ML20040H574

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Monthly Operating Rept for Jan 1982
ML20040H574
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 02/02/1982
From: Van Sickel J
IES UTILITIES INC., (FORMERLY IOWA ELECTRIC LIGHT
To:
Shared Package
ML20040H572 List:
References
NUDOCS 8202180398
Download: ML20040H574 (7)


Text

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y OPERATING DATA REPORT DOCKET NO. _050-0331 DATE February 2,'1982 ickel COMPLETED TELEPIIONE 319-851- BY .L_11ILS_5 OPERATING STATUS

1. Unit Name: Duane Arnold Energy Center Notes
2. Reporting Period: January, 1982
3. Licensed Thermal Power (MWt): 1658 -
4. Nameplate Rating (Gross MWe): 565 (Turbine Rating) -
5. Design ElectricalRating(Ne MWe): 538
6. Maximum Dependable Capacity (Gross M de): 545
7. Maximum Dependable Capacity (Net MWe): 515
8. If Changes Occur in Capacity Ratings'(Items Number 3 Through 7) Since Last Report. Give Reasons:
9. Power Level To Which Restricted. If Any (Net MWe):
10. Reasons For Restrictions.If Any:

11ds Month Yr to.Date Cumulative

744 744 61,368

11. Ilours In Reporting Period
12. Number Of Hours Reactor Was Critical 744 744 ~44,222.7
13. Reactor Reserve Shutdown liours 0 0 0

'14. IIours Generator On-Line 744 744 43,133.4

15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Therrnal Energy Generated (MWH) 971.753 971,753 54,025,151 .
17. Gross Electrical Energy Generated (MWH) 330.241 ._. 330.241- 18,105,281
18. Net Electrical Energy Generated.(MWH) 311,303 311,303 16,942',889
19. Unit Senice Factor 100% 100% 70.3%
20. Unit Availability Factor 100% 100% 70.3%
21. Unit Capacity Factor (Using MDC Net) -

81.2%

  • 81.2% 52.9%
22. Unit Capacity Factor (Using DER Net) 77.8% 77.8% 51.3%
23. Unit Forced Outage Rate - 0.0% 0.0% 16:9%
24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each): . .

Maintenance. Aoril 1.1982, Two weeks .

25. If Shut Down At End Of Report Period. Estimated Date of Startup: )
  • Turbine Rating: 565.7 MWe -

Generator Rating: 663.'5 (MVA) x .90 (Power Factor) = 597 MWe .

e R .

(9/771

I -

AVERAGE DAILY UNIT POWER LEVEL .

DOCKET NO. 050-0331 Duane Arnold UNIT rng ny eggg DATE february 9, 1982 COMPLETED ljy J. Van Sickel TELEPHONE 319-851-561'1 January, 1982 MONTH .

DAY AVERAGE DAILY POWER' LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net) .

(MWe-Net) -

I 220 443 17 2 223 472

,3 3

19 4 328 448 20 5 . 399 444 369 6

' 22 7 451 421 23 s 439 461 24 307 481 9

25 10 386 458 26

' ll 455 501 27 ,

452 502 12 28 13 '444 499 29

.446 375 1.s 30 15 444 494 31 16 449 INSTRUCTIONS On this format,!ist the average daily unit power level in MWe Net for each day in the reportin;t month. Compute to the nearest whole megawatt.

(9/77I

UNITSIIUTDOWNS AND POWER REDUCTIONS DOCKET NO. 050-0331 UNIT NAME Duane Arnold Energy 'Ctr.

DATE February 2. 1982 COMPLETED BY J. Van Sicke' REPORT MONTif Februarv. 1982 TELEPilONE 319-851-5611 No. Date y

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}g Y jgs Licensec Event 8%

p f4 o"

Cause & Corrective Action to H jE 5 jg Report # mO [g Prevent Recurrence o -

s

1. 820109 S 0 H 4 Power was reduced to perform control rod withdrawals'.
2. '820130 S 0 B 4 Power was reduced to allow repair work on the condenser air ejectors.

i

/

I 2 3 4 F: Forced Reason: Method:

  • Exhibit G Instructions S: Scheduled A-Equipment Failure (Explain) I. Manual for Preparation of Data -

B Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C Refueling 3 Automatic Scram. Event Report (LER) File (NUREG-D Regularory Restriction 4-Other (Explain) 0161)

E Operator Training & License Examination F Administrative S C-Operational Error (Explain) Exhibit 1 Same Source (9/77) ll Other (Explain)

~ ~

~~

' Docket no. 050-0331 i Unit _Duane Arnold Energy 0 REFUELING INFORMATION Date February 2, 1982 Completcd by .J. Van Sich

' Telephone 319-851-5611 '

l

1. Name of facility. t A. Du,ane Arnold Energy Center
2. Scheduled date for next refueling shutdown.

A '. September 4, 1982 1

l

3. Scheduled date' for restart following refueling.

A. Unknown -

4. Will refueling or resumption of operation thercafter require a technical specification change or other license amendment?

l A. Yes. New MAPLH',RG tables will have to be included in Technical Specifications. l

5. Scheduled date(s) for submitting propos.cd licensing action and

. supporting information.

!A. Unknown at this time.

6. Important licensing considerations associated with refueling, e.g.,

new or different fuel design or supplier, unreviewed design or per-formance analysis methods, significant changes in' fuel design, new operating procedures.

A. New fuel assemblies to be placed in ,the ' reactor will be more highly j enriched than those. currently in use.

f, 7. The n' umber of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.

A. a) 368 b) 448- .

l

8. The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested

, or ic planned, in number of fuel assemblies.

A. 2050 l 9. The projected date of the last refueling that can be discharged to

!. the spent fuel pool assuming the present licensed capacity.

A. 1998 t

9

Docket No. 050-0331 Unit Dunne Arnold Enctg~v centet Date February 2,1982 .

MAJOR SAFETY RELATED MAINTENANCE d " "

hU e p e 3 9-8 6 DATE SYSTEM COMPONENT DESCRIPTION 1-4-82 Containment Atmospheric RE-8101B Replaced detector.

Control 1-21-82 RHR. Service Water Snubber GBC-1-SS-56 Replaced snubber.

1-25-82 Primary Containment TDS-2260A Replaced switch on temperature module.

1-27-82 RHR CV-2037 -

Replaced valve yoke.

O w

h a

D N

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il -

. Dock;t No. 050-0331

. Unit Duan, Arnold En~rgy C nter

. Data F bruary 2,1982 Completed by J. Van Sickel Telephone 319-851-5611 NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE 1-1 At the beginning of the report period the plant was operating at 244 Mwe.

1-5 A power increase was begun.

1-6 The plant was operating at 474 MWe at 1327 hours0.0154 days <br />0.369 hours <br />0.00219 weeks <br />5.049235e-4 months <br />.

1-7 During normal operation, an offgas stack high/ low flow alarm was received.

The cause was a frozen sample return line.

ETSV Report 82-1 1-8 During surveillance testing, turbine building main steam supply line area high temperature switch TIS 4477, Subchannel B, was found to have a nonconservative out of specification setpoint.

R0 Report 82-1 1-9 Plant load was reduced to allow control rod withdrawals to be performed.

1-10 A load increase was begun.

1-11 The plant was operating at 486 MWe at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br />.

1-12 During surveillance testing, RCIC steam supply high flow PDIS 2441 and PDIS 2442 were found to have out of tolerance setpoints.

R0 Report Pending 1-13 During surveillance testing, reactor low pressure (core spray and RHR valve opening permissive) switch PS 4529 was found to have an out of tolerance setpoint.

R0 Report Pending 1-14 During normal operation torus level recorder LR 4385 was found indicating downscale.

R0 Report Pending During normal operation the "B" containment oxygen analyzer was declared inoperabl e. The redundant analyzer was out of service for design change work.

R0 Report Pending 1-15 During normal operation, offgas stack sample pump 1P-247A was found inoperable. The redundant sample pump had been found inoperable earlier.

ETSV Report 82-2

Dock.t No. 050-0331 Unit Duane Arnold En'rgy C nt~r Date February 2, 1982 Completed by J. Van Sickel-Telephone 319-851-5611 NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE During surveillance testing, drywell high pressure (RPS) switch PS 4315B, was found to have an out of tolerance setpoint.

R0 Report Pending 1-18 A power increase was begun.

1-19 The plant was operating at 533 MWe at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />. A RHRSW system snubber and the valve yoke on CV 2037 were found broken. An evaluation was begun.

1-21 The LPCI system was declared inoperable pending an engineering evaluation as a result of a stress analysis (which was conducted after snubber GBC SS-56 was found broken) which concluded a section of RHR piping may have been overstressed.

R0 Report Pending 1-22 A control rod sequence exchange was completed. A power increase was begun.

1-24 Engineering evaluations, hydrostatic testing, NDT, and operability testing were completed on the RHRSW and LPCI systems and these systems were declare 1 operable.

5 1-25 The plant was operating at 526 MWe at 1440 hours0.0167 days <br />0.4 hours <br />0.00238 weeks <br />5.4792e-4 months <br />.

1-30 Power was reduced to allow repair work to be completed on the "A" main condenser.ai r ejector. A power increase was begun.

1-31 The plant was operating at 537 MWe at 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br />.