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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18011A5401994-08-10010 August 1994 LER 94-017-00:on 940711,automatic Isolation of RHR Sys Shutdown Cooling Suction Outboard Containment Isolation Valve Occurred Due to Inadequate Work Order.Work Order Process for I&C Work Orders Will Be reviewed.W/940810 Ltr ML20046C5721993-08-0606 August 1993 LER 93-015-00:on 930709,unexpected RRP Fast to Slow Speed Downshift Occurred Due to Failure of Both RRP Suction Temp Rtd.Replaced & Returned RTD to Mfg for Failure Analysis. W/930806 Ltr ML20046B7811993-08-0202 August 1993 LER 93-014-00:on 930703,TS 3.0.3 Entered Due to Failure of Racs Power Supply.Replaced 5 Volt Power Supply in Racs cabinet.W/930802 Ltr ML20045G7201993-07-0808 July 1993 LER 93-013-00:on 930608,control Room HVAC Sys Train a Supply Fan Tripped on Overcurrent,Resulting in Both Sys Trains Being Unavailable.Caused by Motor Winding Insulation Failure.Motor Repaired by mfg.W/930708 Ltr ML20045G2171993-07-0707 July 1993 LER 93-012-00:on 930607,noted That HPCS Initiation Signal Resulted in Auto Start of Div 3 DG & ESW Sys.Caused by Failure of Div 3 Reserve Battery Charger.Procedures Used for Insp & Maint of Battery Being modified.W/930707 Ltr ML20044F2161993-05-19019 May 1993 LER 93-011-00:on 930419,identified That Excessive Strainer Differential Pressure Across RHR Suction Strainers Could Have Compromised Long Term Cooling During LOCA Operation. Caused by Inadequate Program requirements.W/930519 Ltr ML20044B6771993-02-22022 February 1993 LER 93-004-00:on 930121,MOV Testing of Main Steam Line Drain & Bypass Outboard Isolation Valve Indicated That Thrust Less than Design Thrust to Close Valve Under Accident Conditions. Review,Per GL 89-10 in progress.W/930222 Ltr ML20029B6431991-03-0808 March 1991 LER 91-007-00:on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper value.W/910308 Ltr ML20029B0971991-03-0101 March 1991 LER 91-006-00:on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being revised.W/910301 Ltr ML20029A6451991-02-22022 February 1991 LER 91-005-00:on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel error.W/910222 Ltr ML20029A3321991-02-15015 February 1991 LER 91-004-00:on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified. W/910215 Ltr ML20028H7521991-01-25025 January 1991 LER 90-041-00:between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo issued.W/910125 Ltr ML20024F7421990-12-14014 December 1990 LER 90-033-00:on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N ML20024F7411990-12-14014 December 1990 LER 90-032-00:on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders ML20028G9181990-09-28028 September 1990 LER 90-020-00:on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being revised.W/900928 Ltr ML20044B1021990-07-13013 July 1990 LER 90-013-00:on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel counseled.W/900713 Ltr ML20043H4801990-06-20020 June 1990 LER 90-011-00:on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction revised.W/900620 Ltr ML20043H5251990-06-20020 June 1990 LER 90-010-00:on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage monitored.W/900620 Ltr ML20043H3841990-06-18018 June 1990 LER 90-009-00:on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut replaced.W/900618 Ltr ML20043E5711990-06-0808 June 1990 LER 89-030-01:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Failure of Two Control Rods Caused by Improper Seat Matl in Associated Scram Pilot Solenoid Valves.Instructions revised.W/900608 Ltr ML20043A7801990-05-18018 May 1990 LER 90-007-00:on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced ML20043A8451990-05-18018 May 1990 LER 90-008-00:on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced ML20042G7731990-05-11011 May 1990 LER 90-006-00:on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel retrained.W/900511 Ltr ML20012D8151990-03-24024 March 1990 LER 90-003-00:on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement implemented.W/900323 Ltr ML20011E1861990-02-0202 February 1990 LER 90-001-00:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised ML20011E1871990-02-0202 February 1990 LER 90-002-00:on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised ML19354E0961990-01-19019 January 1990 LER 89-032-00:on 891228 & 900105,HPCS Sys Declared Inoperable Due to Inoperability of Div 3 Battery.Caused by Low Pilot Cell Voltage,Cell W/Slow Electrolyte Leak & Blown Power Fuse.Fuse & Hydromotor Pump replaced.W/900119 Ltr ML20005E6851990-01-0505 January 1990 LER 89-031-00:on 891206,08 & 15,RWCU Sys Isolations Occurred.Caused by Design Deficiency & Deficiency in Leak Detection/Differential Flow Circuitry Setpoint &/Or Time Delay.Leak Detection Thermocouples relocated.W/900105 Ltr ML20005E0821989-12-26026 December 1989 LER 89-030-00:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Caused by Failure to Return Scram Pilot Valves Used for Rods to Mfg After Recall. Surveillance Instruction revised.W/891226 Ltr ML19354D5991989-12-17017 December 1989 LER 89-029-00:on 891117,heater Bay/Turbine Bldg Vent Gaseous Effluent Particulate & Iodine Samples Not Continuously Collected as Required by Tech Spec 3.3.7.10.Caused by Procedure Deficiency.Procedure revised.W/891217 Ltr ML19325E5901989-11-0303 November 1989 LER 89-028-00:on 891008,concluded That Operation of Fuel Pool Cooling & Cleanup Sys to Upper Containment Pools Caused Containment Vacuum Breaker Actuations.Caused by Unrecognized Sys Interaction.Operating Instruction revised.W/891103 Ltr ML19324B1241989-10-27027 October 1989 LER 89-024-01:on 890723,entry Into Operational Condition 2 Completed W/Suppression Pool Makeup Sys Inoperable & on 890725,vent Valve on Ref Leg Found Open & Uncapped.Caused by Personnel Error.Personnel counseled.W/891027 Ltr ML19325D5121989-10-20020 October 1989 LER 89-027-00:on 890925,loss of Control Power to Emergency Svc Water Sys Pump Discharge Valve a Rendered Sys Inoperable.Caused by Personnel Error Re Jumper Placement. Involved Technicians counseled.W/891020 Ltr ML19325D1581989-10-13013 October 1989 LER 88-025-01:on 880618,reactor Protection Sys (RPS) Bus Inadvertently Deenergized,Resulting in Full RPS Actuation. Caused by Personnel Error W/Contributing Factor of Poor Human Factors Design.Info Tag Installed on Power Switch ML19325D1591989-10-13013 October 1989 LER 89-026-00:on 890913,reactor Thermal Power Level Exceeded That Specified in OL Due to Unexpected Recirculation Sys Flow Control Transient.Caused by Component Failure.Failed Isolation Solenoid Valve Replaced ML19325D9331987-03-27027 March 1987 LER 87-010-00:on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised ML19325C1171987-03-27027 March 1987 LER 87-009-00:on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 revised.W/870327 Ltr 1994-08-10
[Table view] Category:RO)
MONTHYEARML18011A5401994-08-10010 August 1994 LER 94-017-00:on 940711,automatic Isolation of RHR Sys Shutdown Cooling Suction Outboard Containment Isolation Valve Occurred Due to Inadequate Work Order.Work Order Process for I&C Work Orders Will Be reviewed.W/940810 Ltr ML20046C5721993-08-0606 August 1993 LER 93-015-00:on 930709,unexpected RRP Fast to Slow Speed Downshift Occurred Due to Failure of Both RRP Suction Temp Rtd.Replaced & Returned RTD to Mfg for Failure Analysis. W/930806 Ltr ML20046B7811993-08-0202 August 1993 LER 93-014-00:on 930703,TS 3.0.3 Entered Due to Failure of Racs Power Supply.Replaced 5 Volt Power Supply in Racs cabinet.W/930802 Ltr ML20045G7201993-07-0808 July 1993 LER 93-013-00:on 930608,control Room HVAC Sys Train a Supply Fan Tripped on Overcurrent,Resulting in Both Sys Trains Being Unavailable.Caused by Motor Winding Insulation Failure.Motor Repaired by mfg.W/930708 Ltr ML20045G2171993-07-0707 July 1993 LER 93-012-00:on 930607,noted That HPCS Initiation Signal Resulted in Auto Start of Div 3 DG & ESW Sys.Caused by Failure of Div 3 Reserve Battery Charger.Procedures Used for Insp & Maint of Battery Being modified.W/930707 Ltr ML20044F2161993-05-19019 May 1993 LER 93-011-00:on 930419,identified That Excessive Strainer Differential Pressure Across RHR Suction Strainers Could Have Compromised Long Term Cooling During LOCA Operation. Caused by Inadequate Program requirements.W/930519 Ltr ML20044B6771993-02-22022 February 1993 LER 93-004-00:on 930121,MOV Testing of Main Steam Line Drain & Bypass Outboard Isolation Valve Indicated That Thrust Less than Design Thrust to Close Valve Under Accident Conditions. Review,Per GL 89-10 in progress.W/930222 Ltr ML20029B6431991-03-0808 March 1991 LER 91-007-00:on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper value.W/910308 Ltr ML20029B0971991-03-0101 March 1991 LER 91-006-00:on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being revised.W/910301 Ltr ML20029A6451991-02-22022 February 1991 LER 91-005-00:on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel error.W/910222 Ltr ML20029A3321991-02-15015 February 1991 LER 91-004-00:on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified. W/910215 Ltr ML20028H7521991-01-25025 January 1991 LER 90-041-00:between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo issued.W/910125 Ltr ML20024F7421990-12-14014 December 1990 LER 90-033-00:on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N ML20024F7411990-12-14014 December 1990 LER 90-032-00:on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders ML20028G9181990-09-28028 September 1990 LER 90-020-00:on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being revised.W/900928 Ltr ML20044B1021990-07-13013 July 1990 LER 90-013-00:on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel counseled.W/900713 Ltr ML20043H4801990-06-20020 June 1990 LER 90-011-00:on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction revised.W/900620 Ltr ML20043H5251990-06-20020 June 1990 LER 90-010-00:on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage monitored.W/900620 Ltr ML20043H3841990-06-18018 June 1990 LER 90-009-00:on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut replaced.W/900618 Ltr ML20043E5711990-06-0808 June 1990 LER 89-030-01:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Failure of Two Control Rods Caused by Improper Seat Matl in Associated Scram Pilot Solenoid Valves.Instructions revised.W/900608 Ltr ML20043A7801990-05-18018 May 1990 LER 90-007-00:on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced ML20043A8451990-05-18018 May 1990 LER 90-008-00:on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced ML20042G7731990-05-11011 May 1990 LER 90-006-00:on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel retrained.W/900511 Ltr ML20012D8151990-03-24024 March 1990 LER 90-003-00:on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement implemented.W/900323 Ltr ML20011E1861990-02-0202 February 1990 LER 90-001-00:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised ML20011E1871990-02-0202 February 1990 LER 90-002-00:on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised ML19354E0961990-01-19019 January 1990 LER 89-032-00:on 891228 & 900105,HPCS Sys Declared Inoperable Due to Inoperability of Div 3 Battery.Caused by Low Pilot Cell Voltage,Cell W/Slow Electrolyte Leak & Blown Power Fuse.Fuse & Hydromotor Pump replaced.W/900119 Ltr ML20005E6851990-01-0505 January 1990 LER 89-031-00:on 891206,08 & 15,RWCU Sys Isolations Occurred.Caused by Design Deficiency & Deficiency in Leak Detection/Differential Flow Circuitry Setpoint &/Or Time Delay.Leak Detection Thermocouples relocated.W/900105 Ltr ML20005E0821989-12-26026 December 1989 LER 89-030-00:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Caused by Failure to Return Scram Pilot Valves Used for Rods to Mfg After Recall. Surveillance Instruction revised.W/891226 Ltr ML19354D5991989-12-17017 December 1989 LER 89-029-00:on 891117,heater Bay/Turbine Bldg Vent Gaseous Effluent Particulate & Iodine Samples Not Continuously Collected as Required by Tech Spec 3.3.7.10.Caused by Procedure Deficiency.Procedure revised.W/891217 Ltr ML19325E5901989-11-0303 November 1989 LER 89-028-00:on 891008,concluded That Operation of Fuel Pool Cooling & Cleanup Sys to Upper Containment Pools Caused Containment Vacuum Breaker Actuations.Caused by Unrecognized Sys Interaction.Operating Instruction revised.W/891103 Ltr ML19324B1241989-10-27027 October 1989 LER 89-024-01:on 890723,entry Into Operational Condition 2 Completed W/Suppression Pool Makeup Sys Inoperable & on 890725,vent Valve on Ref Leg Found Open & Uncapped.Caused by Personnel Error.Personnel counseled.W/891027 Ltr ML19325D5121989-10-20020 October 1989 LER 89-027-00:on 890925,loss of Control Power to Emergency Svc Water Sys Pump Discharge Valve a Rendered Sys Inoperable.Caused by Personnel Error Re Jumper Placement. Involved Technicians counseled.W/891020 Ltr ML19325D1581989-10-13013 October 1989 LER 88-025-01:on 880618,reactor Protection Sys (RPS) Bus Inadvertently Deenergized,Resulting in Full RPS Actuation. Caused by Personnel Error W/Contributing Factor of Poor Human Factors Design.Info Tag Installed on Power Switch ML19325D1591989-10-13013 October 1989 LER 89-026-00:on 890913,reactor Thermal Power Level Exceeded That Specified in OL Due to Unexpected Recirculation Sys Flow Control Transient.Caused by Component Failure.Failed Isolation Solenoid Valve Replaced ML19325D9331987-03-27027 March 1987 LER 87-010-00:on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised ML19325C1171987-03-27027 March 1987 LER 87-009-00:on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 revised.W/870327 Ltr 1994-08-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in Pnpp to Ceico PY-CEI-NRR-2437, Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With PY-CEI-NRR-2429, Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With PY-CEI-NRR-2424, Monthly Operating Rept for July 1999 for Perry Npp.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Perry Npp.With ML20210J3851999-07-28028 July 1999 Pnpp - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval PY-CEI-NRR-2416, Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With ML20196A1951999-06-17017 June 1999 Instrument Drift Analysis ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application PY-CEI-NRR-2409, Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2393, Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored1999-05-12012 May 1999 Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp PY-CEI-NRR-2399, Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at Pnpp & Use of Table IWB-3514 ML20206D7911999-04-23023 April 1999 Rev 6 to PDB-F0001, COLR for Pnpp Unit 1 Cycle 8,Reload 7 ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20206D8461999-03-31031 March 1999 Rev 1 to J11-03371SRLR, Supplemental Reload Licensing Rept for Pnpp,Unit 1 Reload 7 Cycle 8 PY-CEI-NRR-2389, Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 PY-CEI-NRR-2369, Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 9902271999-03-0303 March 1999 Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 990227 PY-CEI-NRR-2372, Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl PY-CEI-NRR-2356, Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2346, Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position PY-CEI-NRR-2335, Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2329, Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With ML20153B8221998-09-16016 September 1998 Safety Evaluation Accepting Changes to USAR Section 13.4.3, 17.2.1.3.2.2,17.2.1.3.2.2.3 & App 1A PY-CEI-NRR-2323, Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2313, Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2306, Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 1 ML20249A1891998-06-11011 June 1998 SER on Moderate Energy Line Pipe Break Criteria for Perry Nuclear Power Plant,Unit 1 & Requests Addl Info to Demonstrate That Plant & FSAR in Compliance W/Staff Position & GDC as Discussed in SER PY-CEI-NRR-2289, Monthly Operating Rept for May 1998 for Perry,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Perry,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted PY-CEI-NRR-2282, Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D2051998-04-20020 April 1998 SER Authorizing Licensee to Use Code Case N-524 Until Such Time as Code Case Included in Future Rev of RG 1.147 PY-CEI-NRR-2277, Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216G3901998-03-11011 March 1998 SER on Proposed Merger Between Duquesne Light Co & Allegheny Power Sys,Inc ML20216J1401998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2258, Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 11998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 1 1999-09-30
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CENTERi??R ENERGY PERRY NUCLEAR POWER PLANT Maif Address-.
O. BOX 97 Ro M A h ahan
- 10 CENTER ROAD PERRY, OHIO 44081 VICE PRESIDENT NUCLEAR PERRY, OHIO 44081 (216) 259-3737 July 7, 1993 PY-CEI/NRR-1674 L U.S. Nuclear Regulatory Commission Document Control Desk Vashington, D.C. 20555 Perry Nuclear Power Plant Docket No. 50 440 LER 93-012
Dear Sir:
Enclosed is Licensee Event Report 93-012 for the Perry Nuclear Power Plant.
Sincerely, !
f-cW s fg Robert A. StrAtman RAS:LKRtss
Enclosure:
LER 93-012 cc: NRC Project Manager l NRC Resident Inspector ;
NRC Region III i l
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 f5 92i '
EXPIRES 5/31/95 ESilMATED BURDEN PER RESPONFE TO COMPLY WITH 1HiS INFORMATION CCMECTION REQUESf; 50 0 HRS. I'OHWARD LICENSEE EVENT REPORT (LER) COuutNTs ntoARDiNG auRoEN EsTiuiTt TO THc inrOiwiATiON AND RECORDS MANAGEMF NT BRANCH (MN8B 7718. U.S. MA: LEAR REGULATOriY COMMtSSiON, W ASHINGTON, DC 205550001, AND TO THE FAPEHWORK REDUCTION PROJECT (3150 0104), OFTICE OF (See reverse for required numtier of digits / characters for each block) MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
F ACILITY NAME {1) DOCKET NUMBER (2) PAGE (3)
Perry Nuclear Powr Plant, Unit 1 05000 440 1 OF 6 TITLE (4)
Voltage Fluctuations in Battery Charger Output Cause High Pressure Core Spray Actuation EVENT DATE (5) LER NUMBER (6'. REPORT NUMBER (7) OTHER FACILITIES INVOLVED (8)
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MCWTH DAV YEAR YEAR MONTH DAY YEAR Nuuw n NuweR 05000 F ACidiY NAME DOCKET NUMBER
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06 07 93 93 012 00 07 07 93 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR O (Check one or more) (11)
MODE (9) 1 20 402(b) 20 405(c) X 50 73(a)(2)0v) 73.71(b)
POWER 20 405(aH110) 50.36(c)(1) X 50.73(a)(2)(v) 73.71(c)
LEVEL (10) 082 20 405(a)(1)(n) 50.36(c)(2) 50.73(a)(2)(vn) x 01HER 20 405(a)(1)(m) 50.73(a)(2)h) 50.73(a)(2)(vin)(A) PP'W 'n Abw ct below and in Test, NRC 20.405(a)(1)(m) 50.73(a)(2)Di) 50.73(a)(2)(vni)(B) Form aceA) T.S.
20 405(3)(1)M 50 73(a)(2)(m) 50,73(a)(2)(x) 3/4 3.5.1.q LICENSEE CONTACT FOR THIS LER (12)
AAME TELLPHONE NUMHf H pnchsde Area CorJej
, Linda K. Routzahn, Compliance Engineer Extension 5781 (216) 259-3737 I
COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCdlBED IN THIS REPORT (13) -
cAusE s erM cowOu r l WWi ACTURER CAu$[ $YS TEM COMPONE NT MANUFACTURER O
B FJ BYC P319 N SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MON TH DAY YEAR ns SUBMISSION X NO P m. mmwe o a w o NPM'ssoN DoCi DATE (15)
ABSTRACT (umet to 1400 spaces. i e , apprommately 15 singte-spaced typewntten lines) (16)
On June 7, 1993, receipt of a High Pressure Core Spray (HPCS) in. . tion signal resulted in auto start of the Division 3 Diesel Generator and Emergency Service Water System, followed by High Pressure Core Spray injection with suction ~from the Suppression Pool. The cause of the event was failure of the Division 3 Reserve Battery Charger to maintain stable output voltage. The voltage transient tripped the
. 125 VDC to 120 VAC Topaz inverter, which affected the supply to Division 3 transmitters and the associated output signals. Once level transmitter output signals decreased to indicate vessel level 2, the divisional master trip units provided a HPCS initiation signal. Control Room operators secured the system after confirmation of inadvertent initiation.
The power plant responded to the HPCS Initiation as expected. The reactor power, pressure, and level transients were within the limits of the USAR analysis.
Erratic Reserve Charger output and internal control voltages were noted during subsequent testing. All charger components which were considered capable of causing the noted malfunction were replaced, and no further erratic voltages were observed.
Submittal of this report also satisfies the requirements for Technical Specification 3.5.1, action g. which requires a Special Report following any Emergency Core Cooling System actuation and injection into the Reactor Coolant System.
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NRC FORM 366A' U.S. NUCLEAR HEGULATOnY COMMISSION APPROVED DY OMB NO. 3150-0104 EXPIRES 5/31/95 ESTIMAYED BURDEN P( A AESM96E TO COMPLY WTTH THtS LICENSEE EVENT REPORT (LER) E%^AidfEM"nl#ELAr"iO72,,400 TEXT CONTINUATION "
$U E *cS'M "'*N"TO 'Elisi E THE PAPERWOAK REDUCTION PRG1ECT (3tSO4104). OFFCE OF M ANAGEMENT AND SUDGET, WASHINGTON, DC 20M3 FACILITY NAME {t) DOCKIT NUMBE R (2) Lf R NUMBER (4) P AOg (13 g blGUL NT tA. Hk v&o4 NUMBER NUMBEA Perry Nuclear Power Plant, Unit 1 05000 440 2 OF (,3 TLXT pf more stance on repree, m* accatoroet coo **s of NHC Fwm 3rtA) (11; I. Introduction At 0424 hours0.00491 days <br />0.118 hours <br />7.010582e-4 weeks <br />1.61332e-4 months <br /> on June 7, 1993 an inadvertent High Pressure Core Spray (HPCS) [BG) initiation occurred due to the effect of unstable output voltage from the Division 3 Reserve Battery Charger (BYCJ on divisional trip unit power and logic circuits. Prior to the event the plant was operating at 82 percent power, with reactor pressure at 994 psig and saturated conditions.
The Emergency Core Cooling System discharge to reactor coolant system and Engineered Safety Features actuation are being reported pursuant to the requirements of 10CFR50.73(a)(2)(iv). Partial loss of Division 3 instrumentation is reported pet the requirements of 10CFR50.73(a)(2)(v). Appropriate notifications vere made pursuant to the reporting requirements of 10CFR50.72(a),
10CFR50.72(b)(2)(iii)(d), and 10CFR50.72(b)(2)(ii). An unusual event was simultaneously classified due to HPCS flow to the reactor, and terminated at-0430.
Submittal of this report also satisfies the requirements for Technical Specification 3.5.1, action g. which requires a Special Report following any Emergency Core Cooling System actuation and injection into the Reactor coolant System. This was the seventh High Pressure Core Spray injection cycle to date.
The injection nozzle usage factor is currently less than 0.70.
II. Description of the Event Approximately six hours prior to the event, the Unit 1 Division 3 Reserve Charger and the Unit 2 Division 3 Battery [BTRY] had been aligned to supply Unit 1 Division 3 125 VDC Bus ED1C. The Unit 1 Division 3 Charger and Battery had been removed from service in preparation for a battery load test.
On June 7, 1993, at approximately 0424 hours0.00491 days <br />0.118 hours <br />7.010582e-4 weeks <br />1.61332e-4 months <br />, with the plant at 82 percent power and ascension to 35 percent power planned, a High Pressure Core Spray Initiation )
signal was received. The initiation signal resulted from the effect of Division l 3 Reserve Battery Charger output voltage fluctuations on the divisional analog trip unit power and logic circuits. The Division 3 Diesel Generator [DG) and Emergency Service Vater System auto-started. Ten seconds following the initiation signal, the HPCS Pump auto-started. Approximately 4 seconds later the pump had developed sufficient discharge pressure to begin injecting from the Suppression Pool to the reactor vessel. Control Room Operators verified the HPCS initiation to oe inadvertent and secured the HPCS Pump at approximately 0425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br />. The HPCS Discharge Check Valve indicated closed at approximately 0425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br />.
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93 00 7uTw n.u-.a,.u..am. m m. n .w mc m m on In parallel with the llPCS initiation, alarms for Division 3 DC System Trouble and I!PCS Out Of Service, and a status light for Trip Unit Gross Fail vere received.
Operators observed the Division 3 DC Bus voltage to be approximately 150 VDC and the instrument bus power supply to be de-energized. With the instrument power supply de-energized, Operators had no indication of IIPCS flow, discharge pressure, Division 3 reactor level or dryvell pressure indications. At this point HPCS was considered. inoperable, due to loss of monitoring capability. At approximately 0430 hours0.00498 days <br />0.119 hours <br />7.109788e-4 weeks <br />1.63615e-4 months <br /> the Division 3 DC bus voltage returned to normal and the instrument bus power supply re-energized restoring HPCS instrument indications.
Voltage excursions on the 125 VDC bus occurred five times during the next hour, as evidenced by lov level alarms on the sequence of events recorders. Event duration ranged from several milliseconds to several seconds. Since the initial Division 3 initiation signal had not been reset, subsequent initiations did not 7
occur.
By 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> the Unit 1 Division 3 Charger and Battery were realigned to supply the Unit 1 Division 3 125 VDC Bus and the Division 3 Reserve Charger and Unit 2 i Division 3 Battery were secured. At 0616 hours0.00713 days <br />0.171 hours <br />0.00102 weeks <br />2.34388e-4 months <br />, the Division 3 Initiation signal ]
vas reset and HPCS returned to standby readiness condition. The Division 3 -l Diesel Generator was synchronized to the Division 3 4160. Volt Bus and loaded for ;
one hour. Following the diesel run, both the diesel and the Division 3 Emergency l Service Water System were secured and returned to standby readiness condition. i At 0713 hours0.00825 days <br />0.198 hours <br />0.00118 weeks <br />2.712965e-4 months <br />, HPCS vas declared operable. !
i III. Cause of Event The event was caused by the failure of the Division 3 Reserve Charger to maintain a stable output voltage. Charger components which most likely caused the voltage i fluctuations have been replaced. The removed components have been forwarded to the vendor for additional failure analysis. The chargers supply power to a 125 VDC to 120 VAC Topaz inverter [INVT), which in turn feeds a 120 VAC to 24 VDC instrument power supply [JX). The 24 VDC supply provides power to the HPCS instrumentation and analog master trip units. Once the 125VDC Bus voltage vent to approximately 150 volts, the Division 3 instrument power supply inverter units tripped on high voltage. The analog master trip units continued to power their associated transmitters, but with a decreasing voltage. The decreasing voltage caused a decrease in transmitter outputs. Once the output signal from the Division 3 Reactor Level Transmitters decreased to indicate less than vessel level 2, the Division 3 Reactor Level master trip units tripped, energizing their output relays and providing the (sealed in) HPCS initiation signal. ,
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IV. Analysis of Event The power plant response was as expected. This event is described in USAR Chapter 15.5. Reactor Pressure Control and Reactor Level Control Systems responded as expected to changes in reactor level and pressure. As HPCS flow to the vessel increased, reactor power decreased slightly causing a slight drop in reactor pressure. Reactor Level Control responded reducing feed flow to the vessel. Once the HPCS pump was secured the Reactor Level Control System readjusted feed flow and restored vessel level to within its normal band with no reactor operator interaction. Once Reactor Level Control stabilized, reactor power and pressure returned to pre-transient values.
The Rosemount Master Trip Units and Transmitters responded to the instrument bus power loss as expected. HPCS initiation logic responded as expected. The Division 3 Diesel Generator, Emergency Service Vater, and High Pressure Core Spray Systems responded as expected to an initiation signal.
I The impact of this event, inclusive of fatigue, is enveloped by design phase analysis for the reactor, reactor internals, and HPCS piping. Design specifications account for 10 cycles of inadvertent HPCS initiation with injection of 40 degree F vater. Engineering reviev of USAR Chapter 15, Section 15.5.1, " Inadvertent HPCS Startup," identified no irregularities or deficiencies for this event. The event is bounded by the existing safety analysis and is not considered to be safety significant.
The Lov Pressure Core Spray (LPCS) and the Low Pressure Coolant Injection (LPCI) systems are provided to assure that the core is adequately cooled following a loss of coolant accident (LOCA). They provide adequate core cooling capability for all break sizes following depressurization. The HPCS system is provided to assure that the reactor is adequately cooled in the event of a small break LOCA vhich does not result in rapid depressurization of the reactor vessel. .
Additionally, the Automatic Depressurization System (ADS) is provided to reduce pressure during small break LOCAs to allow LPCS and LPCI to perform their functions in time to prevent core damage. The various systems described above, are divided into three Emergency Core Cooling System (ECCS) divisions for operability and Technical Specification compliance purposes. In addition, although not relied on in accident analyses, the Reactor Core Isolation Cooling (RCIC) system provides the same function as the HPCS system. All but the HPCS system vere operable during this event, providing ECCS capability.
HPCS was inoperable for less than three hours during this event. Technical Specifications allow the HPCS system to remain inorserable for fourteen days provided the remaining two ECCS divisions and RCIC are operable.
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V. Previous Similar Events A previous similar event occurred at Perry in 1986. This event was reported in LER 86-41. In the 1986 event, the Reserve Charger was povering Division 3 Bus.
When its output voltage became unstable and resulted in a Division 3 HPCS initiation signal. No injection occurred during the 1986 event. A design change to the system battery chargers was evaluated to incorporate a very high speed, '
electronic high voltage shutdown circuit to allow protective coordination with the instrument power inverters. However, this type of circuit was not available from the manufacturer. In addition, based on the operating history of the charger dssign, the manufacturer did not recommend a design upgrade.
The integrated lov voltage electrical system response was also evaluated with no design change to the analog trip unit power and logic circuits recommended by the NSSS designer at that time. The conclusion of the NSSS designer was that the power system design met divisional safety requirements and that additional control components vould actually decrease safety system reliability.
VI. Corrective Actions Subsequent to the Reserve Charger being removed from service, tests were performed to monitor charger output and internal control voltages. Erratic output voltages were initially observed during the tests, but voltage stabilized after manual adjustment. Discussions with the vendor identified charger components most likely to have contributed to the voltage excursion. These suspect components, the sensing board, amplifier board and float voltage adjustment potentiometer, were replaced and have been forwarded to the vendor for ;
failure analysis. No erratic charger operation was observed during tests conducted after the components were replaced.
Procedures used for periodic inspection and maintenance of battery chargers are being modified to include detailed inspection and cleaning of float voltage adjustment and equalizing voltage potentiometers.
The Unit 1 and Unit 2 Division 3 Batteries were tested per the surveillance requirements of Technical Specification 4.8.2.1(b) following the over voltage transient. All tested attributes were found to be acceptable.
Engineering is evaluating the need for installation of a high voltage shutdown circuit; replacement of the Topaz 125 VDC to 120 VAC inverters; and the effect of the voltage level increase for divisional instrumentation and power supplies, appropriate relays and other equipment that may have a lov tolerance to overvoltage conditions.
NRC FORM 366A F92)
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Prior to this event the HPCS had been aligned to take suction from the Suppression Pool to support Suppression Pool Cleanup Operations. Initial !
estimates are that approximately 500 to 1000 gallons of Suppression Pool water l vere injected to the reactor. Reactor coolant samples were analyzed and determined to be within normal chemistry limits. The HPCS Suppression Pool '
Suction Strainer was inspected and found to be in an acceptable condition.
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