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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217K3301999-10-19019 October 1999 Safety Evaluation Supporting Amend 195 to License DPR-61 ML20206C8761999-04-28028 April 1999 Safety Evaluation Supporting Amend 194 to License DPR-61 ML20238F2131998-08-28028 August 1998 SER Accepting Defueled Emergency Plan for Emergency Planning for Connecticut Yankee Atomic Power Co ML20202D1621998-06-30030 June 1998 Safety Evaluation Supporting Amend 193 to License DPR-61 ML20217K2101998-03-27027 March 1998 Safety Evaluation Supporting Amend 192 to License DPR-61 ML20198M8101997-10-14014 October 1997 SER Accepting Proposed Revs to Util Quality Assurance Program at Facility ML20141K4201997-05-22022 May 1997 Safety Evaluation Supporting Amend 191 to License DPR-61 ML20024J2081994-10-0707 October 1994 SER Authorizing Alternatives Contained in Request for Relief 3-26,per 10CFR50.55(a)(3)(i).Ack Withdrawal of Request for Relief 3-19 ML20058F1151993-11-23023 November 1993 Safety Evaluation Supporting Amends 170,69,169 & 86 to Licenses DPR-61,DPR-21,DPR-65 & NPF-49,respectively ML20059G6411993-11-0101 November 1993 Safety Evaluation Supporting Amend 169 to License DPR-61 ML20059G5261993-10-27027 October 1993 Safety Evaluation Supporting Amend 168 to License DPR-61 ML20057E2011993-10-0404 October 1993 Safety Evaluation Supporting Amend 167 to License DPR-61 ML20057E1921993-10-0404 October 1993 Safety Evaluation Supporting Amend 166 to License DPR-61 ML20058M9291993-09-29029 September 1993 SE Re SEP Topics III-2 & III-4.A, Wind & Tornado Loadings & Tornado Missiles. Licensee Estimated Reactor Core Damage Frequency Reduced Signficantly Such That Likelihood of Core Damage Reasonably Low ML20058M9051993-09-29029 September 1993 Safety Evaluation Supporting Amend 165 to License DPR-61 ML20057A3551993-09-0202 September 1993 Safety Evaluation Supporting Amend 163 to License DPR-61 ML20057A3501993-09-0202 September 1993 Safety Evaluation Supporting Amend 164 to License DPR-61 ML20056G2891993-08-25025 August 1993 Safety Evaluation Supporting Amend 162 to License DPR-61 ML20056D7061993-07-26026 July 1993 Safety Evaluation on SEP VI-4 Re Containment Isolation Sys for Plant.All Penetrations Either Meet Provisions of or Intent of GDCs 54-57 Except for Penetration 39 ML20046C1971993-07-20020 July 1993 SE Granting Relief Request P-9 from Vibration Testing Requirements,Based on Determination That Compliance W/ Vibration Amplitude Measurement Location Requirements Impractical ML20046B3581993-07-14014 July 1993 Safety Evaluation Supporting Amend 161 to License DPR-61 ML20045G6731993-07-0909 July 1993 SER Authorizing Proposed Alternative Tests Per 10CFR50.55a(a)(3)(i).Concludes That Acceptable Level of Quality & Safety Will Be Maintained Using Proposed Alternative Tests Instead of Required Hspt ML20045G6781993-07-0909 July 1993 SER Accepting Licensee Proposed Alternative to ASME Code Section XI Requirements Per 10CFR50.55a(a)(3)(i) ML20045F3931993-06-28028 June 1993 Safety Evaluation Supporting Amend 160 to License DPR-61 ML20045B8061993-06-11011 June 1993 Safety Evaluation Supporting Amend 159 to License DPR-61 ML20044D7921993-05-17017 May 1993 Safety Evaluation Supporting Amend 157 to License DPR-61 ML20035F1421993-04-14014 April 1993 Safety Evaluation Re SEP Topic III-5.A, Effects of Pipe Breaks Inside Containment ML20128E3291993-02-0404 February 1993 Safety Evaluation Granting Util Request for Authorization to Use Portion of Section XI of 1986 Edition of ASME Code for Visual Exams VT-3 & VT-4 to Be Combined Into Single VT-3 ML20128D5231992-11-25025 November 1992 Safety Evaluation Accepting 120-day Response to Suppl 1 to Generic Ltr 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Usi A-46, ML20210E1891992-06-12012 June 1992 Safety Evaluation Considers SEP Topic III-5.B to Be Complete in That If Pipe Breaks Outside Containment,Plant Can Safely Shut Down W/O Loss of Containment Integrity ML20062B7411990-10-22022 October 1990 Safety Evaluation Supporting Amend 132 to License DPR-61 ML20059H3101990-09-0606 September 1990 Revised Safety Evaluation Clarifying Individual Rod Position Indication Testing Exception & Bases for Approving Test Exception ML20059A8021990-08-14014 August 1990 Supplemental Safety Evaluation Accepting Electrical Design of New Switchgear Room at Plant ML20056A5641990-08-0303 August 1990 Safety Evaluation Concluding That Pressurizer Has Sufficient Fracture Toughness to Preclude Fracture of Head W/Flaws Remaining in Component & Pressurizer Acceptable for Continued Svc ML20055G5441990-07-19019 July 1990 Safety Evaluation Supporting Amend 128 to License DPR-61 ML20055G5561990-07-19019 July 1990 Safety Evaluation Supporting Amend 129 to License DPR-61 ML20044A9691990-07-0909 July 1990 Safety Evaluation Supporting Amend 127 to License DPR-61 ML20055E2361990-07-0202 July 1990 Safety Evaluation Supporting Amend 126 to License DPR-61 ML20034C5771990-04-26026 April 1990 Safety Evaluation Supporting Amend 125 to License DPR-61 ML20034A0481990-04-10010 April 1990 Safety Evaluation Granting Exemption Requests from App R ML20012E5021990-03-21021 March 1990 Safety Evaluation Re Reactor Protection Sys Upgrade Phase 1. Sys & Hardware Design Provides Reasonable Assurance to Perform Safety Functions Per Updated FSAR & Tech Specs ML20012E2001990-03-12012 March 1990 Safety Evaluation Accepting Plant Auxiliary Feedwater Actuation Sys as Complying W/Requirements of ATWS Rule 10CFR50.62(c)(1) ML20012E1991990-03-12012 March 1990 Safety Evaluation Concluding That Plant Adequately Meets Intent of 10CFR50.62 & Exempt from Further Mods to Provide Turbine Trip on Indications of ATWS ML20006B4011990-01-22022 January 1990 Safety Evaluation Accepting Proposed Electrical Sys Changes for Fire Protection ML19324B3851989-10-24024 October 1989 Safety Evaluation Supporting Amends 124,35 & 144 to Licenses DPR-61,DPR-21 & DPR-65,respectively ML19325D8631989-10-18018 October 1989 Safety Evaluation Concluding That Large Containment Results in Slow Hydrogen Accumulation Rate & Ensures That Sufficient Time Available to Implement Addl Hydrogen Control Features as May Be Necessary Following Accident ML20247K2531989-09-11011 September 1989 Safety Evaluation Supporting Amends 123 & 41 to Licenses DPR-61 & NPF-49,respectively ML20247E3761989-09-0707 September 1989 Safety Evaluation Supporting Amends 122,34,143 & 40 to Licenses DPR-61,DPR-21,DPR-65 & NPF-49,respectively ML20247A4841989-09-0505 September 1989 Safety Evaluation Supporting Amend 121 to License DPR-61 ML20245J0121989-08-14014 August 1989 Safety Evaluation Accepting Extension of Surveillance Intervals 1999-04-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K3301999-10-19019 October 1999 Safety Evaluation Supporting Amend 195 to License DPR-61 ML20206C8761999-04-28028 April 1999 Safety Evaluation Supporting Amend 194 to License DPR-61 CY-99-047, Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use1999-03-23023 March 1999 Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use 05000213/LER-1999-001, :on 990105,main Stack RM R-14A Pressure Compensating Signal Was Not Calibrated.Caused by Personnel Error.Revised Calibration Procedure.With1999-02-0101 February 1999
- on 990105,main Stack RM R-14A Pressure Compensating Signal Was Not Calibrated.Caused by Personnel Error.Revised Calibration Procedure.With
05000213/LER-1997-016, :on 970825,discovered That Negative Pressure Was Not Maintained in Sf Bldg,Per Design Basis.Caused by Sf Bldg Ventilation Sys Being Based on Lower Pab Ventilation Flow Rates.Corrected Ventilation Sys Design.With1999-01-25025 January 1999
- on 970825,discovered That Negative Pressure Was Not Maintained in Sf Bldg,Per Design Basis.Caused by Sf Bldg Ventilation Sys Being Based on Lower Pab Ventilation Flow Rates.Corrected Ventilation Sys Design.With
ML20206F1971998-12-31031 December 1998 Annual Rept for 1998 for Cyap. with CY-99-027, Annual Rept for 10CFR50.59, for Jan-Dec 1998.With1998-12-31031 December 1998 Annual Rept for 10CFR50.59, for Jan-Dec 1998.With ML20198G9101998-12-22022 December 1998 Proposed Rev 2 of Cyap QAP for Haddam Neck Plant. Marked Up Rev 1 Included 05000213/LER-1997-018, :on 971003,discovered That Sf Bldg Exhaust Fan Did Not Meet Design Basis.Caused by Higher than Expected Pressure in Pab.Design of Sf Bldg Ventilation Sys Was Corrected.With1998-12-0808 December 1998
- on 971003,discovered That Sf Bldg Exhaust Fan Did Not Meet Design Basis.Caused by Higher than Expected Pressure in Pab.Design of Sf Bldg Ventilation Sys Was Corrected.With
05000213/LER-1998-009, :on 980915,noted Excessive CV,SW-CV-963,seat Leakage in SW Supply Piping to SFP Heat Exchangers.Caused by Subject Cv Disc Being Stuck in Open Position.Valve Was Exercised & Freed from Stuck Open Position.With1998-10-14014 October 1998
- on 980915,noted Excessive CV,SW-CV-963,seat Leakage in SW Supply Piping to SFP Heat Exchangers.Caused by Subject Cv Disc Being Stuck in Open Position.Valve Was Exercised & Freed from Stuck Open Position.With
05000213/LER-1998-008, :on 980721,determined That Main Stack Radiation Monitor RMS-14B Samples Were Not Analyzed to Required Detection Level.Caused by Inadequate Design.Immediately Controlled Temp of Radiation Monitor Room.With1998-09-29029 September 1998
- on 980721,determined That Main Stack Radiation Monitor RMS-14B Samples Were Not Analyzed to Required Detection Level.Caused by Inadequate Design.Immediately Controlled Temp of Radiation Monitor Room.With
05000213/LER-1997-021, :on 971124,found Contaminated Matls Offsite. Caused by Breakdown of Health Physics Program in Effect at Time Contaminated Matl Was Released from Site.Revised Procedures.With1998-09-0101 September 1998
- on 971124,found Contaminated Matls Offsite. Caused by Breakdown of Health Physics Program in Effect at Time Contaminated Matl Was Released from Site.Revised Procedures.With
ML20238F2131998-08-28028 August 1998 SER Accepting Defueled Emergency Plan for Emergency Planning for Connecticut Yankee Atomic Power Co 05000213/LER-1998-007, :on 980714,excessive Check Valve Seat Leakage in SW Supply Piping to SFP Heat Exchangers,Occurred.Caused by SW-CV-963 Disc Sticking in Open Position.Increased Test Frequency from Quarterly to Monthly1998-08-13013 August 1998
- on 980714,excessive Check Valve Seat Leakage in SW Supply Piping to SFP Heat Exchangers,Occurred.Caused by SW-CV-963 Disc Sticking in Open Position.Increased Test Frequency from Quarterly to Monthly
CY-98-136, Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line1998-08-12012 August 1998 Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line ML20237B7461998-07-22022 July 1998 1998 Defueled Emergency Plan Exercise Scenario Manual, Conducted on 980722 ML20202D1621998-06-30030 June 1998 Safety Evaluation Supporting Amend 193 to License DPR-61 05000213/LER-1998-005, :on 980511,determined That Design Deficiency Was Found in Main Stack Flow Rate Monitor.Caused by 1974 Mod Change on Original Installation.Declared F-1101 Channel Out of Svc & Develop Means of Estimating Flow1998-06-0909 June 1998
- on 980511,determined That Design Deficiency Was Found in Main Stack Flow Rate Monitor.Caused by 1974 Mod Change on Original Installation.Declared F-1101 Channel Out of Svc & Develop Means of Estimating Flow
05000213/LER-1998-006, :on 980507,design Deficiency Was Found in Stack RM RMS-14B Sampling Lines.Caused by Design Not Meeting ANSI N13.1-1969 Stds.Corrective Action Plan for RMS-14B Is Being Developed1998-06-0808 June 1998
- on 980507,design Deficiency Was Found in Stack RM RMS-14B Sampling Lines.Caused by Design Not Meeting ANSI N13.1-1969 Stds.Corrective Action Plan for RMS-14B Is Being Developed
05000213/LER-1998-004, :on 980507,discovered Design Deficiency in Stack Radiation Monitor RMS-14B Isokinetic Sampling.Caused by Failure to Account for Spent Fuel Bldg Ventilation Flow. Will Develop CAP for RMS-14B1998-06-0404 June 1998
- on 980507,discovered Design Deficiency in Stack Radiation Monitor RMS-14B Isokinetic Sampling.Caused by Failure to Account for Spent Fuel Bldg Ventilation Flow. Will Develop CAP for RMS-14B
05000213/LER-1998-003, :on 980505,compensatory Sampling Frequency Exceeded Time Limit W/Sw Effluent RM Inoperable.Caused by Personnel Error.Individual Was Counseled & Technicians Were Reminded of Sampling within Required Frequency1998-06-0202 June 1998
- on 980505,compensatory Sampling Frequency Exceeded Time Limit W/Sw Effluent RM Inoperable.Caused by Personnel Error.Individual Was Counseled & Technicians Were Reminded of Sampling within Required Frequency
05000213/LER-1998-002, :on 980421,determined That Visual Insp of Switchgear Cable Shaft Sprinkler Sys Was Not Being Performed Once Per 18 Months.Caused by Inadequate Implementation of License Amend.Fire Watch Patrol Established1998-05-19019 May 1998
- on 980421,determined That Visual Insp of Switchgear Cable Shaft Sprinkler Sys Was Not Being Performed Once Per 18 Months.Caused by Inadequate Implementation of License Amend.Fire Watch Patrol Established
05000213/LER-1998-001, :on 980409,seismic Monitor Sp Was Not in Compliance W/Ts.Caused by Inadequate Engineering Review. Submitted Proposed License Amend to Correct Issue1998-05-0707 May 1998
- on 980409,seismic Monitor Sp Was Not in Compliance W/Ts.Caused by Inadequate Engineering Review. Submitted Proposed License Amend to Correct Issue
CY-98-068, Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms1998-04-15015 April 1998 Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms CY-98-045, Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing1998-04-13013 April 1998 Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing ML20217A0001998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Haddam Neck Plant ML20217F0611998-03-31031 March 1998 Historical Review Team Rept ML20217K2101998-03-27027 March 1998 Safety Evaluation Supporting Amend 192 to License DPR-61 CY-98-046, Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal1998-03-12012 March 1998 Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal ML20216D6531998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Haddam Neck Plant ML20217D7381998-02-28028 February 1998 Revised MOR for Feb 1998 Haddam Neck Plant CY-98-012, Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant CY-98-010, Annual Rept for 10CFR50.59,Jan-Dec,19971997-12-31031 December 1997 Annual Rept for 10CFR50.59,Jan-Dec,1997 ML20198N6681997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Haddam Neck Plant ML20217P4861997-12-31031 December 1997 1997 Annual Financial Rept, for Cyap ML20199L5891997-12-24024 December 1997 Independent Analysis & Evaluation of AM-241 & Transuranics & Subsequent Dose to Two Male Workers at Connecticut Yankee Atomic Power Plant 05000213/LER-1997-020, :on 971117,determined That Radioactive Effluent Dose Calculations Were Not Performed within Required Frequency.Caused by Procedure Inadequacy.Will Revise Procedures & Will Enhance Tracking Process1997-12-16016 December 1997
- on 971117,determined That Radioactive Effluent Dose Calculations Were Not Performed within Required Frequency.Caused by Procedure Inadequacy.Will Revise Procedures & Will Enhance Tracking Process
ML20203K4271997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Haddam Neck Plant 05000213/LER-1997-017, :on 970924,identified Three Locations of Detectable Plant Related Radioactivity in on-site Landfill Area.Caused by Failure to Conduct Adequate Survey.Access to Area Controlled1997-11-18018 November 1997
- on 970924,identified Three Locations of Detectable Plant Related Radioactivity in on-site Landfill Area.Caused by Failure to Conduct Adequate Survey.Access to Area Controlled
05000213/LER-1997-019, :on 970808,compensatory Sampling Frequency Exceeded W/Rms Determined Inoperable.Caused by Personnel Error Due to Incorrect Interpretation of Ts.Compensatory Sampling to Be Conducted in Time Frame Required1997-11-17017 November 1997
- on 970808,compensatory Sampling Frequency Exceeded W/Rms Determined Inoperable.Caused by Personnel Error Due to Incorrect Interpretation of Ts.Compensatory Sampling to Be Conducted in Time Frame Required
ML20199B1141997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Haddam Neck Plant 05000213/LER-1997-018, :on 971003,Spent Fuel Building Exhaust Fan Flow Was Found Below Design During Testing.Caused by Personnel Error.Evaluated Replacement of Spent Fuel Building Exhaust Fan Capable of Overcoming Higher Pressures1997-10-30030 October 1997
- on 971003,Spent Fuel Building Exhaust Fan Flow Was Found Below Design During Testing.Caused by Personnel Error.Evaluated Replacement of Spent Fuel Building Exhaust Fan Capable of Overcoming Higher Pressures
ML20198M8101997-10-14014 October 1997 SER Accepting Proposed Revs to Util Quality Assurance Program at Facility ML20198J8811997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Haddam Neck Plant 05000213/LER-1997-015, :on 970813,functional Testing of Radiation Monitoring Sys Was Not Performed as Defined in Ts.Caused by Lack of Understanding of Definition of Acot.Revised Appropriate RMS Surveillance Procedure1997-09-12012 September 1997
- on 970813,functional Testing of Radiation Monitoring Sys Was Not Performed as Defined in Ts.Caused by Lack of Understanding of Definition of Acot.Revised Appropriate RMS Surveillance Procedure
05000213/LER-1996-027, :on 961010,boron Injection Flow Path Below Minimum Required Temperature Was Determined.Caused by Inadequate Design of Heat Trace Controls in Rtd.Boric Acid Flow Paths from Bamt Were Declared Inoperable1997-09-12012 September 1997
- on 961010,boron Injection Flow Path Below Minimum Required Temperature Was Determined.Caused by Inadequate Design of Heat Trace Controls in Rtd.Boric Acid Flow Paths from Bamt Were Declared Inoperable
05000213/LER-1996-016, :on 960801,potential for Inadequate RHR Pump NPSH During Sump Recirculation Was Determined.Caused by Failure to Fully Analyze Containment Pressure & Sump Temperature Response.Redesign of Piping Proposed1997-09-12012 September 1997
- on 960801,potential for Inadequate RHR Pump NPSH During Sump Recirculation Was Determined.Caused by Failure to Fully Analyze Containment Pressure & Sump Temperature Response.Redesign of Piping Proposed
05000213/LER-1997-014, :on 970808,ESFA Occurred Due to Deenergization of High Containment Pressure Actuation Circuits.Reemphasized Expectations of Mgt for Performing non-routine Operational Tasks1997-09-0505 September 1997
- on 970808,ESFA Occurred Due to Deenergization of High Containment Pressure Actuation Circuits.Reemphasized Expectations of Mgt for Performing non-routine Operational Tasks
05000213/LER-1996-021, :on 960828,valve Leakage Resulted in Nitrogen Intrusion Into RCS During Cold Shutdown.Caused by Leaking Valve BA-V-355.Training Has Been Been Provided to Operators on Event & Features & Limitations of Sys1997-09-0505 September 1997
- on 960828,valve Leakage Resulted in Nitrogen Intrusion Into RCS During Cold Shutdown.Caused by Leaking Valve BA-V-355.Training Has Been Been Provided to Operators on Event & Features & Limitations of Sys
05000213/LER-1996-005, :on 960301,spent Fuel Cooling Was Shut Down Due to Discovery of Loose Parts.Caused by Inadequate Design. Piping from Both Sent Fuel Pool Cooling Pumps to Plate Exchanger Were Inspected for Loose Parts w/bore-a-scope1997-09-0505 September 1997
- on 960301,spent Fuel Cooling Was Shut Down Due to Discovery of Loose Parts.Caused by Inadequate Design. Piping from Both Sent Fuel Pool Cooling Pumps to Plate Exchanger Were Inspected for Loose Parts w/bore-a-scope
1999-04-28
[Table view] |
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1 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION SYSTEMATIC EVALUATION PROGRAM TOPIC III-5.A.
l
" EFFECTS OF PIPE BREAKS INSIDE CONTAINMENT" f
CONNECTICUT YANKEE ATOMIC POWER COMPANY l
1 HADDAM NECK PLANT DOCKET NO. 50-213 j
i 1
1.0 INTRODUCTION
i An evaluation performed by the staff as part of the Systematic Evaluation i
Program (SEP) under SEP Topic III-5.A, " Effects of Pipe Breaks Inside
(
Containment" was forwarded to Connecticut Yankee Atomic Power Company l
(CYAPC0/the licensee) by letter dated October 12, 1982.- In that letter the i
NRC staff concluded that (1) the definition of high energy fluid systems, (2) the determination of high energy pipe break locations and break types and (3) the pipe whip and jet impingement assumptions are generally consistent with currently accepted standards. The staff review, however, did identify the t
following 10 issues concerning pipe breaks inside containment which were not i
adequately addressed:
I
(
1.
cascading effect sequences, l
2.
jet impingement from circumferential breaks, 3.
strain level functionality criteria, 4.
containment integrity criteria, 5.
jet impingement effects on target-piping, 6.
effects on instrumentation, s
7.
main coolant loop breaks, i '
9.
main steam / main feedwater interactions, and 8.
plant shutdown Method 3, j
10.
core deluge piping break effects.
1 By letters dated December 17, 1984, and January 29,.1993, CYAPC0 responded to the above issues. An evaluation of these responses is provided below.
j 2.0 EVALUATION l
2.1 CASCADING EFFECT SEOUENCES 4
By letter dated December 17, 1984, CYAPC0 provided the staff with their review l
of the effects of cascading sequences.
The licensee stated that cascading is i
controlled by separation of piping or by physical barriers. For insttnce, cascading effects due to a pipe break in'a loop area are limited to that particular loop or breaks in the steam supply system are limited to that j
b i
9304200325 930414 PDR ADOCK 05000213 i
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-,. _. _... _ - - _ -. - _ _ -. ~. _ _ _ -
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' particular train. Regarding multiple blowdown effects, the licensee states t
the primary system is still limited by the double ended guillotine break of the reactor coolant system (RCS) loop piping, and the secondary side is l
limited by a main steam line break together with the associated feedwater line break which were previously analyzed in their September 17, 1982 submittal.
The licensee states that cascading effects including multiple blowdown transients were addressed and there are no scenarios more limiting than those previously identified.
Based on the licensee's response, the staff concludes that it is conservative to assume that the particular safety system associated l
with or in the area with the postulated pipe break becomes inoperative.
Therefore, the staff agrees that the most limiting scenarios have been addressed and the effects of cascading sequences is controlled by separation of piping or by physical barriers.
2.2 JET IMPINGEMENT FROM CIRCUMFERENTIAL BREAKS By letter dated October 12, 1982, the staff stated that CYAPC0 needed to evaluate circumferential breaks.
Furthermore, in the case of circumferential breaks, jets in conjunction with pipe whip should be considered to sweep the arc travelled during the whip. CYAPC0 has stated that the high energy line break (HELB) analysis considered circumferential breaks and that the jet was assumed to travel the arc defined by the whipping pipe.
Based on the licensee response, the staff considers this issue resolved.
2.3 STRAIN LEVEL FUNCTIONALITY CRITERIA By letter dated October 12, 1982, the staff requested CYAPC0 to clarify the allowable strain level utilized in its HELB analysis.
By letter dated December 17, 1984, CYAPC0 stated the HELB analysis did not take any credit for this type of detailed analysis on impacted equipment. Based on this response the staff concludes that this concern is not applicable to the Haddam Neck Plant HELB analysis and considers this issue reselved.
2.4 CONTAINMENT INTEGRITY CRITERIA By letter dated October 12, 1982, the staff requested CYAPC0 to provide additional information to justify their conclusion that no pipe break could fail the material or degrade in any manner the containment liner. By letter dated December 17,1984, CYAPC0 stated that the crane wall protects the containment liner from most pipe breaks. The containment building wall consists of a 4-1/2 feet thick right circular cylindrical concrete wall lined with a thick steel plate. The liner is 1/4 inch thick on the bottom, 3/8 inch thick on the cylindrical walls and 1/2 inch thick on the dome. The liner plate is flush with the concrete containment wall and attached by Nelson studs 24" on center.
CYAPC0 has determined that the limiting break from a load j
standpoint is a 12" feedwater line break. The feedwater pipe is perpendicular to the containment wall and the only type of interaction which could possibly affect the liner plate integrity would be a ripping action from the jagged edge of a broken pipe.
CYAPC0 states that there does not exist sufficient loading or interaction of the type which could possibly affect the integrity of the liner plate for the most limiting pipe whip or jet impingement.
i l
i In addition, by letter dated January 29, 1993, the licensee stated that as part of their current HELB reverification program, a detailed HELB evaluation was performed on the main steam and feedwater lines inside containment to evaluate the effects of a pipe break on the containment structure. The i
calculations developed main steam and feedwater jet impingement loads and reviewed the potential for pipe interaction with the containment structure.
-l Based on these calculations and evaluations, which considered the piping geometry and location, the support scheme, and the location of pipe breaks, i
the licensee concluded that:
l 1.
Both the main steam and feedwater piping would not impat.t the containment wall following a pipe break, and 2.
the containment structure is capable of withstanding the resultant jet loads without degrading the integrity of the liner plate.
Based on the above the staff concludes that there is no HELB inside containment that could cause damage to the containment liner to degrade the liner's function as an environmental barrier. The staff considers this issue resolved.
2.5 JET IMPINGEMENT EFFECTS ON TARGET PIPING By letter dated October 12, 1982, the staff requested CYAPC0 to clarify how they used the size differential criteria in the jet impingement effects evaluation. By letter dated December 17, 1984, CYAPC0 stated an evaluation of jet impingement of piping targets was performed. CYAPC0 stated that due primarily to the physical separation of required safety systems, it is not possible to lose all three of the available shutdown methods. Therefore, CYAPC0 concludes that the plant can achieve a safe shutdown when considering the effects of jet impingement on piping regardless of ratio of pipe sizes.
Based on this response the staff concludes this issue resolved.
2.6 EFFECTS ON INSTRUMENTATION An evaluation of the minimum instrumentation required for safe shutdown, assuming a worst case incident where nonphysically separated instrumentation is rendered inoperable by a single HELB, determined the following minimum sets of instrumentation for each shutdown method-
\\
SHUTDOWN METHOD RE001 RED INSTRUMENTS
- 1. Main Feed a.
Pressurizer Level b.
Pressurizer Pressure c.
Steam Generator Level d.
Loop T-hot or Core Exit Thermocouples L
..-.-.---.J
.. )
- 2. Auxiliary Feedwater a.
Pressurizer Level b.
Pressurizer Pressure c.
Steam Generator Level d.
Loop T-hot or Core Exit Thermocouples e.
Demineralized Water Storage Tank Level
- 3. Feed-and-Bleed a.
Pressurizer Level b.
Pressurizer Pressure
~
c.
Loop T-hot or Core Exit Thermocouples d.
Refueling Water Storage Tank Level, Volume Control Tank Level e.
Pressurizer Relief Valve Monitors, Containment Water l
Level, and Containment High Range Radiation Detectors f.
Containment Pressure g.
RCS Wide-range pressure A discussion of the above instrumentation follows:
a.
Pressurizer Level - CYAPC0 replaced the transmitters for the main control l
board mounted equipment for the three loops of pressurizer level during Cycle 14. While this upgrade provided separation of safety and non-safety l
systems, it did not reduce the degree of independence, separation, and isolation provided in the original design. Therefore, in the case of the loss of pressurizer level instrumentation due to a HELB, the plant could shutdown using feed-and-bleed which does not need pressurizer level or pressurizer pressure indication. The licensee has noted that feed-and-bleed is the least c
desirable of the shutdown methods and would only be used for a HELB where the reactor coolant system remains intact and the steam generators or systems l
servicing them are not available.
Plant emergency procedures would not l
require the operator to use feed-and-bleed for the loss of pressurizer level due to a HELB.
Even if there is a loss of pressurizer level or pressure indication, CYAPCO's emergency operating procedures (E0Ps)-would continue to use main feed or auxiliary feedwater and rely on other indications to verify primary system heat removal. As noted earlier CYAPC0 considers feed-and-bleed j
to be the option of last choice when all other options have been exhausted.
l The E0Ps support this philosophy. However, losing pressurizer level indication will inhibit safety injection termination. The termination criteria for safety injection is based on part in regaining pressurizer level.
i This means in effect, a partial feed-and-bleed (i.e., the operator will inject i
but will not open the power operated relief valves) is used in conjunction with Plant Shutdown Methods 1 and 2.
Based on the above, the staff agrees that even with a loss of pressurizer level there is sufficient means to safely cooldown the plant and that the licensee has minimized reliance on feed-and-bleed to cool down the plant.
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Pressurizer Pressure - CYAPC0 states that in the case where pressurizer pressure instrumentation is lost due to a HELB, RCS pressure instruments would be used instead. The RCS pressure instruments are physically separated from the pressurizer pressure instrumentation. The staff agrees that the RCS pressure instrumentation could be used instead of pressurizer pressure instrumentation for use in Plant Shutdown Methods 1, 2, or 3.
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Steam Generator Level - CYAPC0 states that modifications have been made to the wide-range level indication instrumentation.
Each steam generator now has two redundant Class IE wide-range level detectors.
In addition, even though one channel of steam generator level instrumentation for all four steam generators is routed in one conduit, the redundant channels have been routed taking into account HELBs. As part of the Steam Generator Level Instrumentation Upgrade, the licensee will modify the steam generator narrow-range instrumentation such that it is redundant and physically separated.
Based on the above, the staff concludes that the steam generator level i
instrumentation is redundant and physically separated and this issue is resolved.
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Loop T or Core Exit Thermocouples - The licensee states that the l
cabling of"these instruments inside containment was upgraded and is now l
physically separated and redundant. The staff considers this issue resolved.
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Refueling Water Storage Tank Level, Volume Control Tar.k Level, and l
Demineralized Water Storage Tank Level - The licensee states that all these instruments are outside the containment and are not affected by pipe breaks inside containment. The staff considers this issue resolved.
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Pressurizer Relief Valve Monitor, Containment Water Level, Containment High Range Radiation Detectors - Containment Water Level and Containment High Range Radiation Detectors were installed in response to NUREG-0737 and are all physically separated and redundant.
Pressurizer Relief Valve Monitor, which was also installed in response to NUREG-0737, utilizes a single channel.
l However, other indications of relief valve position are available such as
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temperature elements in the common power-operated relief valve (PORV) header and in the line to the pressurizer relief tank, and relief tank level, pressure, or temperature.
Based on_the above, the staff concurs that sufficient instrumentation exists to determine Pressurizer Relief Valve position and considers this issue resolved.
2.7 MAIN COOLANT LOOP BREAKS By letter dated October-12, 1986, the staff requested CYAPC0 to verify that the seismic loads assumed in Unresolved Safety Issue (USI) A-2 are compatible with the seismic loads assumed in the SEP and that the reactor coolant pressure boundary (RCPB) leakage detection systems, the type and number of the systems provided be commensurate with the guidelines of Regulatory Guide 1.45.
By letters dated December 17, 1984 and June 16, 1989, CYAPC0 confirmed that SEP seismic analysis performed for the Haddam Neck Plant demonstrated that the maximum bending movements do not exceed the allowable limit specified in 1
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.. l Generic Letter (GL) 84-04.
This seismic analysis identified certain RCS modifications necessary to ensure that loads on the RCS piping will be within i
those assumed in USI A-2.
All but one of the subject RCS modifications were i
I completed during the 1987-1988 refueling outage. The only remaining modification was the replacement of steam generator hold-down bolts. The modifications to the steam generator hold-down bolts were not necessary as the i
safety factors on the bolts were determined to be within allowable limits. By License Amendment No. 116, dated May 31, 1989, the staff approved technical specifications that govern the operability of leakage detection systems that are capable of detecting an RCS leak of I gpm for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. By letter dated July 11, 1989, the staff concluded that CYAPC0 met the conditions specified in GL 84-04 so that the asymmetric blowdown loads resulting from double ended pipe breaks in main coolant loop piping need not be considered as a design basis for the Haddam Neck Plant. Based on the above, the staff considers this issue to be resolved.
1 2.8 PLANT SHUTDOWN METHOD 3 By letter dated October 12, 1982, the staff requested CYAPC0 to identify under what circumstances plant shutdown method 3 (feed and bleed) is intended j
to be used and how the energy is removed from the primary system.
By letter l
dated December 17, 1984, CYAPC0 stated that Method 3 is to be used when the reactor coolant pressure boundary remains intact and the steam generators or systems servicing them are not available for normal heat removal. Reliance on feed-and-bleed is minimal. Therefore, feed-and-bleed is needed when:
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a pipe break outside containment were to compromise capability to inject either main or auxiliary feedwater into the steam generators, 2.
a pipe break inside containment were to compromise capability i
to utilize the steam generators to remove core decay heat, and 3.
some other failure resulting in the loss of steam generator decay heat removal.
Feed-and-bleed entails injecting water into the RCS with a charging pump (or HPSI pump) and allowing water to discharge from the pressurizer power-operated relief valves (PORVs) into the pressurizer relief tank and then into the containment sump. The water would be drawn from the sump, cooled by the.
4 residual heat removal heat exchangers and returned to the suction of the charging pumps or high-pressure safety injection (HPSI) pumps. CYAPC0 has qualified the low temperature overpressure protection system (pipes and valves) so that it is qualified for the temperature, pressure, and flow conditions that would exist.
Feed and bleed is the least desirable shutdown method. However, for a limited set of pipe break locations in portions of the main steam, feedwater and auxiliary steam piping feed-and-bleed is the primary cooling method.
The licensee has committed to several modifications to decrease the reliance on Plant Shutdown Method 3, feed-and-bleed. The licensee proposed the following modifications to be completed during the next two outages:
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implement a dedicated erosion / corrosion program for the piping in the Terry turbine building to reduce the probability of pipe break in the Terry turbine room, 2.
install a motor driven auxiliary feedwater pump, powered by l
emergency onsite power source, outside of the Terry turbine room, 3.
provide direct injection flow path to the steam generators, 4.
dedicate the demineralized water storage tank to the auxiliary feedwater system, and 5.
house the electric auxiliary feedwater pump, the automatic initiation support skids and direct injection piping and valves in a new seismically designed enclosure.
The licensee is also considering physical separation of the Terry turbines and pumps which would further reduce the reliance on feed-and-bleed.
By License Amendment dated February 24, 1992, the staff agreed that the above i
modifications and erosion / corrosion program would reduce the probability of a HELB in the Terry turbine and the reliance on feed-and-bleed to an acceptable level. The licensee has adequately responded to our request for information regarding feed-and-bleed.
2.9 MAIN STEAM /FEEDWATER INTERACTIONS By letter dated October 12, 1982, the staff requested CYAPC0 to clarify the apparent inconsistency between the matrix and interaction evaluation of the main steam line breaks. By letter dated December 17, 1984, CYAPC0 stated that the scenario given in the interaction evaluation is correct and that for a given main steam line break, the only potential feedwater line interaction occurs with the feedwater line corresponding to the steam generator. The matrix is in error but the evaluation is correctly stated.
Based on the above the staff considers this issue resolved.
2.10 CORE DELUGE PIPING BREAKS By letter dated October 12, 1982, the staff questioned CYAPC0, coald a single active failure in the emergency power system be a more limiting case than the loss of the motor operated valve in the unaffected train for o core deluge line break.
By letter dated January 29,1993, CYAPC0 stated ns result of the LOCA reanalyses and the analyses performed in support of perranent modifications to resolve various single failure vulnerabilities associated with the ECCS, CYAPC0 did determine that the limiting single failure after a i
core deluge line break is the failure of a diesel. However, CYAPC0 performed-analyses which demonstrate that for a break of this size, adequate results are obtained for the injection phase without any credit from the low-pressure injection system (LPSI). A postulated core deluge line break would behave differently in the recirculation phase than the same size break occurring i
elsewhere in the RCS. This is due to the higher LPSI flowrate associated with 4
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.. j a core deluge line break which causes an earlier time to recirculation. The long-term modifications described in CYAPCO's April 1, 1987, letter have been.
analyzed and show acceptable results for all postulated single failures.
The staff concurs with the licensee's analysis and considers this issue resolved.
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3.0 CONCLUSION
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The staff has completed its review of SEP Topic III-5.A and concludes that if a pipe were to break inside containment, the plant can safely shutdown without-loss of containment integrity. The licensee has provided three shutdown methods (Main Feed, Auxiliary.Feedwater, and Feed and Bleed). There is no-HELB !aside containment which could incapacitate all three shutdown methods.
l In addition, piping integrity is maintained by two inspection programs:
inservice inspection and erosion / corrosion. While these-programs cannot preclude the possibility of a high energy line break inside containment they do improve the probability that a high energy line break will not occur.
Based on the above, the staff considers SEP Topic III-5.A to be complete.
Principal Contributor:
A. Wang Date: April 14, 1993 i
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