ML20041B801

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LER 82-009/03L-0:on 820122,during Normal Operation,Mounting Bracket for Turbine Stop Valve D,Train a Proximity Switch Discovered Broken.Caused by Excessive Vibration.Bracket Repaired & Switch Remounted
ML20041B801
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 02/18/1982
From: Palmer R
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20041B788 List:
References
LER-82-009-03L, LER-82-9-3L, NUDOCS 8202250215
Download: ML20041B801 (1)


Text

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REPORT DATE

  1. 8 t,0 bl DOCKE T NUh?BEH bd EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o ! .- l lDURING NORMAL OPERATION, IT WAS DISCOVERED THAT THE MOUNTING BRACKET FOR TUREINE STOP [

[ o 13 l l VALVE D, TRAIN A PROXIMITY SWITCH HAD BROKEN. THE PROXIMITY SWITCH PROVIDES THE TUR- l THE REDUNTANT l Inl4llBINE STOP VALVE CLOSURE INDICATION FOR THE REACTOR PROTECTION SYSTEM.

lo isi ! STOP VALVE SWITCH WAS OPERABLE AT THIS TIME. THIS EVEftT IS NON-CONSERVATIVE WITH l loIsil RESPECT TO TECHNICAL SPECIFICATION 3.3.1.1, TABLE 3.3-1 ITEM 18.b. PREVIOUS OCCUR- l I o { il l RENCES OF A SIMILAR NATURE INCLUDE: 50-316/81-022,80-069, 050. I I

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JJ 34 35 J6 4J 42 43 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h li)olIINVESTIGATION REVEALED THAT THE MOUNTING BRACKET HAD BROKEN DUE TO EXCESSIVE VIBRATION.]

lili1 lTHE MOUNTING BRACKET WAS REPAIRED, THE PROXIMITY SWITCH WAS REMOUNTED AND TESTED I gii-il SATISFACTORILY. NEW BRACKETS HAVE BEEN DESIGNED AND WILL BE INSTALLED DURING THE I Iiiil l NEXT 00' AGE OF SUFFICIENT DURATION. UNTIL THEN THE BRACKETS WILL BE INSPECTED WEEKLY l l

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