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05000317/LER-1990-01920 July 1990LER 90-019-00:on 900622,determined That Inadequate Breaker Coordination Resulted in Condition Outside Design Basis. Root Cause of Improperly Sized Breaker Not Determined. W/900720 LtrTime of Discovery
05000318/LER-1987-005, Revised LER 87-005-00,correcting Block 15 to Reflect 870501 as Supplemental Rept Expected Submittal Date6 August 1987Revised LER 87-005-00,correcting Block 15 to Reflect 870501 as Supplemental Rept Expected Submittal Date
05000317/LER-1984-004, Updated LER 84-004-01:on 840228,charging Pumps 12 & 13 Taken Out of Svc Due to Excessive Packing Leakage.Caused by Plunger Packing Failure.Evaluation of Alternative Charging Pump Packing Matls in Progress25 April 1984Updated LER 84-004-01:on 840228,charging Pumps 12 & 13 Taken Out of Svc Due to Excessive Packing Leakage.Caused by Plunger Packing Failure.Evaluation of Alternative Charging Pump Packing Matls in Progress
05000318/LER-1983-043, Updated LER 83-043/03X-1:on 830809,following Reactor Trip, Steam Generator Safety Valve Failed to Reseat.Caused by Missing Pin.Valves Inspected to Ensure That Blowdown Ring & Pin Not worn.W/840330 Ltr30 March 1984Updated LER 83-043/03X-1:on 830809,following Reactor Trip, Steam Generator Safety Valve Failed to Reseat.Caused by Missing Pin.Valves Inspected to Ensure That Blowdown Ring & Pin Not worn.W/840330 Ltr
05000318/LER-1983-046, Updated LER 83-046/03X-1:on 830906,penetration Room Exhaust Fan 21 Would Not Start on Containment Isolation Sys Signal While Performing Surveillance Test STP-0-22.Caused by Intermittently Failing Module.Module removed.W/84033030 March 1984Updated LER 83-046/03X-1:on 830906,penetration Room Exhaust Fan 21 Would Not Start on Containment Isolation Sys Signal While Performing Surveillance Test STP-0-22.Caused by Intermittently Failing Module.Module removed.W/840330 Ltr
05000317/LER-1983-046, Updated LER 83-046/01X-1:on 830816,swing Diesel Generator 12 Shut Down on Loss of Fuel Oil During Surveillance.Caused by Isolation of Day Tank Level Switches,Preventing Fuel Oil Transfer Pump & Low Level Alarm actuation.W/8403330 March 1984Updated LER 83-046/01X-1:on 830816,swing Diesel Generator 12 Shut Down on Loss of Fuel Oil During Surveillance.Caused by Isolation of Day Tank Level Switches,Preventing Fuel Oil Transfer Pump & Low Level Alarm actuation.W/840330 Ltr
05000317/LER-1981-058, Updated LER 81-058/03X-1:on 810721,emergency Diesel Generator 12 to 4 Kv Bus 21 out-of-svc.Caused by Stuck Auxiliary Contact in Emergency Diesel Generator 12 Output Breaker to 4 Kv Bus 14.Switch replaced.W/840330 Ltr30 March 1984Updated LER 81-058/03X-1:on 810721,emergency Diesel Generator 12 to 4 Kv Bus 21 out-of-svc.Caused by Stuck Auxiliary Contact in Emergency Diesel Generator 12 Output Breaker to 4 Kv Bus 14.Switch replaced.W/840330 Ltr
05000317/LER-1983-034, Updated LER 83-034/03X-1:on 830525,ECCS Pump Room Cooler 12 Taken Out of Svc.Cause Unknown.Supply Piping & Strainers Disassembled,Inspected & Cleaned.New Mechanical Preventive Maint Procedures implemented.W/840306 Ltr6 March 1984Updated LER 83-034/03X-1:on 830525,ECCS Pump Room Cooler 12 Taken Out of Svc.Cause Unknown.Supply Piping & Strainers Disassembled,Inspected & Cleaned.New Mechanical Preventive Maint Procedures implemented.W/840306 Ltr
05000318/LER-1981-025, Updated LER 81-025/03X-1:on 810430 & 0514,reactor Protective Sys Channel B Trip Units 1,3,7,8 & 10 Bypassed to Investigate Problem w/T-hot Channel B.Caused by Failure of Two Oscillators in Transmitter Circuitry5 March 1984Updated LER 81-025/03X-1:on 810430 & 0514,reactor Protective Sys Channel B Trip Units 1,3,7,8 & 10 Bypassed to Investigate Problem w/T-hot Channel B.Caused by Failure of Two Oscillators in Transmitter Circuitry
05000317/LER-1981-032, Updated LER 81-032/03X-1:on 810420,reactor Protective Sys Channel D Hi Power Thermal Margin/Low Pressure & Axial Shape Index Trip Units Bypassed for Maint.Caused by Oscillator Noise in transmitter.W/840305 Ltr5 March 1984Updated LER 81-032/03X-1:on 810420,reactor Protective Sys Channel D Hi Power Thermal Margin/Low Pressure & Axial Shape Index Trip Units Bypassed for Maint.Caused by Oscillator Noise in transmitter.W/840305 Ltr
05000317/LER-1983-037, Updated LER 83-037/03X-1:on 830718,response Time of Trip Circuit Breakers 3 & 4 Undervoltage Trip Devices Slower than Tech Spec Limits.Caused by Setpoint Drift.Setpoints adjusted.W/840305 Ltr5 March 1984Updated LER 83-037/03X-1:on 830718,response Time of Trip Circuit Breakers 3 & 4 Undervoltage Trip Devices Slower than Tech Spec Limits.Caused by Setpoint Drift.Setpoints adjusted.W/840305 Ltr
05000318/LER-1983-036, Updated LER 83-036/03X-1:on 830719,response Time for Reactor Trip Circuit Breakers 4 & 7 Undervoltage Devices Indicated Slower than Tech Spec Limits.Caused by Setpoint Drift & Worn Front Frame Assembly mechanisms.W/840305 Ltr5 March 1984Updated LER 83-036/03X-1:on 830719,response Time for Reactor Trip Circuit Breakers 4 & 7 Undervoltage Devices Indicated Slower than Tech Spec Limits.Caused by Setpoint Drift & Worn Front Frame Assembly mechanisms.W/840305 Ltr
05000317/LER-1983-049, Updated LER 83-049/03X-1:on 830818,auxiliary Feedwater Pump 11 Found Inoperable.Caused by Stage & Shaft piece-balance Being Bound Up.Parts replaced.W/840305 Ltr5 March 1984Updated LER 83-049/03X-1:on 830818,auxiliary Feedwater Pump 11 Found Inoperable.Caused by Stage & Shaft piece-balance Being Bound Up.Parts replaced.W/840305 Ltr
05000318/LER-1981-030, Updated LER 81-030/03X-1:on 810305,discovered Temp Transmitter 122HB Out of Tolerance in Nonconservative Direction.Caused Two Oscillators Producing Noise on Transmitter Output.Transmitter replaced.W/840305 Ltr5 March 1984Updated LER 81-030/03X-1:on 810305,discovered Temp Transmitter 122HB Out of Tolerance in Nonconservative Direction.Caused Two Oscillators Producing Noise on Transmitter Output.Transmitter replaced.W/840305 Ltr
05000318/LER-1983-074, Updated LER 83-074/03X-1:on 831223,main Steam Supply Valve to Steam Driven Auxiliary Feedwater (AFW) Pumps Failed, Causing AFW Pump 21 to Start.Caused by Insufficient Torque on Casing Cap Screws.New Diaphragm installed.W/8402099 February 1984Updated LER 83-074/03X-1:on 831223,main Steam Supply Valve to Steam Driven Auxiliary Feedwater (AFW) Pumps Failed, Causing AFW Pump 21 to Start.Caused by Insufficient Torque on Casing Cap Screws.New Diaphragm installed.W/840209 Ltr
05000317/LER-1983-047, Updated LER 83-047/03X-1:on 830822,control Room Air Conditioner Compressor 12 Failed to Run W/Start Signal. Caused by Compressor Trip Due to High Pressure.High Pressure Switch reset.W/840126 Ltr26 January 1984Updated LER 83-047/03X-1:on 830822,control Room Air Conditioner Compressor 12 Failed to Run W/Start Signal. Caused by Compressor Trip Due to High Pressure.High Pressure Switch reset.W/840126 Ltr
05000318/LER-1983-064, Updated LER 83-064/03X-1:on 831105,after Obtaining Results of Unit 1 HPSI Flow Balance Test,Six Unit 2 HPSI Header Isolation Valves Required Adjustment.Caused by Inadequate Procedures.Maint Procedures revised.W/840124 Ltr24 January 1984Updated LER 83-064/03X-1:on 831105,after Obtaining Results of Unit 1 HPSI Flow Balance Test,Six Unit 2 HPSI Header Isolation Valves Required Adjustment.Caused by Inadequate Procedures.Maint Procedures revised.W/840124 Ltr
05000318/LER-1983-052, Revised LER 83-052/03X-1:on 830928,auxiliary Feedwater Pump 23 Found Inoperable Due to Tripped Protective Relays. Probably Caused by Workers Shorting Internal Breaker Circuits When Working Scaffolding W/Door open.W/831028 Ltr28 October 1983Revised LER 83-052/03X-1:on 830928,auxiliary Feedwater Pump 23 Found Inoperable Due to Tripped Protective Relays. Probably Caused by Workers Shorting Internal Breaker Circuits When Working Scaffolding W/Door open.W/831028 LtrScaffolding
05000318/LER-1983-007, Followup LER 83-007/01T-0:on 830203,de-energization of Reactor Protection Sys (RPS) Channels Caused PORV & Pressurizer Quench Tank Rupture Disk to Open.Caused by Blown Fuse in RPS Channel a Due to Crossed Leads in Inverter 2118 February 1983Followup LER 83-007/01T-0:on 830203,de-energization of Reactor Protection Sys (RPS) Channels Caused PORV & Pressurizer Quench Tank Rupture Disk to Open.Caused by Blown Fuse in RPS Channel a Due to Crossed Leads in Inverter 21
ML20062N31813 August 1982LER-021/03L-0:on 820714,22B Safety Injection Tank Pressure Found Decreased to 197 Psig on 820427.Caused by Loop Isolator Failure.Isolator Replaced
05000317/LER-1982-022, Updated LER 82-022/01T-1:on 820503,total Type B & C Penetration Leakage Calculations Compared to Wrong Spec. Caused by Incorrectly Revised Local Leak Rate Surveillance Test Procedure.Procedure Revised22 July 1982Updated LER 82-022/01T-1:on 820503,total Type B & C Penetration Leakage Calculations Compared to Wrong Spec. Caused by Incorrectly Revised Local Leak Rate Surveillance Test Procedure.Procedure Revised
ML20062F70814 December 1978/01x-0 on 781213:reactor Was Made Critical w/11 Component Cooling Heat Exchanger Out of Svc & 11 Saltwater sub-sys Partially Drained.Caused by Personnel Error
ML20062G11914 December 1978/03L-0 on 781117: 5 Halon sub-sys Discharged When Door to 22 Inverter Was Open.Caused by Thermal Detector Being Overly Sensitive to Rate of Rise of Temp.When Door Opened,Internal Airflow Disturbed,Setting Off DetectorContinuous fire watch
ML20062E9217 December 1978/03L-0 on 781113:during Normal Oper the Containment Particulate Radioactivity Monitor Failed Low at 1110.Caused by Disconnection of Signal Cable to Monitor. Cable Connected & Monitor Returned to Svc
ML20062E8967 December 1978/03L-0 on 781115:during Normal Oper Periodic Water Inventory Balance Indicated That Unidentified Reactor Coolant Leakage Was 1.72 Gpm at 0600.Leak Identified as Cracked Weld
ML20062D80124 November 1978/03L-0 on 781115:RWT Level Discovered to Be at 455 Inches.Caused by Rad-Chem Technician'S Failure to Fully Close Local Sample Valve After Drawing Routine Sample. Technician Has Been Reinstructed in Valve Sampling
ML20062D71824 November 1978/03L-0 on 781103:in Routine Surveillance test,11 Auxiliary Feed Pump Was Tripped Per Procedure & Oper Was Unable to Reset Throttle Valve Due to Binding.Assembly Was Freed Upon Lubrication of Stem & Nut
ML20062D76917 November 1978/03L-0 on 781031:solenoid Valve 1-SV-4043 for Main Steam Isolation Valve Hydraulic Accumulators Was Leaking Due to Failure of 1 of 4 O Ring Seals.Cause of Ring Failure Unknown.All 4 Seals Replaced & Valve Returned to Svc
ML20062D34116 November 1978/03L-0 on 781020:pump for Radiat Monitors Seized, Perhaps Due to Graphite Particles from Pump Being Deposited in Bearings.A Normal End of Life Failure.Code Pump Model 6
ML20062D04713 November 1978/01t-0 on 781025:during LPPT in Mode 2,containment Air Lock Was Opened to Repair Failed Oper Mechanism & Was Kept Ajar,Due to Misunderstanding Between Supervisor & Maintenance Personnel.All Personnel Have Been Reinstructed
ML20062D03610 November 1978/03L-0 on 781025:during Oper,Reactor Protec Instru Wide Range Logarithmic Neutron Flux Monitor Channel a Read 2 Decades Lower than Other Channels,Due to Connector,For Channel a Not Being Dried Completely When Recently Cleaned
ML20062C8042 November 1978/01T-0 on 781023:during Routine Test of Steam Generator Isolation Signal logic,21 Main Steam Isolation Valve Failed to Shut Upon Sgisa & Sgisb Signal or Hand Switch in Control Room,Due to Sticking MSIV Solenoid Valves
ML20062C69424 October 1978/01X-0 on 781023:during Inspec of Steam Generator Isolation Signal logic,21 Main Steam Isolation Valves Failed to Shut When Given Sgisa & Sgisb Signal.Cause Undetermined