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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARNG-99-1415, Monthly Operating Rept for Sept 1999 for Daec.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Daec.With NG-99-1226, Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With NG-99-1115, Monthly Operating Rept for July 1999 for Daec.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Daec.With NG-99-0963, Monthly Operating Rept for June 1999 for Daec.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Daec.With NG-99-0835, Monthly Operating Rept for May 1999 for Daec.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Daec.With NG-99-0682, Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With NG-99-0530, Monthly Operating Rept for Mar 1999 for Daec.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Daec.With NG-99-0330, Monthly Operating Rept for Feb 1999 for Daec.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Daec.With NG-99-0020, Monthly Operating Rept for Dec 1998 for Daec.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Daec.With NG-98-2010, Monthly Operating Rept for Nov 1998 for Daec.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Daec.With NG-98-1875, Monthly Operating Rept for Oct 1998 for Daec.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Daec.With NG-98-1717, Monthly Operating Rept for Sept 1998 for Daec.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Daec.With ML20153B4141998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DAEC NG-98-1389, Monthly Operating Rept for July 1998 for DAEC1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DAEC ML20236R3251998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DAEC ML20249B5171998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DAEC ML20247H9381998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DAEC ML20216F6791998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for DAEC NG-98-0650, Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center NG-98-0398, Monthly Operating Rept for Feb 1998 for DAEC1998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for DAEC NG-98-0252, Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center NG-98-0017, Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center1997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center NG-97-2118, Monthly Operating Rept for Nov 1997 for DAEC1997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DAEC NG-97-1959, Monthly Operating Rept for Oct 1997 for DAEC1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for DAEC NG-97-1781, Monthly Operating Rept for Sept 1997 for Duane Arnold Energy Center1997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Duane Arnold Energy Center ML20217C3491997-08-31031 August 1997 Revised MOR for Aug 1997 for DAEC ML20210V1851997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for DAEC NG-97-1452, Monthly Operating Rept for July 1997 for DAEC1997-07-31031 July 1997 Monthly Operating Rept for July 1997 for DAEC NG-97-1258, Monthly Operating Rept for June 1997 for DAEC Per GL 97-021997-06-30030 June 1997 Monthly Operating Rept for June 1997 for DAEC Per GL 97-02 NG-97-1033, Monthly Operating Rept for May 1997 for Duane Arnold Energy Center1997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Duane Arnold Energy Center NG-97-0894, Monthly Operating Rept for Apr 1997 for Duane Arnold Energy Ctr1997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Duane Arnold Energy Ctr NG-97-0674, Monthly Operating Rept for Mar 1997 for Duane Arnold Energy Ctr1997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Duane Arnold Energy Ctr NG-97-0453, Monthly Operating Rept for Feb 1997 for Duane Arnold Energy Center1997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Duane Arnold Energy Center NG-97-0308, Monthly Operating Rept for Jan 1997 for Duane Arnold Energy Center1997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Duane Arnold Energy Center NG-97-0059, Monthly Operating Rept for Dec 1996 for Duane Arnold Energy Center1996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Duane Arnold Energy Center NG-96-2647, Monthly Operating Rept for Nov 1996 for Duane Arnold Energy Center1996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Duane Arnold Energy Center NG-96-2447, Monthly Operating Rept for Oct 1996 for Duane Arnold Energy Center1996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Duane Arnold Energy Center NG-96-2166, Monthly Operating Rept for Sept 1996 for DAEC1996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for DAEC NG-96-1913, Monthly Operating Rept for Aug 1996 for DAEC1996-08-31031 August 1996 Monthly Operating Rept for Aug 1996 for DAEC NG-96-1713, Monthly Operating Rept for Jul 1996 for DAEC1996-07-31031 July 1996 Monthly Operating Rept for Jul 1996 for DAEC NG-96-1481, Monthly Operating Rept for June 1996 for Duane Arnold Energy Ctr1996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Duane Arnold Energy Ctr NG-96-1298, Monthly Operating Rept for May 1996 for Duane Arnold Energy Center1996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Duane Arnold Energy Center NG-96-1055, Monthly Operating Rept for Apr 1996 for Duane Arnold Energy Center1996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Duane Arnold Energy Center NG-96-0825, Monthly Operating Rept for Mar 1996 for DAEC1996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for DAEC NG-96-0624, Monthly Operating Rept for Feb 1996 for DAEC1996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for DAEC NG-96-0320, Monthly Operating Rept for Jan 1996 for DAEC1996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for DAEC ML20096C3101995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Duane Arnold Energy Ctr NG-95-3516, Monthly Operating Rept for Nov 1995 for Duane Arnold Energy Ctr1995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Duane Arnold Energy Ctr NG-95-3235, Monthly Operating Rept for Oct 1995 for Duane Arnold Energy Ctr1995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Duane Arnold Energy Ctr NG-95-3057, Monthly Operating Rept for Sept 1995 for Duane Arnold Energy Ctr1995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Duane Arnold Energy Ctr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H8991999-10-18018 October 1999 SER Approving Licensee Requests for Relief NDE-R001 (Part a & B),NDE-R027,NDE-028,NDE-R029,NDE-R030,NDE-R032 & NDE-R035. Relief Request NDE-036,denied & Relief Request NDE-R-034, Deemed Unnecessary NG-99-1415, Monthly Operating Rept for Sept 1999 for Daec.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Daec.With ML20212H2381999-09-22022 September 1999 Safety Evaluation Supporting Amend 228 to License DPR-49 NG-99-1226, Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With NG-99-1115, Monthly Operating Rept for July 1999 for Daec.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Daec.With NG-99-0963, Monthly Operating Rept for June 1999 for Daec.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Daec.With ML20195G9901999-06-0909 June 1999 Safety Evaluation Supporting Amend 227 to License DPR-49 NG-99-0835, Monthly Operating Rept for May 1999 for Daec.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Daec.With ML20206N7551999-05-13013 May 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safey-Related Power-Operated Gate Valves NG-99-0682, Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With NG-99-0530, Monthly Operating Rept for Mar 1999 for Daec.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Daec.With ML20207G0251999-03-0303 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety- Related MOVs at Duane Arnold & That Licensee Adequately Addressed Actions Requested in GL 96-05 NG-99-0330, Monthly Operating Rept for Feb 1999 for Daec.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Daec.With ML20202B4311999-01-26026 January 1999 Safety Evaluation Accepting Request for Approval to Use ASME Code Case N-508-1 in ISI Program for Duane Arnold Energy Ctr ML20202B3851999-01-26026 January 1999 Safety Evaluation Addressing Thermo-Lag Related Ampacity Derating Issues.Ampacity Derating Analysis Results Acceptable NG-99-0020, Monthly Operating Rept for Dec 1998 for Daec.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Daec.With ML20206N3211998-12-0707 December 1998 Final Part 21 Rept Re Piston Failure of MSIV Actuator at Daec.Rept Indicates That No Reportable Defect Exists,Per 10CFR21 NG-98-2010, Monthly Operating Rept for Nov 1998 for Daec.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Daec.With ML20196F9571998-11-24024 November 1998 Rev 20 to QA Program Description,Ufsar 17.2 for Daec NG-98-1875, Monthly Operating Rept for Oct 1998 for Daec.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Daec.With NG-98-1767, Cyclic Rept of Facility Changes,Tests & Experiments,Fire Plan & Commitment Changes,For Period from 970301-980930. with1998-09-30030 September 1998 Cyclic Rept of Facility Changes,Tests & Experiments,Fire Plan & Commitment Changes,For Period from 970301-980930. with NG-98-1717, Monthly Operating Rept for Sept 1998 for Daec.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Daec.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML20153B4141998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DAEC NG-98-1389, Monthly Operating Rept for July 1998 for DAEC1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DAEC ML20236X5321998-07-29029 July 1998 Safety Evaluation Re USI A-46 Program Implementation for Plant ML20236W0021998-07-29029 July 1998 Safety Evaluation Accepting Request for Relief NDE-R020 Re Third 10-yr ISI Interval of Plant,Per 10CFR50.55a(a)(3(i) ML20236S2541998-07-14014 July 1998 Special Rept 98-01:on 980629,diesel-driven Fire Pump Was Inoperable for Greater than Seven Days.Caused by Sheared Off Tie Rods on Accessory Drive End of Engine.Evaluated Condition,Procured Parts & Replaced Tie Rods ML20236R3251998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DAEC ML20249B5171998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DAEC ML20247P5651998-05-18018 May 1998 Part 21 Rept Re Model SA-A101 MSIV A' Actuator Showing Evidence of Internal Leakage,In Both Directions Past Pneumatic Piston.Situation Being Reviewed to Determine If Failure Could Pose Substantial Safety Hazard ML20247K1881998-05-0808 May 1998 Rev 0 to Cycle 16 COLR, for May 1998 ML20247H9381998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DAEC ML20217K7251998-04-16016 April 1998 Correction to SE of Relief Request MC-R001 Re Qualification Requirements for non-destructive Exam Personnel Performing Containment Insp ML20216J9171998-04-16016 April 1998 Safety Evaluation Accepting Relief Request MC-R001 for First 10-yr Interval of Containment Insp Program Per 10CFR50.55a (a)(3)(ii),per 971219 Request ML20217K0471998-04-0101 April 1998 Safety Evaluation Authorizing Proposed Alternative in Relief Request NDE-R004 for Plant Third 10-yr ISI Interval,Based on Finding That Compliance W/Code Would Result in Hardship W/O Compensating Increase in Level of Quality & Safety ML20217H8831998-04-0101 April 1998 Safety Evaluation Supporting Request for Relief for Third ISI Program ML20216F6791998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for DAEC NG-98-0650, Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center ML20217F8841998-03-23023 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Program Plan Requests for Relief for Plant NG-98-0398, Monthly Operating Rept for Feb 1998 for DAEC1998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for DAEC ML20199L3481998-01-31031 January 1998 Rev 0 to Duane Arnold Energy Ctr Emergency Action Level (EAL) Technical Basis Document NG-98-0252, Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center ML20249B3391997-12-31031 December 1997 Central Iowa Power Coopertive 1997 Annual Rept ML20249B3351997-12-31031 December 1997 1997 Annual Rept for Corn Belt Power Cooperative ML20249B3331997-12-31031 December 1997 1997 Annual Rept for Alliant Corporation NG-98-0017, Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center1997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center NG-97-2118, Monthly Operating Rept for Nov 1997 for DAEC1997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DAEC ML20199J6841997-11-21021 November 1997 SER Approving Relief Requests to Second 10-year Inservice Inspection Interval for Duane Arnold Energy Center NG-97-1959, Monthly Operating Rept for Oct 1997 for DAEC1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for DAEC 1999-09-30
[Table view] |
Text
< ! . 327104fC Appd
,e Poh IA s2324 Tewnone 319 8517611 fas 319 8517611 UTILITIES December '5,1997 NO 97-2118 Mr. A. Bill ceach Regional Administrator Region 111 U.S. Nuclear Regulatory Commission 801 Warrenville Road Lisle,IL 60532-4351
Subject:
Duane Arnold Energy Center Docket No: 50-331 Operating License: DPR-49 November 1997 Monthly Operating Report File: A 118d
Dear Mr. Beach:
Please find enclosed the Duane Amold Energy Center Monthly Operating Report for November 1997. The report has been prepared in accordance with the guidelines of NRC Generic Letter 97-02: Revised Contents Of The Monthly Operating Report and distribution has been made in accordance with DAEC Technical Specifications, Section 6.ll.l.c.
Very truly yours, lb Gary VanMiddlesworth
=s Y
Plant Manager-Nuclear <(/
s GDV/RDW g Enclosures
.:60353 9712230307 971130
. ll!I.lill!Il. !.ll.II. Il.l PDR ADOCK 05000331 R PDR A9 IES Incastna Company
Mr. A. Bill Beach NO 97 2118 December 15,1997 Page 2 0f 2 ;
-cc: i U.S.Nmlear Regulatory Commission Ms. Lisa Stump i Atta: Document Control Desk lowa State Utilities Board [
s- Mall Station Pl-37 Lucas State Office Building j i Washington, DC 20555-0001 (Orig.) Des Moines,IA 50319 -i Ms. Barbara Lewis -
Dr. William A. Jacobs, Jr.
McGraw lilli,Inc. ODS Associates,Inc. ;
- 1200 0 Street NW, Suite 1100 1850 Parkway Place, Suite 720 i
. Washington, DC 20005 Marietta, GA 30068-8237 l
Mr. Dennis Murdock Mr. Dale Arends !
t Centrallowa Power Cooperative Corn Belt Power Cooperative l Box 2517 130013th Street North !
Cedar Rapids,IA 524% liumboldt,IA 50548 l.
Document Control Dek Mr. Al Outterman j INPO P.ecords Center Morgan, Lewis, Bochius l 700 Galleria Parkway 1800 M St.N W ;
Atlanta, OA 30339 5957 Washington, DC 20036-5859 l l
Mr. Olenn Kelly DOCU Project Manager !
I Whitellint North NRC Resident Inspector Mail Stop 13E21 ,
11555 Rockville Pike !
Rockville, MD 20852 i
t
i
, . OPERATING DATA REPORT DOCKET NO. 50-0331 i DATE: 12/15/97 l
{ Unit: Duane Amold Encrev Center '
- COMPLETED BY
- Richard Woodward i TELEPilONE: f 3191851-7318 l OPERATING STATUS ;
Aw: rage Daily Power Level f ,
- 1. Unit Name: Duane Arnold Enerry Center 500 l
! 2. Reporting Period: November 1997 400
- 3. Licensed Thermal Power (MW th ): Ifil l 4. Nameplate Rating (Gross MWe DER): 565.7 (Turbine) $ I 2200
- 5. Design Electrical Rating (Net MWe DER): 111
- 6. Maximum Dependable Capacity (Gross MW e MDC): M9
! 0
- 7. Maximum Dependable Capacity (Net MW e MDC): flQ
.: I 6 11 16 21 26
- 8. If Changes Occur in Capacity Ratings (items Number 3 through Day ,
- 7) since the last report, Give Reasons
- Not Aeolicable
- 9. Power Level to Which Restricted, if Any (Net Mw e ): E
- 10. Reasons for Restrictions, if Any: N/A
- November-97 1997 Cumulative l 11. IIours in Reporting Period 720.0 8,016.0 200,136.0
- 12. Number ofIlours Reactor Was Critical 720.0 7,528.5 154,022.5
- 13. Reactor Resene Shutdown llours 0.0 0.0 192.8
! 14. IIours Generator On-Line 720.0 7,384.0 150,405.1
! 15. Unit Reserve Shutdown Hours 0.0 0.0 ~E6
- 16. Gross lhermal Energy Generated (MWH) 1,180,377.6 11,839,843.9 213,492,955.0 Gross Electrical Energy Generated (MWH) 404,210.0 3,987,760.0 71,576,806.6 1 . Net Electiical Energy Generated (MWH) 381,623.0 3,762,903.9 67,178,462.9 l . Unit Service Factor 100.0 % 92.1 % 75.2 % I
. Unit Availability Factor 100.0 % 92.1 % 75.2 %
l . Unit Capacity Factor (Using MDC Net) 101.9 % 90.3 % 70.7 % i
. 22. Unit Capacity Factor (Using DER Net) 98.5 % 87.3 % 67.7 %
- 23. Unit Forced Outage Rate 0.0% 1.4% 9.8% i l 24. Shutdowm Scheduled Over Next 6 Months (Type, Date, and Duration of each)
- Refueling, April 2,1998,45 days ,
- 25. If Shutdown at End of Report Period. Estimated Date of Startup: N/A f
i
. . . -. _. ._ -._ _ . - - _- .- -- . - . . _ . - . _. ~- . . . -. -
I AVERAGE DAILY UNIT POWER LEVEL DOCKET NO: $0-0331 DATE: 12/15/97 Unit: Duane Amold Enerav Center ,
COMPLETED BY: Richard Woodward i TELEPHONE: O 19)851 7318 l
MONTil November 1997 i i
Day Average Daily l Power Level .
I blU l Z . 421.9 !
3 331.9 i 4 334.9 }i 3 329.7 6 339.1 ,
7 333.5 5 334.6 ..
333.7 9
10 330.2 11 339.1 12 334.6 l'
13 337.1 lb 337.0 17 336.7 15 337.1 !
19 337.7 20 ~ TER 21 537.4 22 337.4 23 335.2 4 24 337.6 23 333.2 26 533.
27 330.0 j 25 334.5 29 332.5 30 455.4 31 #N/A l
L y , , = , , , , _ ,yy -
- c. s. , .n iy.. ,, . , , _ . , . - , . _ . - , y..
REFUELING INFORMATION
- . DOCKET NO: 50-0331 DATE: 12/15/97 !
Unit: Duane Arnold Energy Center COMPLETED BY: Richard Woodward :
TELEPHONE: (319) 85173I B l
- 1. Nasme ofincility. !
Duane Arnold Energy Center >
- 2. Scheduled date for next refueling shutdown.
April 2,1998
- 3. Scheduled date for restart following refueling.
- - May 17,1998
- 4. Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?
Yes. RTS 296, proposes fuel discharge as early as 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> after shutdown (versus current 120 hour0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> >
requirement),
improved Technical Specifications (ITS) approval needed for refuel outage planning. :
- 5. Scheduled dale (s) for submit:Ing proposed licens.ag action and supporting information.
RTS 296, " Refueling Operations" submitted October 3,1997.
N/A. (ITS submitted October 30,1996.)
- 6. Important ficensing considerhtions associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
N/A
- 7. Current and projected fuel assemblies inventory:
Number of Fuel Projected date oflast Assemblies refueling that can be discharged ,
(after allowing margin for maintenance of continuous full core
_ discharge capability _)_
_ _ _ _ Installed in reactor core (following refueling) 368 n/a pisc}arged fmm, core to Spent Fuel Storage Pool 1528 n/a Installed Capacity of Spent Fuel Storage Pool 2411 2001 L_icensed Capact!y_of Spent Fuel Storage Pool (with rcracking) 2829 2006 Licensed Capacity of S,nent Fuel Storage Pool and Cask Pool 3152 2010 (with veracking) t
i
, t .
. a - :
DOCKET NO.: 50-0331 DATE: 12/15/97 Unit: Duane Arnold Enercy Center COMPLETED BY: Richard Woodward TELEPHONE: (3191 851-7318 Monthly Operational Overview for November 1997:
De plam operat.d at full licensed thennal power throughout the month except:
- !1/01/97 21:00. I1/03/97 01:45, to perform a control rod sequence exchange and turbine testing e 11/03/9712:00 15:15, to reduce recirculation flow to pull control rods to increase reactor load line (rod pull) e i1/04/97 02:30 01:45, rod-pull e 11/05/97 09:50 13:30, to pertorm High Pressure Coolant Injection (HPCI) Operability testing e 11/06/9713:30 20.00, for testing of the plant process computer '
e i1/07/9712:00 16:30, for testing of the plant process cutapt:Tr e 11/11/9714:00 14:30, to adjust electro-hydraulic (EHC) system pressure-set bias ;
e 11/12/97 01:00 03:00, rod-pull e 11/21/9710:20 16:00, to perform maintenance on the plant process computer -
e 11/29/97 23:00 11/30/9714:00 to perform turbine control valve testing. '
ne total of these capacit, losses amounted to the equivalent of 6.3 full power hours (FPH,,). Other generation losses (those which would occur even at continuous full thermal power operation) netted to -0.9 FPH,,. (Negative net losses result from cooler-than-design (seasonal) circulation water temperatures at the condenser inlet).
Allocation of Production & Losses: Electncal Capacity I actor I ull Power Output % of 565.7 MWs Equivalent MWe (Design Rating) llours (FPIteq)
Actual Metered Net 1:lectric Output 53D=0 93.7% 674 6 Actur.: Metered Plant Flectric leads 314 56% 40 0 Ofr 1.ine Capacity losses: 00 0 0'r. 0.o MhUnplannad Capachv lasses: 00 0.0% 0.0 Vormal Capacity Losses (Avg '/ill Powr" MWth < 165s) 03 0.1% OA 21;Ltug PJunned Capecuy lesses:
11/13: 4 4 FPileg (CRD sequence exchange)
I1/2940; 1.5 fPlicq (Rod pull,Turbbe Control Valve testing) 46 0.7% $M (ner ) Weather losics - condenser pressure <2.75 In lig / Circ Water Temp < 74.5 'F 33 06% 4.3 l'.mcicney Losses (Weather-Norm-Ihtt-rowr ArWe > 565.7 D sign) 00 00% Of Metering 14sses(Avg indic AfWe Avg A(W//e) 2.7 0.5% 3.4 Cucluded losses (const down, lack or grid demand, etc.) gf gyj Q1 Design Grose Electric Output E E 212,2 At 2022 on November 13,1997, with the plant operating at 100% power, a spurious primary containment isolation system (pCIS) group VI isolation occurred which resulted m the automatic closure of the outboard liactor Core Isolation Cooling (RCIC) steam supply isolation valve. De isolation signal originated from a RCiC room area differential temperature switch and continued for approximately 38 seconds before resetting itself. Operators dispatched to the RCIC toom continned that a stear. leak did not exist. The saspect switch, which had been installed in September 1997, was replaced and the isolation was cleared. Folicwing the isolation, extensive testing failed 10 indicate a cause for the event. He isoladon is considered to be spurious, here wano effect on plant operation or safety During the time the isolation was present, RCIC was
. inoperable, llowever, RCIC h not considered an emergency core cooling system and credit is not taken for RCIC to mitigate any accidents described in the safety analysis. LERN9712 Licensing Action Summary:
Plant Availability: 100.0 % Unplanned Anu Scrams (while/ critical) this month: 0 Nurnber of reportable events: 1 Unplanned Auto Scraria (while/ critical)last 12 months: 0
DOCKETNO: 50-03]l DATE: 12/1567 Unit - Duane Arnold Enerry Center COMPLETED BY: Richard Woodward TELEPHONE: G19) 351-7318 UNIT SHUIDOWNS AND PO%IR REDUCTIONS REPORT MONDL November 1997 No. Date Type Duration Reason Method of Licensee Event Syvem Code Comp. Code . Cause .
(1) (Hours) (2) Shutting Report # (4) (5)
Dowin Reactor (3) 12 11/1-367 S 0 B 5 NA- TA PCV To perform control:od pattern sequence exchange (5.4 full- and turbine control valve testing, power-hours equsvalent) -
'1 - F: Forced Reason 3 - Method. 4 - Exhibit G-Instructions for S: Scheduled A-Equipment Failure (Explain) 1-Manual Preparation ofData Entry I B-Maintenance or Test 2-Manual Scram Sheets for Licensee Event C-Refueling 3-Automatic Scram Report (LER) File (NUREG-D-Regulatory Ros n. Gun 4-Continued 0161) ,
E-Operator Training & License Exarnination 5-Reduced Load '
F-Administrative 9-Other(Explain) 5 -Exhibst I (Same Source)
G-Operanonal Error (Explain)
H-Other(Exclain)
L e
t-a*
S e . .
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--4.-. . . . . ~ . . . . . - , _