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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18011A5401994-08-10010 August 1994 LER 94-017-00:on 940711,automatic Isolation of RHR Sys Shutdown Cooling Suction Outboard Containment Isolation Valve Occurred Due to Inadequate Work Order.Work Order Process for I&C Work Orders Will Be reviewed.W/940810 Ltr ML20046C5721993-08-0606 August 1993 LER 93-015-00:on 930709,unexpected RRP Fast to Slow Speed Downshift Occurred Due to Failure of Both RRP Suction Temp Rtd.Replaced & Returned RTD to Mfg for Failure Analysis. W/930806 Ltr ML20046B7811993-08-0202 August 1993 LER 93-014-00:on 930703,TS 3.0.3 Entered Due to Failure of Racs Power Supply.Replaced 5 Volt Power Supply in Racs cabinet.W/930802 Ltr ML20045G7201993-07-0808 July 1993 LER 93-013-00:on 930608,control Room HVAC Sys Train a Supply Fan Tripped on Overcurrent,Resulting in Both Sys Trains Being Unavailable.Caused by Motor Winding Insulation Failure.Motor Repaired by mfg.W/930708 Ltr ML20045G2171993-07-0707 July 1993 LER 93-012-00:on 930607,noted That HPCS Initiation Signal Resulted in Auto Start of Div 3 DG & ESW Sys.Caused by Failure of Div 3 Reserve Battery Charger.Procedures Used for Insp & Maint of Battery Being modified.W/930707 Ltr ML20044F2161993-05-19019 May 1993 LER 93-011-00:on 930419,identified That Excessive Strainer Differential Pressure Across RHR Suction Strainers Could Have Compromised Long Term Cooling During LOCA Operation. Caused by Inadequate Program requirements.W/930519 Ltr ML20044B6771993-02-22022 February 1993 LER 93-004-00:on 930121,MOV Testing of Main Steam Line Drain & Bypass Outboard Isolation Valve Indicated That Thrust Less than Design Thrust to Close Valve Under Accident Conditions. Review,Per GL 89-10 in progress.W/930222 Ltr ML20029B6431991-03-0808 March 1991 LER 91-007-00:on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper value.W/910308 Ltr ML20029B0971991-03-0101 March 1991 LER 91-006-00:on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being revised.W/910301 Ltr ML20029A6451991-02-22022 February 1991 LER 91-005-00:on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel error.W/910222 Ltr ML20029A3321991-02-15015 February 1991 LER 91-004-00:on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified. W/910215 Ltr ML20028H7521991-01-25025 January 1991 LER 90-041-00:between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo issued.W/910125 Ltr ML20024F7421990-12-14014 December 1990 LER 90-033-00:on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N ML20024F7411990-12-14014 December 1990 LER 90-032-00:on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders ML20028G9181990-09-28028 September 1990 LER 90-020-00:on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being revised.W/900928 Ltr ML20044B1021990-07-13013 July 1990 LER 90-013-00:on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel counseled.W/900713 Ltr ML20043H4801990-06-20020 June 1990 LER 90-011-00:on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction revised.W/900620 Ltr ML20043H5251990-06-20020 June 1990 LER 90-010-00:on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage monitored.W/900620 Ltr ML20043H3841990-06-18018 June 1990 LER 90-009-00:on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut replaced.W/900618 Ltr ML20043E5711990-06-0808 June 1990 LER 89-030-01:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Failure of Two Control Rods Caused by Improper Seat Matl in Associated Scram Pilot Solenoid Valves.Instructions revised.W/900608 Ltr ML20043A7801990-05-18018 May 1990 LER 90-007-00:on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced ML20043A8451990-05-18018 May 1990 LER 90-008-00:on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced ML20042G7731990-05-11011 May 1990 LER 90-006-00:on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel retrained.W/900511 Ltr ML20012D8151990-03-24024 March 1990 LER 90-003-00:on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement implemented.W/900323 Ltr ML20011E1861990-02-0202 February 1990 LER 90-001-00:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised ML20011E1871990-02-0202 February 1990 LER 90-002-00:on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised ML19354E0961990-01-19019 January 1990 LER 89-032-00:on 891228 & 900105,HPCS Sys Declared Inoperable Due to Inoperability of Div 3 Battery.Caused by Low Pilot Cell Voltage,Cell W/Slow Electrolyte Leak & Blown Power Fuse.Fuse & Hydromotor Pump replaced.W/900119 Ltr ML20005E6851990-01-0505 January 1990 LER 89-031-00:on 891206,08 & 15,RWCU Sys Isolations Occurred.Caused by Design Deficiency & Deficiency in Leak Detection/Differential Flow Circuitry Setpoint &/Or Time Delay.Leak Detection Thermocouples relocated.W/900105 Ltr ML20005E0821989-12-26026 December 1989 LER 89-030-00:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Caused by Failure to Return Scram Pilot Valves Used for Rods to Mfg After Recall. Surveillance Instruction revised.W/891226 Ltr ML19354D5991989-12-17017 December 1989 LER 89-029-00:on 891117,heater Bay/Turbine Bldg Vent Gaseous Effluent Particulate & Iodine Samples Not Continuously Collected as Required by Tech Spec 3.3.7.10.Caused by Procedure Deficiency.Procedure revised.W/891217 Ltr ML19325E5901989-11-0303 November 1989 LER 89-028-00:on 891008,concluded That Operation of Fuel Pool Cooling & Cleanup Sys to Upper Containment Pools Caused Containment Vacuum Breaker Actuations.Caused by Unrecognized Sys Interaction.Operating Instruction revised.W/891103 Ltr ML19324B1241989-10-27027 October 1989 LER 89-024-01:on 890723,entry Into Operational Condition 2 Completed W/Suppression Pool Makeup Sys Inoperable & on 890725,vent Valve on Ref Leg Found Open & Uncapped.Caused by Personnel Error.Personnel counseled.W/891027 Ltr ML19325D5121989-10-20020 October 1989 LER 89-027-00:on 890925,loss of Control Power to Emergency Svc Water Sys Pump Discharge Valve a Rendered Sys Inoperable.Caused by Personnel Error Re Jumper Placement. Involved Technicians counseled.W/891020 Ltr ML19325D1581989-10-13013 October 1989 LER 88-025-01:on 880618,reactor Protection Sys (RPS) Bus Inadvertently Deenergized,Resulting in Full RPS Actuation. Caused by Personnel Error W/Contributing Factor of Poor Human Factors Design.Info Tag Installed on Power Switch ML19325D1591989-10-13013 October 1989 LER 89-026-00:on 890913,reactor Thermal Power Level Exceeded That Specified in OL Due to Unexpected Recirculation Sys Flow Control Transient.Caused by Component Failure.Failed Isolation Solenoid Valve Replaced ML19325D9331987-03-27027 March 1987 LER 87-010-00:on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised ML19325C1171987-03-27027 March 1987 LER 87-009-00:on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 revised.W/870327 Ltr 1994-08-10
[Table view] Category:RO)
MONTHYEARML18011A5401994-08-10010 August 1994 LER 94-017-00:on 940711,automatic Isolation of RHR Sys Shutdown Cooling Suction Outboard Containment Isolation Valve Occurred Due to Inadequate Work Order.Work Order Process for I&C Work Orders Will Be reviewed.W/940810 Ltr ML20046C5721993-08-0606 August 1993 LER 93-015-00:on 930709,unexpected RRP Fast to Slow Speed Downshift Occurred Due to Failure of Both RRP Suction Temp Rtd.Replaced & Returned RTD to Mfg for Failure Analysis. W/930806 Ltr ML20046B7811993-08-0202 August 1993 LER 93-014-00:on 930703,TS 3.0.3 Entered Due to Failure of Racs Power Supply.Replaced 5 Volt Power Supply in Racs cabinet.W/930802 Ltr ML20045G7201993-07-0808 July 1993 LER 93-013-00:on 930608,control Room HVAC Sys Train a Supply Fan Tripped on Overcurrent,Resulting in Both Sys Trains Being Unavailable.Caused by Motor Winding Insulation Failure.Motor Repaired by mfg.W/930708 Ltr ML20045G2171993-07-0707 July 1993 LER 93-012-00:on 930607,noted That HPCS Initiation Signal Resulted in Auto Start of Div 3 DG & ESW Sys.Caused by Failure of Div 3 Reserve Battery Charger.Procedures Used for Insp & Maint of Battery Being modified.W/930707 Ltr ML20044F2161993-05-19019 May 1993 LER 93-011-00:on 930419,identified That Excessive Strainer Differential Pressure Across RHR Suction Strainers Could Have Compromised Long Term Cooling During LOCA Operation. Caused by Inadequate Program requirements.W/930519 Ltr ML20044B6771993-02-22022 February 1993 LER 93-004-00:on 930121,MOV Testing of Main Steam Line Drain & Bypass Outboard Isolation Valve Indicated That Thrust Less than Design Thrust to Close Valve Under Accident Conditions. Review,Per GL 89-10 in progress.W/930222 Ltr ML20029B6431991-03-0808 March 1991 LER 91-007-00:on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper value.W/910308 Ltr ML20029B0971991-03-0101 March 1991 LER 91-006-00:on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being revised.W/910301 Ltr ML20029A6451991-02-22022 February 1991 LER 91-005-00:on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel error.W/910222 Ltr ML20029A3321991-02-15015 February 1991 LER 91-004-00:on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified. W/910215 Ltr ML20028H7521991-01-25025 January 1991 LER 90-041-00:between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo issued.W/910125 Ltr ML20024F7421990-12-14014 December 1990 LER 90-033-00:on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N ML20024F7411990-12-14014 December 1990 LER 90-032-00:on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders ML20028G9181990-09-28028 September 1990 LER 90-020-00:on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being revised.W/900928 Ltr ML20044B1021990-07-13013 July 1990 LER 90-013-00:on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel counseled.W/900713 Ltr ML20043H4801990-06-20020 June 1990 LER 90-011-00:on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction revised.W/900620 Ltr ML20043H5251990-06-20020 June 1990 LER 90-010-00:on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage monitored.W/900620 Ltr ML20043H3841990-06-18018 June 1990 LER 90-009-00:on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut replaced.W/900618 Ltr ML20043E5711990-06-0808 June 1990 LER 89-030-01:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Failure of Two Control Rods Caused by Improper Seat Matl in Associated Scram Pilot Solenoid Valves.Instructions revised.W/900608 Ltr ML20043A7801990-05-18018 May 1990 LER 90-007-00:on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced ML20043A8451990-05-18018 May 1990 LER 90-008-00:on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced ML20042G7731990-05-11011 May 1990 LER 90-006-00:on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel retrained.W/900511 Ltr ML20012D8151990-03-24024 March 1990 LER 90-003-00:on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement implemented.W/900323 Ltr ML20011E1861990-02-0202 February 1990 LER 90-001-00:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised ML20011E1871990-02-0202 February 1990 LER 90-002-00:on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised ML19354E0961990-01-19019 January 1990 LER 89-032-00:on 891228 & 900105,HPCS Sys Declared Inoperable Due to Inoperability of Div 3 Battery.Caused by Low Pilot Cell Voltage,Cell W/Slow Electrolyte Leak & Blown Power Fuse.Fuse & Hydromotor Pump replaced.W/900119 Ltr ML20005E6851990-01-0505 January 1990 LER 89-031-00:on 891206,08 & 15,RWCU Sys Isolations Occurred.Caused by Design Deficiency & Deficiency in Leak Detection/Differential Flow Circuitry Setpoint &/Or Time Delay.Leak Detection Thermocouples relocated.W/900105 Ltr ML20005E0821989-12-26026 December 1989 LER 89-030-00:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Caused by Failure to Return Scram Pilot Valves Used for Rods to Mfg After Recall. Surveillance Instruction revised.W/891226 Ltr ML19354D5991989-12-17017 December 1989 LER 89-029-00:on 891117,heater Bay/Turbine Bldg Vent Gaseous Effluent Particulate & Iodine Samples Not Continuously Collected as Required by Tech Spec 3.3.7.10.Caused by Procedure Deficiency.Procedure revised.W/891217 Ltr ML19325E5901989-11-0303 November 1989 LER 89-028-00:on 891008,concluded That Operation of Fuel Pool Cooling & Cleanup Sys to Upper Containment Pools Caused Containment Vacuum Breaker Actuations.Caused by Unrecognized Sys Interaction.Operating Instruction revised.W/891103 Ltr ML19324B1241989-10-27027 October 1989 LER 89-024-01:on 890723,entry Into Operational Condition 2 Completed W/Suppression Pool Makeup Sys Inoperable & on 890725,vent Valve on Ref Leg Found Open & Uncapped.Caused by Personnel Error.Personnel counseled.W/891027 Ltr ML19325D5121989-10-20020 October 1989 LER 89-027-00:on 890925,loss of Control Power to Emergency Svc Water Sys Pump Discharge Valve a Rendered Sys Inoperable.Caused by Personnel Error Re Jumper Placement. Involved Technicians counseled.W/891020 Ltr ML19325D1581989-10-13013 October 1989 LER 88-025-01:on 880618,reactor Protection Sys (RPS) Bus Inadvertently Deenergized,Resulting in Full RPS Actuation. Caused by Personnel Error W/Contributing Factor of Poor Human Factors Design.Info Tag Installed on Power Switch ML19325D1591989-10-13013 October 1989 LER 89-026-00:on 890913,reactor Thermal Power Level Exceeded That Specified in OL Due to Unexpected Recirculation Sys Flow Control Transient.Caused by Component Failure.Failed Isolation Solenoid Valve Replaced ML19325D9331987-03-27027 March 1987 LER 87-010-00:on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised ML19325C1171987-03-27027 March 1987 LER 87-009-00:on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 revised.W/870327 Ltr 1994-08-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in Pnpp to Ceico PY-CEI-NRR-2437, Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With PY-CEI-NRR-2429, Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With NUREG-1482, SE Approving Licensee Relief Requets PR-2,PR-3,PR-6,VR-6, VR-7,VR-10,PR-4,PR-5,VR-4,VR-5,VR-9,VR-1 & VR-3 Related to Inservice Testing Program,Second ten-year Interval for Perry Nuclear Power Plant1999-08-0909 August 1999 SE Approving Licensee Relief Requets PR-2,PR-3,PR-6,VR-6, VR-7,VR-10,PR-4,PR-5,VR-4,VR-5,VR-9,VR-1 & VR-3 Related to Inservice Testing Program,Second ten-year Interval for Perry Nuclear Power Plant PY-CEI-NRR-2424, Monthly Operating Rept for July 1999 for Perry Npp.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Perry Npp.With ML20210J3851999-07-28028 July 1999 Pnpp - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval PY-CEI-NRR-2416, Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With ML20196A1951999-06-17017 June 1999 Instrument Drift Analysis ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application PY-CEI-NRR-2409, Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2393, Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored1999-05-12012 May 1999 Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp PY-CEI-NRR-2399, Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at Pnpp & Use of Table IWB-3514 ML20206D7911999-04-23023 April 1999 Rev 6 to PDB-F0001, COLR for Pnpp Unit 1 Cycle 8,Reload 7 ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected PY-CEI-NRR-2389, Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20206D8461999-03-31031 March 1999 Rev 1 to J11-03371SRLR, Supplemental Reload Licensing Rept for Pnpp,Unit 1 Reload 7 Cycle 8 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 PY-CEI-NRR-2369, Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 9902271999-03-0303 March 1999 Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 990227 PY-CEI-NRR-2372, Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 PY-CEI-NRR-2356, Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2346, Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position PY-CEI-NRR-2335, Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2329, Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With ML20153B8221998-09-16016 September 1998 Safety Evaluation Accepting Changes to USAR Section 13.4.3, 17.2.1.3.2.2,17.2.1.3.2.2.3 & App 1A PY-CEI-NRR-2323, Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2313, Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2306, Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 1 ML20249A1891998-06-11011 June 1998 SER on Moderate Energy Line Pipe Break Criteria for Perry Nuclear Power Plant,Unit 1 & Requests Addl Info to Demonstrate That Plant & FSAR in Compliance W/Staff Position & GDC as Discussed in SER ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted PY-CEI-NRR-2282, Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D2051998-04-20020 April 1998 SER Authorizing Licensee to Use Code Case N-524 Until Such Time as Code Case Included in Future Rev of RG 1.147 PY-CEI-NRR-2277, Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216G3901998-03-11011 March 1998 SER on Proposed Merger Between Duquesne Light Co & Allegheny Power Sys,Inc ML20216J1401998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2258, Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 11998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 1 1999-09-30
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On February 27, 1987 at 1905, a failure of two control air solenoid valves r'endered Division I and 11 Diesel Generators (DG) inoperable. In addition at 0100 on February 28, 1987 while returning Division 1 Diesel Generator to standby status an unexpected autostart of the Diesel Generator Building ventilation System occurred. The two control air solenoids were discovered failed during the performance of Diesel Generator tasting. The valves were replaced and the D!esel Generators retested satisfactority by 0142 on February 28.
No cunctusive cause of f ailure f or the solenoid valves could be identified.
Both leaking solenoid valves had previously been identified for replacement due to leakage, with work requests initiated but not yet implemented. The reuse of the imeediate SG failures was the accelerated degraded condition of 1
the leaking solenoid valves. At discovery, the conditions were evaluated not to require immediate action, thus expeditious replacement did not occur.
To prevent recurrence, the administrative procedure for DG reports and recc,rds will be revised to require a review of DG work orders to ensure the 1
appropriate priority is assigned. Additionally, an evaluation will he performed to better define the service life for the air control solencid valves.
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On Tebruary 27,1987 at 1905, a f alture of two control air solenoid valves i rendered Division I and II Diesel Generators (DG) inoperable. In addition, at j 0100 on Tebruary 28, 1987 while returning Division I Diesel Generator to '
standby status after maintenancej an unexpected autostart of the Diesel Generator Building Ventilation System (DGBVS)(VJ) supply f an (TAN) for the Division I Diesel Generator occurred. At the time of these events, the plant was in Operational Condition 1 (power Operation) with reactor thermal power approximately 29% of rated. Reactor coolant temperature was approximately $10 degrees and reactor vessel (RPV) pressure was approximately 935 psig.
i On Tebruary 27, 1987 a special Test Instruction ($XI-0007) " Diesel Generator i Start on a Single Admission Valve-Division I" was being performed to l demonstrate the diesel generator ability to start on a single starting air l admission valve. During performance of the test the Senerator field did not l flash. The failure to flash was believed to be due to the special l configuration required by the SXI, and the Diesel Generator was still considered operable. Subsequently, the Division I Diesel Generator was stopped and restarted in accordance with the System Operating Instruction (S01)-R43 " Division I and 11 Diesel Generator System" to verify operability. 1 At 1708 the Division I Diesel Generator did not perform as expected by the SOI I
and was declared inoperable because the field did not flash until approximately 2 minutes af ter starting. Troubleshooting of the failure was initiated immediately. l i
l Technical Specification 3.8.1.1 action statement b. requires demonstration of operability of the remaining OPERABLE diesel generators by performing !
Surveillence Requirements 4.81.1.2 a.4 and 4.8.1.1.2.a.5 separately for each i diesel generator within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. At 1738 Surveillance Instruction (SVI)- !
R43-71318 " Diesel Generator Start and Load Division II" was initiated. The l Division II Diesel Generator also failed the SVI due to an overspeed trip and ,
subsequent failure of its field to flash. The Division II Diesel Generator l l
was declared inoperable at 1905.
Troubleshooting of the Division 1/11 DG identified the problem as excessive air leakage past the 3 way energized air solenoid valves (Delaval Part fT-586-061 Humphrey Products Model No. TOG 2El-3-10-35). The valves were replaced and survelliance testing initiated. At 2234 on February 27 and 0142 i on February 28 the Surveillances were completed on Division I and II Diesel respectively. Division I was declared operable at 0135 and Division II at .
0345 on Tebruary 28, 1987. The cause of the overspeed trip on Division II was/ !
due to an inproper adjustment of the mechanical governor / This incorrect /
adjustment was not considered as a factor in Operability and was subsequently !
readjusted on March 14, 1987. Additionally at 0100 while securing the Division I Diesel Generator following its surveillance run, a DGBVS (Division .
- 1) supply fan autostarted unexpectedly.
The cause of the DGBVS is believed to be a result of electrical noise within the tachometer circuitry. Substantial troubleshooting and investigation has been performed on previous similar events (see Licensee Event Reports86-019, l 86-031, 86-042 and 86-082).
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0 l0 mnva== emesma .mamemet==manwim No conclusive cause of f ailure for the solenoid valves could be identi led.
The volve manufacturer was contacted and responded that failures seldo.n occurred and that the most common f ailure developed when the poppets, made from BUNA-N, were subjected to an incompatible lubricant or excessive heat.
These valves are subjected to temperatures near the upper end of the qualified operating range and are continuously energised. These factors are believed to eventually cause degradation of the material within the valve resulting in air leakage and eventual f ailure. Both leaking solenoid valves had previously been identified for replaceteent due to leakage, with work requesta initiated but not yet implemented. In addition, several Surveillance Tests had been run successfully subsequent to identifying the leaking valves. The cause of the immediate diesel failures was the accelerated degraded condition of the leaking solenoid valves. At discovery, the conditions were evaluated not to l require immediate action, thus expeditious replacement did not occur.
l Subsequently it was determined that the control air pressure regulators whic supply air to these solenoid valves were malfunctioning and may have I contributed to the diesel failure (Delaval Part (F-579-061; Bellofram Model No. 241-960-069 Type 50). \61~71 l The Standby Diesel Generator System provides an independent source of AC power to the Division 1, 2, 3 Class 1E buses in the event of loss of the redundant offsite power supply. During the time period Class 1E Power was available from at least two physically independent circuits from the transmission network to the onsite electric distribution system. AdditionaH y, the High Pressure Core Spray diesel generator and system were verified operable during this timeframe. However, the event is considered safety significant because the loss of Division I and II backup power supplies results in conditions outside of the design basis under certain accident scenarios. No previous similar events were identified.
The following corrective actions have been or will be completed to prevent recurrence:
- 1. Those diesel generators air control solenoid valves which have been in service and continuously energized for over 6 months will be replaced.
- 2. Plant Administrative Procedure (PAP)-1705 " Diesel Generator Reports and Records" will be revised to require a periodic review of diesel generator work order priorities with the Work Review Committee to ensure the appropriate work priority is assigned.
- 3. An engineering evaluation will be performed to establish a better defined service life for the air control solenoid valves.
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- 4. A design review will be conducted to minimise the application of
- ontinuously energised solenoid valves in the diesel generator control air panel and to evaluate replacement of solenoid valves containing BUNA-N material with Viton asterial.
- 5. An engineering design change will be implemented to upgrade the control techometer.
- 6. The f ailed control air solenoid valves will be returned to the vendor for performance of failure analysis.
Energy Industry Identification Systems Codes are identified in the text as [XX).
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""* 2 ** March 27, 1987 I p PY-CE!/NRt4620 L j
in U.S. Nuclear Reguistory Come(solon
, Document Control Desk i Weshington, D.C. 20555
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Perry Nuclear Power Plant l Docket No. 50-440 l
Ltte'87-009-00 and 87-010-00 j i
Dear Stra Enclosed are Licensee Event Reporte 87409-00 and 8741040 !
for the Perry Nuclear Power Plant, j
- s: l Very truly yours, . t (7
.Murray R. Edele n# .- l
' senior Vice ' President ]
j . Nuclear Croup
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Enclosure:
Leas 87-009-00 and 87-010-00 f ~
1
.; cc 'raul Leech ,
K. Connaughton f
' U.S. Nuclear Regulatory Coenlosion i j 799 Roosevelt Road !
f Clen Ellyn, IL. 60137 l l
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