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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18011A5401994-08-10010 August 1994 LER 94-017-00:on 940711,automatic Isolation of RHR Sys Shutdown Cooling Suction Outboard Containment Isolation Valve Occurred Due to Inadequate Work Order.Work Order Process for I&C Work Orders Will Be reviewed.W/940810 Ltr ML20046C5721993-08-0606 August 1993 LER 93-015-00:on 930709,unexpected RRP Fast to Slow Speed Downshift Occurred Due to Failure of Both RRP Suction Temp Rtd.Replaced & Returned RTD to Mfg for Failure Analysis. W/930806 Ltr ML20046B7811993-08-0202 August 1993 LER 93-014-00:on 930703,TS 3.0.3 Entered Due to Failure of Racs Power Supply.Replaced 5 Volt Power Supply in Racs cabinet.W/930802 Ltr ML20045G7201993-07-0808 July 1993 LER 93-013-00:on 930608,control Room HVAC Sys Train a Supply Fan Tripped on Overcurrent,Resulting in Both Sys Trains Being Unavailable.Caused by Motor Winding Insulation Failure.Motor Repaired by mfg.W/930708 Ltr ML20045G2171993-07-0707 July 1993 LER 93-012-00:on 930607,noted That HPCS Initiation Signal Resulted in Auto Start of Div 3 DG & ESW Sys.Caused by Failure of Div 3 Reserve Battery Charger.Procedures Used for Insp & Maint of Battery Being modified.W/930707 Ltr ML20044F2161993-05-19019 May 1993 LER 93-011-00:on 930419,identified That Excessive Strainer Differential Pressure Across RHR Suction Strainers Could Have Compromised Long Term Cooling During LOCA Operation. Caused by Inadequate Program requirements.W/930519 Ltr ML20044B6771993-02-22022 February 1993 LER 93-004-00:on 930121,MOV Testing of Main Steam Line Drain & Bypass Outboard Isolation Valve Indicated That Thrust Less than Design Thrust to Close Valve Under Accident Conditions. Review,Per GL 89-10 in progress.W/930222 Ltr ML20029B6431991-03-0808 March 1991 LER 91-007-00:on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper value.W/910308 Ltr ML20029B0971991-03-0101 March 1991 LER 91-006-00:on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being revised.W/910301 Ltr ML20029A6451991-02-22022 February 1991 LER 91-005-00:on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel error.W/910222 Ltr ML20029A3321991-02-15015 February 1991 LER 91-004-00:on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified. W/910215 Ltr ML20028H7521991-01-25025 January 1991 LER 90-041-00:between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo issued.W/910125 Ltr ML20024F7421990-12-14014 December 1990 LER 90-033-00:on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N ML20024F7411990-12-14014 December 1990 LER 90-032-00:on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders ML20028G9181990-09-28028 September 1990 LER 90-020-00:on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being revised.W/900928 Ltr ML20044B1021990-07-13013 July 1990 LER 90-013-00:on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel counseled.W/900713 Ltr ML20043H4801990-06-20020 June 1990 LER 90-011-00:on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction revised.W/900620 Ltr ML20043H5251990-06-20020 June 1990 LER 90-010-00:on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage monitored.W/900620 Ltr ML20043H3841990-06-18018 June 1990 LER 90-009-00:on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut replaced.W/900618 Ltr ML20043E5711990-06-0808 June 1990 LER 89-030-01:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Failure of Two Control Rods Caused by Improper Seat Matl in Associated Scram Pilot Solenoid Valves.Instructions revised.W/900608 Ltr ML20043A7801990-05-18018 May 1990 LER 90-007-00:on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced ML20043A8451990-05-18018 May 1990 LER 90-008-00:on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced ML20042G7731990-05-11011 May 1990 LER 90-006-00:on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel retrained.W/900511 Ltr ML20012D8151990-03-24024 March 1990 LER 90-003-00:on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement implemented.W/900323 Ltr ML20011E1861990-02-0202 February 1990 LER 90-001-00:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised ML20011E1871990-02-0202 February 1990 LER 90-002-00:on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised ML19354E0961990-01-19019 January 1990 LER 89-032-00:on 891228 & 900105,HPCS Sys Declared Inoperable Due to Inoperability of Div 3 Battery.Caused by Low Pilot Cell Voltage,Cell W/Slow Electrolyte Leak & Blown Power Fuse.Fuse & Hydromotor Pump replaced.W/900119 Ltr ML20005E6851990-01-0505 January 1990 LER 89-031-00:on 891206,08 & 15,RWCU Sys Isolations Occurred.Caused by Design Deficiency & Deficiency in Leak Detection/Differential Flow Circuitry Setpoint &/Or Time Delay.Leak Detection Thermocouples relocated.W/900105 Ltr ML20005E0821989-12-26026 December 1989 LER 89-030-00:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Caused by Failure to Return Scram Pilot Valves Used for Rods to Mfg After Recall. Surveillance Instruction revised.W/891226 Ltr ML19354D5991989-12-17017 December 1989 LER 89-029-00:on 891117,heater Bay/Turbine Bldg Vent Gaseous Effluent Particulate & Iodine Samples Not Continuously Collected as Required by Tech Spec 3.3.7.10.Caused by Procedure Deficiency.Procedure revised.W/891217 Ltr ML19325E5901989-11-0303 November 1989 LER 89-028-00:on 891008,concluded That Operation of Fuel Pool Cooling & Cleanup Sys to Upper Containment Pools Caused Containment Vacuum Breaker Actuations.Caused by Unrecognized Sys Interaction.Operating Instruction revised.W/891103 Ltr ML19324B1241989-10-27027 October 1989 LER 89-024-01:on 890723,entry Into Operational Condition 2 Completed W/Suppression Pool Makeup Sys Inoperable & on 890725,vent Valve on Ref Leg Found Open & Uncapped.Caused by Personnel Error.Personnel counseled.W/891027 Ltr ML19325D5121989-10-20020 October 1989 LER 89-027-00:on 890925,loss of Control Power to Emergency Svc Water Sys Pump Discharge Valve a Rendered Sys Inoperable.Caused by Personnel Error Re Jumper Placement. Involved Technicians counseled.W/891020 Ltr ML19325D1581989-10-13013 October 1989 LER 88-025-01:on 880618,reactor Protection Sys (RPS) Bus Inadvertently Deenergized,Resulting in Full RPS Actuation. Caused by Personnel Error W/Contributing Factor of Poor Human Factors Design.Info Tag Installed on Power Switch ML19325D1591989-10-13013 October 1989 LER 89-026-00:on 890913,reactor Thermal Power Level Exceeded That Specified in OL Due to Unexpected Recirculation Sys Flow Control Transient.Caused by Component Failure.Failed Isolation Solenoid Valve Replaced ML19325D9331987-03-27027 March 1987 LER 87-010-00:on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised ML19325C1171987-03-27027 March 1987 LER 87-009-00:on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 revised.W/870327 Ltr 1994-08-10
[Table view] Category:RO)
MONTHYEARML18011A5401994-08-10010 August 1994 LER 94-017-00:on 940711,automatic Isolation of RHR Sys Shutdown Cooling Suction Outboard Containment Isolation Valve Occurred Due to Inadequate Work Order.Work Order Process for I&C Work Orders Will Be reviewed.W/940810 Ltr ML20046C5721993-08-0606 August 1993 LER 93-015-00:on 930709,unexpected RRP Fast to Slow Speed Downshift Occurred Due to Failure of Both RRP Suction Temp Rtd.Replaced & Returned RTD to Mfg for Failure Analysis. W/930806 Ltr ML20046B7811993-08-0202 August 1993 LER 93-014-00:on 930703,TS 3.0.3 Entered Due to Failure of Racs Power Supply.Replaced 5 Volt Power Supply in Racs cabinet.W/930802 Ltr ML20045G7201993-07-0808 July 1993 LER 93-013-00:on 930608,control Room HVAC Sys Train a Supply Fan Tripped on Overcurrent,Resulting in Both Sys Trains Being Unavailable.Caused by Motor Winding Insulation Failure.Motor Repaired by mfg.W/930708 Ltr ML20045G2171993-07-0707 July 1993 LER 93-012-00:on 930607,noted That HPCS Initiation Signal Resulted in Auto Start of Div 3 DG & ESW Sys.Caused by Failure of Div 3 Reserve Battery Charger.Procedures Used for Insp & Maint of Battery Being modified.W/930707 Ltr ML20044F2161993-05-19019 May 1993 LER 93-011-00:on 930419,identified That Excessive Strainer Differential Pressure Across RHR Suction Strainers Could Have Compromised Long Term Cooling During LOCA Operation. Caused by Inadequate Program requirements.W/930519 Ltr ML20044B6771993-02-22022 February 1993 LER 93-004-00:on 930121,MOV Testing of Main Steam Line Drain & Bypass Outboard Isolation Valve Indicated That Thrust Less than Design Thrust to Close Valve Under Accident Conditions. Review,Per GL 89-10 in progress.W/930222 Ltr ML20029B6431991-03-0808 March 1991 LER 91-007-00:on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper value.W/910308 Ltr ML20029B0971991-03-0101 March 1991 LER 91-006-00:on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being revised.W/910301 Ltr ML20029A6451991-02-22022 February 1991 LER 91-005-00:on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel error.W/910222 Ltr ML20029A3321991-02-15015 February 1991 LER 91-004-00:on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified. W/910215 Ltr ML20028H7521991-01-25025 January 1991 LER 90-041-00:between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo issued.W/910125 Ltr ML20024F7421990-12-14014 December 1990 LER 90-033-00:on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N ML20024F7411990-12-14014 December 1990 LER 90-032-00:on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders ML20028G9181990-09-28028 September 1990 LER 90-020-00:on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being revised.W/900928 Ltr ML20044B1021990-07-13013 July 1990 LER 90-013-00:on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel counseled.W/900713 Ltr ML20043H4801990-06-20020 June 1990 LER 90-011-00:on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction revised.W/900620 Ltr ML20043H5251990-06-20020 June 1990 LER 90-010-00:on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage monitored.W/900620 Ltr ML20043H3841990-06-18018 June 1990 LER 90-009-00:on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut replaced.W/900618 Ltr ML20043E5711990-06-0808 June 1990 LER 89-030-01:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Failure of Two Control Rods Caused by Improper Seat Matl in Associated Scram Pilot Solenoid Valves.Instructions revised.W/900608 Ltr ML20043A7801990-05-18018 May 1990 LER 90-007-00:on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced ML20043A8451990-05-18018 May 1990 LER 90-008-00:on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced ML20042G7731990-05-11011 May 1990 LER 90-006-00:on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel retrained.W/900511 Ltr ML20012D8151990-03-24024 March 1990 LER 90-003-00:on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement implemented.W/900323 Ltr ML20011E1861990-02-0202 February 1990 LER 90-001-00:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised ML20011E1871990-02-0202 February 1990 LER 90-002-00:on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised ML19354E0961990-01-19019 January 1990 LER 89-032-00:on 891228 & 900105,HPCS Sys Declared Inoperable Due to Inoperability of Div 3 Battery.Caused by Low Pilot Cell Voltage,Cell W/Slow Electrolyte Leak & Blown Power Fuse.Fuse & Hydromotor Pump replaced.W/900119 Ltr ML20005E6851990-01-0505 January 1990 LER 89-031-00:on 891206,08 & 15,RWCU Sys Isolations Occurred.Caused by Design Deficiency & Deficiency in Leak Detection/Differential Flow Circuitry Setpoint &/Or Time Delay.Leak Detection Thermocouples relocated.W/900105 Ltr ML20005E0821989-12-26026 December 1989 LER 89-030-00:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Caused by Failure to Return Scram Pilot Valves Used for Rods to Mfg After Recall. Surveillance Instruction revised.W/891226 Ltr ML19354D5991989-12-17017 December 1989 LER 89-029-00:on 891117,heater Bay/Turbine Bldg Vent Gaseous Effluent Particulate & Iodine Samples Not Continuously Collected as Required by Tech Spec 3.3.7.10.Caused by Procedure Deficiency.Procedure revised.W/891217 Ltr ML19325E5901989-11-0303 November 1989 LER 89-028-00:on 891008,concluded That Operation of Fuel Pool Cooling & Cleanup Sys to Upper Containment Pools Caused Containment Vacuum Breaker Actuations.Caused by Unrecognized Sys Interaction.Operating Instruction revised.W/891103 Ltr ML19324B1241989-10-27027 October 1989 LER 89-024-01:on 890723,entry Into Operational Condition 2 Completed W/Suppression Pool Makeup Sys Inoperable & on 890725,vent Valve on Ref Leg Found Open & Uncapped.Caused by Personnel Error.Personnel counseled.W/891027 Ltr ML19325D5121989-10-20020 October 1989 LER 89-027-00:on 890925,loss of Control Power to Emergency Svc Water Sys Pump Discharge Valve a Rendered Sys Inoperable.Caused by Personnel Error Re Jumper Placement. Involved Technicians counseled.W/891020 Ltr ML19325D1581989-10-13013 October 1989 LER 88-025-01:on 880618,reactor Protection Sys (RPS) Bus Inadvertently Deenergized,Resulting in Full RPS Actuation. Caused by Personnel Error W/Contributing Factor of Poor Human Factors Design.Info Tag Installed on Power Switch ML19325D1591989-10-13013 October 1989 LER 89-026-00:on 890913,reactor Thermal Power Level Exceeded That Specified in OL Due to Unexpected Recirculation Sys Flow Control Transient.Caused by Component Failure.Failed Isolation Solenoid Valve Replaced ML19325D9331987-03-27027 March 1987 LER 87-010-00:on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised ML19325C1171987-03-27027 March 1987 LER 87-009-00:on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 revised.W/870327 Ltr 1994-08-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in Pnpp to Ceico PY-CEI-NRR-2437, Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With PY-CEI-NRR-2429, Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With NUREG-1482, SE Approving Licensee Relief Requets PR-2,PR-3,PR-6,VR-6, VR-7,VR-10,PR-4,PR-5,VR-4,VR-5,VR-9,VR-1 & VR-3 Related to Inservice Testing Program,Second ten-year Interval for Perry Nuclear Power Plant1999-08-0909 August 1999 SE Approving Licensee Relief Requets PR-2,PR-3,PR-6,VR-6, VR-7,VR-10,PR-4,PR-5,VR-4,VR-5,VR-9,VR-1 & VR-3 Related to Inservice Testing Program,Second ten-year Interval for Perry Nuclear Power Plant PY-CEI-NRR-2424, Monthly Operating Rept for July 1999 for Perry Npp.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Perry Npp.With ML20210J3851999-07-28028 July 1999 Pnpp - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval PY-CEI-NRR-2416, Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With ML20196A1951999-06-17017 June 1999 Instrument Drift Analysis ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application PY-CEI-NRR-2409, Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2393, Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored1999-05-12012 May 1999 Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp PY-CEI-NRR-2399, Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at Pnpp & Use of Table IWB-3514 ML20206D7911999-04-23023 April 1999 Rev 6 to PDB-F0001, COLR for Pnpp Unit 1 Cycle 8,Reload 7 ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected PY-CEI-NRR-2389, Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20206D8461999-03-31031 March 1999 Rev 1 to J11-03371SRLR, Supplemental Reload Licensing Rept for Pnpp,Unit 1 Reload 7 Cycle 8 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 PY-CEI-NRR-2369, Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 9902271999-03-0303 March 1999 Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 990227 PY-CEI-NRR-2372, Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 PY-CEI-NRR-2356, Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2346, Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position PY-CEI-NRR-2335, Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2329, Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With ML20153B8221998-09-16016 September 1998 Safety Evaluation Accepting Changes to USAR Section 13.4.3, 17.2.1.3.2.2,17.2.1.3.2.2.3 & App 1A PY-CEI-NRR-2323, Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2313, Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2306, Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 1 ML20249A1891998-06-11011 June 1998 SER on Moderate Energy Line Pipe Break Criteria for Perry Nuclear Power Plant,Unit 1 & Requests Addl Info to Demonstrate That Plant & FSAR in Compliance W/Staff Position & GDC as Discussed in SER ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted PY-CEI-NRR-2282, Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D2051998-04-20020 April 1998 SER Authorizing Licensee to Use Code Case N-524 Until Such Time as Code Case Included in Future Rev of RG 1.147 PY-CEI-NRR-2277, Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216G3901998-03-11011 March 1998 SER on Proposed Merger Between Duquesne Light Co & Allegheny Power Sys,Inc ML20216J1401998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2258, Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 11998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 1 1999-09-30
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G 8' THE CLEVELAND ELECTRI P.O. ROX 97 3 PERMY, OHIO 44041 5 TELEPHONE (216) 2694737 FMOW CLEVELAND: 479 1200 3
5 ADDMEsS 10 CENTER ROAD TELtX: 2416s0 ANsWEMBACet: CCIPRYO j i
Al KAplan Serving The Best locatica in the Nation PERRY NUCLEAR POWER PLANT !
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94WLI684 GNNf' November 3, 1989 !
PY-CE1/NRR-1089 L l U.S. Nuclear Regulatory Commission Document Control Desk j Washington, D. C. 20555 ;
Perry Nuclear Power Plant l Docket No. 50-440 j LER 89-028 Gentlemen Enclosed is Licensee Event Report 89-028 for the Perry Nuclear Power Plant.
Note that per Section 6.2.1.1 4.2 of the USAR: " Vacuum breaker opening for i other than the inadvertent containment spray actuation scenarios presented in this section is considered a non-EST actuation. Conditions which result in .
changes to the containment atmosphere, (such as containment venting and cooling, suppression pool level changes and weather changes), and subsequently ,
result in containment vacuum breaker operation, are considered normal and l expectsd, and are bounded by the limiting inadvertent containment spray situation." However, based upon the unexpected operational impact on the ;
. Containment Vacuum Relief System, this event is being reported as an unexpected Engineered Safety Feature actuation.
Very truly yours, kA Al Kaplan h !
k Vice President t Nuclear Group l AKinjc Enclosure LER 89-028 .
cc T. Colburn >
P. Hiland '
U.S. NRC Region 111 i g 8911000044 891103 PDR ADOCK0500gO S
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- ' Operation of Fuel Pool Cooling and Cleanup System to the Upper Containment Pools Causes Air Evacuation and Containment Vacuum Breaker Actuations eve =1 oats e ten mun.en m mecoet pare eri etwen enciutin swvo6voo e esoest se Dat vtam vlam O'(6'y , 6 '7M upse t s. oav vtAh 86Det.howt0 DOCattaspesetaw o 15 010 l 0 l l l ll0 ll l
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.ast .Ct rating Instruction was revised to provide a caution that FPCC Upper ]
Containment Pools operation with a low surge tank level can cause containment '
vacuue breaker actuation. Additionally, actions were initiated to revise FPCC i
Surge 'iank Low Level Alarm setpoints. As part nf the established l requalitication training program all plant licensed operators will be l l instructei on the lessons learned from this event.
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"'ni Perry Nuclear Power Plant. Unit 1 o js j o l o j o l 4l 4l 0 8l9 - q 2l 8 -
0l 0 0l2 or 0l3 m, w . cs m.mm i On October 8, 1989 it was concluded that operation of the Fuel Pool Cooling l and Cleanup System (FPCC) [DA) to the Upper Containment Pools (UCP) caused i Containment Vacuum Relief System [BF) vacuum breaker [VACB) actuations that 1 occurred between September 19 and October 8, 1989. Flow from the UCP to the FPCC Surge Tank [TK) was secured for additional testing. Tne plant was in 1 Operational Condition 1 (Power Operation) at approximately 100 percent of l rated thermal power. The Reactor Pressure Vessel [RPV) was at saturated 1 conditions at approximately 1000 psig.
On October 2, 1989 it was noted that containment vacuum breakers cycled , !
repeatedly between September 19 and September 30, 1989. Plant Operators I postulated that containment vacuum breaker cycling might be related to )
containment lower air lock [AL) maintenance. An investigation was initiated j to determine if lower containment air lock inner door maintenance, during the 1 September 19 thru 30 time frame, contributed to the containment vacuum breaker cycling problem. The lower containment air lock was tested with helium to check for leakage from the air lock to the annulus. No leakage was detected. l As no correlation was found between the maintenance and vacuum breaker t actuation, the investigation continued to investigate other potential causes.
On October 6, 1989 at 0414 a containment vacuum breaker opened for approximately 5 minutes. The lower containment airlock was checked and the inner door was verified shut and sealed. At 0700 another containment vacuum breaker alarmed as if open, but no indicating light came on indicating the vacuum breaker was open. Action was initiated to correct the "open indication" problem. At 0945 an Investigation Team was formed to determine the cause of containment vacuum breaker cycling. Between October 6 and Occober 8, 1989, containment vacuum breakers cycled approximately 49 times.
I
- While performing a plant tour on October 8, the Shift Supervisor noticed an i
unusual sound coming from the return line from the UCP to the FPCC Surge Tank.
l At 0957 the flow from the UCP to the FPCC Surge Tank was isolated.
l Containinent pressure increased and the containment vacuum breakers stopped l cycling.
l l
On October 9, 1989 FPCC flow to the UCP was restored at the request of the Investigation Team. A smoke tester was used to verify that air was being drawn into the UCP Skimmers [SKR). It was also determined that air '
entrainment in the FPCC UCP Return Line was dependent upon Surge Tank level.
When Surge Tank level was decreased beyond a specific value, air entrainment I started. Further testing from October 9 thru October 12 determined l quantitative relationships between FPCC Flow to UCP, FPCC Surge Tank Level, I
and air entrainment in the FPCC UCP Return Line.
The root cause of the containment vacuum breaker actuations was a previously unrecognized system interaction. FPCC System Operating Instruction (S01-G41(FPCC)) allowed too wide of an operational band for flow to the UCP and too wide of an operational band for Surge Tank Level. This allowed FPCC
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0 l0 0l3 - or 0l3 l ru, u-. m nc m mn enm to be operated in a manner which caused air to be entrained in the FPCC UCP !
Return Line. Removal of this air irom containment caused a decreasing pressure which caused containment vacuum breaker actuation.
The Containment Vacuum Relief System is designed to. prevent any pressure differential acting inward on the Containment Vessel from exceeding the design value of 0.8 paid in the event of an inadvertent Containment Spray Initiation.
This is described in Section 6.2.1.1.4.2 of the USAR. " Vacuum breaker opening for other than the inadvertent containment spray actuation scenarios presented j in this section is considered a non-ESF actuation. Conditions which result in changes to the containment atmosphere, (such as containment venting and i cooling, suppression pool level changes and weather changes), and subsequently result in containment vacuum breaker operation, are considered normal and expected, and are bounded by the limiting inadvertent containment spray situations." However, based upon the operational impact on the Containment Vacuum Relief System, this event is being reported as an unexpected Engineered :
Safety Feature actuation.
During this event the vacuum breakers opened as designed and their safety function was not impaired. There were also two additional redundant vacuum -
breakers available. The FPCC System is designed to remove decay heat >
generated by spent fuel stored in the spent fuel storage pool. In addition, this system maintains the purity, clarity, and level of water in the UCP and the fuel storage pools in the Fuel Handling Building. In the event of a Loss of Coolant Accident, FPCC would have been isolated from containment and air entrainment would have stopped. ;
Although containment atmosphere was being moved to the Intermediate Building by this event, the air was monitored by the Intermediate Building Exhaust ,
Radiation Monitor before being released to atmospaere through the Unit 1 plant vent. No abnormal effluent release rates were present during this event.
Both FPCC and the Containment Vacuum Relief System were operated in accordance with their designs and all operator actions taken were in accordance with approved procedures. Consequently, this event had no safety significance. No previous similar events were identified.
In order to prevent recurrence, S01-C41 (FPCC) was revised to restrict Surge Tank level and flow to dCP to prevent entraining air in the return line. The Containment Vacuum Relief System Operating Instruction was revised to state that FPCC UCP operation with a low Surge Tank level can cause containment vacuum breaker actuation. Also actions were initiated to raise FPCC Surge Tank Low Level Alarm Instrumentation setpoints to enhance maintaining FPCC Surge Tank level within its restricted operational band. As part of the established requalification training program all plant licensed operators will be instructed on the lessons learned from this event.
Energy Industry Identification System Codes are identified in the text as
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