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Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B5661999-01-27027 January 1999 Unit 1 Steam Generator Layup Chemistry Out of Specification During 970924 Through 971231. ML17325B4511998-12-15015 December 1998 Rev 1 to ER-98-009, Preliminary Waste Characterization of DC Cook SG Lower Assemblies. ML17335A2741998-09-0101 September 1998 Rev 0 to ER-98-009, Preliminary Waste Characterization of DC Cook SG Lower Assemblies. ML17335A1921998-07-10010 July 1998 Non-proprietary Cook Unit 1 SG Operability Re-Review. ML17334A6151998-01-0606 January 1998 Containment Sump Operability Determination. ML17333B0921997-10-0909 October 1997 MAAP4 Analyses of DC Cook Containment Response to Small Break Loca. ML17333B0041997-08-14014 August 1997 Responses to RAI on Holtec Rept HI-951389 DC Cook Spent Fuel Pool. ML17333A9561997-07-21021 July 1997 Generator U1R97 Condition Monitoring & Operational Assessment. ML17333A9571997-07-21021 July 1997 Generators U1R97 2 Volt Interim Plugging Criteria Rept. ML17333A5641996-08-31031 August 1996 Final Rept, Reactor Vessel Nozzle Bore Data Evaluation. ML17333A2821995-12-31031 December 1995 DC Cook Nuclear Plant USI A-46 Seismic Evaluation Rept. ML17333A2801995-12-31031 December 1995 DC Cook Nuclear Plant USI A-46 Safe Shutdown Equipment List Rept. ML17333A2761995-12-31031 December 1995 DC Cook Unit 1 1995 Interim Plugging Criteria 90 Day Rept. ML17333A2891995-12-22022 December 1995 Updated Thermal-Hydraulic Analysis of Spent Nuclear Fuel Pool DC Cook Nuclear Plant Indiana Michigan Power Co. ML17333A3251995-11-30030 November 1995 Criticality Analysis of DC Cook Nuclear Plant New Fuel Storage Vault W/Credit for Integral Fuel Burnable Absorbers, for Nov 1995 ML17333A2831995-11-0606 November 1995 DC Cook Nuclear Plant USI A-46 Relay Evaluation Rept. ML17333A3321995-07-31031 July 1995 DC Cook Nuclear Plant Boric Acid Concentration Reduction. ML17333A9051995-07-25025 July 1995 Rev 0 to NRC GL 86-10 Technical Evaluation App R Section III.G.2(b) Twenty Foot Separation Between Redundant Components W/No Intervening Combustibles,Fire Zone 6M & Fire Zone 6S. ML17332A8021995-06-15015 June 1995 EDG Load-Run Performance & Reliability During Short & Long Duration Test Periods TER ML17333A9061995-06-0505 June 1995 Rev 0 to NRC GL 86-10 Technical Evaluation,App R Section III.G.2(b) Twenty Foot Separation Between Redundant Components W/No Intervening Combustibles Fire Zone 44N & Fire Zone 44S. W/Two Oversize Drawings ML17332A7611995-05-0505 May 1995 Svc Water Sys Operational Performance Insp (Swsopi) Self- Assessment Rept. ML17332A5841995-02-28028 February 1995 DC Cook Nuclear Plant IPE for External Events Revised Fire Pra. ML17332A5851995-02-28028 February 1995 DC Cook Nuclear Plant Units 1 & 2 Addendum to Seismic PRA Notebook. ML17332A7121994-12-0505 December 1994 Evaluation of Cook Ipe/Hra Matls. ML17332A3731994-10-24024 October 1994 Assessment of Indications in DC Cook Unit 2 Head Penetration 75. ML17332A4141994-08-25025 August 1994 Rev 0 to HI-941183, Spent Nuclear Fuel Pool Thermal- Hydraulic Analysis Rept for DC Cook Nuclear Plant. ML17331B4301994-06-13013 June 1994 Rev 0 to DC Cook Nuclear Plant E-Plan Classification Vs NUMARC/NESP-007 Deviation Basis Document. ML17331B4391994-06-0909 June 1994 1 Cycle 13 IPC Assessment. ML17331B1331993-12-31031 December 1993 DC Cook Units 1 & 2 Main Steam Safety Valve Lift Setpoint Tolerance Relaxation. ML17331B1411993-12-0909 December 1993 Suppl Info for DC Cook Unit 1 Ipc. ML17331B1691993-12-0707 December 1993 Reactor Protection & Control Process Instrumentation Replacement Project at Donald C Cook Nuclear Plant Units 1 & 2,Reactor Protection Sys Functional Diversity Assessment. ML17331B1961993-09-30030 September 1993 Control Rod Misalignment Analysis. ML17331A0631993-02-28028 February 1993 DC Cook Nuclear Plant Hydrogen Control Evaluation Summary Rept. ML17329A7141992-12-16016 December 1992 DC Cook Nuclear Plant Units 1 & 2 Reliability & Mtbf Analysis Reactor Protection & Control Sys Replacement Project. ML17329A7161992-12-16016 December 1992 DC Cook Nuclear Plant Units 1 & 2 Summary Rept for Response Time Evaluations Reactor Protection & Control Sys Replacement Project. ML17329A7071992-12-16016 December 1992 Engineering Analysis of Temperature & Humidity Effects on Foxboro Spec 200 Instrumentation Reactor Protection & Control Sys Replacement Project. ML17329A7091992-12-16016 December 1992 Preliminary Emi/Rfi Evaluation Aepsc Reactor Protection & Control Sys Replacement Project. ML17329A7131992-12-16016 December 1992 DC Cook Nuclear Plant Units 1 & 2 Failure Modes & Effect Analysis (FMEA) Protection Set 1 Foxboro Spec 200 Reactor Protection & Control Sys Replacement Project. ML17329A7111992-12-16016 December 1992 Engineering Analysis of Grounding Issues Reactor Protection Process Control Group Replacement Project DC Cook Nuclear Plants Units 1 & 2. ML17329A7101992-12-16016 December 1992 DC Cook Nuclear Plant Units 1 & 2 Summary Rept for Sys Power Quality Evaluation Reactor Protection & Control Sys Replacement Project. ML17329A7171992-12-15015 December 1992 Reactor Protection & Control Process Instrumentation Replacement Project at DC Cook Nuclear Plant Units 1 & 2 TS Compliance Assessment. ML17329A7121992-12-15015 December 1992 Regulatory Requirements & Industry Standards Associated W/Reactor Protection Portion of Reactor Protection & Control Process Instrumentation Replacement Project. ML17329A7201992-12-14014 December 1992 Reactor Protection & Control Process Instrumentation Replacement Project at DC Cook Nuclear Plant Units 1 & 2 Reactor Protection Sys Functional Diversity Assessment. ML17329A7181992-12-14014 December 1992 Reactor Protection & Control Process Instrumentation Replacement Project at DC Cook Nuclear Plants Units 1 & 2 Qualification Compliance. ML17329A7151992-12-10010 December 1992 Reactor Protection & Control Process Instrumentation Replacement Project at DC Cook Nuclear Plant Units 1 & 2 Functional Requirement Summary. ML17329A7191992-12-10010 December 1992 Reactor Protection & Control Process Instrumentation Replacement Project at DC Cook Nuclear Plant Units 1 & 2 Test Program Summary. 1999-09-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
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IS%58 HOLTEC Hdltec Center, 555 Lincoln Drive West. IVlarfton NJ 08 "53 Telephone (609) 797- 0900 Fax (609) 797 - 0909 I N T E R N A T I 0 N A L REVIEW AND CER7IHCATlON LOG DOCUMENT MAME:- Responses to RAI on Holtec Report HI-951389 forthe O.C. Cook Spent Fuel Pool HOLTEC DOCUMENT I.D. NUMBER: 971763 70851 HOLTEC PROJECT NUMBER:
CUSTOMER/CUENT: American Electri Power RFVlSION BLOCK X
REVISION AUTHOR & REVIEWER & APPROVED& DIST.
NUMBER 'ATE DATE DATE ORIGINAL tNbREyyg &P~ Sv z %Ger
'Y-wV "8"l p
~
it-(97 REVISION I REVISION 2 REVISION 3 REVISION 4 REVISION 5 REVISION 6 This document conforms to the requirements of the design specification and the applicable sections of the governing codes.
Note: Signatures and printed names required in the review block.
A revhion of this document will be ordered by the Project Manager and carried out ifany of its contents is materially affected during evolution of this project. The determination as to the need for revision will be made by the Project Manager with input from others, as deemed necessary by him.
Must be Project Manager or his designee.
x Distribution: C: Client M: Designated Manufacturer F: Florida Office Report categoly on the cover page indicates the contractual status of this document as A = to be submitted to client for approval I = for client's information N = not submitted externally THE REVISION CONTROL OF THIS DOCUMENT IS BY A
SUMMARY
OF REVISIONS LOS" PLACED BEFORE THE TEXT OF THE REPORT.
97G825GG95 97G8<9 POR AOQCK GSGGGM5 P POa
SUMMARY
OF REVISIONS REVISION 0: This revision contain the following sections and pages.
Title Page Review and CertiGcation Log Summary ofRevision Log Table of Contents Figures Appendix A Appendix 8* 14
~ Note: This appendix contains Holtec proprietary information, is therefore not distributed. This appendix is available for review at Holtec's corporate ofices.
Holtec Report HX-971763 Holtec Project 70851'
K,Nil I;0.
'l Xntro duction TABMOF CONTENTS
~ae 2.0 AEP Request - Description of Analysis Methods 3.0 NRC Request I 4.0 NRC Request 2 5.0 NRC Request 3 6.0 References Tables Figures Appendix A Proprietary Appendix B~
'ote: This appendix contains Holtec proprietary information, is therefore rot distributed. This appendix is available for review at Holtec's corporate offices.
Holtec Report HI-9? 1763 Holtec Project 70851
1.0 INTRODVCTION This report documents analyses performed. in support of American Electric Power (AEP) personnel responding to a USNRC'Request.for Additional Information (RA@ on the thennal-hydrauEcanaIysis of theCook Nuclear Plant'spent fuel "pool. (SFP) P}; This report addresses the use ofthe Unit 2 uprated reactor power in decay heat calculations.
Sections 2.0 through 5.0 each contain the response to an individual NRC or ABP question.
Where appropriate, references to and comparisons with the result of the previous analyses [1} are performed. Not all of these four sections contain analyses.
Holtec Report HI-971763 page 1 Holtec Project 70851
2.0 AEP REQUEST - DESCRIPTION OF ANALYSISMETHODS 2.1'ecay Heat Analysis Method All;decay heat calculations. are performed using implementations.of the-OIUGB52 [2J computer code developed at Oak Ridge National Laboratory. This program has a long history of use in the commercial nuclear power industry for both isotope production and thermal power calculations.
The OMGEN2 code is a rigorous isotope generation and depletion code which accurately predicts the products and by-products of Qssion and the resulting heat generation rates.
The decay heat generation rate in the pool consists of two components: the decay heat generated by previously discharged fuel assemblies and the decay heat generated by &eshly (recently) discharged assemblies. The decay heat contribution of previously discharged fuel assemblies changes very little over short periods of time, and is therefore held constant in the analyses.
Because of the nature of exponential decay, this simplification is conservative. The Holtec QA Validated LONGOR [3] computer proem, which incorporates the ORIGEN2 code, is used to calculate this decay heat component.
The decay heat contribution of the freshly discharged 'fuel assemblies changes substantially over even very short periods of tune. 'I'his decay heat contribution is therefore evaluated as time>>
varying. The Holtec QA Validated BULKTEM [4] computer pro~~ which incorporates the ORIGEN2 code, is used to calculate this decay heat component.
2.2 Bulk SFP Temperature Analysis Method Due to the time-varying decay heat component, the total decay heat is also time-varying. The bulk SFP temperature is therefore'calculated as a function of time. The following energy balance is solved to obtain the temperature at each instant in time:
C = Q ( )-0 ('1)-0 (T) where:
C is the SFP thermal capacity, Btu/'F T is the bulk SFP temperature, 'F z is the time after reactor shutdown, hr Qc+w) is the decay heat generation, Btu/hr QHx(T) is the SFPCS heat rejection, Btu/hr
~Ap(T) is the evaporative'heat,loss, Btu/hr The evaporative heat loss term includes both evaporative and sensible heat transfer from the surface of the SFP. The implementation of this term has been benchmarked against actual in-plant test data [5]. The solution of this first-order ordinary differential equation is performed using the BULKTEM pro~ [43 Holtec Report HI-971763 page 2 Holtec Project 70851
Tune-to-Boil Analysis Method I:o11owing a loss of forced cooling, the continuing decay heat load in the SFP will cause the bulk SFP temperature to use. The equatioa energy balance. which defines this transient phenomena is sitmhr to the.ODE.presented in Section 22, but does not include the.QRz term and does include a time varying SFP thermal capacity, to account for the evaporative water losses. The time available for corrective action before bulk SFP boiling occurs is determined using the Holtec QA Validated TBOIL computer program [6].
The decay heat generation and evaporative heat loss terms in this formulation are identical to those defined in Section 2.2, except for the following two differences:
o The decay heat is calculated using the correlations of USNRC Branch Technical Position ASB 9-2 I'7] instead of ORIGEH2.
~ No incremental credit is yven for evaporative heat loss at SFP bulk temperatures greater than 170'F.
2.4 Local Temperatures Analysis Method
\
The decay heat generated by the fuel assemblies stored in the SFP induced a buoyancy driven flow Geld upward through the fuel rack ceHs. Cooler water is supplied to the bottom of the racks cells through the rack-to-wa)l gaps and rack-to-floor plenum.
A computational method for modeling this phenomena is given by Sin~~ et al. I'8). The method presented in the reference has been incorporated into the Holtec QA Validated computer pro~
THERPOOL [9), this is used to perform this analysis.
Holtec Report HI-971763 page 3 Holtec Project 70851
3.0 NRC REQUEST 1 "With regard to the spent fuel pool (SFP) cooling analyses for the normal refueling scenarios, Case lA and 2'as presented in February 1, 1996 submitta1 are based on the spent &el assunblies dischar ed Gom Unit.1 during Cycle.25A Since Unit 2.
will be operating at a higher power level than Unit 1 (3588 MWt vs 3250 MVt),
the analyses for Case IA and 2 should be revised based on the spent fuel assemblies discharged trom the Unit 2 reactor during Cycle 20B. Also, Tables 3, 4 and 5, and Figures I, 3, 6 and 8 should be revised to include the results from the above revised analyses."
In addition to the difference in reactor thermal power between Unit 1 and Unit 2, there are differences in the maximum burnup, initial U~q enrichment and &el assembly uranium weight.
These, differences are summarized in the Table 1. All of the values in Table I are extracted from Reference 1.
As requested, the cases designated as IA and 2 are re-evaluated using the Unit 2 values for the four parameters presented in Table I. All input values are taken from Reference I, and all inputs except those presented in Table 1 are identical to those used in the reference work. Unlike the oriynal .calculations, however, the thermal transient evaluations performed in ths report utilize version 3.0 of the BULKTEM program tl I]. This newer version of the BULKTEM code contains modification to the evaporative loss correlations [12], which are slightly more accurate than the original correlations, The effects of this modification on the results of the analysis are minimal.
The results of the maximum SFP bulk temperature analyses are presented in Table 2, where they are also compared with the previously reported values (I]. Temperature profiles for each case are presented in Figures 1 and 2. Net decay heat load and evaporative heat loss pro6les for each case are presented in Figures 3 and 4. As expected, the maximum bulk SFP temperatures are marginally higher than previously reported.
The results of the bulk temperature analysis are propagated through to the time-to-boil and local temperature analyses, the results of which are presented and compared with the corresponding previously reported values [I] in Tables 3 and 4, respectively. As expected, the minimum time-to-boil is slimly less than previously reported, and the maximum evaporation rate and local temperatures are slightly higher than previously reported.
Holtec Report HX-971763 page 4 Holtec Project 70851
4.0 NRC REQUEST 2 "In.the analyses for the scenario of back-to-back Rll core discharge with two SFF trains (Case,3),"'pent fuel assembEes Rom Unit 2;are assutned,to be 'ooling discharged m three:groups'each with. a diQerent burnup:vaIue= Provide curves to show the decay heat rates as a function of time generated in the SFP Rom each of these youps."
Figure S presents the decay heat profiles for each of the three groups of the Rll core discharge batch for Case 3. As expected, the decay heat generation rate and the reactor exposure are directly proportional.
Holtec Report HI-971763 page 5 Holtec Project 70851
~
5.0 NRC REQUEST 3 "In the response (A 4) to the staQ's RAX presented in Pebtuary 1,'1996 submittal, decay heat generation rates for spent fuel assemblies Rom each previous discharge cycle are provided Decay heat generation rates Rom. these previously discharged spent fuel assemblies are also provided in the Attachments 2 and 3 to the letter dated August 1, 1996. However, decay heat generation rates presented in August 1, 1996 submittal deviate significantly Rom that presented in Pebruaty 1, 1996 submittal. Provide clarification and justification for this discrepancy."
The February 1, 1996 submittal is in response to an NRC RAI on Holtec Report HI-941183. The August 1, 1996 submittal is in response to an NRC RAI on Holtec Report HI-951389. A discussion of these diQ'erences between these decay heat generation rates has previously been provided in response I.C of the August 1, 1996 submittal [10].
Holtec Report HI-971763 page 6 Holtec Project 70851
6.0 REFEIU2lCES
[1] "Updated Thermal-Hydraulic Analysis of Spent Nuclear Fuel Pool,.- Donald C. Cook Nuclear Plant" Holtec Report HI-951389, Revision'.-
[2] A.G. CrofE "ORNL Isotope Generation and Depletion, A User's Manual for the ORIGEN2 Computer Code," ORNL/TM-7175, RSIC/CCC-371, Oak Ridge National Laboratory, July 1980.
[3] "QA Documentation for LONGOR v1.0," Holtec Report HI-951390, Revision 0.
[4] "QA Documentation for BULKTEMv2.0," Holtec Report HI-951391, Revision 0.
[5] Wang, Yu, "Heat Loss to the Ambient trom Spent Fuel Pool: Correlation of Theory with Experiments," Holtec Report HI-90477.
[6] "QA Documentation for TBOIL v1.6," Holtec Report HI-92832, Revision 2.
[7] USNRC Branch Technical Position ASB 9-2, "Residual Decay Energy for Linet Water Reactors for Long Term Coolino Revision 2, July 1981.
[8] Sin+~, K.P. et. al., 'Method for Computing the Maximum Water Temperature in a Fuel Pool Containing Spent Nuclear Fuel", Heat Transfer Engineering, Volume 7, Number 1-2, pp. 72-82, 1986.
[9] "QA Validation for THERPOOL v 1.2", Holtec Report HI-87120, Revision 2.
[10] Letter Gom E.E. Fitzpatrick (AEP) to USNRC, Docket Numbers 50-315 and 50-316, Document ID AEP:i&C.C:1202B, Attachment 1, Response 1.C.
fl 1] "QA Documentation for BULKTEMv3.0", Holtec Report Hl-951391, Revision 1.
[12] "An Improved Correlation for Evaporation from Spent Fuel Pools," Holtec Report HI-971664, Revision 0.
Holtec Report HI-971763 page 7 Holtec Project 70851
T P
TABLE 1 DIFFERENCES BEWVEEN UNIT I AND UNIT 2 NORMALDISCHARGES Parameter Unit I Value Qmt 2 Valee Reactor Thermal Power (MVt) 3,250 3,588 Maximum Average Burnup (MWdMTU) 52,200 68,400 Initial U~ Enrichment (%) 3.50 4.00 Assembly Uranium Weight (kg) 461 410 Holtec Report H1-971763 Holtec Project 70851
TABLE 2 RESULTS OF MAXIMUMBULKSPP TEMPERATURE ANALYSES Parameter Current Results (Unit 2) Previous Results (Unit 1)
Case IA Magnum SFP Temperature 156.56'F 154 37'F Coincident Time After Shutdown 138.0 hrs 138.0 hrs Coincident Net Heat Load to HXs 28.50x10 Btu/hr 27.19xl0 Btu/hr Coincident Evaporative Heat Loss 2.79x10 Btu/hr 2.35x10 Btu/hr Case 2 Maximum SFP Temperature 129.84'F 128.68oF Coincident Time After Shutdown 130.0 hrs 131.0 hrs Coincident Net Heat Load to HXs 30.75x10 Btu/hr 29.32x10 Btu/hr Coincident Evaporative Heat Loss 0.99xlO Btu/hr 0.57xl0 Btu/hr Holtec Report HI-971763 Holtec Project 70851
TABLK3 RESULTS OF BOILINGTMFS ANALYSES Parameter Current Results (Unit 2) Previous Results (Unit I)
Case lA Time to Start of Boiling 8.53 hrs 9AS hrs Maximum Evaporation Rate 66.83 gpm 63.35 gpm Case 2 Time to Start of Boiling 12.11 hrs 13.37 hrs Maximum Evaporation Rate 67.30 gpm 63.64 gpm Holtec Report HI-971763 Hol tee Project 70851
TABLE 4 RESULTS OF MAXIMUMLOCALTEMPERATURES ANALYSIS (Case.IA Only)
Parameter Current Results (Unit 2) Previous Results (Unit 1)
No Blocka~e Maximum Local Water Temperature 166 O' 163.6'P Maximum Fuel Clad Temperature 216.3'P 214.5'P 50% Blocha e Maximum Local Water Temperature 226. lop 223 5'F Maximum Fuel Clad Temperature 256.8'P 254 3oP Holtec Report HI-971763 Holtec Project 70851
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FlGURE 1: Spent Fuel Pool Bulk Wateg Temperature Profiles Case 1A, Normal Discharge, 1 Cooling Train .
160 155 150 0
" 1<5 E
~ 140 63 135-130 0 50 100 150 200 250 300 350 400 450 500 Time After Reactor Shutdown (hrs)
Hoitec Report Hl-971763 Holtec ProJect 70851
F fGURE 2: Spent Fuel Pool Bulk Water Temperature Profiles Case 2, Normal Discharge, 2 Cooling Trains 130 C
128 126 LL 124 Q 122 L
~~ 120 Ql 118 116 114 50 100 150 . 200 250 300 350 400 450 500 Time After Reactor Shutdown (hrs)
Holtec Report Hi-971763 Holteo pro/cot 70851
FIGURE 3: Spent Fuel Pool Decay Heat Load and Loss Profiles Case 1A, Normal Discharge, 1 Cooling Train 35.0E46 30.0E+6 Net Decay Heat Load 25.0E46 .-
M 4I Vl 0
C 20.0E+6 x'aCl C
cf
'0 tl$
O '15.0E+6 C$
x C 10.0E46 Q
n 5.0E+6 Evaporative Heat Loss 000.0E+0 50 100 150 200 250 300 350 400 450 500 Time After Reactor Shutdown (hrs)
Holtec Report Hl-9?1763 Holtec Project 70851
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FIGURE 4: Spent Fuel Pool Decay Heat Load and Loss Profiles Case 2, Normal Discharge, 2 Cooling Trains 35.0E46 30.0E+B Net Decay Heat Load 3
25.0E+6 ~ ~
g 20.0E+6 '
o 15.0E+B 5 10.0E4B A
z 5.0E+B-Evapora(ive Heat Loss 000.0E40 50 100 150 200 250 300 350 400 500 Time After Reactor Shutdown (hrs)
Hoitec Report Ht-971763 Hottec ProJect,70851
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FIGURE 6: Decay Heat Generation Rate for Each Discharge Batch ln the Full Core Back-to-Back Discharge Case 3 15.0E+6 Three Exposure Cycles 14.0E+6 Two Exposure Cycles 13.0E+6 Pg 12.0Et6 PL c 11.0E+6 One Exposure Cycle 10.0E+6 6
9.0E+6 n
8.0E+6 .
7.0E<6 6.0E+6 50 100 150 200 250 300 350 400 450 500 Tlrne After Second Reactor Shutdown (hrs)
Holtec Report Hl-971763 Holtec Project 70851
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ATTACHMENT 2 TO AEP:NRC:1202D RESPONSE TO QUESTION 4 REQUEST FOR ADDITlONAL INFORMATION REGARDING REFUELING OPERATIONS DECAY TIME to AEP:NRC:1202D Page 1 NRC uestion 4.0 "Is full-core offload a current practice during normal refueling?"
Res onse to uestion 4.0 Current practice is to perform full core offloads.