with an unacceptably large number of unintentional i shutdowns (SCRAMS), most of which seem to be caused by the control system itself, although there ,
seems to be a year-to-year decrease of these. l There were two US NRC inspections in 1995. The required annual audit was conducted by an outside )
consultant; recommendations were made and the Reactor Operations Committee has responded to these recommendations. The normal in-house audits of the radiation protection program, safety and I housekeeping, and records were also performed and the recommendations acted upon. l A. Staff, Licenses, and Training The staff consists of four Senior Reactor Operators. There have been no staffing changes during this period.
W. L. Rigot- Reactor Supervisor T. J. Quinn Assistant Reactor Supervisor J. D. Romick Assistant Reactor Supervisor M. E. Buchmann Senior Reactor Operator i
Licenses are current. Rigot and Quinn licenses will be up for renewal in 1999, while the Buchmann and Romick licenses will be up for renewal in 1997. All operators took medical examinations during 1995.
The current two-year re qualification program started in the second quarter 1994 and will be completed during 1996. Four quarterly re qualification sessions were held during 1995; all operators have participated and successfully completed the requirements for these sessions. The .
i SROs are current with operating experience and participation in hypothetical emergency drills, Reactor Operation Committee meetings, an annual operating examination, and the annual fuel inventory.
Operation of the reactor is an important part of the training program, since this reactor is operated i on an as-needed basis, which results in numerous operations each involving reactivity manipulations, use of the control console, placement and retrieval of samples and handling of radioactive materials. The minimum experience of an operator during 1995 was 30.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> of
. actual operating time, involving 192 reactivity manipulations, and the maximum experience was 218.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> of actual operating time, involving 765 reactivity manipulations. Furthermore, each licensed person performed about 1/4 of the daily checkout procedures and at least two monthly ,
checkout procedures; one of the monthly checkouts (an extensive combination of tasks involving the physical plant, the control system, and operating characteristics) was performed under the direction of another SRO as part of the annual operating examination.
J. A. Grappin has replaced R. M. A. Hahne as the Radiation Safety Officer and sits as a member of the committee.
S. B. Butts Facility Director;Chauman W. L. Rigot Reactor Supervisor
- J. A. Grappin Radiation Safety Officer
! T. J. Quinn Assistant Reactor Supervisor l
T. D. Lickly Researth Associate i .
- TRIGA is a registered trademark of General Atomics l
I 19 March 1996- Page I of 3 Qfe edn- . ..
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w
- DOW TRIGA RESEARCH REACTOR ANNUAL REPORT - 1995 S. B. Butts is the Research Manager in charge of the Dow MMhigan Division Inorganic, Environmental and Thermal Analysis group of the Analytical Sciences Laboratory; Rigot and Quinn report administratively to Butts; Grappin is the Dow Midland location Radiation Safety Officer as well as the TRIGA Radiation Safety Officer and reports, as does Lickly, to the Dow Environmental, Health, Safety and Security department.
B. Reactor Operating Experience The reactor was operated for 2.05 Megawatt-days during 1995 for a total of 348 hours0.00403 days <br />0.0967 hours <br />5.753968e-4 weeks <br />1.32414e-4 months <br /> (an average of 17.8% of the available normal working hours) and 1,611 reactivity manipulations, including checkouts and testing as well as the irradiadon of samples.
C. Major Changes During 1995 there were no major changes in the facility and there were no authorizations of new -l tests or experiments significantly different than those performed previously.
D. Unscheduled Shutdowns There were 33 unscheduled shutdowns (SCRAMS) during 1995, down from 42 during 1994,47 during 1993,59 during 1992 and 72 during 1991. During the almost ten years following 1-1-81 the yearly average was 6 SCRAMS, with a high of 9 (1983) and a low of 3 (1989), using the control instrumentation installed in 1971 and 1973. After installation of the new console there were 4 SCRAMS during installation and startup in the last two weeks of December, 1990,72 during 1991,59 during 1992,47 during 1993 and 42 during 1994. Some of these were related 1 to hardware problems which have since been fixed, but a large majority seem to be due to two aspects of the control system: computer crashes and noise in the digital smoothing process which produces the period signal.
About 94% of the SCRAMS were associated with the operation of the console: the digital smoothing process (about 24 %), computer crashes (about 55%), period SCRAMS at the count-rate / Campbell crossover (about 6 %), and others (about 9 %). About 6 % of the SCRAMS were associated with operator errors.
The difference in the total number of SCRAMS between 1994 and 1995 can be attributed to a
- better understanding by the operators of the algorithm used for generating the digital input to the safety channel and a better overall understanding of the operation of the console.
E. Major Preventive and Corrective Maintenance of Safety Significance In March of this year there were difficulties in the ability of the pneumatic system to reliably deliver samples to and from the reactor. When samples were not retumed from the rea:: tor, the reactor was secured and the samples were manually removed. General Atomics was contacted and a recommendation for a replacement motor was given. The. motor was ordered and installed. The system has operated with no interruptions since installation. This has improved the reliability of the system, minimized unnecessary shutdowns, and reduced the possibility of increased exposure from manual removal of the samples from the reactor terminus.
19 March 1996- Page 2 of 3 l
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\ . .
"/. DOW TRIGA RESEARCH REACTOR ANNUAL REPORT - 1995 F. Radioactive Effluents -
! The only radioactive material normally released to the environment from the facility is argon-41, l
which is produced from activation of the natural argon dissolved in the pool water and l
subsequently escapes from the pool into the reactor room and from there to the outside of the
- building, and from the natural argon present in the air used to transport samples from a laboratory into a terminus in the core of the reactor.
l i
Since 1993 the reactor room air particulate monitor sporadically indicated very slight increases of air-borne radioactivity over the natural background levels. These increases were of the order of the background level and the sum of background plus the anomalous radioactivity was never more than about one-fourth the level required to trip the alarm on the air particulate monitor.
Overall the average release after dilution or diffusion is estimated to be less than 25% of the ,
allowed or recommended maximum concentration. (
l l During one operation on September 18,1995, while operating at 250 kilowatts the continuous air monitor increased to a level higher than previously observed. Previous attempts to identify the isotope causing the increased radiation levels in the reactor room have been impossible due to the low activities observed. However during this run, when the filter was removed from the continuous air monitor and a gamma ray spectrum taken of the emitted radiation, there was a l i
significant increase in the magnesium-27 activity. An investigation showed that a press-fit joint on the exhaust tube from the pneumatic system had separated. The joint was taped and the j l
reactor operated at 250 kilowatts; no increase in the continuous air monitor reading was observed. The magnesium-27 activity was assumed to come from the fast neutron reaction of aluminum on the interior of the pneumatic tube. Subsequent experiments confirmed these assumptions. At the highest observed level the concentration of magnesium-27 in the reactor room, the effluent concentration was less than 5% of the limit. The continuous air monitor trace l
! observed on September 18.1995 is consistent with previous traces, with respect to buildup and decay rates. The conclusion is that the previous increases in the continuous air monitor were also due to magnesium-27 from the pneumatic system. The elevated level reoccurred in December and it was assumed that the magnesium-27 must be coming from the switches / valves which control the direction of travel of samples within the pneumatic system. These are one-way valves and should not allow air from the pneumatic system into the reactor room. Since these valves are part of the original installation of the facility, it is possible that they no longer seat perfectly. New one-way valves have been ordered and will be installed in 1996.
G. Radiation Exposures Radiation exposures received by facility personnel and visitors are monitored using film badges and thermoluminescent detectors. No persons have received exposures approaching 25% of those allowed or recommended in 10CFit20.
W. L. Rigot 4 Reactor Supervisor 13 March 1996 ,
l 19 March 1996 Page 3 of 3 i
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