05000318/LER-1983-052, Revised LER 83-052/03X-1:on 830928,auxiliary Feedwater Pump 23 Found Inoperable Due to Tripped Protective Relays. Probably Caused by Workers Shorting Internal Breaker Circuits When Working Scaffolding W/Door open.W/831028 Ltr

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Revised LER 83-052/03X-1:on 830928,auxiliary Feedwater Pump 23 Found Inoperable Due to Tripped Protective Relays. Probably Caused by Workers Shorting Internal Breaker Circuits When Working Scaffolding W/Door open.W/831028 Ltr
ML20086A578
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 10/28/1983
From: Basso L, Porter R, Russell L
BALTIMORE GAS & ELECTRIC CO.
To: Murley T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-83-052-03X, LER-83-52-3X, NUDOCS 8311160036
Download: ML20086A578 (3)


LER-2083-052, Revised LER 83-052/03X-1:on 830928,auxiliary Feedwater Pump 23 Found Inoperable Due to Tripped Protective Relays. Probably Caused by Workers Shorting Internal Breaker Circuits When Working Scaffolding W/Door open.W/831028 Ltr
Event date:
Report date:
3182083052R00 - NRC Website

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o 12 l l At 1715 during normal operations. 23 Auxiliary Feedwater (AFW) Pump l 10 l3 l [ was found to be inoperable (T.S. 3.7.1.2.a) . At 2120 the pump was l l 0 l4 l l returned to service. During this period the remaining AFW pumps l l o l 5 l I remained operable. Similar events: none. l 1018ll l 1017ll l lolBil i 1 s ..

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h

[ 1 l 0 l l Investigation formd n11 #23 AFW Piten motor brenkr=r (C.E. AMH 4.76-250- l l i l 1 l l ID) protective relays tripped. The relays were reset. No operational l

l 1 l 2 I I problems were found. Suspected cause is workers shortine internal break- I lil3ll er circuits when working scaffolding while grouting at cubicle base with i I1!4ll door open. A faci 11tv chance to add n1nrms is being investiented. l

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LER NO. 83-52/3X, Rev. 1 DOCKET No. 50-318 LICENSE NO. DPR 69 EVENT DATE 09-23-83 REPORT DATE 10-28-83 ATTACHhENT ,

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (CONT'D)

Upon investigation, all the protective relays in #23 AFW Pump motor breaker (Ger.eral Electric Co. AMH 4.76-250-ID) were found tripped, thus the 186 lockout device was also tripped. The relays were reset.

No operational problems were revealed to account for actuation of the relays. Suspected cause is accidental shorting of internal switchgear circuits by personnel working scaffolding in the room while grouting was being done at the cubicle base with the door open.

A Facility Change is being investigated such that operators will be alerted of such out-of-service switchgear conditions. An update will be submitted upon completion of the investigation. .

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P.0, B O X 14 7 5 B ALTIMOR E. M A R YLAN D 21203 NUCLE AR POWER DEPARTMENT CALVERT CLIFFS NUCLEAR POE_ A PLANT LUSBY. M ARYLAND 20657 October 28, 1983 Dr. Thomas E. Murley Docket No. 50-318 Regional Administrator License No. DPR 69 U. S. Nuclear Regulatory Commission Region 1 631 Park Avenue King of Prussia, PA 19406

Dear Dr. Murley:

In accordance with Technical Specification 6.9 please find the attached revision to LER 83-52/3X, Rev. 1.

Should you have any questions regarding this report, we would be pleased to discuss them with you.

Very truly yours, L. B. Russell Plant Superintendent LBR:LFB:bsb cc: Director, Office of Management Information and Program Control Messrs: A. E. Lundvall, Jr.

J. A. Tiernan

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