ML20062E896

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/03L-0 on 781115:during Normal Oper Periodic Water Inventory Balance Indicated That Unidentified Reactor Coolant Leakage Was 1.72 Gpm at 0600.Leak Identified as Cracked Weld
ML20062E896
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 12/07/1978
From: Carroll J, Watkins K
BALTIMORE GAS & ELECTRIC CO.
To:
Shared Package
ML20062E894 List:
References
LER-78-039-03L-01, LER-78-39-3L-1, NUDOCS 7812130174
Download: ML20062E896 (1)


Text

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