Letter Sequence Other |
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TAC:11011, (Approved, Closed) TAC:12395, (Approved, Closed) TAC:44070, (Approved, Closed) TAC:45275, (Approved, Closed) TAC:45323, (Approved, Closed) TAC:45392, (Approved, Closed) TAC:45441, (Approved, Closed) TAC:45471, (Approved, Closed) TAC:45501, (Approved, Closed) TAC:45609, (Open) TAC:46426, (Approved, Closed) |
Initiation
- Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request
- Acceptance...
Results
Other: B12630, Proposed Tech Specs,Adding New Surveillance Requirement Re Control Room Habitability, ML19241B419, ML19241B427, ML19254D272, ML19263C802, ML19310A426, ML19321A695, ML19330B754, ML19339A509, ML19339A598, ML19343A382, ML19345E132, ML19347C739, ML20049H553, ML20050C507, ML20052A948, ML20053D721, ML20066D300, ML20071G129
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MONTHYEARML19256A1121978-10-27027 October 1978 Application for Amend to License DPR-35,changing Tech Specs to Accomodate New Steamline Break Protection Sys Scheduled for Installation in Spring of 1979.Fee Paid Project stage: Request ML20071G1291978-12-14014 December 1978 Forwards Addl Info Re Lic Amend Appl Covering Eval of Low Feedwater Flow Reactor Trip Setpoint Change Project stage: Other ML19263C8021979-02-0505 February 1979 Lists Individual Fee Classes for 781027 Application for Tech Spec Changes.Requests Submittal of Addl $13,500 Fee. Any Overcharges Will Be Refunded Project stage: Other ML19276E2751979-03-0707 March 1979 Forwards Addl Info Requested at 790223 Meeting Re Proposed Steam Break Protection Sys Project stage: Meeting ML19270F9971979-03-12012 March 1979 Summary of 790223 Meeting W/Westinghouse & Duquesne Light Re Steamline Break Protection Sys.W/Supporting Documentation Project stage: Meeting ML19241B4271979-07-13013 July 1979 Tech Spec Change Requests 42 & 47 Re Mod to ECCS Project stage: Other ML19241B4191979-07-13013 July 1979 Forwards Tech Spec Change Requests 42 & 47 Re Amend to App a of DPR-72.Change Is Required Prior to Startup After Completion of Planned ECCS Mod,Which Could Be Accomplished as Early as 790722 Project stage: Other ML19274G1021979-07-31031 July 1979 Forwards Request for Addl Info to Util Proposed Steam Break Protection Sys & N-1 Loop Operation Project stage: RAI ML19208B5691979-08-21021 August 1979 Forwards Safety Evaluation Re Electrical,Instrumentation & Control Aspects of Deletion of Reactor Trip on Turbine Trip Below 50% Power Project stage: Approval ML19254D2721979-10-18018 October 1979 Forwards Addl Info Re Proposed Steam Break Protection Sys Per Tech Spec Change Request 35.Proposed Tech Spec Re Maint of Required Shutdown Margin & Revised Reactivity Control Sys Tech Specs Encl Project stage: Other ML19259D6001979-10-18018 October 1979 Summary of 791009 Meeting W/Util Re Proposed Steamline Break Protection Project stage: Meeting ML19256G0641979-12-17017 December 1979 Discusses Review of NRC 791213 Request Re Commitment to Implement TMI Lessons Learned Task Force Category a Requirements by 800101.Intends to Implement Recommendations During Current Refueling Outage Project stage: Other ML19309A8581980-03-28028 March 1980 Forwards Documents Re Investigation Into Extended Outages at Facility.Documents Include Trial Staff Statement Before PA Public Util Commission,Consumer Advocate Statement & CN Dunn Testimony Project stage: Request ML19309H2151980-04-15015 April 1980 Notification of 800422 Meeting W/Util in Bethesda,Md to Discuss & Review Decay Heat Exchanger Sys Integrity & Operation Project stage: Request IR 05000302/19800181980-05-0707 May 1980 IE Insp Rept 50-302/80-18 on 800331-0411.No Noncompliance Noted.Major Areas Inspected:Previous Insp Findings,Fuel Receipt,Refueling Activities,Maint Activities & IE Bulletin 79-01B Project stage: Request IR 05000334/19800081980-05-0707 May 1980 IE Insp Rept 50-334/80-08 on 800324-28.No Noncompliance Noted.Major Areas Inspected:Qa Program Review,Qa/Qc Administrative Design Change & Mod Control,Measurement & Test & Previous Insp Items Project stage: Request ML19310A4261980-06-0909 June 1980 Responds to & Schedule for Implementation of TMI-2-related Requirements.Discusses Shift Manning,Scope & Criteria for Licensing Exam,Procedures for Feedback of Operating Experience & Control Room Habitability Project stage: Other IR 05000412/19800061980-07-0303 July 1980 IE Insp Rept 50-412/80-06 on 800602-06.Noncompliance Noted: Failure to Return Used or Damaged Welding Electrodes to Issue Station & Failure to Provide Adequate Protection for Equipment in Temporary Storage Project stage: Request ML19321A6951980-07-21021 July 1980 Forwards Schedule for Commitments to TMI-2 Related Requirements,Per NRC 800507 Request.Affidavit Encl Project stage: Other ML19330B7541980-07-31031 July 1980 Informs of Intentions to Withdraw Commitment to Adopt Guidance of IE Circular 80-02,due to Wording of IE Circular 80-02 & Application of Circular Re Work Situations Project stage: Other ML19338D4281980-08-20020 August 1980 Notification of Contract Execution,Mod 4 to Engineering Assistance Re Hearings for South Tx Antitrust & Comanche Peak Antitrust Proceedings Project stage: Other ML19343A3821980-09-15015 September 1980 Tech Specs 3/4 3-38,requesting Changes Re Model License Conditions,Emergency Feedwater Initiation & Flow Monitoring, Diverse Containment Isolation & Emergency Power Supply to Pressurizer Heaters Project stage: Other ML19343A3791980-09-15015 September 1980 Application to Amend App a to Ol,Changing Aspects of NUREG-0578 Including Model License Conditions & Emergency Feedwater Initiation & Flow Monitoring.Affidavit & Certificate of Svc Encl Project stage: Request ML19338D7401980-09-16016 September 1980 Confirms 800909 Telcon Re Basis for Selecting Essential Sys Regarding Clarification of NUREG-0578 Item 2.1.4 Project stage: Other ML19338D5631980-09-17017 September 1980 Confirms 800904 Telcon Re Compliance w/NUREG-0578,Item 2.1.3.b Concerning Wide Range Pressure Inputs & Resistance Temp Detector Uncertainty.Util Will Upgrade nonsafety-grade Input to Safety Grade During Second Refueling Project stage: Other ML19339A5091980-10-24024 October 1980 Withdraws Tech Specs Change Request 47,implementing Items Contained in NRC 790516 Confirmatory Order.Util Considers Specs Requested in Eisenhut & Provided in Change Request 64,Revision 1,as Representing Latest Position Project stage: Other ML19339A5981980-10-29029 October 1980 Advises of Status Re Shift Staffing,In Response to Interim Criteria in NRC Project stage: Other ML19339B2141980-10-31031 October 1980 Advises That Util Has Not Made Plans to Conduct Any Qualification Tests During Next 2 Yrs.Nrc Will Be Notified in Event of Decision to Conduct Tests Project stage: Request ML20002B1321980-10-31031 October 1980 Immediate Action Ltr 80-46 Enumerationg Actions Taken by Util.Requests Response If Such Actions Differ from Actions Actually Planned by Util Project stage: Other ML19345E1321980-12-17017 December 1980 Responds to Re Confirmation of Commitment to Meet Implementation Dates Contained in NUREG-0737.Requests Extension for Proposed Mods Re Auto Trip of Reactor Coolant Pumps Project stage: Other ML19347C7391980-12-31031 December 1980 Forwards Nonproprietary & Proprietary Versions of Response to NUREG-0737. Proprietary Version Available in Central Files Only Project stage: Other ML19341C8461981-02-11011 February 1981 Forwards Amend 39 to License DPR-66,safety Evaluation & Notice of Issuance & Availability Project stage: Approval ML20049H5531982-02-24024 February 1982 Provides Info on Item II.K.3.5 Re Automatic Trip of Reactor Coolant Pumps During Loca,Per NUREG-0737 Requirements. Status Submitted in Has Not Changed Project stage: Other ML20042B9261982-03-16016 March 1982 Forwards Request for Addl Info for Review of TMI Action Items 2.A.2.1,upgrading Senior Reactor Operator & Reactor Operator Training & II.B.4,training for Mitigating Core Damage Project stage: RAI ML20050C5071982-03-24024 March 1982 Ack Commitment in to Meet Reporting Requirement Provided in NRC Re Relief & Safety Valve Failures.Info Missing from 1981 Annual Rept.Requests That Rept Be Updated W/Errata Sheet to Correct Discrepancy Project stage: Other ML20052A9481982-04-23023 April 1982 Requests Addl Info Re TMI Action Plan Item II.K.3.3, Reporting Relief Valve & Safety Valve Failures.Response within 30 Days Requested Project stage: Other ML20052G1951982-05-10010 May 1982 Informs of No Relief or Safety Valve Failures or Challenges During Apr-Dec 1980 in Response to 820423 Request for Documentation & Commitment to NUREG-0737,Item II.K.3.3, Reporting Relief & Safety Valve Failures & Challenges Project stage: Request ML20053D7211982-05-27027 May 1982 Forwards Westinghouse Transmitting SAR for Deletion of Reactor Trip Following Turbine Trip Below 50% Power.Review Requested Against NUREG-0737,Item II.K.3.10 Concerns Project stage: Other ML20066D3001982-11-0303 November 1982 Informs That Since Unit 1 Anticipatory Trip Mod Is Enveloped by Unit 2 Analysis Basis,Analysis May Be Applied to Unit 1 Per Requirements of TMI Item II.K.3.10, Proposed Anticipatory Trip Mod Project stage: Other ML20084C5841984-04-24024 April 1984 Discusses 830808 Program Plan Rept for Detailed Control Room Design Review Containing Section Entitled, Mgt & Staffing, Outlining Min Qualification for Team Members.Resumes Encl Project stage: Request A06182, Responds to 861029 Request for util-proposed Tech Spec Changes Re Reporting of Safety Valve & Relief Valve Failure & Challenges,Control Room Habitability & Secondary Water Chemistry.Schedule for Submittal of Amend Requests Encl1986-12-10010 December 1986 Responds to 861029 Request for util-proposed Tech Spec Changes Re Reporting of Safety Valve & Relief Valve Failure & Challenges,Control Room Habitability & Secondary Water Chemistry.Schedule for Submittal of Amend Requests Encl Project stage: Request B12630, Proposed Tech Specs,Adding New Surveillance Requirement Re Control Room Habitability1987-08-0303 August 1987 Proposed Tech Specs,Adding New Surveillance Requirement Re Control Room Habitability Project stage: Other ML20236N0591987-08-0303 August 1987 Application for Amend to License DPR-65,adding New Surveillance Requirement Re Control Room Habitability.Fee Paid Project stage: Request 1980-06-09
[Table View] |
Responds to & Schedule for Implementation of TMI-2-related Requirements.Discusses Shift Manning,Scope & Criteria for Licensing Exam,Procedures for Feedback of Operating Experience & Control Room Habitability| ML19310A426 |
| Person / Time |
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| Site: |
Beaver Valley |
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| Issue date: |
06/09/1980 |
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| From: |
Dunn C DUQUESNE LIGHT CO. |
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| To: |
Eisenhut D Office of Nuclear Reactor Regulation |
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| References |
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| TASK-2.K.3.10, TASK-2.K.3.12, TASK-TM TAC-11011, TAC-12395, TAC-44070, TAC-45275, TAC-45323, TAC-45392, TAC-45441, TAC-45471, TAC-45501, TAC-45609, TAC-46426, NUDOCS 8006170532 |
| Download: ML19310A426 (4) |
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Text
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June 9, 1980 Director of Nuclear Reactor Regulation United States Nuclear Regulatory Commission Attn:
D. G. Eisenhut, Acting Director Division of Operating Reactors Washington, DC 20555
Reference:
Beaver Valley Power Station, Unit No. 1 Docket No. 50-334 Five Additional TMI-2 Related Requirements Gentlemen:
We have carefully reviewed your letter dated May 7, 1980, and your schedule for implementation, and the following are Duquesne Light Company's commi %ents for Beaver Valley Unit No. I with regard thereto.
Item 1.A.1.3 - Shift Manning We have not received correspondence which provides guidance as to what is required by this item.
However, we are aware of IE Circular 80-02
" Nuclear Power Plant Staff Work Hours," and we commit to adopt the guidance of IE Circular 80-02 by August 1, 1980, to the extent that the guidance provided in that Circular is encompassed by the requirements of this item.
Without further NRC definition as to what is met by " Personnel Require-ments," we are unable to commit to the schedule date set forth in the May 7, 1980, letter.
Item 1.A.3.1 - Revise Scope and Criteria For Licensing Examinations Effective immediately, Duquesne Light Company commits to the position stated in the March 28, 1980, letter on this subject.
Item 1.C.5 - Procedures For Feedback of Operating Experience to Plant Staff Duquesne Light Company commits that by January 1, 1981, it shall have reviewed its procedures, revised them as necessary and placed them into effect to assure that operating information pertinent to plant safety, originating both within and outside the utility organization, is continually supplied to operators and other personnel and is incorporated into training and retraining programs.
k SM 8006170
d Beaver Valley Power Station, Unit No. 1 Docket No. 50-334 Five Additional TMI-2 Related Requirements Page 2 Item II.K.3.1 - Install and Test Automatic PORV Isolation System Duquesne Light Company will commit to studying the feasibility and desirability of the Automatic PORV Isolation System as well as developing a suitable design, if feasible and desirable, by July 1, 1981, and to install and test the system during the next refueling cycle subsequent to July 1, 1981. We are aware of a Westinghouse Owners Group analysis from which the conclusion can be drawn that the failure of an Automatic PORV Isolation System could Lapair the ultimate heat sink function and increase the inten-sity of some transients. Further, failure to isolate stuck-open PORVs has been analyzed and no core uncovery results.
In addition, plant modifica-tions, procedure changes and operator training required by NUREG 0578 implementation provide assurance that malfunctioning PORVs will be isolated.
Item,II.K.3.2 - PORV Failure Report A generic report on PORV failure will be submitted to the NRC by January 1, 1981.
Item II.K.3.3 - Reporting Safety and Relief Valve Challenge Further failures of relief and safety valves at Beaver Valley will be reported to the NRC and documented in the annual report.
Item II.K.3.5 - Automatic RCP Trip In our August 28, 1979, response to IE Bulletin 79-06C, we reference the Westinghouse Owners Group analysis of delayed RCP trip during small break LOCAs documented in WCAP-9584. This WCAP is the basis for the West-inghouse and Owners Group position on RCP trip (I.E.: Automatic RCP trip is not necessary for a Westinghouse PWR since sufficient time is available for manual tripping of the RCPs. This philosophy has been incorporated in the Westinghouse emergency operating instructions which were reviewed and approved by the NRC Bulletins and Orders Task Force and subsequently incor-porated in the Beaver Valley Emergency Operating Procedures.
In addition, the Westinghouse criteria (basically a RCS pressure below the shutoff head of SI pumps) provides for continued RCP operation and therefore forced circulation and decreased reliance on operator action for non-LOCA events.
As requested by the NRC in a letter dated April 15, 1980, and as discussed with the NRC during the May 22, 1980, meeting on this subject, we anticipate that the Westinghouse Owners Group will provide predictions of the LOFT test L3-6.
The NRC has indicated that small break tests at the semiscale and LOFT facilities as well as Owners Group test predictions will aid in NRC resolution of this issue. Therefore, we believe that it is not appropriate to take any additional actions on this issue until the results of the NRC sponsored testing (in particular L3-5 and L3-6) and Owners Group predictions are completed and the results evaluated.
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Beaver Valley Power Station, Unit No. 1 Docket No. 50-334 Five Additional THI-2 Related Requirements Page 3 Item II.K.3.9 - PID Modification We understand that for Beaver Valley this modification is accomplished by setting the derivative time constant in the appropriate PID controller to "0FF."
This modification will be accomplished prior to plant restart from the current shutdown period.
Item II.K.3.10 - proposed An*.icipatory Trip Modification We have submitted a requeet for technical specification change (Amend-ment No. 46 dated May 14, 1980) which includes this item. We believe that increasing this trip setting to the proposed higher level is important in reducing the number of spurious trips which can challenge plant systems un-necessarily. Particularly below 30 percent power, the plant is subject to increased turbine trips while the feedwater system is being operated manual-ly, bus transfers are taking place and the rod control system is in manual.
Except during the startup and shutdown operations, the plant is not operated low power levels, and therefore, on a percent of operating time basis, at challenges to plant systems due to a stuck open PORV is little affected by an increase in seepoint of this anticipatory trip.
Item II.K.3.12 - Confirm Existence of Anticipatory Reactor Trip on Turbine Trip Beaver Valley has an anticipatory reactor trip on turbine trip.
Item II.K.3.17 - Report On Outage of ECCS Systems We will prepare a report listing outage dates and lengths and causes of outages for all ECCS systems for the past five years of operation and will submit this report by January 1, 1981.
Item II.K.3.25 - Loss of AC Power On Pump Seals We do not believe this item is applicable to Beaver Valley.
Item II.K.3.29 - Study to Demonstrate Performance of Isolation Condensers We do not believe this item is applicable to Beaver Valley.
Item II.K.3.30 - Revised Small Break LOCA Methods To Show Compliance With 10CFR50 Appendix K The present Westinghouse small break evaluation model used to analyze Beaver Valley is in conformance with 10CFR50 Appendix K.
However, Westing-house has indicated that they will, nevertheless, address the specific NRC items contained in NUREG-0611 in a model change schedule for completion by January 1, 1982.
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e Beaver Valley Power Station, Unit No. 1 Docket No. 50-334 Five Additional TMI-2 Related Requirements Page 4 Item II.K.3.31 - Plant Specific LOCA Analysis To Show Compliance With 10CFR50.46 The present Westinghouse small break evaluation model and small break LOCA analysis for Beaver Valley are in conformance with 10CFR50 Appendix K and 10CFR50.46. As stated in answer to the previous Item II.K.3.30, Westing-house plans to submit a new small break evaluation model to the NRC for review by January 1, 1982.
If the results of this new Westinghouse model (and subsequent NRC review and approval) indicate that the present small break LOCA analysis for Beaver Valley are not in conformance with 10CFR50.46, a new analysis utilizing the new and approved Westinghouse model will be submitted to the NRC in accordance with the NRC schedule.
Item II.K.3.44 - Evaluation of Anticipated Transients With Single Failure We do not believe that this item is applicable to Beaver Valley.
Item III.D.3.4 - Control Room Habitability We have recently reviewed habitability requirements for the control room and have installed chlorine detectors to warn of a chlorine leak of sufficient size to effect habitability. This chlorine detection system, combined with other features described in the FSAR, meet the intent of habitability requirements for the control room.
We will complete the review required by this item by January 1981 and will make necessary control room modifications, if any, by January 1983.
Should you have any questions regarding this response, do not hesistate to contact my office.
Very truly yours, nn y i
C. N. Dunn Vice President, Operations cc:
Mr. D. A. Beckman, Resident Inspector U.S. Nuclear Regulatory Commission Beaver Valley Power Station Shippingport, Pennsylvania 15077 U.S. Nuclear Regulatory Commission c/o Document Management Branch Washington, D.C.
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