LER 97-024-03:on 970917,material Discovered in Containment Degrades Containment Recirculation Sump & Resulted in Condition Outside Design Basis.Caused by Inadequate Specification & Procedures.Procedures RevisedML17334A667 |
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Cook |
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Issue date: |
03/04/1998 |
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From: |
Schoepf P AMERICAN ELECTRIC POWER CO., INC. |
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Shared Package |
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ML17334A668 |
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References |
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LER-97-024, LER-97-24, NUDOCS 9803100031 |
Download: ML17334A667 (6) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors ML17335A5171999-02-11011 February 1999 LER 99-002-00:on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted ML17335A5141999-02-10010 February 1999 LER 99-001-00:on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:RO)
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors ML17335A5171999-02-11011 February 1999 LER 99-002-00:on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted ML17335A5141999-02-10010 February 1999 LER 99-001-00:on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
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Text
NRC FORH 366 .S.~
~ NUCLEAR REGULATORY COMHISSION PROVED BY OMB Ho. 3150 0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY MITH THI INFORHATIOH COLLECTION REOUEST: 50.0 HRS. FORHAR LICENSEE EVENT REPORT (LER) COMMENTS REGARDIHG BURDEN ESTIMATE To TH INFORMATION AND RECORDS MANAGEMENT BRANCH (MNB 7714), U.ST NUCLEAR REGULATORY COMHISSION, lIASHINGTON, DC 20555-0001, AND TO THE PAPERER REDUCTION PROJECT (3150 0104), OFF ICE 0 HANAGEHEHT AND BUDGET MASHINGTON DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) Page 1 of6 Donald C. Cook Nuclear Plant - Unit 1 50.315 TITLE (4)
Material Discovered in Containment Degrades Containment Recirculation Sump and Results in Condition Outside Design Basis EVENT DATE 5 LER NUMBER 6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8 SEQUEHTIAL REVISION FACILITY NAME DOCKET NUHBER MONTH DAY YEAR YEAR NUHBER NUMBER MONTH DAY YEAR Cook Unit 2 50-316 FACILITY HAME DOCKET NUMBER 09 17 97 97 024 03 03 04 98 OPERATIHG THIS REPORT IS SUBMITTED PURSUANT To THE REQUIREHENTS OF 10 CFR : Check one or mor e 11 MODE (9) 20.2201(b) 20 '203(a)(3)(l) 50.73(a)(2)(iii) 73.71(b)
POWER 0
20.2203 0 1 20.2203 a 3 ii 50.73 a 2 iv 73.71o LEVEL (10) 20.2203(a)(2)(l) 20.2203(a)(4) 50.73(a)(2)(v) OTHER 20.2203 a 2 ii 50.36 c 1 50.73 a 2 vii (Specify in 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(viii)(A) Abstract below and in Text, 20.2203(a)(2)(iv) 50.73(a)(2)(l) 50.73(a)(2)(viii)(B) HRC Form 366A) 20.2203(a)(2)(v) 50.73(a)(2)(ii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER 12 NAME TELEPHONE NUMBER (Include Area Code Mr. Paul Schoepf, Safety Related Mechanical Engineering Superintendent 616/465-5901, x2408 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN HIS REPORT 3 REPORTABLE REPORTABLE CAUSE SYSTEH COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER To NPRDS To NPRDS SUPPLEMENTAL REPORT EXPECTED 14 EXPECTED HONTH DAY YEAR YES SUBHISSION X (If yes, complete EXPECTED SUBHISSION DATE).
No DATE (15) 04 30 98 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On September 11, 1997, a fibrous material, known as Fiberfrax, was identified in an electrical cable tray inside the Unit 2 containment. An investigation was initiated to determine the scope and magnitude of this condition. On September 17, 1997, with Units 1 and 2 in cold shutdown, it was determined that Fiberfrax was present in both containments in enough quantity to potentially cause excessive blockage of the containment recirculation sump screen during the recirculation phase of a Loss of Coolant Accident and render the sump inoperable. An ENS notification was made at 1629 hours0.0189 days <br />0.453 hours <br />0.00269 weeks <br />6.198345e-4 months <br /> on September 17, 1997, under 10CFR50.72(b)(2)(i), as a condition which was found while the reactor was shutdown, which if it had been found while the reactor was operating, would have resulted in the nuclear power plant being outside the design basis. As part of the investigation, reviews were conducted of industry information related to containment sump strainer blockage, and plant insulation specifications. Walkdowns were conducted of both containments and other potential material threats to blockage of the recirculation sump were identified and dispositioned.
The root cause of this condition has been attributed to inadequate specifications and procedures which did not preclude or strictly control these types of materials. The materials have either been removed from the containments, or have been evaluated and determined to not constitute a substantial threat to the recirculation sump. Additionally, the condition of containment coatings was reviewed and repair of some coatings has been undertaken. Specifications and procedures are being revised and lor developed to preclude or strictly control materials inside containment which could block the recirculation sump.
Analysis using models for debris generation and transport is ongoing to definitively determine the effect the materials would have had on the sump and the safety related equipment which take suction from it. This information will be provided to the NRC when it becomes available. The projected date for submittal of that information is April 30, 1998.
9S03i0003i 050003i5 980304"'DR ADQCK S PDR
NRC FORM 366A U UCLEAR REGULATORY COMHISSION PROVED BY OMB No. 3150-0104 a EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY MITM TMI INFORMATION COLLECTION REQUEST: 50.0 HRS. FORllAR LICENSEE EVENT CONTINUATION COHMENTS REGARDING BURDEN ESTIMATE To TH INFORMATION AND RECORDS MAHAGEMEHT BRANCH (MNB 7714), U.S. NUCLEAR REGULATORY COMMISSION, MASHINGTON, DC 20555-000'I, AND TO THE PAPERER REDUCTION PROJECT (3150 0104), OFFICE 0 MANAGEMENT AND BUDGET WASHINGTON DC 20503 NAME 1 DocKET NUMBER 2 LER NUMBER 6 PAGE 3'ACILITY YEAR SEQUENTIAL REVISION Cook Nuclear Plant - Unit 1 50-315 97 024 03 2OF6 TEXT ($ f sore space $ s required. use addlttooal NRC Fons 366A's) (17)
C Unit 1 was in Mode 5, Cold Shutdown Unit 2 was in Mode 5, Cold Shutdown v
On September 11, 1997, a fibrous material, known as Fiberfrax, was identified in an electrical cable tray inside the Unit 2 containment. An investigation was initiated to determine the scope and magnitude of this condition. On September 17, 1997, at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br />, with Units 1 and 2 in cold shutdown, it was determined that the Fiberfrax was present in both containments in enough quantity to potentially cause excessive blockage of the containment recirculation sump screen during the recirculation phase of a Loss of Coolant Accident (LOCA), and render the sump inoperable. An NRC prompt notification was made at 1629 hours0.0189 days <br />0.453 hours <br />0.00269 weeks <br />6.198345e-4 months <br /> on September 17, 1997, under 10 CFR 50.72(b)(2)(i), as a condition which was found while the reactor was shutdown, which if it had been found while the reactor was operating, would have resulted in the nuclear power plant being outside the design basis.
Investigation determined that the fibrous material identified in the Unit 2 containment cable tray was "damming" material, which was a by-product from the installation of an adjacent foam fire stop. A series of three design changes installed the fire stops in 12 cable trays in the Unit 1 containment and in 15 cable trays in the Unit 2 containment. Installation of the fire stop and damming material was guided by a procedure, 12CHP5021.ECD.005, "Installation, Replacement and Repair of Silicone Fire Barrier Penetration Seals." The procedure and its referenced specification (DCC-FP-101-QCN, "Fire Barrier Penetration Seals" ), allowed the option to leave damming material in place or remove it "as required," without additional guidance. The installers left the damming material in place since the fiber impregnates in and cures to the foam, removal would have required cutting the material from the foam, and there was no requirement to remove it.
The existence of exposed fibrous material inside the containments is inconsistent with thermal insulation specifications, which require that thermal insulation be covered with 10 mil stainless steel jacketing.
Industry information related to containment sump strainer blockage was revisited and used as guidance for the conduct of additional containment walkdowns to identify whether other potential threats existed to the recirculation sumps. Walkdowns identified the presence of other materials which were considered potential threats to blockage of the recirculation sump. These materials included other fibrous insulation and miscellaneous material.
Fibrous insulation material known as Temp-Mat, which was either exposed or encapsulated in stainless steel Jacketing or stainless steel mesh, was identified in several localized areas both in the annulus (inactive sump) and lower volume (active sump), primarily where insulation had been removed for repair or weld examinations. Some fiberglass insulation material was also identified on a few lines.
Miscellaneous materials such as tape, labels and equipment stored in the containments were also Identified and questioned with respect to their qualification for the containment environment, their condition and their potential for recirculation sump blockage.
Finally, the condition of coatings was also reviewed, including their qualification and condition. A limited amount of unqualified coatings was identified, as well as some coatings which showed signs of degradation or lack of suitable adhesion.
HRC FORM 366A U UCLEAR REGULATORY COMMISSION PROVED BY OMB NO. 3150-0104 EXPIRES 5/3'I/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY UITM THI INFORMATION COLLECTIOH REOUEST: 50.0 HRS. FORNAR LICENSEE EVENT CONTINUATION COMMENTS REGARDING BURDEN ESTIMATE TO TH INFORMATION AND RECORDS MANAGEMENT BRANCH (MHB 7714), U.S. NUCLEAR REGULATORY COMHISSIOH, NASHIHGTON, DC 20555-0001, AHD TO THE PAPERNOR REDUCTION PROJECT (3150-0104), OFFICE 0 MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME 1 DOCKET NUMBER 2 LER NUMBER 6 PAGE 3 YEAR SEQUENl'IAL REVISION Cook Nuclear Plant - Unit 1 50-315 97 024 03 3OF6 TEXT (if more space is required. use addit(ooal NRC Form 366A's) (17)
The root cause of this condition has been attributed to inadequate specifications and procedures which did Iiot preclude or strictly control these types of materials.
al sis f he Eve This event is reportable under 10CFR 50.72(b)(2)(i), as a condition which was found while the reactor was shutdown, which if it had been found while the reactor was operating, would have resulted in the nuclear power plant being outside the design basis and was reported via ENS on September 17, 1997, under that provision of 10CFR50.72. This LER is therefore submitted in accordance with 10CFR50.73(a)(2)(ii), as a condition outside the design basis.
An evaluation of the impact of the identified material noted that much of the material was in locations remote from the recirculation sump, and/or was in localized areas, and therefore, individually did not constitute a significant threat to the recirculation sump. Furthermore, the precise interaction of this material with the recirculation sump could not be predicted with certainty, due to the lack of models to determine post-accident debris generation and transport.
However, given the quantity and variety of materials considered, and the lack of detailed models to study post-accident debris generation and transport in Pressurized Water Reactors (PWRs), blockage of the sump cannot be discounted. A discussion of the materials identified, considered and either removed or dispositioned, follows.
With regard to the fibrous material inside containment cable trays, the cable trays are 12 inches wide and 6 inches high. The length of the damming material varies with each installation, but averages approximately 1 foot.
Therefore, the amount of fibrous damming material is approximately 0.5 cubic feet ( ft per installation. Based on this material being installed in 12 and 15 containment cable trays in Units 1 and 2 respectively, an estimate of the amountofthis material is 6 ft'in Unit1 and 7.5 ft'in Unit2. As previously noted, the fibrous material cures to the adjacent foam fire stop during the installation process. The 27 locations where this material was installed were in the containment annulus or vertically adjacent instrument room. These areas contain relatively low energy lines, and are physically separated from and not in good communication with the active sump, which contains the recirculation sump, although some communication did exist between these two volumes of containment in past operating cycles. The cable trays are either of a steel mesh or a solid design, with mesh, slotted or solid covers, which provides some protection against the material's potential to migrate to the recirculation sump. Although the fibrous material in containment cable trays represents a potential threat to the recirculation sump, the threat to the sump was considered relatively minor given the physical configuration of the material and its location. This material has been removed from the containments.
With regard to the broader issue of other fibrous material, this material was installed in a several locations in both containments. In considering post-accident debris threats, the containment area of primary concern for communication with the recirculation sump is the lower volume which contains the reactor coolant system (RCS) loop piping and components. This area, which is inside the crane wall, is referred to as the active sump volume. An adjacent annular region outside the crane wall, referred to as the inactive sump volume, is not in good communication with the recirculation sump, and therefore, material in that area represents a relatively minor threat to recirculation sump blockage. Fibrous material in the active sump which was considered a potential threat to sump blockage included both exposed material and material covered with stainless jacketing in areas near to the RCS loop piping. A total of 333 pounds (Ibs) and 167 Ibs of fibrous material was removed from these areas in Units 1 and 2, respectively, which was well distributed in the lower volume. As a point of information, this material has a volume of approximately 10 ft '/lb.
NRC FORH 366A U UCLEAR REGULATORY COMMISSION PROVED BY OMB NO. 3150 0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THI INFORMATION COLLECTION REOUEST: 50.0 HRS. FORWAR LICENSEE EVENT CONTINUATION COMMENTS REGARDING BURDEN ESTIMATE TO TH INFORMATION AND RECORDS MANAGEMENT BRAHCH (HNB 7714), U.ST NUCLEAR REGULATORY COMHISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWOR REDUCTION PROJECT (3150-0104), OFFICE 0 MANAGEHENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME 1 DOCKET NUMBER 2 LER HUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION Cook Nuclear Plant - Unit 1 50-315 97 024 03 4 OF 6 TEXT (if more space is required. use additional NRC Form 366A's) (17)
I s f Ev o 'd Some fibrous material was also removed from the regions outside the crane wall (inactive sump volume), however, this material was primarily dispositioned by ensuring that any fibrous material was well covered in securely fastened stainless steel jacketing.
material, which was a piece roughly 10 foot by 10 foot, represents approximately 15 ft each containment.
'f In February, 1998, additional fibrous material was discovered in the ice condenser area of both units. The fibrous additional material for Another possible debris threat considered was the Containment Auxiliary Filter units located in the lower volume of each containment. These filter units had not been used since early plant operation. Although earlier analyses, which took credit for Leak Before Break (LBB), indicated the units would withstand the jet forces associated with postulated accidents, current guidance ruled that LBB may not be used when determining debris generation. The filter media in the ventilation units represented another source of debris. A total of 2980 Ibs of material associated with these units was removed from each containment (100 Ibs HEPA filter, 2880 Ibs charcoal).
Several different types of tape were identified in the containments and evaluated. Gray duct tape was noted in several areas of both containments including the upper and lower regions of the ice condenser, the lower volume (active sump) and annulus (inactive sump). Although the tape was securely affixed, and in most cases a transport path to the recirculation sump would be tortuous, transport of this material to the recirculation sump could not be discounted. Therefore, identified duct tape, approximately 100 square feet (ft') in Unit 1 and 200 ft'n Unit 2, was removed. Black electrical tape and white fiberglass tape were also identified and reviewed. These tapes were inspected to ensure good adhesion, and minor amounts of loose tape were removed in some areas.
Labels used for equipment identification were inspected and found to be in good condition. A few labels which were peeling were either removed or replaced. Overall, labels were not considered to constitute a significant threat to sump blockage due to their good adhesion.
Coatings were evaluated from the perspective of qualifications and condition. Most containment coatings were confirmed qualified for use in the containment. A few areas were identified to have unqualified coatings and some areas were noted to show signs of degradation or lack of suitable adhesion. Areas of loose coatings were removed and new coatings were applied in some cases. A total of 3850 Ibs of coatings were removed from the Unit 1 containment and 680 Ibs were removed from the Unit 2 containment. The most notable area of repair was the floor of the Unit 1 lower volume, where coatings were electively removed down to base concrete and new coatings were applied. This accounts for the large mass of coatings removed from that unit. Due to the amounts of loose coatings, and the unavailability of debris generation and transport models, transport of this material to the sump could not be discounted.
I The practice of storing equipment in the containments was also reviewed. This includes equipment such as welding machines, vacuums and manlifts, which are used during outages. Although this equipment was reviewed at the time of installation for proper seismic mounting, reviews did not consider debris generation and impact on debris transport due to localized velocity effects. This equipment was removed from the containments where its impact on debris generation or transport could not be discounted.
NRC FORM 366A U UCLEAR REGULATORY COMMISSION PROVED BY OHB HO. 3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY MITH THI INFORMATION COLLECTIOH REQUEST: 50.0 HRS. FORllAR LICENSEE EVENT CONTINUATION COMMENTS REGARDING BURDEN ESTIMATE TO TH INFORMATION AND RECORDS MANAGEMENT BRANCH (MNB 7714), U.S. NUCLEAR REGULATORY COMMISSION, IIASHINGTON, DC 20555-0001, AND TO THE PAPERNOR REDUCTION PROJECT (3150-0104), OFFICE 0 MANAGEMENT AND BUDGET NASNINGTON DC 20503.
FACILITY NAME 'I DOCKET NUMBER 2 LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION Cook Nuclear Plant - Unit 1 50-315 97 024 03 5 OF 6 TEXT (if sore space is required. use additional NC Fore 366A's) (17) al o e ve co 'd Given the variety of locations and quantity of materials in combination with the lack of a model for debris generation and transport, blockage of the recirculation sump could not be discounted and the sumps were therefore considered inoperable in the as-found condition. In anticipation of the need for more detailed analyses for debris generation and transport to address the generic issue of sump/strainer blockage for PWRs, efforts are underway to develop models to study actual sump debris threats cause by this material.
An assessment of the operability of the containment recirculation sump is being prepared, which considers work ongoing and completed in the current outages, such as removal of fibrous insulation, insulation repair and coatings repair. This assessment will document the operability of the sumps in the as-left condition.
~*'
The Fiberfrax material has been removed from 12 cable trays in the Unit 1 containment and from 15 cable trays in the Unit 2 containment.
The procedure which guides the installation of Cable Tray Fire Stops has been revised to require that damming and forming materials, which are not encapsulated, be removed from containment for any future fire stop installations.
The related specification, which is referenced by the procedure, has also been revised to disallow fibrous damming materials to be left in place in the containment buildings.
Additional fibrous material was removed from the containments where it was considered a threat to the recirculation sump. The general condition of thermal insulation was reviewed and repairs were undertaken, where appropriate, to ensure that any remaining fibrous material was not exposed. Action Requests have been generated to remove the additional fibrous material from the ice condenser area that was discovered in February, 1998. This material will be removed prior to startup.
The Containment Auxiliary Filter Units, which contained both charcoal and HEPA filters, have been removed from the containments.
Miscellaneous materials such as tape and labels were examined and evaluated. Material was removed or repaired where it was considered a threat to the recirculation sump Miscellaneous equipment, previously stored in the containments, has been removed where its impact on debris generation and transport could not be discounted.
A critical review of containment coatings was undertaken. Based on a review of the qualification and condition of coatings, a program of coatings remediation was undertaken which included both removal of loose coatings and repair of coatings which showed signs of degradation or lack of suitable adhesion. Of particular note, coatings on the floor of the Unit 1 lower containment were removed down to the concrete, and the floor was resurfaced.
A specification will be prepared to provide a single repository of comprehensive industry and plant specific guidance on requirements for installation and use of materials in the containments, including guidance on limits for degradation of this material. This will be completed prior to the next refueling outage on either unit.
NRC FORH 366A U UCLEAR REGULATORY COHMISSION PPROVED BY OMB NO. 3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPOHSE TO COMPLY MITH THI INFORHATION COLLECTION REQUEST: 50.0 HRS FORNAR LICENSEE EVENT CONTINUATION COMMENTS REGARDING BURDEN ESTIHATE TO TH INFORMATION AND RECORDS MANAGEHENT BRANCH (MHB 7714), U.S. NUCLEAR REGULATORY COMMISSION,
'WASHINGTON~ DC 20555 0001 'ND To THE PAPERNOR REDUCTION PROJECT (3150-0104), OFFICE 0 MANAGEHENT AND BUDGET IIASHINGTON DC 20503.
FACILITY NAME 1 DOCKET NUMBER 2 LER NUHBER 6 PAGE 3 YEAR SEQUENTIAL REVISION Cook Nuclear Plant - Unit 1 50-315 97 024 03 6 OF 6 TEXT (if more space is required. use additional NRC Form 366A's) (17) aiedC o nt I 0 Not applicable os laEe s None