ML20217C349

From kanterella
Jump to navigation Jump to search
Revised MOR for Aug 1997 for DAEC
ML20217C349
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 08/31/1997
From: Woodward R
IES UTILITIES INC., (FORMERLY IOWA ELECTRIC LIGHT
To:
Shared Package
ML20217C356 List:
References
NUDOCS 9710010365
Download: ML20217C349 (4)


Text

_. ._ __ _ _ _ -_ _ _ _ _ _ _ _ _ _ _ _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ .

OPERATING DATA REPORT 4

DOCKET NO: 50-0331 DATE: 09'1597 Unit: Ihiane Arnold linercy Center COhtPLETED 11Y: Eichard Woodward

TELEPilONE: (319)851 7318
OPERATING STATUS 1

A verage Daily l'ower Level i

1. Unit Name: Duane Arnold Enercy Center 500
2. Reporting Period: Aunust 1997 3. 400 '

300

3. $ 200 1icensed'lhermall'ower(htW th h lfl 2 100 0

j 4. Nameplate Rating (Gross hiWe DER): 565 7 (Turbine)

6 I 11 16 21 26 31 1 5. Design Electrical Rating (Net htW e DER): 11[

Day

6. Maximum Dependable Capacity (Gross htW h1DC): fM -- - - - - I e
7. hiaximum Dependable Capacity (Net htW, MDC): 1;LO
8. If Changes occur in Capacity Ratings (items Number 3 through 7) since the last report, Give Reasons: Not Annlicable
9. Power Level to Which Restricted,if Any(Net hiw e k N!6
10. Reasons for Restrictions,if Any: N!.&

l August 97 1997 Cumulative i 1. Ilours in Reportmg Period 744.0 5,831.0 197,951.0

12. Number ofIlours Reactor Was Critical 639.0 5,437.3 151,931.4
13. Reactor Reserve Shutdown llours 0.0 0.0 192.6
14. Ilours Generator on Line 617.8 5,304.7 148,325.8
15. Unit Reserve Shutdown llours 0.0 0.0 0.0
16. Gross 1hennal Energy Generated (htWil) 975,794.4 8,461,339.9 210,114,651.0

~

< 17. ilross Electrical Energy Generated (h1Wil) 319,974.0 2,843,9R2.0 70,433,028.6

18. Net Electrical Energy Generated (hiWil) 301,570.1 2,683,183.5 66,098,742.5 19 Unit Service Factor 83.0 % 91.0% 74.9 %
20. Unit Availability Factor 83.0 % 91.'Oh 74.9 %
21. Unit Capacity Factor (Using MDC Net) 77.9 % 88.5 % 70.3 %
22. Unit Capacity Factor (Using DER Net) 75.3 % 85.5 % 67.4 %
23. Unit forced Outage Rate 0.0% 0.0% 9.9%

~

24. Shutdowns Scheduled Over Next 6 hionths (Type, Date, and Duration of each): N/A

, 25. If Shutdown at End of Report Period, Estimated Date of Startup: N/A 9710010365 970915 4

PDR ADOCK 05000331 R PDR

,, . . . -. .- - - - - - .. - __ -_ = - . - . . . - - - - . . . _ . . - -. -

, AVERAGE DAILY UNIT l'OWER LEVEL DOCKET NO: 50 0331 DATE: 09'1597 Unit: lhiane Amold Enerry Center

' COMPLETED DY: Richard Woodward TELEPil0NE: {319)851 7318 MONTil August 1997 Day Averagelhily

~ihiW5 Set) 1 521.9 2 516.7 3 -515.2 4 517.2 5 525.4 6 524.4 7 523.7 8 522.3 9 518.6 10 476.0 11 519.6 12 520.8 13 522.2 14 520.2 15 516.9 16 513.1 17 519.6 18 522.9 19 523.3 20 518.3 21 522.3 22 519.3 23 80.8 24 0.0 25 0.0 26 0.0 27 0.0 28 0.0 29 147.0 30 410.4 31 516.5

i

, IWFUELING INFORMATION DOCKET NO: $0-0.UI DATE: 09/15'97 Unit: Duane Arnold Enercy Center COMPLETED !!Y: Richard Woodward TELEPilONE: (3191831 7318

1. Name of facility.

Duane Arnold Energy Center

2. Scheduled date for next refueling shutdown.

April 2,1998

3. Scheduled date for restnrf. following refueling.

a May IW8

4. Will refueling or resumption of operation thereafter require a technical specification change or othtr license amendment?

No. (Improved Technical Specincations (ITS) approval needed for refueling outage planning.)

5. Scheduled date(s) for submitting proposed licensing, action and supporting information.

N/A. (ITS st bmitted October 10.1996.)

6. Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures. ,

N/A

7. Current and projected fuel assemblies inventory:

Number of Fuel Projected date oflast Assemblies refueling that can be discharged .

(after allowing margin for maintenance of continuous full core discharge capability)

Installed in reactor core (following refueling) 368 n/a

~DischargTd fro'nic,ofe"ti Spent fuel St'odge'IEl ~ Y-~1$28 n/a Mstalled Capacity of Spjnt Fuel Storage Pool I 2411 2001 Licensed Capacity of Spent I uel Storage Pool (with reracking) 2829 2006 Licensed Capacity of Spent Fuel Storage Pool and Cask Pool 3152 2010 *

(with teracking)

_,.7 I

e

, l

) DOCKET NO.: $0-0331 DATE: 09/15/97 i Unit: Duane Arnold Fnerev Center

' COhiPLETED llY: Richard Woodward ,

TELEPilONE: 0 19)851 7318 '

hionthly Operational Overview for August 1997:

'the plant operated at licensed thermal power throughout the month escept:

e 8'6 20:30 21:30, 8/Il 23:00 24:00, & 8/31 10:l$.11:05: to reduce recirculation now for control rod withdrawals, 0.2 Full Power flours equivalent (FPilm) e 8/9 22:00 8/10 23:00; to perform Turbine Valve & hialn Steam isolation Valve (hlSIV) Testing,2.2 FPity e 8/20 09:45 16:30: 11PCI Testing 0.1 FPil y e 8/22 22:00 8/2313:01: Reduce power in preparation for shutdown to repair condenser tube leak,6.4 Pily e 8/23 13:01 - 8/28 19:13: Shutdown,126.2 FPit y -

e 8'2819:13 8/3100:00: Startup,25.2 FPit y

! e 8'01 8/31: routine wcather, capacity and ef0ciency losses, l$.0 FPily.

Allocation cfl*roduction & Louest 1.le6trical Lapacity l actor l ull tomvr Output  % of $65.7 h1We i quis alent htWe (Design Rating) llours Actual Metered Nel 1:lectric Output 404 8 71.7% 532 4 Actual h,teteyd Plant I:lectric trad 253 45% 333 f acluded losses- 00 0 0*& 00

, Off.t.ine: Repair Condemer Tube I cak 8/2313 01. R'2819.13 96 0 17.0 % 126 2 linplanned On l.ine Capacity losses:

Ramp-down R/22 22.00 8/2313 01 start-up: t/2R 1913 8/3100 00 24 0 41% 31 6 Wentner losses condenser prenure >2 75 in lig / Circ Water Temp > 74.5 *r 5.5 0.9% 7.2 Normal Capacity loues ( Avg?l'ull Power

  • MWth < 1658) 03 0.1% 04 Other Planud On ljne Capacity lanes:

IU6 20 30-21:30,8/li 23:00 24 00, & R/31 10.1511:05: Adjust lead 1.Inc 89 22 00 8/10 23 00; Turb Valve & hisly resting t/20 09 45 16 30. IIPCI Testin4 23 04% 3 (l Metering losses ( Asg indie htWe . Avg htWile) 13 0.2% 1.7

, I mclency lanes (Weather Noam-l'ull Power MWe > $65.7 Design) M 11% G Design Gross I.lcrtrle Output },M,2 109 0 % M At 0746 on August 797, Primary Containment isolation System (PCIS) Group 2 and Group 4 alarms were received,

indicating isolation ie outboard valves for Drywell Floor and Equipm.at Drain Sumps and Shutdown Cooling System.

, initial ins esdgation found a PCIS fuse blown. Operations declared a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Limiting Condition for Operation (LCO) per Technical Specifications ( TS) 3.6.C.4 for the inoperability of the drywell Coor and equipment drain sumps. hiaintenance personnel inves'lgated and found that a failed PCIS relay coil had caused the blown fuse. They replaced the failed relay coil, and the dryw cli Door and equipment drain system was thereby reestablished, and the LCO exited. The total duration of this cvent Was approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and within TS requirements. This failed relay (a CR120A model) had been in service, in the normally.cnergized state, for approximately 23 years, it is believed that the failure is age related, and that degradation had escalated rapidly since the previous thermography inspection . To preclude further system interruptions, coil replacement of the remaining 16 normally energized CR120A relay coils is scheduled to be accomplished by st rtup from i

Refuel Outage l$, projected for hiay 1998 (LER #9710).

Iicensine Action Summary:

i Plant Availability: 83.0 % Unplanned Auto Scrams (while/ critical) this month: 0 .

Number of reportable events: 1 Unplanned Auto Scrams (while/ critical)last 12 months: 0

, -- -._- , - . - . - - . . - - - -._ - .