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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18065B1151997-12-0909 December 1997 LER 97-013-00:on 971110,failure to Closure Test Two Check Valves Resulted in Violation of TS 6.5.7 Occurred.Caused by Close Function for Check Valves.Check Valves Tested to Confirm Proper Closure Capability ML18067A7751997-11-11011 November 1997 LER 97-011-00:on 971012,primary Coolant Pump Was Started W/Sg Temperatures Greater than Cold Leg Temperature.Caused by Inadequate Procedures & Operator Decision Making.Critique of Event Conducted W/Operators Involved ML18067A7581997-10-30030 October 1997 LER 97-010-00:on 970930,determined That Inadequacy in App R Analysis Resulted in Condition Outside Design Basis of Plant.Caused by Missing Cable in Circuit & Raceway Schedule. Developed New Evaluation Re ASD Valves Validation ML18067A7461997-10-23023 October 1997 LER 97-009-00:on 970923,discovered Procedure Weakness Re Implementation of App R Shutdown Methodology.Caused by Human Error.Revised Off-Normal Procedure ONP-25.2, Alternate Safe Shutdown Procedure. ML18067A7191997-10-10010 October 1997 LER 97-008-00:on 970912,spurious Valve Operation Could Result in Loss of Shutdown Capabilities Per 10CFR50,App R, Section Iii.L,Was Discovered.Caused by Failure to Validate Info from App R.Design Bases for SW Backup Reviewed ML18067A6951997-09-24024 September 1997 LER 97-007-00:on 970826,discovered Inadequate Testing of DG Sequencer Control Relay Contacts.Caused by Oversight on Part of Personnel Involved in Installation of Facility Change FC-800.Tested 106D-1/XL & 106D-2/XL Relay Contacts ML18067A5651997-06-0303 June 1997 LER 96-013-01:on 961115,DC Breaker Failed During Testing for as-found Trip Setting.Failure Caused by Oversight within Preventive Maint Program.Breaker Was Replaced & Tested ML18067A5461997-05-12012 May 1997 LER 97-006-00:on 970412,overtime Limits Were Exceeded for Radiation Protection Technicians.Caused by Inadequate Design,Review & Proper Verifications of Overtime Work Schedule.Communicate Overtime Limitation Responsibilities ML18067A4431997-03-24024 March 1997 LER 97-004-00:on 970221,trip of High Pressure Safety Injection Pump Occurred While Filling Safety Injection Tank Resulting in TS Violation.Caused by Particle Lodged Between Surface of Indication disk.Y-phase Relay Was OOS ML18067A4391997-03-21021 March 1997 LER 97-005-00:on 961220,operation of Plant Outside Design Basis Occurred Due to an Unacceptable Repair on Main Steam Isolation Valves.Pipe Plugs Permanently Repaired ML18067A4401997-03-21021 March 1997 LER 97-003-00:on 961101,four Piping Lines Were Determined to Be Potentially Susceptible to Pressurization Due to Containment Temperature Increase During an Accident.Cac Discharge Piping Will Be verified.W/970321 Ltr ML18066A8931997-02-21021 February 1997 LER 97-002-00:on 970123,failure to Meet TSs 4.5.2d(1)(b) for Testing of Emergency Escape Airlock Occurred.Caused by Missed Surveillance.Emergency Escape Air Lock Testing Was Completed & Declared operable.W/970221 Ltr ML18066A8751997-02-0505 February 1997 LER 97-001-00:on 970106,TAVE Temp Dropped Below Minimum Temp for Criticality.Caused by Control Rod Withdrawal Rate to Increase Power Not Sufficient to Match Increase in Steam. Turbine Bypass Valve Actuator repaired.W/970205 Ltr ML18066A8041996-12-23023 December 1996 LER 96-014-00:on 961124,class 1E Raychem Cable Splices Were Installed Incorrectly.Caused by Incorrectly Made Electrical Splices.Total of 270 Splices Have Been Replaced within Containment ML18066A7831996-12-16016 December 1996 LER 96-013-00:on 961115,DC Breaker Failure During Testing for as-found Trip Setting Occurred.Cause Under Investigation.All molded-case Circuit Breakers in DC Distribution Panels Were Replaced ML18065A9951996-10-0404 October 1996 LER 96-002-01:on 960116,initiated TS Required Shutdown Due to Safeguards Cable Fault.Both Sets (Six Cables) of Cables Were Replaced & Installed Through Turbine Generator Bldg ML18065A9171996-09-0909 September 1996 LER 95-012-00:on 960809,TS Violation Occurred,Due to No Senior Reactor Operator in Cr.Caused by Extensive Remodeling.Cr Remodeling completed.W/960909 Ltr ML18065A8961996-08-29029 August 1996 LER 96-011-00:on 960730,CR Continuous Air Monitor Alarm Setpoint Improperly Established.Caused by Failure to Utilize Mod Process in 1988 Leading to Failure to Properly Select & Calibrate Instruments ML18065A8811996-08-20020 August 1996 LER 96-005-01:on 960207,determined Fuse on Main Supply to Two Safety Related DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Lack of Thorough Associated Circuits Analysis.Supply Fuse to Panels Replaced ML18065A8741996-08-16016 August 1996 LER 96-010-00:on 960717,high Pressure Safety Injection Pump Tripped While Filling Safety Injection Tank.Caused by Faulty 150/151Y-207 Time Overcurrent Relay.All Similar Relays in Time Overcurrent Application Have Been Inspected ML18065A8651996-08-12012 August 1996 LER 96-009-00:on 960712,identified Penetration Seal Deficiency on Fire Barriers Caused by Failure to Perform & Document Comprehensive Fire Barrier Evaluation.Developed Basis document.W/960812 Ltr ML18065A8601996-08-0202 August 1996 LER 96-006-01 on 960207,discovered Limits of Design Analysis Could Have Been Violated.Subsequent Tests & Analyses Facility Did Not Exceed Basis.Operating Procedures Have Been Revised to Treat 2530 Megawatts Limit as Absolute Limit ML18065A8321996-08-0101 August 1996 LER 96-003-01:on 960115,alternate Shutdown Panel Inverter Resulted in Unavailability of Panel.Replaced Defective Inverter Alarm Logic Board ML18065A7691996-06-12012 June 1996 LER 96-008-00:on 960513,fire Door Not Maintained Open in Accordance W/Design Basis.Cause Under Investigation. Engineering Evaluation Performed & Revised Documents, Surveillance & Test procedures.W/960612 Ltr ML18065A6901996-05-0101 May 1996 LER 95-001-01:on 950302,malfunction of Left Channel DBA Sequencer Resulted in Inadvertent Actuation of Left Channel Safeguards Equipment.Replaced microprocessor.W/960501 Ltr ML18065A6681996-04-22022 April 1996 LER 96-007-00:on 960321,inadequate Emergency Lighting & Ventilation in post-fire Safe Shutdown Areas.Caused by App R Program Documentation Insufficient to Demonstrate Regulatory Compliance.Lighting modified.W/960422 Ltr ML18065A5721996-03-11011 March 1996 LER 96-006-00:on 960207,average Reactor Power Level Exceeded License Limit Due to Insufficient Procedural Guidance. GOP-12 Revised to Treat 2,530 Mwt Limit as Absolute Limit Requiring Immediate Corrective Action If Exceeded ML18065A5261996-03-0101 March 1996 LER 96-005-00:on 960202,fuse on Main Supply to Two SR DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Inadequate Electrical/App R Design Review.Implemented Hourly Fire tours.W/960301 Ltr ML18065A5111996-02-19019 February 1996 LER 94-012-02:on 940427,determined That Internal Ground in Thermal Margin Monitor Causes Nonconformance W/Rps Design Basis.Incorporated RPS Failure Modes & Effects Analysis in Plant DBD.W/960219 Ltr ML18065A5061996-02-19019 February 1996 LER 96-004-00:on 960118,SIS Disabled W/Primary Coolant Sys Greater than 300 F.Caused by Personnel Error.Permanent Maint Procedure to Disable/Enable SIS Actuation on Low Pressurizer Pressure Will Be Revised to Align W/Ts ML18065A5021996-02-15015 February 1996 LER 96-003-00:on 960115,technicians Found Low Voltage cut- Off for Alternate Shutdown Panel Inverter Set That Resulted in Unavailability of Panel.Caused by Inadequate Post Mod. Readjusted Set Point to Minimum setting.W/960215 Ltr ML18065A4581996-01-31031 January 1996 LER 96-001-00:on 960103,failed to Test Duplicate Equipment. Caused by STS No Longer Containing Requirement for cross- Train Testing of Duplicate Components.Will Submit Request to Delete Subj Requirements from TS.W/960131 Ltr ML18065A4421996-01-19019 January 1996 LER 95-016-00:on 951226,did Not Analyze Primary Coolant Samples within 72 H.Caused by Belief Acceptability to Save Pcs Samples for Choride Analysis Past 72 H.Counseled Chemistry Supervision.W/960119 Ltr ML18065A4041996-01-15015 January 1996 LER 95-014-00:on 950119,PCP Oil Collection Deficiencies Created by FC-860 Piping Mod.Caused by Inadequate DBD for Sys & Lack of Review by Experienced Fire Protection Personnel.Updated Design Basis documentation.W/960115 Ltr ML18065A3291995-12-0404 December 1995 LER 95-013-00:on 951103,circuit Fuse Coordination Deficiency Which Affects App R Safe Shutdown Equipment Noted.Design of Fuse Coordination in Potential Transformer Circuits Will Be Evaluated & Modified as required.W/951204 Ltr ML18065A2361995-11-0202 November 1995 LER 95-012-00:on 950701,discovered Unqualified Electrical Connection in Containment SW Outlet Valve Controller.Caused by Failure of Assigned Engineers to Available Info.Replaced Wire Nuts W/Inline Butt connections.W/951102 Ltr ML18065A2051995-10-20020 October 1995 LER 95-008-01:on 950728,discovered That None of Four Containment High Pressure Channels Would Initiate Reactor Trip Due to Programmatic Deficiencies.Administrative Procedure (AP) 9.44,AP 9.45 & AP 10.44 Will Be Revised ML18065A0841995-09-18018 September 1995 LER 95-011-00:on 950817,CR 40 Withdrawal Occurred When Given Insertion Signal Due to skill-based Error in Crimping & Removing Foreign Matl from CRDM Motor Connection Box.Crd Package replaced.W/950918 Ltr ML18065A0681995-09-14014 September 1995 LER 95-010-00:on 950815,ESFA Resulted in Manual Rt Following Isolation of Pcs.Replaced Failed Instrument Line ML18065A0651995-09-0808 September 1995 LER 95-009-00:on 950728,discovered Lack of Procedural Guidance for Pump Repair Following Fire.Proposed Use of Power Supply Breaker Did Not Adequately Address Effect of Loss of Control Power.Performed Independent Assessment ML18064A8781995-08-28028 August 1995 LER 95-008-00:on 950728,discovered During Design Change Testing That None of Four Containment High Pressure Channels Would Initiate Rt.Caused by Programmatic Deficiencies. Reviewed Selected Tests & Mods from Recent Refueling Outage ML18064A8831995-08-21021 August 1995 LER 95-007-00:on 950720,discovered That 12 Instrument Loops Had V-bolted Type Qualified Cable Splices Connected to Wires W/Exposed Kapton Insulation.Caused by Human Error.All V- Bolted Splices Replaced w/in-line design.W/950821 Ltr 1999-09-02
[Table view] Category:RO)
MONTHYEARML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18065B1151997-12-0909 December 1997 LER 97-013-00:on 971110,failure to Closure Test Two Check Valves Resulted in Violation of TS 6.5.7 Occurred.Caused by Close Function for Check Valves.Check Valves Tested to Confirm Proper Closure Capability ML18067A7751997-11-11011 November 1997 LER 97-011-00:on 971012,primary Coolant Pump Was Started W/Sg Temperatures Greater than Cold Leg Temperature.Caused by Inadequate Procedures & Operator Decision Making.Critique of Event Conducted W/Operators Involved ML18067A7581997-10-30030 October 1997 LER 97-010-00:on 970930,determined That Inadequacy in App R Analysis Resulted in Condition Outside Design Basis of Plant.Caused by Missing Cable in Circuit & Raceway Schedule. Developed New Evaluation Re ASD Valves Validation ML18067A7461997-10-23023 October 1997 LER 97-009-00:on 970923,discovered Procedure Weakness Re Implementation of App R Shutdown Methodology.Caused by Human Error.Revised Off-Normal Procedure ONP-25.2, Alternate Safe Shutdown Procedure. ML18067A7191997-10-10010 October 1997 LER 97-008-00:on 970912,spurious Valve Operation Could Result in Loss of Shutdown Capabilities Per 10CFR50,App R, Section Iii.L,Was Discovered.Caused by Failure to Validate Info from App R.Design Bases for SW Backup Reviewed ML18067A6951997-09-24024 September 1997 LER 97-007-00:on 970826,discovered Inadequate Testing of DG Sequencer Control Relay Contacts.Caused by Oversight on Part of Personnel Involved in Installation of Facility Change FC-800.Tested 106D-1/XL & 106D-2/XL Relay Contacts ML18067A5651997-06-0303 June 1997 LER 96-013-01:on 961115,DC Breaker Failed During Testing for as-found Trip Setting.Failure Caused by Oversight within Preventive Maint Program.Breaker Was Replaced & Tested ML18067A5461997-05-12012 May 1997 LER 97-006-00:on 970412,overtime Limits Were Exceeded for Radiation Protection Technicians.Caused by Inadequate Design,Review & Proper Verifications of Overtime Work Schedule.Communicate Overtime Limitation Responsibilities ML18067A4431997-03-24024 March 1997 LER 97-004-00:on 970221,trip of High Pressure Safety Injection Pump Occurred While Filling Safety Injection Tank Resulting in TS Violation.Caused by Particle Lodged Between Surface of Indication disk.Y-phase Relay Was OOS ML18067A4391997-03-21021 March 1997 LER 97-005-00:on 961220,operation of Plant Outside Design Basis Occurred Due to an Unacceptable Repair on Main Steam Isolation Valves.Pipe Plugs Permanently Repaired ML18067A4401997-03-21021 March 1997 LER 97-003-00:on 961101,four Piping Lines Were Determined to Be Potentially Susceptible to Pressurization Due to Containment Temperature Increase During an Accident.Cac Discharge Piping Will Be verified.W/970321 Ltr ML18066A8931997-02-21021 February 1997 LER 97-002-00:on 970123,failure to Meet TSs 4.5.2d(1)(b) for Testing of Emergency Escape Airlock Occurred.Caused by Missed Surveillance.Emergency Escape Air Lock Testing Was Completed & Declared operable.W/970221 Ltr ML18066A8751997-02-0505 February 1997 LER 97-001-00:on 970106,TAVE Temp Dropped Below Minimum Temp for Criticality.Caused by Control Rod Withdrawal Rate to Increase Power Not Sufficient to Match Increase in Steam. Turbine Bypass Valve Actuator repaired.W/970205 Ltr ML18066A8041996-12-23023 December 1996 LER 96-014-00:on 961124,class 1E Raychem Cable Splices Were Installed Incorrectly.Caused by Incorrectly Made Electrical Splices.Total of 270 Splices Have Been Replaced within Containment ML18066A7831996-12-16016 December 1996 LER 96-013-00:on 961115,DC Breaker Failure During Testing for as-found Trip Setting Occurred.Cause Under Investigation.All molded-case Circuit Breakers in DC Distribution Panels Were Replaced ML18065A9951996-10-0404 October 1996 LER 96-002-01:on 960116,initiated TS Required Shutdown Due to Safeguards Cable Fault.Both Sets (Six Cables) of Cables Were Replaced & Installed Through Turbine Generator Bldg ML18065A9171996-09-0909 September 1996 LER 95-012-00:on 960809,TS Violation Occurred,Due to No Senior Reactor Operator in Cr.Caused by Extensive Remodeling.Cr Remodeling completed.W/960909 Ltr ML18065A8961996-08-29029 August 1996 LER 96-011-00:on 960730,CR Continuous Air Monitor Alarm Setpoint Improperly Established.Caused by Failure to Utilize Mod Process in 1988 Leading to Failure to Properly Select & Calibrate Instruments ML18065A8811996-08-20020 August 1996 LER 96-005-01:on 960207,determined Fuse on Main Supply to Two Safety Related DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Lack of Thorough Associated Circuits Analysis.Supply Fuse to Panels Replaced ML18065A8741996-08-16016 August 1996 LER 96-010-00:on 960717,high Pressure Safety Injection Pump Tripped While Filling Safety Injection Tank.Caused by Faulty 150/151Y-207 Time Overcurrent Relay.All Similar Relays in Time Overcurrent Application Have Been Inspected ML18065A8651996-08-12012 August 1996 LER 96-009-00:on 960712,identified Penetration Seal Deficiency on Fire Barriers Caused by Failure to Perform & Document Comprehensive Fire Barrier Evaluation.Developed Basis document.W/960812 Ltr ML18065A8601996-08-0202 August 1996 LER 96-006-01 on 960207,discovered Limits of Design Analysis Could Have Been Violated.Subsequent Tests & Analyses Facility Did Not Exceed Basis.Operating Procedures Have Been Revised to Treat 2530 Megawatts Limit as Absolute Limit ML18065A8321996-08-0101 August 1996 LER 96-003-01:on 960115,alternate Shutdown Panel Inverter Resulted in Unavailability of Panel.Replaced Defective Inverter Alarm Logic Board ML18065A7691996-06-12012 June 1996 LER 96-008-00:on 960513,fire Door Not Maintained Open in Accordance W/Design Basis.Cause Under Investigation. Engineering Evaluation Performed & Revised Documents, Surveillance & Test procedures.W/960612 Ltr ML18065A6901996-05-0101 May 1996 LER 95-001-01:on 950302,malfunction of Left Channel DBA Sequencer Resulted in Inadvertent Actuation of Left Channel Safeguards Equipment.Replaced microprocessor.W/960501 Ltr ML18065A6681996-04-22022 April 1996 LER 96-007-00:on 960321,inadequate Emergency Lighting & Ventilation in post-fire Safe Shutdown Areas.Caused by App R Program Documentation Insufficient to Demonstrate Regulatory Compliance.Lighting modified.W/960422 Ltr ML18065A5721996-03-11011 March 1996 LER 96-006-00:on 960207,average Reactor Power Level Exceeded License Limit Due to Insufficient Procedural Guidance. GOP-12 Revised to Treat 2,530 Mwt Limit as Absolute Limit Requiring Immediate Corrective Action If Exceeded ML18065A5261996-03-0101 March 1996 LER 96-005-00:on 960202,fuse on Main Supply to Two SR DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Inadequate Electrical/App R Design Review.Implemented Hourly Fire tours.W/960301 Ltr ML18065A5111996-02-19019 February 1996 LER 94-012-02:on 940427,determined That Internal Ground in Thermal Margin Monitor Causes Nonconformance W/Rps Design Basis.Incorporated RPS Failure Modes & Effects Analysis in Plant DBD.W/960219 Ltr ML18065A5061996-02-19019 February 1996 LER 96-004-00:on 960118,SIS Disabled W/Primary Coolant Sys Greater than 300 F.Caused by Personnel Error.Permanent Maint Procedure to Disable/Enable SIS Actuation on Low Pressurizer Pressure Will Be Revised to Align W/Ts ML18065A5021996-02-15015 February 1996 LER 96-003-00:on 960115,technicians Found Low Voltage cut- Off for Alternate Shutdown Panel Inverter Set That Resulted in Unavailability of Panel.Caused by Inadequate Post Mod. Readjusted Set Point to Minimum setting.W/960215 Ltr ML18065A4581996-01-31031 January 1996 LER 96-001-00:on 960103,failed to Test Duplicate Equipment. Caused by STS No Longer Containing Requirement for cross- Train Testing of Duplicate Components.Will Submit Request to Delete Subj Requirements from TS.W/960131 Ltr ML18065A4421996-01-19019 January 1996 LER 95-016-00:on 951226,did Not Analyze Primary Coolant Samples within 72 H.Caused by Belief Acceptability to Save Pcs Samples for Choride Analysis Past 72 H.Counseled Chemistry Supervision.W/960119 Ltr ML18065A4041996-01-15015 January 1996 LER 95-014-00:on 950119,PCP Oil Collection Deficiencies Created by FC-860 Piping Mod.Caused by Inadequate DBD for Sys & Lack of Review by Experienced Fire Protection Personnel.Updated Design Basis documentation.W/960115 Ltr ML18065A3291995-12-0404 December 1995 LER 95-013-00:on 951103,circuit Fuse Coordination Deficiency Which Affects App R Safe Shutdown Equipment Noted.Design of Fuse Coordination in Potential Transformer Circuits Will Be Evaluated & Modified as required.W/951204 Ltr ML18065A2361995-11-0202 November 1995 LER 95-012-00:on 950701,discovered Unqualified Electrical Connection in Containment SW Outlet Valve Controller.Caused by Failure of Assigned Engineers to Available Info.Replaced Wire Nuts W/Inline Butt connections.W/951102 Ltr ML18065A2051995-10-20020 October 1995 LER 95-008-01:on 950728,discovered That None of Four Containment High Pressure Channels Would Initiate Reactor Trip Due to Programmatic Deficiencies.Administrative Procedure (AP) 9.44,AP 9.45 & AP 10.44 Will Be Revised ML18065A0841995-09-18018 September 1995 LER 95-011-00:on 950817,CR 40 Withdrawal Occurred When Given Insertion Signal Due to skill-based Error in Crimping & Removing Foreign Matl from CRDM Motor Connection Box.Crd Package replaced.W/950918 Ltr ML18065A0681995-09-14014 September 1995 LER 95-010-00:on 950815,ESFA Resulted in Manual Rt Following Isolation of Pcs.Replaced Failed Instrument Line ML18065A0651995-09-0808 September 1995 LER 95-009-00:on 950728,discovered Lack of Procedural Guidance for Pump Repair Following Fire.Proposed Use of Power Supply Breaker Did Not Adequately Address Effect of Loss of Control Power.Performed Independent Assessment ML18064A8781995-08-28028 August 1995 LER 95-008-00:on 950728,discovered During Design Change Testing That None of Four Containment High Pressure Channels Would Initiate Rt.Caused by Programmatic Deficiencies. Reviewed Selected Tests & Mods from Recent Refueling Outage ML18064A8831995-08-21021 August 1995 LER 95-007-00:on 950720,discovered That 12 Instrument Loops Had V-bolted Type Qualified Cable Splices Connected to Wires W/Exposed Kapton Insulation.Caused by Human Error.All V- Bolted Splices Replaced w/in-line design.W/950821 Ltr 1999-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18066A6901999-11-0101 November 1999 Rev 5 to Palisades Nuclear Plant Colr. ML18066A6761999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Palisades Nuclear Plant ML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6351999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Palisades Nuclear Plant ML18066A6771999-08-31031 August 1999 Operating Data Rept Page of MOR for Aug 1999 for Palisades Nuclear Plant ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A6061999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Palisades Nuclear Plant.With 990803 Ltr ML18066A5201999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Palisades Nuclear Plant.With 990702 Ltr ML18066A4841999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Palisades Nuclear Plant.With 990603 Ltr ML18066A6371999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant ML18068A5941999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant.With 990503 Ltr ML18066A4161999-04-0101 April 1999 Rev 4 to COLR, for Palisades Nuclear Plant ML18066A4501999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Palisades Nuclear Plant.With 990402 Ltr ML18066A4671999-03-31031 March 1999 Rev 0 to SIR-99-032, Flaw Tolerance & Leakage Evaluation Spent Fuel Pool Heat Exchanger E-53B Nozzle Palisades Nuclear Plant. ML18068A5351999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Palisades Nuclear Plant.With 990302 Ltr ML18066A3931999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Palisades Nuclear Plant.With 990202 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML20206F6131998-12-31031 December 1998 1998 Consumers Energy Co Annual Rept. with ML18066A3651998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Palisades Nuclear Plant.With 990105 Ltr ML18066A3421998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Palisades Nuclear Plant.With 981202 Ltr ML18066A3301998-11-11011 November 1998 Part 21 Rept Re Potential Safety Hazard Associated with Wrist Pin Assemblies for FM-Alco 251 Engines at Palisades Nuclear Power Plant.Caused by Insufficient Friction Fit Between Pin & Sleeve.Supplier of Pin Will No Longer Be Used ML18068A4921998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Palisades Nuclear Plant.With 981103 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A3181998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Palisades Nuclear Plant ML18066A2901998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Palisades Nuclear Power Plant.With 980903 Ltr ML18066A3191998-08-31031 August 1998 Revised Monthly Operating Rept Data for Aug 1998 for Palisades Nuclear Plant ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237E0301998-07-31031 July 1998 ISI Rept 3-3 ML18066A2701998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Palisades Nuclear Plant.W/980803 Ltr ML18066A2311998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Palisades Nuclear Plant ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A3061998-06-18018 June 1998 SG Tube Inservice Insp. ML20249C4951998-06-17017 June 1998 Rev 1 to EA-GEJ-98-01, Palisades Cycle 14 Disposition of Events Review ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18066A1711998-06-0101 June 1998 Part 21 Rept Re Impact of RELAP4 Excessive Variability on Palisades Large Break LOCA ECCS Results.Change in PCT Between Cycle 13 & Cycle 14 Does Not Constitute Significant Change Per 10CFR50.46 ML18066A1741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Palisades Nuclear Plant.W/980601 Ltr ML18066A2321998-05-31031 May 1998 Revised MOR for May 1998 for Palisades Nuclear Plant ML18068A4701998-05-31031 May 1998 Annual Rept of Changes in ECCS Models Per 10CFR50.46. ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18066A2331998-04-30030 April 1998 Revised MOR for Apr 1998 for Palisades Nuclear Plant ML18068A3461998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Palisades Nuclear Plant.W/980501 Ltr ML18066A3411998-04-22022 April 1998 Rev 0 to EMF-98-013, Palisades Cycle 14:Disposition & Analysis of SRP Chapter 15 Events. ML18065B2071998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Palisades Nuclear Plant.W/980403 Ltr ML20217C2741998-03-31031 March 1998 Independent Review - Is Consumers Energy Method (W Method) of Determining Palisades Nuclear Plant Best Estimate Fluence by Combining Transport Calculation & Dosimetry Measurements Technically Sound & Does It Meet Intent of Pts ML18066A2341998-03-31031 March 1998 Revised MOR for Mar 1998 for Palisades Nuclear Plant ML18068A3041998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Palisades Nuclear Plant.W/980302 Ltr ML18066A2351998-02-28028 February 1998 Revised MOR for Feb 1998 for Palisades Nuclear Plant ML18065B1641998-02-0505 February 1998 Rev 0 to Regression Analysis for Containment Prestressing Sys at 25th Year Surveillance. ML18067A8211998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Palisades Nuclear Plant.W/980203 Ltr 1999-09-30
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Text
consumers Power GB Slade GenerafMariager l'DWERINli .
MICHlliAN"S l'IUlliRESS Palisades Nuclear Plant: 27780 Blue Star Memorial Highway, Covert, Ml 4904.3 .
November 25, 1992 Nuclear RegulatorY Commission*
Document Control Desk Washington, DC 20555
- DOCKET 50~255 - LICENSE DPR PALISADES PLANT -
LICENSEE EVENT REPORT 92-039 - AUTOMATIC REACTOR TRIP ON LOSS OF LOAD RESULTING FROM UNSTABLE VOLTAGE TO THE TURBINE CONTROL SYSTEM COMPUTERS Licensee_ Event Report (LER)92-039 is attached.* This event is reportable in accordance with 10 £FR 50.73(a)(2)(iv) as an event that resulted in the automatic actuation of the reactor protective system; Gerald B Slade General Manager CC Administrator, Region III, USNRC NRC Re~ident Inspector - Palisades Attachment 9212030486 921125 PDR ADOCK 05000255 S . PDR
NAC Form 366
!9-BJI
U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 i66
. LICENSEE EVENT REPORT (LERI FACILITY NAME 11 I DOCKET NUMBER 121 PAGE 131 Palisades Plant 01s101010121s1s ' I OF 0 1s TITLE 141 AUTOMATIC REACTOR TRIP ON LOSS OF LOAD RESULTING FROM UNSTABLE VOLTAGE TO THE TITRRTNF. rnN'T'ROT * ~V~'T'F.M f'OMPTT'T't;>l2~ '
EVENT. DATE 161 LEA NUMBER 161 REPORT DATE 161 OTHER FACIL.ITIES INVOLVED !Bl SEQUENTIAL REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR N/A 0161010101 I
11 0 310 9 2 912 0 13 19 010 i 1. 1 .21s. 912 N/A 0161010101 I THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR I: ICh<<:lc one OI' mOl'9 of rM followifl(ll 11 1 I OPERATING N MOOE 191 I
20.4021bl 20.406icl
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- 73.71(bl POWER, LEVEL 1101 ii o Io. - 20.40610111 Hil 20.40611111 lliil 20.40610111 l(iiil 60.381cll1 I 60.381cll21
- 60. 7 31oll2Hil 60.731ell21M 60.731ell2Hviil
. 60.731oll211viiiHAI 73.71 lei OTHER !Specify in Abatroct below and in Text.
- 20.4061oll1 Hivl 20.40611111 IM - 60. 7 3 loll211iil 60.731oH211iiil LICENSEE CONTACT FOR THIS LER 1121
- 60. 7 3 loll211viiillBI 60.731oll211xl NRC Form 386AI .
NAME TELEPHONE NUMBER William L. Roherts, Staff Licensing Engineer sARtA,cj°~ J 1 I I 4 I - I aI 9 I , I 3 s
COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MANUFAC- REPORTABLE MANUFAC-
- REPORTABLE CAUSE SYSTEM COMPONENT TUR ER TO NPROS CAUSE. SYSTEM COMPONENT. TURER TO NPRDS I I I I I I I I I I *I I I I I I I I I I I I I I I I I I MONTH DAY YEAR n
SUPPLEMENTAL REPORJ' EXPECTED 1141 EXPECTED SUBMISSION Y.ES Vf yu~ cOl'np/*t* EXPECTEf SUBMISSION DATEI *
~NO DATE 1161 ABSTRACT ILimir ro 1400 - ... i.* .. appro*im.r.Jy fihfffl. llin~-* typewrin.n linul I 181 *,
I *1 I
On Octobet 30, 1992~ at 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />, the plant was operating at 100% ~ower. As a result of a turbine gen~rator trip the reactor automatically tri~ped on a loss of load si~nal. The turbine generator trip was initiated by coincident s utdown of the primary an backu~
computers in the turbine generator digital electrohydraulic (DEHf control system. Pant response to the event was good, with no safety significant *devia ions or anomalies noted.
BD design the* DEH com~u~ers were being s~~pl ied from a single ~nin~erruptable ~ower sup~ly
( PS{. The cause of his ev~nt was a fa1 ure.of.the UPS to maintain ~ro~er vo tage at~ he
. inpu to the DEH ~ower supplies. Volta~e variations at the UPS out~u (i.e., the DEH 1nput
- . power suppl1) cou d not be handled by t e DEH system and all four D H computers * . **
- automatical y went to their fail safe condition tripping the turbine generator. . . .
Corrective action for this event included addin~ redundancy to the computer power circuits;
.adlusting volta9e and installing new cables on he existing power source; installing two new vo ta?e regulating transformers in the back-up power source; install in~ new power supplies in al four DEH data processing computers; and adding alarms to the DE control room console. .
' NRC Form 3118A li-831
- .e LICENSEE EVENT REPORT (LERI TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO_. 3160-¢1 O*
EXPIRES:. 8/31186
-: FACILITY NAME 111 . DOCKET NUMBER 121 LER NUMBER 131 PAGE l'I .
SEQUENTIAL REVISION YEAR NUMBER
. Palisades Plant o I s Io Io Io I2 I s Is 9 12 - o I 3 I 9 - o I o . ol 2 oF ob
" EVENT DESCRIPTION On October 30, I992, at approximately 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />, the plant was operating at IOO% power with all systems in normal full power alignment, when the reactor automatically tripped on a loss of load signal. The loss of load signal was a result of an unstable voltage (power supply) to the turbine digital electrohydraulic (DEH) control iystem [TG;CPU] computers.'
Subsequently all four of the DEH data processing units shut down, causing a turbine trip signal which enabled the associated Reactor Protective System loss of load trip. Low ste~m ~enerator levels in both generators injtiated an AFWAS and the start of one
Operations entered Emergency Operating Procedure (EOP) I, ~Post Trip Actions" and later EOP 2, "Trip Recovery" to stabi 1i ze the p1ant in hot sh.utdown. The trip recovery actions . *
. included emergency boration that was due to the failure of Bus IA to transfer to start~up power and. the resulting loss of 2 of the 4 operating primary coolant pumps.
- A post trip review*was completed shortly after the event. The following are highlights from the post trip review report~ -
- The 4I60 VAC non-safety related Bus IA supplying two of the.four primary coolant pumps~ failed to transfer to start-up power from station power, resulting in the loss of two primary coolant puinps.
- The secondary rod pos.iti*on for control rod drive number I6 remained at its*.
previous indication of about 73 inches following the.trip~ the primary indication showed that the control rod had dropped to the bottom of the core.
Two of the four plant control room event recorders (3 and 4), did not activate on the trip. -
This event is rep6rtable in a~corda~ce with .IO CFR 50.73 (a)(2)(iv) as an event that
.resulted in the automatic actuation of the reactor protective system.
CAUSE OF THE EVENT The cause of this event was a failure of the uninterruptable power supply (UPS) to maintain proper voltage at the input to the DEH power supplies. Voltage variations at the UPS output (i.e. the DEH power supply input) could not be handled by the DEH system and.
the DEH computers automatically went to their fail safe condition .. All four DEH computers shut down, tripping the turbine generator. This turbine generator trip resulted in the 1oss of 1oad trip of the reactor. * * ..
ANALYSIS OF THE EVENT
- The plant had previously tripped on July 1 and July 24, 1992, on Joss of load. sig~als
'generated from a loss of power to the DEH system. After the July 1, 1992 event, post trip testing had dup 1i cated the p1ant trip by what was determined to be loose computer .*
./.
NRC Form 388A (1-831 LICENSEE EVENT REPORT !LERI TEXT CONTiNUATION U.S. NUCLEAR REGUUITORY COMMISSION APPROVED OMB NO. 3160-<1.10'
- EXPIRES: 8/3i186 FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAL REVISION YEAR NUMBER NUMBER Palisades Plant Q 5 Q Q Q 2 5 5 9 2 - Q 3. 9 - Q Q Q 3 . OF Q connecting cables. Following the July 24, I992 plant trip, it had been determined that input voltage fluttuations to the DEH computer~ had been the probable cause for both the July I, I992 and the July 24~ I992 plant trips~ The July 24, I992 plant trip occurred coincident with the performance of a plant test which calls for the plant sequ~ncer tb simultaneously start a number of safety injection system loads. The starting of this equipment resulted in a mqmentary system voltage drop. This low voltage input was
_interpreted by the DEH as a loss of primary power. The DEH then attempted to switch to its secondary power source. The DEH's power supply voltage dropped to below approximately 4.5 volts while it was seeking a stable power source from its secondary power supply, and when the voltage went lower than 4.5 VAC, the DEH shut itself down to prevent damage.
With the DEH not in operation a turbine trip was initiated. To correct this deficiency an uninterruptable power supply with an extended.battery capacity was added to the system to filter any erratic incoming voltage to the DEH data processing units power supplies; On October 30, I992, by design, the DEH computers were being supplied from a single uninterruptable power supply. Because of the low and unstable input voltage condition, the UPS sw.itched to. a bypass condition _where it was no longer trying to condition the .
- incoming voltage. As a result of .this switching, the lOw and fluctuating voltage was now fed directly to the DEH computer DC po~er supplies. We estimate that the UPS had been:.
powering the DEH at approximately I32 VAC. When the UPS was bypassed the* unfiltered line voltage now powering the DEH DC power supplies was estimated to be approximately I08 VAC directly from the plant distribution panel. The DEH power supplies could ncit withstand
- this -approximate -24 .VAC transient in its power feed and since the UPS was the prtm_a.ry power source to the two controlling and the two standby computers, all .four computers shut down and the turbine trip signal was initiated. * *
- Subsequent investigation has shown that the UPS was designed to switch to its battery back-up at an input voltage of approximately 176 VAC. The voltage ~upplied to th~ UPS was determined to be, on average, approximately I82 VAC versus a normal input voltage of 208 VAC plus or minus IO%. It is estimated that the voltage t~ the UPS varied fro~ a low lev~l of 176 VAC to a highest level of I87 VAC preceding the tri~. It is believed that this low and varying voltage condition for extended periods of tiine led to the UPS inverter shutting down its rectifier and placing the UPS in the bypass mode.
The 4I60 VAC non-safety related Bus IA supplying two of the four primary coolant pumps failed to transfer to start-up power from station power, resulting in the loss of two
- primary ~oolant pumps. This start~up ~ower breaker had been replaced with a spare following a similar failure to transfer during the July I, I992 plant trip: Investi~ation of the July-I failure to transfer found that the breaker.cubicle interlock was not properly aligned. Corrective actions were taken and the breaker operated successfully during three subsequent plant trips prior to the October 30, I992 plant trip.
NRC Form 388A e- U.S. NUCLEAR REGULATORY COMMISSION 11-831 APPROVED OM8 NO. 31S0--01*0,
- EXPIRES
- . 8/31 /86 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAL. REVISION YEAR *. NUMBER NUMBER Palisades Plant 0 I5 I0 I0 I0 I2 I5 I5 9 I2 - 0 I3I9 - 0. I0 0 I4 OF 0 I5 During diagnostic testing following tha October 30 plant trip, using both the spare installed breaker and the breaker that was removed in July, we were able to rec*reate the breaker failure to close. Review of a video tape of the breaker in operation showed that the cubicle interlock foot pedal bounces during breaker operation. The purpose of this interlock is to ensur~ that the breaker is tri~ped prior to moving the breaker within the cubicle or withdrawirig the breaker from the cubicle .. The bouncing of the foot pedal allows it to strike the trip lever and trip the breaker. Visual inspection also showed that the metal floor of the breaker cubicle has an approximate three-eights inch bow. This flex in the floor apparently amplifies the interlotk pedal bounce since installation of
. temporary shims allowed successful 'testing of the breaker. A temporary modification was installed to pin the interlock foot pedal to prevent inadvertent operation. Operation of the breaker is not affected, but the pin must be removed before tha breaker c~n be
- withdrawn from the cubicle.
A blown fuse was found in the common DC supply to control room event recorders .3 and 4.
_The fuse was replaced. Work order history has shown that this fuse has a history of blowing without finding a root cause. Replacement fuses with visual indicatibn of blown condition were _insta1led and they will be checked frequently to assure that the event
- recorders remain in service unt i 1 a re so 1ut ion_ to the fuse b1owing is fou_nd.
During initial troubleshooting to investigate why the secondary rod position for control rod 16 i~dicated 73._inches when the rod was at the bottom of the core, the relay for the secondary rod position was tapped and the indication returned to its proper reading. The secondary position indication problems are- being tracked by enginee-ring as* a lohg range operations concern item and therefore are being addressed on a programmatic basis.
While a reactor trip on losi of lbad is a challenge to. the plant safety systems because of the plant trip, all plant safety systems performed as designed and no significant safety deviations or anomalies were noted~
CORRECTIVE ACTION The existing DEH DC power suppiies were changed to a.power supply which has improved switching and input voltage tolerance. -
The AC power supply to the back-up DEH tomputers was provi~ed with power from a source independent of the UPS. This provides a degree of redundancy for the priinary, and backup computers. -
Taps were changed on the transformer supplying power to the UPS to re~tor~ the voltage to a nominal 208 VAC from the previous 198 VAC. Further, additional electrical ca6le was run between the power panel and the UPS to reduce th~ voltage drop to less than 3% of nominal.
Voltage regulating transformers were installed to the DEH power supply inputs not supplied by the UPS, to help to condition the input voltage_ and to reduce the tisk of unregulated voltage reaching the computers.
NRC Form 398A U.S. NUCLEAR REGULATORY COMMISSION 19-831 ~OVED OMB NO. 3160-010' EXF'lRES: '8/31186 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111 DOCKET NUMBER 121
- LER NUMBER 131 SEQUENTIAL REV1!110N YEAR NUMBER NUMBER Palisades Plant
- 0 5 0 0 0 .2 5 5 9 2 - 0 .3 9 - Q Q Q 5 OF Q 5 Alarms "UPS On Battery", and "UPS On Bypass", were added to the DEH system to.provide the controJ* room operators with an early warning of potential UPS problems.
- Temporary voltage wave-form disturbance analyzers were installed on the DEH and UPS systems to monitor voltage conditi-0ns during system operation for the remainder of this operating cycle.
All of the above mentioned enhancements were successfully tested and prov~n to have significantly improved the tolerance of the DEH system to known or* expected voltage transients~
In addition to the temporary modific*tion that was installed to pin the trip lever of the start-up power breaker to prevent inadvertent operation, the following longer term actions are planned as part of our corrective action process: * *
- Disas~emble and inspect the spare 4160 volt breaker to assure that no other problems exist with it. . *
- Evaluate the replacement of existing springs, of all 2400/4160 volt breaker foot petals, with stronger springs to prevent or reduce pedal bounce during a clo_se operation. . *
- Walk-down all 2400/4160 VAC bre~ker cubicles and inspect for warped or bowed floors and evaluate methods to reduce cubicle "floor boun~e" during breaker*
operation. * . ..
- Review work order hi story files for evidence of any other medium voltage breaker malfunctions that may need to be investigated.
ADDITIONAL INFORMATION Related recent plant trips have been reported in Licensee Event Reports92-034 and 92-035 ..
LICENSING CORRESPONDENCE\COMMITMENT TRACKING RECORD-
SUMMARY
DATE: November 25, 1992 DOCKET 50-255 LICENSE DPR~20 - PALISADES PLANT LICENSEE EVENT REPORT 92-039 Automatic Reactor Trip On Loss Of Load Resulting From Unstable Voltage~o The Turbine Control System Computer~
SUMMARY
- Transmits LER 92-039 which describes the October 30, 1992 plant trip. The.
reactor tripped when the turbine generator tripped. The turbine tri~ resulted from the DEH computers' response to a voltage transient which occurred when the UPS went to bypass and the DEH system was switched to a low voltage plant feed.
Previous Previous NRC Letters Dated: LC _ _ __ CPCo Letters Dated: LC LC - - -
LC -'--------'--- LC--
LC LC - -
UFI NO: 950-73*20*01*01 Individuals Originator: Concurrences: Concurrences: Providing Info:
WLRoberts TJPalmisano GBSlade TE Leva PMDonne1ly JLKuemin TCAnderson Special KEOsborne JLHanson MTNordin Di stri but ion: RSWesterhof MTNordin TE Leva *psE LOG PRC MTG*
NPAD LOG COMMITMENT TRACKING COMMITMENTS MADE:
Assigned Individual:
Related CA Document No: CTS Commitment No:. - - - - - - -
- Commitment To.Be Made' Resident? Resident Document:
COMMITMENTS CLOSED:.
Provide report to NRC within 30 days of the event.
Related CA Document No:E-PAL-92-067 CTS Commitment.No:.
Additional -Information Needed for CTS Entry:
System Code:
Suggested Keywords: