:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised| ML20011E186 |
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| Site: |
Perry  |
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| Issue date: |
02/02/1990 |
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| From: |
Hegrat H CLEVELAND ELECTRIC ILLUMINATING CO. |
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| To: |
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| Shared Package |
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| ML20011E185 |
List: |
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| References |
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| LER-90-001, LER-90-1, NUDOCS 9002090006 |
| Download: ML20011E186 (3) |
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-.,, n ei On January 7, 1990, at 1132, a reactor scram occurred due to a reactor water level of less than Level 3 (+177.7 inches above the top of active fuel). The low water level occurred after an improper transfer of 480 volt AC power supplies resulted in a comentary power interruption to the feudwater control circuitry and a total loss of feedwater flow.
The cause of this event was Personnel Error, inattention to detail. An operator Inadvertently pulled the wrong fuses, which resulted in the 480 volt bus being l
deenergized when the bus transfer was made.
t To prevent recurrence, the operator has been counseled on the importance of paying close attention to detail when operating plant equipment. The system operating instruction was revised and supplemental training on live-bus transfers was developed.
Investigation is being performed into possible design changes to increase j
Feedwater Control System availability in the event of loss of non-essential busses.
As part of the established requalification training program, all plant licensed operators will be instructed on the lessons learned from this event.
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l Submittal of this report also meets the requirements for Technical Specification 3.5.1 Action g. which requires a Special Report following any Emergency Core Cooling System actuation and injection into the Reactor Coolant System.
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oNe u-muu nn On January 7, 1990, at 1132, a reactor scram occurred due to reactor pressure vessel [RPV) water level less than Level 3 (+177.7 inches above top of active fuel (TAF)). Prior to the event, the plant was in Operational Condition 1 (Power Operation) at approximately 100 percent of rated thermal power with the reactor pressure vessel at saturated conditions at approximately 1025 psig.
On January 7, 1990, at approximately 1100, a non-essential 480 volt bus was being transferred to its alternate power supply, in accordance with System Operating Instruction (S01-R10) " Plant Electrical System," in preparation for scheduled maintenance. Operators inadvertently removed the wrong control power fuses and upon completion of the transfer, bus F-1-C became completely deenergized.
The resulting power interruption to feedwater control circuitry caused a complete loss of feedwater flow as well as a shift of Reactor Recirculation System [AD) pumps to slow speed.
Both Turbine Driven Feedwater Pumps (TDFP) went to minimum speed. The rapid decrease in reactor water level resulted in a reactor scram at Level 3, at 1132, and Reactor Core Isolation Cooling (RCIC)[BN) and High Pressure Core Spray (HPCS) [BG) initiation at Level 2 (+129.8 inches above TAF) approximately 5 seconds later. The RCIC initiation signal caused the Main Turbine and both TDFPs to trip which resulted in the Motor Driven Feedwater Pump (MDFP) auto-starting at minimum flow. Minimum RPV level reached during this event was approximately +78 inches above TAF. As a result of the injections f rom the HPCS and RCIC systems RPV level was restored to normal operating range at approximately 1136. At 1143, an " Unusual Event" was declared due to HPCS initiation. All off-normal and plant emergency instructions were appropriately implemented. At 1138. HPCS was shutdown to standby readiness and the MDFP was used to control RPV level. The RCIC cystem isolated, at 1209, due to equipment room high differential temperature with no resultant effect on RPV water level due to MDFP availability (refer to LER 90-002). At 1216, bus F-1-C was reenergized. The " Unusual Event" was terminated at 1228.
This was the fifth HPCS injection cycle to da te, including those performed during startup testing activities, and the injection nozzle usage f actor is currently less than 0.70.
The post scram evaluation was completed, a plan to test the RCIC system differential temperature instrumentation under operating conditions was developed, and the plant entered Operational Condition 2 (Startup) on January 15, 1990, at 2359.
The cause of this event was Personnel Error, inattention to detail. S01-R10 directs control power fuses to be pulled to disable a tie breaker interlock allowing both the normal and alternate power supply to be tied to bus F-1-C at the same time, permitting bus power to be transferred without interruption. An operator pulled the wrong fuses despite the fuses being clearly labeled and the fuses being clearly identified by the procedure. Because the wrong fuses were
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pulled, the tie breaker tripped immediately upon closure, removing the alternate power supply f rom the bus just before the operator disconnected the normal power supply.
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=ac e mmwnn A loss of feedwater flow at 100 percent of rated power has been analyzed as discussed in Chapter 15 (Section 15.2.7) of the Perry Updated Safety Analysis Report (USAR). The analyzed transient results in a reactor scram at Level 3, and the initiation of HPCS and RCIC at level 2.
All plant conditions were within the envelope of the USAR analysis, and all plant Technical Specification related systems responded as designed to maintain the plant in a safe condition with the exception of the RCIC isolation.
The RCIC System Isolation is separately addressed in LER 90-002.
Based on the performance of plant equipment in response to the previously analyzed transient, this event is not considered to be safety significant. A similae event has been previously documented by LER 88-012 in which the Reactor scrammed from 100 percent of rated power due to a loss of feedwater caused by personnel error and procedural inadequacy. The corrective actions, which included counseling the operators involved, operator training on the sequence of events, and revision of the applicable system operating instruction, could notg have prevented the January 7, 1990 event.
To prevent recurrence, the operator has been counseled on the importance of paying close attention to detail when operating plant equipment. Also, S01-R10 was revised to have operators ensure that tie breakers stay energized before removing power during live bus transfers. Additionally, a training video tape has been made on live-bus transfers. All on-shift Electrical Operator personnel are being trained to this tape and it was incorporated into the Electrical Operator training program. Also investigation is being performed into possible design changes to increase Feedwater Control system availability in the c. vent of loss of non-essential busses. As part of the established requalification training program, all plant licensed operators will be instructed on the lessons learned from this event.
Submittal of this report also meets the requirments for Technical Specification 3.5.1 Action g, which requires a Special Report following any Emergency Core Coolng System actuation and injection into the Reactor Coolant System.
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Energy Industry Identification System Codes are identified in the text as [XX].
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| 05000440/LER-1990-001, :on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised |
- on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised
| | | 05000440/LER-1990-002, :on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised |
- on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised
| | | 05000440/LER-1990-003, :on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement Implemented |
- on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement Implemented
| | | 05000440/LER-1990-004, :on 900329,determined That 12 Snubbers Not Inspected on 900302 & Two Snubbers Not Inspected on 900327, Per Tech Spec 4.7.4.Caused by Program Inadequacy.Procedures Changed & Snubber Program Evaluated |
- on 900329,determined That 12 Snubbers Not Inspected on 900302 & Two Snubbers Not Inspected on 900327, Per Tech Spec 4.7.4.Caused by Program Inadequacy.Procedures Changed & Snubber Program Evaluated
| | | 05000440/LER-1990-005, :on 900405,HPCS Declared Inoperable Due to Fuel Oil Sediment Exceeding Tech Spec Limits.Caused by Fuel Oil & Storage Tank Degradation,Due to Contaminant in Biocide Additive.Contaminated Biocide Additive Removed |
- on 900405,HPCS Declared Inoperable Due to Fuel Oil Sediment Exceeding Tech Spec Limits.Caused by Fuel Oil & Storage Tank Degradation,Due to Contaminant in Biocide Additive.Contaminated Biocide Additive Removed
| | | 05000440/LER-1990-006, :on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel Retrained |
- on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel Retrained
| | | 05000440/LER-1990-007, :on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced |
- on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced
| | | 05000440/LER-1990-008, :on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced |
- on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced
| | | 05000440/LER-1990-009, :on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut Replaced |
- on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut Replaced
| | | 05000440/LER-1990-010, :on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage Monitored |
- on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage Monitored
| | | 05000440/LER-1990-011, :on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction Revised |
- on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction Revised
| | | 05000440/LER-1990-013, :on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel Counseled |
- on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel Counseled
| | | 05000440/LER-1990-014, :on 900621,trains of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode of Operation.Caused by Multiple Personnel Errors.Personnel Reinstructed Re Using Appropriate Drawings for Application |
- on 900621,trains of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode of Operation.Caused by Multiple Personnel Errors.Personnel Reinstructed Re Using Appropriate Drawings for Application
| | | 05000440/LER-1990-016, :on 900710,condensate Storage Tank Level Low Actuation Instrumentation Failure Resulted in HPCS Shift. Caused by Component Failure.Rosemount Master Trip Unit Replaced |
- on 900710,condensate Storage Tank Level Low Actuation Instrumentation Failure Resulted in HPCS Shift. Caused by Component Failure.Rosemount Master Trip Unit Replaced
| | | 05000440/LER-1990-017, :on 900814,thermal Power Exceeded Authorized Limits Due to Feedwater Heater Level Control Failure.Caused by Component Failure W/Contributing Procedural Deficiency. Off Normal Instruction Enhanced |
- on 900814,thermal Power Exceeded Authorized Limits Due to Feedwater Heater Level Control Failure.Caused by Component Failure W/Contributing Procedural Deficiency. Off Normal Instruction Enhanced
| | | 05000440/LER-1990-018, :on 900817,determined That Containment Average Temp/Relative Humidity Not Verified within Tech Spec Figure 3.6.5.2-1 Limits.Caused by Programmatic Weakness in Use of Process Computer Sys Info to Determine Tech Spec Compliance |
- on 900817,determined That Containment Average Temp/Relative Humidity Not Verified within Tech Spec Figure 3.6.5.2-1 Limits.Caused by Programmatic Weakness in Use of Process Computer Sys Info to Determine Tech Spec Compliance
| | | 05000440/LER-1990-019, On 900817 & 0901,liquid Radiological Effluent Releases Performed W/Radioactive Effluent Monitoring Instrumentation Inoperable W/O Completing Independent,Per Tech Spec 3.3.7.9.On 900820,channel Improperly Calibr | On 900817 & 0901,liquid Radiological Effluent Releases Performed W/Radioactive Effluent Monitoring Instrumentation Inoperable W/O Completing Independent,Per Tech Spec 3.3.7.9.On 900820,channel Improperly Calibr | | | 05000440/LER-1990-020, :on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being Revised |
- on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being Revised
| | | 05000440/LER-1990-021, :on 900907,MSIV Failed to Close Following Successful Slow Closures |
- on 900907,MSIV Failed to Close Following Successful Slow Closures
| | | 05000440/LER-1990-023, :on 900907,reactor Protection Sys Bus Deenergization & Shutdown Cooling Isolation Occurred During Surveillance Testing Due to Personnel Error.Personnel Instructed on Ramifications of Inattention During Tests |
- on 900907,reactor Protection Sys Bus Deenergization & Shutdown Cooling Isolation Occurred During Surveillance Testing Due to Personnel Error.Personnel Instructed on Ramifications of Inattention During Tests
| | | 05000440/LER-1990-024, :on 900909,determined That Failure to Properly Control Surveillance Testing Resulted in Suppression Pool Instrumentation Being Out of Svc.Caused by Procedural Deficiency.Licensed Operators Trained to Lessons Learned |
- on 900909,determined That Failure to Properly Control Surveillance Testing Resulted in Suppression Pool Instrumentation Being Out of Svc.Caused by Procedural Deficiency.Licensed Operators Trained to Lessons Learned
| | | 05000440/LER-1990-025-01, Responds to NRC Ltr Re Violations Noted in Insp Rept 50-440/90-20 on 900920-1116.Corective Actions:Valve Repair & Rebuilding,Per LER 90-025-01,dtd 901123 & Restoration of Six MSIV That Required Disassembly to Original Condit | Responds to NRC Ltr Re Violations Noted in Insp Rept 50-440/90-20 on 900920-1116.Corective Actions:Valve Repair & Rebuilding,Per LER 90-025-01,dtd 901123 & Restoration of Six MSIV That Required Disassembly to Original Condition | | | 05000440/LER-1990-027, :on 900925,personnel Error Resulted in Air Roll of Div 1 Diesel Generator |
- on 900925,personnel Error Resulted in Air Roll of Div 1 Diesel Generator
| | | 05000440/LER-1990-028, :on 901009,failure to Perform Surveillance Resulted in Inoperable Containment Isolation Valves |
- on 901009,failure to Perform Surveillance Resulted in Inoperable Containment Isolation Valves
| | | 05000440/LER-1990-030, :on 901011,failure to Perform Required Surveillance Prior to Resuming Fuel Movement Discovered |
- on 901011,failure to Perform Required Surveillance Prior to Resuming Fuel Movement Discovered
| | | 05000440/LER-1990-031, :on 901022,control Rod Withdrawn W/O First Demonstrating by Channel Check That Scram Discharge Vol Level Instrumentation Operable |
- on 901022,control Rod Withdrawn W/O First Demonstrating by Channel Check That Scram Discharge Vol Level Instrumentation Operable
| | | 05000440/LER-1990-032, :on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders |
- on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders
| | | 05000440/LER-1990-033, :on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N |
- on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N
| | | 05000440/LER-1990-034, :on 901125,discovered That Reactor Pressure Vessel Water Level Instrumentation Equalizing Valve Mispositioned.Caused by Personnel Error.Equalizing Valve Closed & Walkdown Performed |
- on 901125,discovered That Reactor Pressure Vessel Water Level Instrumentation Equalizing Valve Mispositioned.Caused by Personnel Error.Equalizing Valve Closed & Walkdown Performed
| | | 05000440/LER-1990-036, :on 901207,control Rod Scram Accumulator Level Switch Inoperable Throughout Second Fuel Cycle in Violation of Tech Spec 3.1.3.3.Caused by Unidentified Sys Interaction. Sys Operating Instruction Revised |
- on 901207,control Rod Scram Accumulator Level Switch Inoperable Throughout Second Fuel Cycle in Violation of Tech Spec 3.1.3.3.Caused by Unidentified Sys Interaction. Sys Operating Instruction Revised
| | | 05000440/LER-1990-038, :on 901211,control Room Noble Gas Radiation Monitor Inoperable for More than 7 Days W/O Taking Compensatory Actions.Caused by Personnel Error.Valve Lineup Instruction Changed & Monitor Will Be Included in Training |
- on 901211,control Room Noble Gas Radiation Monitor Inoperable for More than 7 Days W/O Taking Compensatory Actions.Caused by Personnel Error.Valve Lineup Instruction Changed & Monitor Will Be Included in Training
| | | 05000440/LER-1990-039, :on 901211,discovered That Both Loops of Containment Spray Mode of RHR Sys Inoperable.Caused by Inadequate Instructions.Instructions Revised to Include Isolation Valve for Position Verification |
- on 901211,discovered That Both Loops of Containment Spray Mode of RHR Sys Inoperable.Caused by Inadequate Instructions.Instructions Revised to Include Isolation Valve for Position Verification
| | | 05000440/LER-1990-040, :on 901218,RWCU Isolation Occurred While Correcting Cause of RWCU Sys Outboard Isolation Valves Not Opening.Caused by Personnel Error.Panel & Tools Inspected for Shorting & Fuses Replaced |
- on 901218,RWCU Isolation Occurred While Correcting Cause of RWCU Sys Outboard Isolation Valves Not Opening.Caused by Personnel Error.Panel & Tools Inspected for Shorting & Fuses Replaced
| | | 05000440/LER-1990-041, :Between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo Issued |
- Between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo Issued
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