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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18011A5401994-08-10010 August 1994 LER 94-017-00:on 940711,automatic Isolation of RHR Sys Shutdown Cooling Suction Outboard Containment Isolation Valve Occurred Due to Inadequate Work Order.Work Order Process for I&C Work Orders Will Be reviewed.W/940810 Ltr ML20046C5721993-08-0606 August 1993 LER 93-015-00:on 930709,unexpected RRP Fast to Slow Speed Downshift Occurred Due to Failure of Both RRP Suction Temp Rtd.Replaced & Returned RTD to Mfg for Failure Analysis. W/930806 Ltr ML20046B7811993-08-0202 August 1993 LER 93-014-00:on 930703,TS 3.0.3 Entered Due to Failure of Racs Power Supply.Replaced 5 Volt Power Supply in Racs cabinet.W/930802 Ltr ML20045G7201993-07-0808 July 1993 LER 93-013-00:on 930608,control Room HVAC Sys Train a Supply Fan Tripped on Overcurrent,Resulting in Both Sys Trains Being Unavailable.Caused by Motor Winding Insulation Failure.Motor Repaired by mfg.W/930708 Ltr ML20045G2171993-07-0707 July 1993 LER 93-012-00:on 930607,noted That HPCS Initiation Signal Resulted in Auto Start of Div 3 DG & ESW Sys.Caused by Failure of Div 3 Reserve Battery Charger.Procedures Used for Insp & Maint of Battery Being modified.W/930707 Ltr ML20044F2161993-05-19019 May 1993 LER 93-011-00:on 930419,identified That Excessive Strainer Differential Pressure Across RHR Suction Strainers Could Have Compromised Long Term Cooling During LOCA Operation. Caused by Inadequate Program requirements.W/930519 Ltr ML20044B6771993-02-22022 February 1993 LER 93-004-00:on 930121,MOV Testing of Main Steam Line Drain & Bypass Outboard Isolation Valve Indicated That Thrust Less than Design Thrust to Close Valve Under Accident Conditions. Review,Per GL 89-10 in progress.W/930222 Ltr ML20029B6431991-03-0808 March 1991 LER 91-007-00:on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper value.W/910308 Ltr ML20029B0971991-03-0101 March 1991 LER 91-006-00:on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being revised.W/910301 Ltr ML20029A6451991-02-22022 February 1991 LER 91-005-00:on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel error.W/910222 Ltr ML20029A3321991-02-15015 February 1991 LER 91-004-00:on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified. W/910215 Ltr ML20028H7521991-01-25025 January 1991 LER 90-041-00:between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo issued.W/910125 Ltr ML20024F7421990-12-14014 December 1990 LER 90-033-00:on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N ML20024F7411990-12-14014 December 1990 LER 90-032-00:on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders ML20028G9181990-09-28028 September 1990 LER 90-020-00:on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being revised.W/900928 Ltr ML20044B1021990-07-13013 July 1990 LER 90-013-00:on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel counseled.W/900713 Ltr ML20043H4801990-06-20020 June 1990 LER 90-011-00:on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction revised.W/900620 Ltr ML20043H5251990-06-20020 June 1990 LER 90-010-00:on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage monitored.W/900620 Ltr ML20043H3841990-06-18018 June 1990 LER 90-009-00:on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut replaced.W/900618 Ltr ML20043E5711990-06-0808 June 1990 LER 89-030-01:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Failure of Two Control Rods Caused by Improper Seat Matl in Associated Scram Pilot Solenoid Valves.Instructions revised.W/900608 Ltr ML20043A7801990-05-18018 May 1990 LER 90-007-00:on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced ML20043A8451990-05-18018 May 1990 LER 90-008-00:on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced ML20042G7731990-05-11011 May 1990 LER 90-006-00:on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel retrained.W/900511 Ltr ML20012D8151990-03-24024 March 1990 LER 90-003-00:on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement implemented.W/900323 Ltr ML20011E1861990-02-0202 February 1990 LER 90-001-00:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised ML20011E1871990-02-0202 February 1990 LER 90-002-00:on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised ML19354E0961990-01-19019 January 1990 LER 89-032-00:on 891228 & 900105,HPCS Sys Declared Inoperable Due to Inoperability of Div 3 Battery.Caused by Low Pilot Cell Voltage,Cell W/Slow Electrolyte Leak & Blown Power Fuse.Fuse & Hydromotor Pump replaced.W/900119 Ltr ML20005E6851990-01-0505 January 1990 LER 89-031-00:on 891206,08 & 15,RWCU Sys Isolations Occurred.Caused by Design Deficiency & Deficiency in Leak Detection/Differential Flow Circuitry Setpoint &/Or Time Delay.Leak Detection Thermocouples relocated.W/900105 Ltr ML20005E0821989-12-26026 December 1989 LER 89-030-00:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Caused by Failure to Return Scram Pilot Valves Used for Rods to Mfg After Recall. Surveillance Instruction revised.W/891226 Ltr ML19354D5991989-12-17017 December 1989 LER 89-029-00:on 891117,heater Bay/Turbine Bldg Vent Gaseous Effluent Particulate & Iodine Samples Not Continuously Collected as Required by Tech Spec 3.3.7.10.Caused by Procedure Deficiency.Procedure revised.W/891217 Ltr ML19325E5901989-11-0303 November 1989 LER 89-028-00:on 891008,concluded That Operation of Fuel Pool Cooling & Cleanup Sys to Upper Containment Pools Caused Containment Vacuum Breaker Actuations.Caused by Unrecognized Sys Interaction.Operating Instruction revised.W/891103 Ltr ML19324B1241989-10-27027 October 1989 LER 89-024-01:on 890723,entry Into Operational Condition 2 Completed W/Suppression Pool Makeup Sys Inoperable & on 890725,vent Valve on Ref Leg Found Open & Uncapped.Caused by Personnel Error.Personnel counseled.W/891027 Ltr ML19325D5121989-10-20020 October 1989 LER 89-027-00:on 890925,loss of Control Power to Emergency Svc Water Sys Pump Discharge Valve a Rendered Sys Inoperable.Caused by Personnel Error Re Jumper Placement. Involved Technicians counseled.W/891020 Ltr ML19325D1581989-10-13013 October 1989 LER 88-025-01:on 880618,reactor Protection Sys (RPS) Bus Inadvertently Deenergized,Resulting in Full RPS Actuation. Caused by Personnel Error W/Contributing Factor of Poor Human Factors Design.Info Tag Installed on Power Switch ML19325D1591989-10-13013 October 1989 LER 89-026-00:on 890913,reactor Thermal Power Level Exceeded That Specified in OL Due to Unexpected Recirculation Sys Flow Control Transient.Caused by Component Failure.Failed Isolation Solenoid Valve Replaced ML19325D9331987-03-27027 March 1987 LER 87-010-00:on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised ML19325C1171987-03-27027 March 1987 LER 87-009-00:on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 revised.W/870327 Ltr 1994-08-10
[Table view] Category:RO)
MONTHYEARML18011A5401994-08-10010 August 1994 LER 94-017-00:on 940711,automatic Isolation of RHR Sys Shutdown Cooling Suction Outboard Containment Isolation Valve Occurred Due to Inadequate Work Order.Work Order Process for I&C Work Orders Will Be reviewed.W/940810 Ltr ML20046C5721993-08-0606 August 1993 LER 93-015-00:on 930709,unexpected RRP Fast to Slow Speed Downshift Occurred Due to Failure of Both RRP Suction Temp Rtd.Replaced & Returned RTD to Mfg for Failure Analysis. W/930806 Ltr ML20046B7811993-08-0202 August 1993 LER 93-014-00:on 930703,TS 3.0.3 Entered Due to Failure of Racs Power Supply.Replaced 5 Volt Power Supply in Racs cabinet.W/930802 Ltr ML20045G7201993-07-0808 July 1993 LER 93-013-00:on 930608,control Room HVAC Sys Train a Supply Fan Tripped on Overcurrent,Resulting in Both Sys Trains Being Unavailable.Caused by Motor Winding Insulation Failure.Motor Repaired by mfg.W/930708 Ltr ML20045G2171993-07-0707 July 1993 LER 93-012-00:on 930607,noted That HPCS Initiation Signal Resulted in Auto Start of Div 3 DG & ESW Sys.Caused by Failure of Div 3 Reserve Battery Charger.Procedures Used for Insp & Maint of Battery Being modified.W/930707 Ltr ML20044F2161993-05-19019 May 1993 LER 93-011-00:on 930419,identified That Excessive Strainer Differential Pressure Across RHR Suction Strainers Could Have Compromised Long Term Cooling During LOCA Operation. Caused by Inadequate Program requirements.W/930519 Ltr ML20044B6771993-02-22022 February 1993 LER 93-004-00:on 930121,MOV Testing of Main Steam Line Drain & Bypass Outboard Isolation Valve Indicated That Thrust Less than Design Thrust to Close Valve Under Accident Conditions. Review,Per GL 89-10 in progress.W/930222 Ltr ML20029B6431991-03-0808 March 1991 LER 91-007-00:on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper value.W/910308 Ltr ML20029B0971991-03-0101 March 1991 LER 91-006-00:on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being revised.W/910301 Ltr ML20029A6451991-02-22022 February 1991 LER 91-005-00:on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel error.W/910222 Ltr ML20029A3321991-02-15015 February 1991 LER 91-004-00:on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified. W/910215 Ltr ML20028H7521991-01-25025 January 1991 LER 90-041-00:between 901212 & 28,inoperable Reactor Pressure Vessel Level Instrumentation Channels Resulted in HPCS Sys Being Inoperable & in Tech Spec Violation.Caused by Personnel Error.Memo issued.W/910125 Ltr ML20024F7421990-12-14014 December 1990 LER 90-033-00:on 901120,Train B of Control Room HVAC Sys Actuated Unexpectedly in Emergency Recirculation Mode.Caused by Inadequate Instruction.Procedure Revised Re Correct Guidance During Loss of Power to Bus K-1-N ML20024F7411990-12-14014 December 1990 LER 90-032-00:on 901116,disconnecting Wires to Test Relay Contact Resulted in RHR a Shutdown Cooling Sys Isolation. Caused by Procedure Deficiency & Inadequate Instructions. Personnel Trained Re Review of Work Orders ML20028G9181990-09-28028 September 1990 LER 90-020-00:on 900831,maint Activities on Control Room Emergency Recirculation Sys Resulted in Tech Spec Violation & Compromise of Safety Sys.Caused by Program Deficiency. Maint Acitivities & Insp Being revised.W/900928 Ltr ML20044B1021990-07-13013 July 1990 LER 90-013-00:on 900619,discovered That Main Steam Line Radiation Monitor C Inoperable for Greater than Time Allowed by Tech Specs 3.3.1.a & 3.3.1.b.Caused by Personnel Error. Personnel counseled.W/900713 Ltr ML20043H4801990-06-20020 June 1990 LER 90-011-00:on 900521,discovered That Divisional LPCI & LPCS Sys Inoperable in Excess of Tech Spec Action Limits Between 871119-23 & 891218-22.Caused by Procedural Deficiency.Sys Operating Instruction revised.W/900620 Ltr ML20043H5251990-06-20020 June 1990 LER 90-010-00:on 900521,Tech Spec Action Requirements Not Implemented for Inoperable Control Rod Scram Accumulators. Caused by Inadequate Procedures & Malfunctioning Transformer.Analyzer Reset & Leakage monitored.W/900620 Ltr ML20043H3841990-06-18018 June 1990 LER 90-009-00:on 900517,RHR Sys B HX Bypass Valve Failed to Reposition on Demand,Rendering RHR Sys Train Operable for Containment Spray Cooling Mode of Operation.Caused by Failure of Valve Stem Nut.Stem Nut replaced.W/900618 Ltr ML20043E5711990-06-0808 June 1990 LER 89-030-01:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Failure of Two Control Rods Caused by Improper Seat Matl in Associated Scram Pilot Solenoid Valves.Instructions revised.W/900608 Ltr ML20043A7801990-05-18018 May 1990 LER 90-007-00:on 900418,ruptured Seal on Outer Door of Upper Containment Airlock Occurred Causing Loss of Containment Integrity.Caused by Inadequate Communications & Equipment Failure.Seal on Outer Door Replaced ML20043A8451990-05-18018 May 1990 LER 90-008-00:on 900420,unexpected Isolation of RWCU Sys Occurred.Caused by Component Failure.Faulty Transmitter Transmitter Identified & Replaced ML20042G7731990-05-11011 May 1990 LER 90-006-00:on 900411,control Room Emergency Recirculation Sys Found to Be Inoperable & Tech Specs 3.0.3 Entered on Three Occasions.Caused by Operator Error & Component Failure,Respectively.Personnel retrained.W/900511 Ltr ML20012D8151990-03-24024 March 1990 LER 90-003-00:on 900222 & 23,discovered That Stroke Time Measurements Not Performed in Both Directions for motor- Operated Valves in safety-related Sys.Caused by Program Deficiency.Procedural Enhancement implemented.W/900323 Ltr ML20011E1861990-02-0202 February 1990 LER 90-001-00:on 900107,reactor Scram Occurred After Improper Transfer of 480-volt Ac Power Supplies Resulted in Total Loss of Feedwater Flow & Power Interruption.Caused by Personnel Error.Operator Counseled & Instructions Revised ML20011E1871990-02-0202 February 1990 LER 90-002-00:on 900107,RCIC Sys Isolated Due to High Differential Temp Signal Detected Across RCIC Room Cooler Following Reactor Scram Due to Loss of Feedwater Flow. Caused by Design Deficiency.Procedures Re Flow Rate Revised ML19354E0961990-01-19019 January 1990 LER 89-032-00:on 891228 & 900105,HPCS Sys Declared Inoperable Due to Inoperability of Div 3 Battery.Caused by Low Pilot Cell Voltage,Cell W/Slow Electrolyte Leak & Blown Power Fuse.Fuse & Hydromotor Pump replaced.W/900119 Ltr ML20005E6851990-01-0505 January 1990 LER 89-031-00:on 891206,08 & 15,RWCU Sys Isolations Occurred.Caused by Design Deficiency & Deficiency in Leak Detection/Differential Flow Circuitry Setpoint &/Or Time Delay.Leak Detection Thermocouples relocated.W/900105 Ltr ML20005E0821989-12-26026 December 1989 LER 89-030-00:on 891125,plant Entered Tech Spec 3.0.3 Due to Two Untrippable Control Rods.Caused by Failure to Return Scram Pilot Valves Used for Rods to Mfg After Recall. Surveillance Instruction revised.W/891226 Ltr ML19354D5991989-12-17017 December 1989 LER 89-029-00:on 891117,heater Bay/Turbine Bldg Vent Gaseous Effluent Particulate & Iodine Samples Not Continuously Collected as Required by Tech Spec 3.3.7.10.Caused by Procedure Deficiency.Procedure revised.W/891217 Ltr ML19325E5901989-11-0303 November 1989 LER 89-028-00:on 891008,concluded That Operation of Fuel Pool Cooling & Cleanup Sys to Upper Containment Pools Caused Containment Vacuum Breaker Actuations.Caused by Unrecognized Sys Interaction.Operating Instruction revised.W/891103 Ltr ML19324B1241989-10-27027 October 1989 LER 89-024-01:on 890723,entry Into Operational Condition 2 Completed W/Suppression Pool Makeup Sys Inoperable & on 890725,vent Valve on Ref Leg Found Open & Uncapped.Caused by Personnel Error.Personnel counseled.W/891027 Ltr ML19325D5121989-10-20020 October 1989 LER 89-027-00:on 890925,loss of Control Power to Emergency Svc Water Sys Pump Discharge Valve a Rendered Sys Inoperable.Caused by Personnel Error Re Jumper Placement. Involved Technicians counseled.W/891020 Ltr ML19325D1581989-10-13013 October 1989 LER 88-025-01:on 880618,reactor Protection Sys (RPS) Bus Inadvertently Deenergized,Resulting in Full RPS Actuation. Caused by Personnel Error W/Contributing Factor of Poor Human Factors Design.Info Tag Installed on Power Switch ML19325D1591989-10-13013 October 1989 LER 89-026-00:on 890913,reactor Thermal Power Level Exceeded That Specified in OL Due to Unexpected Recirculation Sys Flow Control Transient.Caused by Component Failure.Failed Isolation Solenoid Valve Replaced ML19325D9331987-03-27027 March 1987 LER 87-010-00:on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised ML19325C1171987-03-27027 March 1987 LER 87-009-00:on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 revised.W/870327 Ltr 1994-08-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in Pnpp to Ceico PY-CEI-NRR-2437, Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With PY-CEI-NRR-2429, Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With NUREG-1482, SE Approving Licensee Relief Requets PR-2,PR-3,PR-6,VR-6, VR-7,VR-10,PR-4,PR-5,VR-4,VR-5,VR-9,VR-1 & VR-3 Related to Inservice Testing Program,Second ten-year Interval for Perry Nuclear Power Plant1999-08-0909 August 1999 SE Approving Licensee Relief Requets PR-2,PR-3,PR-6,VR-6, VR-7,VR-10,PR-4,PR-5,VR-4,VR-5,VR-9,VR-1 & VR-3 Related to Inservice Testing Program,Second ten-year Interval for Perry Nuclear Power Plant PY-CEI-NRR-2424, Monthly Operating Rept for July 1999 for Perry Npp.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Perry Npp.With ML20210J3851999-07-28028 July 1999 Pnpp - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval PY-CEI-NRR-2416, Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With ML20196A1951999-06-17017 June 1999 Instrument Drift Analysis ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application PY-CEI-NRR-2409, Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2393, Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored1999-05-12012 May 1999 Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp PY-CEI-NRR-2399, Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at Pnpp & Use of Table IWB-3514 ML20206D7911999-04-23023 April 1999 Rev 6 to PDB-F0001, COLR for Pnpp Unit 1 Cycle 8,Reload 7 ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected PY-CEI-NRR-2389, Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20206D8461999-03-31031 March 1999 Rev 1 to J11-03371SRLR, Supplemental Reload Licensing Rept for Pnpp,Unit 1 Reload 7 Cycle 8 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 PY-CEI-NRR-2369, Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 9902271999-03-0303 March 1999 Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 990227 PY-CEI-NRR-2372, Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 PY-CEI-NRR-2356, Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2346, Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position PY-CEI-NRR-2335, Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2329, Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With ML20153B8221998-09-16016 September 1998 Safety Evaluation Accepting Changes to USAR Section 13.4.3, 17.2.1.3.2.2,17.2.1.3.2.2.3 & App 1A PY-CEI-NRR-2323, Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2313, Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2306, Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 1 ML20249A1891998-06-11011 June 1998 SER on Moderate Energy Line Pipe Break Criteria for Perry Nuclear Power Plant,Unit 1 & Requests Addl Info to Demonstrate That Plant & FSAR in Compliance W/Staff Position & GDC as Discussed in SER ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted PY-CEI-NRR-2282, Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D2051998-04-20020 April 1998 SER Authorizing Licensee to Use Code Case N-524 Until Such Time as Code Case Included in Future Rev of RG 1.147 PY-CEI-NRR-2277, Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216G3901998-03-11011 March 1998 SER on Proposed Merger Between Duquesne Light Co & Allegheny Power Sys,Inc ML20216J1401998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2258, Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 11998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 1 1999-09-30
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- ee._m 6200 Dok 1ree Bouteoro Mod Aosress inoependenceOH PO Box 9406) 216-44T3100 C6eveionc.OH 441014661 June 8, 1990 PY-CEI/NRR-1186 L U.S. Nuclear Regulatory Comeission Document Control Desk Washington, D.C. 20555 Perry Nuclear Power Plant Docket No. 50-440 LER 89.030/1 Dear Sir Enclosed is Licensee Event Report 89-030/1 for the Perry Nuclear Power Plant.
Since ly I t ' 8, Lu Michael D. Lysl;er Vice President, Nuclear - Perry MDL:njc
Enclosure:
LER 89-030/1 cc T. Colburn NRC Resident inspector U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137 9006130151 900608 PDR S
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On November 25, 1989 between 1433 and 1R15 two control rods were inoperable due to being untrippable, requiring e'.try into Technical Specification (TS) 3.0.3. Laboratory analysis later determined the.; the failure of the two control rods was due to improper 6 seat material in the associeced scram pilot solenoid valves.
The root cause control rod failure was inadequate implementation of the Nonconformance l Control Program. The scram pilot valves used for rods 34-47 and 34-51 had been recalled by the manufacturer in 1985 but were not returned to the supplier prior to their installation during the 1989 refueling outage. The root cause of the entry into TS 3.0.3 is personnel error. During scram time testing, control room personnel observed 2 failures of rod 34-47 and then declared the rod operable after 2 successful retests. It was not until after the subsequent failure of rod 34-51 that the operability of rod 34-47 was reevaluated. Control rod 34-47 should not have been declared operable without an adequate evaluation for the observed failures.
To prevent recurrence, surveillance instructions have been modified to address actions to be taken when rods fail testing. The operators involved in this event have been coached with respect to equipment operability and the conduct of testing and troubleshooting. The procedure lor surveillance test control has been modified to include actions to be taken whet. unsatisfactory test results are encountered, as well as a requirement to analyze ant'. evaluate the causes for the unsatisfactory results prior to declaring the compor.rnt back in service. Additionally, all licensed operators have been trained on the 1e.ssons learned from this event and the philosophy of test control performance as im%emented by the procedural changes described above. l temCP.rm He16491
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,8KT # ausse esas e soeuseet esse asussenw 44C Apun m W1h On November 25, 1989 between 1413 and 1815 two control rods were inoperable due s
to being untrippable, resulting in conditions requiring entry into Technical i
. Specification (TS) 3.0.3. At the time of the event, the plant was in Operational Condition 1 (Power Operation) with the reactor at 78 percent of rated thermal power. The Reactor Pressure Vessel (RPV) pressure was at saturated pressure and r temperature conditions at approximately 990 psig.
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@ During the first refuel outage, 59 of the 177 installed scram pilot solenoid y valves were replaced as part of routine preventative maintenance for equipment
.- qualification reasons. On July 30, 1989, during retest procedures following this :
replacement, co Grol rode 34-47 and 34-51 each failed to satisfy scram time testing requirementa on the initial attempt; however, because the control rod l timing t e s were satisfied on subsequent attempts, the rods were declared
! operable and returned to service. Although the rods were considered operable, t system engineering personnel documented the event on a condition report, specifying the corrective actions to test these control rods during the next scheduled scram time surveillance.
As a result of this condition report's corrective actions, control rods 34-47 and 34-51 were specifically included in the test population for the November 25, 1989 surveillance activities. The following chronology describes the events of that ,
testing as they specifically relate to control rods 34-47 and 34-51.
November 25, 1989 .
0600 A power reduction was initiated to facilitate scram time testing in i accordance with Surveillance Instruction (SVI-Cll-T1006) " Control Rod Maximum Scram Insertion Time". !
0631 The power reduction was completed. Reactor power at 78%.
1337 Rod 34-47 was tested and failed to move.
1340 Rod 34-47 was tested again, failing to meet scram time criteria.
' 1356 Red 34-47 was tested satisfactorily.
f 1404 Rod 34-47 was tested satisfactorily.
1413 Rod 34-51 was tested and failed to move.
1433 Rod 34-51 was retested and failed to move. '
1439 Rod 34-51 was declared inoperable.
1458 Rod 34-51 was hydraulically disarmed at position 48 (full out) to satisfy action requirements of TS 3.1.3.1.a.l.b.
1502 Rod 34-51 was verified to be separated from other inopecable control rods by at least two control cells as required by TS 3.1.3.1.a.
1503 Scram time testing was suspended.
1503 Ceneral Electric Company (GE) was requested to complete a shutdown margin calculation for the current conditions, assuming control rod 34-51 stuck at l position 48 and the most reactive rod fails to scram.
1730 GE responded that shutdown margin for current conditions was insufficient to satisfy TS requirements.
1810 Rod 34-51 was rearmed.
1815 Rod 34-51 was hydraulically inserted to position 00 and disarmed.
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2208 Rod 34-47 was inserted to position 00 and disarmed.
y November 26, 1989 n1 3 0341 Hydrrulic Control Unit (HCU) 34-51 was restored after replacing the scram j pilot valve.
H 0437 Rod 34-51 was declared operable after unisolating and satisfactorily ,
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completing scram time testing.
0505 HCU 34-47 was restored after replacing the scram pilot valve.
0517 Rod 34-47 was declared operable af ter unisolating and satisf actorily completing scram time testing.
ev 0600 Operations Section management confirmed the failure of the operators to enter TS 3.0.3 for two untrippable control rods.
~ 0700 Operations Section manager contacted the Resident inspector.
In review of the timeline provided above, it should be noted that prior to the performance of the tests, control room supervisory personnel were not aware of the specific reasons for inclusion of the two subject control rods in the test population. As a result, the initial failures of rod 34-47 to satisfy surveillance requirements were attributed to faulty test switches which were used to initiate the single rod scram functions tested in this activity, and the rod .
was not immediately declared inoperable. After the failure of control rod 34-51 to insert, the control rod was declared inoperable due to being untrippable.
Only after discussion with Lead Reactor Engineering personnel performing the testing did control room supervisory personnel realize the significance of the failures documented on July 30, and declared control rod 34-47 inoperable due to being untrippable.
2 TS 3.1.3.1 describes actions to be taken when control rods are inoperable.
Because the number of control rods inoperable due to being untrippable is limited to one, the plant was in a condition governed by TS 3.0.3 during the time when both control rods 34-47 and 34-51 were withdrawn and inoperable due to being untrippable. Because rod 34-47 should have been considered inoperable irom initial failure at 1337 until inserted at 2208, this condition existed from the time of failure of rod 34-51.at 1423 until insertion of rod 34-51 at 1815. Upon review of the event, Operations Section management personnel recognized the failure to enter TS 3.0.3 and notified the NRC Resident Inspector. Although the one-hour requirement to initiate action was not satisfied, control rod 34-51 was fully inserted and TS 3.0.3 was exited prior to the time the unit would have been
< required to be in Startup. It should also be noted that all requirements were satisfied for those TS which control room personnel considered applicable during the event.
On November 27, 1989, after plant management reviewed the event, actions were initiated to verify the operability of the remaining control rods. An additional 1 I
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-55 control rods were scram-time tested on November 27-28. Including all control
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*YoM*"r'eWEk'E8"'Er'UY"TeTefuelo4tagewhichhadnotbeensatisfactorilytested during previous activities condu;ted on November 25, 1990. Included in this l sample were the two control rode which had failed previously and had been repaired. Direction had been provided to operations personnel to commence a plant shutdown if any rod failed to scram or to satisfy scram time test criteria
, due to malfunctioning scram pilot valves. All control rods tested demonstrated satisfactory scram times.
In addition to the scram-time testing activities, inspection and failure analysis was initiated for the scram pilot solenoid valves removed f rom the 11ydraulic Control Units (11C0) f or rods 34-47 and 34-51. Initial inspection showed that the elastomer seat material in the suspect valves (ASCO Model Number flV176-816-1) appeered by physical characteristics to be urethane, rather than Viton, which is ;
specified for this application. After initial inspection, the valves were transported to an independent laboratory for further analysis and preliminary results indicated that the material was urethane. Further investigation revealed that the subject scram pilot solenoid valves were included in a shipment which was recalled by ASCO in 1985 because of the possibility that the seat elastomer may not have been properly upgraded from urethane to Viton. In all, 34 valves were recalled from Perry, of which 22 were returned for refurbishment. The remaining 12 valves were apparently returned to stock without being rebuilt. In addition to the 2 which failed on November 25, research of documentation and an inspection of all 177 control rod HCU's determined the location of five additional recalled valves which were installed during the 1989 refueling outage.
, Although functioning properly, these five valves were replaced on November 29, 1989 with appropriate replacement parts, and were transported to an independent laboratory for further analysis. The remaining five recalled valves have been identified and are either being used for training aids or had been discarded during the refuel outage aftet failing preoperational reating due to air leaka.
. Initial analysis indicated elastomer parts within the valve bodies of t% two j* failed valves were not Viton, the seat material for which the valve was qualified. This was apparent when red exhaust port seats were discovered in the valves which failed. Further, when the next five valves were dismantled, three j of the elastomer seats, were green and two were black. Color is an indicator of j material type for clastomers, green and red are atypical for Viton. Discussion i with the valve vendor indientad it ens possible that the red material was a
- urethane. Laboratory analysis of the seven elastcmer samples determined five to l be urethane. The red elastomer is possibly a soft, polyester urethane; the green seat material shows some characteristics of a harder, isocyanate based urethane, or cathene. The black elastomer material is Viton.
p Microscopic observation and analytical results determined that the failure of the a valves was a result of the urethane seat material adhering to the brass exhaust port. The presence of a sticky yellow foreign material, the degradation of the elastomer, and the migration of valve metals into the elastomer residue found on the exhaust port support this conclusion. This result is consistent with the use of urethane, since these clastomers are extremely susceptible to chemical attack from oils, lubricants or solvents which have been used in the manufacture of l' solenoid valves.
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0l 1 0l5 or o l7 rut . w. we w anvim The root cause of the failure of control rode 34-47 and 34-51 to satisfy criteria for scram times was inadequate implementation of the Nonconformance Control Program. ASCO issued a letter to General Electric (CE) on April 29, 1985 in which they indicate that 40 valves shipped to GE may not have been rebuilt with Viton-A material for the disc holder assembly. GE subsequently determined that g$ 34 of these valves had been shipped to Perry. Quality Control personnel at Perry N generated a nonconformance report (NR) on June 7,1985 to control the y circumstances of the recall. However, only 22 of the 34 valves were listed on the NR since a CE site internal letter initiated on the same date indicated that the remaining 12 valves were rebuilt with kits supplied by ASCO. The NR was '
closed concurrent with the return of the 22 valves on December 13, 1985.
Investigation has determined that no documentation exists that would confirm that the 12 valves omitted from the NR were in fact refurbished in 1985. If the program had been implemented correctly, work documents would have been provided by CE with their NR disposition to confirm the refurbishment. The absence of this evidence should have resulted in the initiation of an additional NR for the 12 suspect valves. In conclusion, the NR disposition provided by CE was unsubstantiated and project personnel should have ensured that the work documents were available and complete to support the GE NR disposition.
The root cause of the entry into TS 3.0.3 is personnel error. Control rod 34-47 should not have been declared operable after repeated failures to satisfy scram-time criteria without an adequate evaluation of cause for the two observed .
failures. Additionally, all personnel involved with the scam-time testing, l
including licensed control room operators, should have been fully aware of the
. circumstances requiring surveillance testing of control rods 34-47 and 34-51 on l November 25, 1989. The documented evidence of previous failures of these control L rods under similar or identical circumstances was critical to the licensed j control room operators in the determination of operability. With the proper
- g determination that control rod 34-47 was inoperable at the time of the initial Q.; failure, action requirements of TS 3.1.3.1 could have been satisfied, and entry
.a into TS 3.0.3 could have been avoided.
The Control Rod Drive Hydraulic (AA) (CRDH) system provides the hydraulic driving head for insertion, withdrawal, and scamming of control rods. Within this system are HCU's which provide the reactor scram function. The CRDH System provides water at 1720 psig to the HCU. The HCU is equipped with a hydraulic cylinder with an internal free floating piston. The piston separates water on top from l nitrogen gas underneath. The HCU is precharged with N 3gas to a pressure of I about 1200 psig. Charging water pressure compresses the precharge to about 1720 psig.
l r .The scram signal is generated by instrumentation in the Reactor Protection System
[RPS} and transmitted to the CRDH System affecting the positions of several air-operated valves. The scram signal results in a loss of electrical power to the scram pilot valve solenoids, de-energizing them. It also energizes the backup scram valve solenoids. This causes the scram pilot and backup valve inlet u.c . m.i
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""F6f?'s"f5"$1'6TS'"TTHf!MA'E ports to open. The scram pilot valves are arranged so that the trip signal from RPS busses A and B must be removed from both coils before the valves operate. This prevents the inadvertent scram of a single Control Rod Drive Mechanism (AA] (CRDM) in the event of a failure of one of the pilot valve coils. The scram pilot valves open both the scram inlet and the outlet vglves. The backup scram valves vent the entire scram air header to assist in scram valve operation. The Redundant Reactivity Control System (RRCS) t also provides a means of venting air pressure from the scram air header by
[' causing the opening of additional vent and drain valves on selected signals or manual initiation.
When the inlet and outlet scram valves open, water in the scram accumulator and charging line is admitted underneath the CRDM drive piston, and the water above the piston is vented to the scram discharge volume. The large differential pressure between the accumulator and the SDV produces a large upward force on the control rod thus forcing it into the core region. In addition to the accumulator, reactor pressure can also be used to scram the control rods. Upon a scram, the accumulator provides the pressure to insert the control rod. As the accumulator discharges, its pressure drops rapidly. If the accumulator pressure drops below the reactor pressure, reactor pressure forces a ball check valve in the CRDM to unsest, blocking accumulator pressure and allowing reactor pressure to complete the drive stroke. At reactor pressure greater than 600 psig, reactor pressure alone is capable of scramming the drive.
The inoperability of Control Rods 34-47 and 34-51 was based on the partial inability to respond to a reactor scram signal due to potential misoperation of the associated Scram Pilot valves. A problem with operability of these valves, would impede timely rod insertion in the event of an initiation of RPS until the backup scram valves or RRCS depressurized the entire scram air header. Since the backup scram valves and RRCS were available, the scram functions for those rods would have occurred in the event of an RPS actuation. All remaining control rods j had demonstrated acceptable scram functions during rod timing tests on August 6, j 1989 during post-refuel outage startup testing. The scram function, therefore, would have satisfactorily shutdown the reactor in the event of a scram.
Additionally, during the entire event operators had the ability to insert all control rods using normal drive pressure. Approved Off-Normal and Plant Emergency Instructions are in place to provide direction to the operators during any event in which a control rod does not insert on an RPS actuation. This event, therefore, is not considered to be safety significant.
To determine if the inaccurate disposition of the 1985 NR was an indication of a negative trend or an isolated case, the project initiated an NR review for the time period from 1981 to 1985, during which CE had NR disposition review responsibility. In all, 876 NR's were reviewed, of which 45 were identified i which concerned vendor supply problems. Particular emphasis was placed on the NR's in this category. No anomalies were identified during this review and this inaccurate disposition of the subject NR is considered an isolated event.
Current site procurement procedures require full evaluation and documentation of actions taken in response to suct issues.
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The operators involved in this event have been coached with respect to equipment operability and the conduct of testing and troubleshooting. Plant Administrative F Procedure (PAP-1105) " Surveillance Test Control" has been modified '.o include actions to be taken when unsatisfactory test results are encountered as well as a
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requirement to analyze and evaluate the causes for the unsatisfaccory results
- prior to declaring the component back in service. All licensed aperators have been trafned on the lessons learned from this event and the phi'.osophy of test ,
control performance as implemented by the procedural changes at described above. 1 l
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