|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
[Table view] |
Text
ACCELERATED DISTRIBUTION DEMOYSTRATIQN SYSTEM 1
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8812210144 DOC.DATE: 88/12/14 NOTARIZED: NO DOCKET N FACIL:STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529 AUTH. NAME AUTHOR AFFILIATION SHRIVER,T.D. Arizona Nuclear Power Project, (formerly Arizona Public Serv HAYNES,J.G. Arizona Nuclear Power Project (formerly Arizona Public Serv RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 88-014-00:on 881116,reactor generator level.
trip due to low steam, W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:Standardized plant. 05000529 /
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD .1 1 CHAN,T 1 1 'DAVIS,M 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2
.ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 ARM/DCTS/DAB .1 1 DEDRO 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 1 1 NRR/DEST/MEB 9H 1 1 9H7'RR/DEST/MTB 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D -1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/QAB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR/DREP/RAB 10 1 1 NRR/DREP/RPB 10 2 2 NRR/DRISJS 9A 1 1 NUDOCS-ABSTRACT 1 1 BEG Pl-IZ~ 0 1 1 RES/DSIR/EIB 1 1 RES/DSR/PRAB 1 1 RGN5 FILE Ol 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 FORD BLDG HOY,A 1 ~ 1 H ST LOBBY WARD 1 ~ 1 . LPDR "1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 S
. NOTES:
NOTE TO ALL "RIDS" RECZPIENIS:
PZZASE HELP US TO REDUCE. WASTE! COHZAC1'IHE DOCUMENI'MENTAL DESK, RXM P1-37 (EXT. 20079) KO ELZKBQXZ YOUR NME ZMH DZSTfKBUTIGN LISTS'OR DOCUMEKZS YOU DGNiT NEEDf TOTAL NUMBER OF COPIES REQUIRED: LTTR 46 ENCL 45
41 ii J
NRC Form 255 UA. NVCLEAR REOULATOAY COMMISSION (543P Q APPROVEO OMS NO. 21504101 LICENSEE EVENT REPORT HLER) EXPIRES: SISIIES FACILI'TY NAME (I) DOCKET NVMSER (2) PA E Pa 1 o TITLE ICI Verde Uni t 2 0 5 0 0 0 52 9>or-0 8 Reactor Tri Oue to Low Steam Generator Level EVENT DATE (5) LER NUMSER LS) REPORT DATE (7I OTHER FACILITIES INVOLVED (5)
MONTH OAY YEAR SEOUENTIAL ...+c OAY FACILITY NAMES DOCKET NUMSERISI YEAR NUMEEII NA NUMOER MON'TH YEAR N/A 0 5 0 0 0 1116 88 8 8 014 00 1 21 4 8 8 N/A 0 5 0 0 0 THIS REPORT IS SUSMITTEO PURSUANT TO THE REOUIAEMENTS OF 10 CFR $ : IChrch onr ot mote Ol the lollowinII l1'll OPERATINO MODE IS) 20A02(bl 20A05(cl 50.724)(2) (IrI 72.71St)
~OWER 20AOS( ~ I III I II SOM(cl (I) 50.72(el)2)(rl 72.71)c)
LEYEL 0 1 0 20.c05(el(1)(E) 50.25(e) (2) 50.724) l2) (rEI OTHEA ISprcIIF In Abtarct below end in Trr t, HI(C Itonn 20A05(e Illl(IEI 50.72(e l(2) (Il 50.7241(2) (r)III(AI SSSAI 20AOS (r l(1 l(Ir) 50.724)(2) (Iil lb.7 2 Ie) (2) (r)E II 5 I 20A05(e) II)(r) 50.7 24) (2) (III) 50.72(e) (2) lcl LICENSEE CONTACT FOR THIS LER l12)
NAME TELEPHONE NUMSER AREA CODE Timoth O. Shriver, Compliance Manager 60,23 9 3 2 521
'g COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCAISED IN THIS REPORT (12)
CAUSE SYSTEM COMPONENT MANUFAC.
TVAER EPOATASLE TO NPRDS 4H~+ CAlln E tlE COMPONENT MANUFAC TVRER EPORTASLE l TO NPADS SP A B I S V B 3 5 0 N RK@% ~4M SUPPLEMENTAL REPORT EXPECTED IICI MONTH DAY YEAR EXPECTED SUSMISSION DATE (15)
YES IIIyrt, Complete EXPECTED SUSMISSIOlY OATSI X NO AssTRAcT ILlmlt to leod tprcrt. I.r., rpptonlmetrty Illtrrn clncl>tprcr typnw/ttrn linrtl (15)
At approximately 0237 HST on November 16, 1988 Palo Verde Unit. 2 was in Mode 1 (POWER OPERATION) at approximately 10 percent power when a reactor trip occurred. Unit 2 was being shut down to identify and repair a reactor coolant system (RCS) leak, which was,within Technical Specification limits for continued operation, when the trip occurred as a result of low steam generator
.water level. The reactor trip was. uncomplicated and stable conditions were achieved at approximately 0247 HST terminating the event. There were no Engineered Safety Feature actuations and none were necessary.
The cause of the low steam generator water level was inadequate feedwater flow due to main feedwater pump speed being too slow for the existing plant conditions. The cause of the RCS leak was excess packing leakage as a result of a broken packing gland follower bolt on an instrument isolation valve.
As corrective action to prevent recurrence, procedural changes have been implemented, an evaluation of the feedwater pump control system is being performed, and programs for implementation of plant modifications will be evaluated and'revised where appropriate.
There have been no previous similar events. ~l 7~
SS12210144 SS1214 PDR ADGCK 05000529 8 PDC NIIC ratm SCE
4l '
Y
HRC Form 844A V.S. HVCLEAR REOVLATORY COMMISSION 19$ >l LICENSEE EVENT REPORT {LER) TEXT CONTINUATION APPROVEO OMS HO SISOWIO4 EXPIRES: 8/81/88 FACILITY NAME (11 DOCKET HVMSER Ql LER HVMSER IS) PACE ISI V EAR ~)OP. SEOVENTIAL REVISION NUM SR NVMSSR Palo Verde Unit TEXT ///more Sooce 14 2
reeoleK Foe ~ ///rmo/H/IC Fo/III JNA'4/117l o 5 o o o 52 98 801 4 00,02 OF 0 8 I. DESCRIPTION OF WHAT OCCURRED:
A. Initial Conditions:
On November 16, 1988, Palo Verde .Unit 2 was in Mode 1 (POWER OPERATION) performing a plant shutdown to investigate and repair a Reactor Coolant System (RCS)(AB) leak. Immediately prior to the reactor (RCT)(AC) trip discussed below,'eactor power was approximately 10 percent.
B. Reportable Event Description (Including Dates and Approximate Times of Major Occurrences):
Event Classification: Automatic. actuation of the Reactor Protecti.on System (RPS)(JC).
On November 16, 1988 at approximately 0237 MST Palo Verde Unit 2 was in Mode 1 (POWER OPERATION) at approximately 10 percent power when a reactor trip occurred due to low steam generator (SG)(AB) water level. The low steam generator water level resulted from main feedwater pump (P)(SJ) speed being inadequate to supply feedwater to the steam generators during a power reduction. There were no engineered safety features (ESF)(JE) actuations and none were necessary. The event was properly diagnosed as an Uncomplicated Reactor Trip. At approximately 0247 MST both steam generator levels had been raised to above their trip setpoints and stable conditions were achieved. The event lasted approximately 10 minutes.
Prior to the reactor trip, Palo Verde Unit 2 was being shut down to investigate and repair the cause of 'an unidentified leak. Initial indications of a leak became a'pparent on November 7, 1988 when day-shift operations personnel (utility, licensed and non-licensed) noted an unexplained increase in the reactor cavity sump (WK) level over the previous few days. Initial estimates of the leakage into the sump were approximately 0.5 gallon per hour (0.008 gallon per 'h
.minute).
It should be noted that Technical Specification 3.4.5.2 allows 1.0 gallon per minute (gpm) unidentified Reactor Coolant System (RCS) leakage. Therefore, assuming that the leakage into the reactor cavity sump was unidentified reactor coolant system leakage, continued plant operation was allowed.
Investigation was initiated to identify the cause of the leakage.
On November 8, 1988, troubleshooting was performed on the reactor cavity sump level indicator (LI)(WK) and it was determined that the level indicator was operating properly. Furthermore, no significant trends or changes were noted in containment (NH)
NRC /ORM 144A 19 SSI
0 NRC for>> 844A U.S. NUCLEAR REGULATORY COMMISSION I844I LICENSEE EVENT REPORT {LER) TEXT CONTINUATION APPROVEO OMS NO. SI50&104 EXPIRES: 8/31/48 fACILII'YNAME III OOCKET NUMSER ICI LER NUMSER IS) ~ AGE IS)
JCGVCNZ/AL ACV/CION NVMCCA ~+ NVMCCA Palo Verde Unit 2 o 5 o o o 5 2 9 8 8 0 1 4 0 0 0 3 QF 0 8 TEXT //l /Atuf cfecu /I /P//cwed, u>> //tu//M/H/IC fPNA JSSA'r/ I IT) atmosphere samples for iodine, noble gas, or particulate
.radioactivity. Therefore, preparations were made to enter the containment to visually search for the cause of the leakage.
The initial containment entry to investigate the cause of the leakage was made on November 9, 1988. Initial attempts were unsuccessful in identifying the source of the leakage so the investigation continued. On November 15, 1988, a steam leak was discovered in the vicinity of the number 1 RCS hot leg. The exact source of the leakage was indeterminate due to the existing radiological conditions and presence of water vapor. Therefore, management prudently decided to shut down Unit 2 to facilitate further inspections and repairs.
At approximately 2000 .HST on November 15, 1988, a power reduction from 100 percent power was commenced. At approximately 15 percent power, the Feedwater Control System (FM)(JB) automatically redirected feedwater flow from the steam generator's economizer region to the downcomer region (i.e., both steam generator economizer regulating valves (FCV)(SJ) shut, both downcomer regulating valves (FCV)(SJ) opened); Concurrent with the redirection of feedwater flow, the operating main feedwater pump speed reduced to approximately 3759 revolutions per minute (RPM),
and the Feedwater Control System control methodology changed such that steam generator level controlled the amount of feedwater flow (vice a combination of measured feedwater and steam flow as well as the steam generator level). As a result of the main feedwater pump speed decreasing, inadequate discharge head was developed to overcome steam generator pressure at the low power conditions.
Steam generator levels decreased until a reactor trip occurred at approximately 0237 HST on November 16, 1988. The reactor trip resulted from a steam generator number,2 low level trip signal.
The event was properly diagnosed as an uncomplicated reactor trip.
Following the trip, the RB" Train Essential Auxiliary Feedwater Pump (BA)(P) and the Non-essential Auxiliary Feedwater Pump were manually started to feed both steam generators't approximately 0247 HST both steam generator levels had been raised to above their trip setpoints and, the event was terminated:
On November 16, 1988, the RCS leak was determined to be valve packing leakage from one of the Plant Protection System (JS)
Channel D Steam Generator differential pressure transmitter (PDT) root isolation valves ( ISV). The valve was appropriately repaired on November 19, 1988.
NAC PI/AM SCCA (4 44<
4 NRC Form 344A U.S. NUCLEAR REOVLATORY COMMISSION 19S/I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMS NO. 3150WIOI EXPIRES'. S/31ISS FACILITY NAME III OOCKET NUMSER (11 LER NUMSER ISI ~ AOE I31 YEAR 5EOUENTIAL AEVISION NUM45II NUM44II Palo Verde Unit Il IeeoeNE 2 o s o o o 5 2 9 8 801 4 00 04 oF 0 8 TEXT IIP more 4Oece Foe edaRNrINI WIC Fonrr SILAS I I Ill During the inspection being conducted to identify the source of the RCS leakage, it was discovered that the water from the leaking valve was flowing through small cracks in a concrete wall for the incore instrumentation (IG) chase. An engineering evaluation of this condition was initiated.
C. Status of structures, systems, or components that were inoperable at the start of the event that contributed to the event:
Not applicable - no components, systems, or structures were inoperable at the start that contributed to the event.
D'. Cause of each component or system failure, if known:
The failed bolt was manufactured from carbon steel and was exposed to boric-acid from the reactor coolant system. The boric acid degraded the bolt until tensile forces resulted in failure.
E. Failure known:
mode, mechanism, and effect of each failed component, if The RCS leak resulted from a broken packing gland follower bolt.
The broken bolt allowed the packing gland follower to cant which reduced the compression on the packing and resulted in excess packing leakage.
F. For failures of components with multiple functions, list of systems or secondary functions, that were also affected:
Not applicable - there were no component failures with multiple functions.
G. For failure that rendered a train of a safety system inoperable, estimated time elapsed from the discovery of the failure until the train was returned to service:
Not applicable - no safety systems were rendered inoperable. The failed bolting resulted in packing leakage significantly below Technical Specification 3.4.5.2 limits.
Hethod of discovery of. each componen'- or system failure or procedural error:
The broken bolting was, discovered during ANPP's investigation into the reason for the reactor cavity sump level increase (see Section I.B). There were no system failures. Procedural inadequacies were discovered as a result of ANPP's Post Trip Review process.
NNC 4 OIIM 5444 19 SSI
0 '
NRC Porro 3OSA (843 I U 8 NUCLEAR REOVLATORY COMMISSION LICENSEE EVENT REPORT {LER) TEXT CONTINUATION APPROVEO OMS NO 3ISOWIOO EXPIRES: 8/31/88 PACILITY NAME III OOCIIET NVMSER Il) LER NUMSER IS) PACE I3)
- i>Pi SSQVSNTIAL 5 Lo AtvloloN O 'N NVM tA NVMOtA Palo Verde Unit TEXT llfmore oooco II reOI/inN/, ooo 2
akNliorW H/IC Porrrr 38EA8/ I IT) o s o o o 529 88 0 1 4 0 0 05or 0 8 I. Cause of Event:
There were concurrent contributory causes which resulted in the reactor trip. The first cause is that the automatic Feedwater Control System response was not adequate in maintaining a sufficient feedwater pump speed following the period that feedwater flow to the steam generators shifted from the economizer region to the downcomer region. In part, this was due to main feedwater pump speed adjustments which were made by operations personnel during normal power operations (The adjustments procedurally were required to minimize economizer valve oscillations). The adjustments, coupled with a programmed main feedwater pump speed limitation when feedwater flow shifts to the downcomer region, resulted in pump speed being too slow for the existing plant conditions. It should be noted that a site modificati.on was installed in July 1988 which lowered the main feedwater pump minimum speed. The site modification was originally implemented to resolve Feedwater Control System (FWCS) performance problems in Unit l. It had been necessary to take manual control of the FWCS, vice leaving it in automatic, during low power operations in order to prevent overfeeding the steam generators. The site modification was also prepared and implemented in Units 2 and 3 and,the resulting FWCS was more versatile; however, the system potentially required operator action during certain plant conditions. Inadequate reviews were conducted for identifying and delineating the necessary operator actions. This was especially important for Unit 2 since the steam pressure is approximately 20 psi higher in Unit 2 than Unit I during low power operations.
Another contributory cause is that procedural controls utilized at low power operations (i.e., below twenty percent power) did not contain explicit .guidance for 'ensuring that the proper adjustments were made to the automatic main feedwater pump speed control to compensate for the adjustments made at normal power operations. As a result of implementing the site modification to reduce minimum feedwater pump speed, procedure revisions were not initiated which would have provided additional'uidance for ensuring adequate feedwater supply.
Another concern, which may have had an impact on this event, involves operator performance. Control Room operating personnel (utility, licensed) on-shift during the power reduction did not take the appropriate compensatory measures which would have maintained main feedwater pump speed at an adequate level for feeding the steam generators. This would have required adding significant positive bias to the feed pump speed controller which was not addressed in the procedure. If additional information regarding this concern is identified which would significantly alter the perception of this event, a supplement to this report will be submitted.
voc ~ IIAM 5ooo IS $ 3I
NRC Fotw 344A'SA)
U.S. NUCLEAR REOULATOR Y COMMISSION LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPAOVEO OM8 NO. 3)SOLI Of EXPIRES: 8/3) /88 FACILITY NAME I'l OOCI)ET NUMSER )3)
LE/I NUMSEI) (4) ~ AOE )3)
@j Sf QVE NT/AL Pa) /IEV/SION v.,'VMSf/I Mv. NI/Mf4 A Palo Verde Unit 2 o so o o 52 9 88 0 1 4 0 0 06or- 0 8 TEXT //P /lMlP f//PCP /4 nPPV/)P/L V>> /RIRNPM//V/IC //Pnll 34SAY/ I)7)
There were no unusual characteristics of the work location which contributed to this event. Except as noted above, procedural controls have been determined to be adequate.
The concrete walls surrounding the incore instrumentation chase consist of mass concrete placed to form the chase, access shaft, ventilation shaft, and reactor cavity. The walls are variable thickness and are load bearing in that 'they transfer loads from the primary shield above to the containment basemat. The walls are under constant compression with relatively low stress levels.
There are no flexual or tensile stress loads. The cracks identified in the incore chase concrete wall are vertical cracks probably induced by mass volume changes which resulted from temperature changes. This type of crack formation is not unusual.
J. Safety System Response:
The following manual and automatic safety system responses occurred:
Plant Protection System automatic initiation of reactor trip.
Essential Auxiliary Feedwater Pump "B" was manually started by Control Room personnel.
K. Failed Component Information:
The broken packing gland follower bolt was supplied as part of the valve manufactured by Borg Warner. The model number of the valve is 77540. The failed bolt is manufactured from A540 Grade B23 carbon steel material.
II. ASSESSMENT OF THE SAFETY CONSEQUENCES AND IMPLICATIONS OF THIS EVENT:
There were no safety consequences or implications resulting from this event. There was no impact on public health and safety. The uncomplicated reactor trip occurred per design as a result of the low steam generator water level. Water'evel remained above the point which would have required an automatic Auxiliary Feedwater Actuation (JE)(BA). Adequate heat removal capabilities existed throughout the event. This event could not have occurred at higher power levels because the Feedwater Control System swapover from the economizer to the downcomer is controlled by Nuclear Instrumentation at 15 percent power.
There were no safety consequences or implications resulting from the bolting failure on the differential pressure transmitter isolation valve. Leakage through the valve's. packing as a result of the failed bolt remained below Technical Specification limits for continuous operation. There are two packing gland follower bolts on the affected valve. The other bolt remained functional throughout the event.
'allC ~ 0/IM 344@
)98)i
II NRC Fo/III 344A'8431 0 U.S. NUCLEAR REOULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPRPVEO OM8 NP. 3150&184 EXPIRES: 8/31/88 FACILITY NAME LII OOCIEET NUMEER 131 LER NUMEER (41 PACE 131 YEAR:~gN< SEPVENTIAL ':~I AEVISIQN r)Ip.'VMSER NVMSSA Palo Verde Unit
/I Ieewaf.
2 o s o o o 529 8 8 0 1 4 00 07 OF 0 8 TEXT ////INv4 44444 444 aAM/on4////IC fomI 355l'4/ 1171 There are no safety consequences or implications resulting from the cracks in the incore instrument chase concrete wall. The type of crack formation is not unusual. Since the cracks are vertical, no load transfer path is interrupted and no other design function is compromised. The structural design basis of the containment internal structure is unchanged by the cracks.
I I I. CORRECTIVE ACTIONS:
A. Immediate:
The failed bolt as well as the other remaining bolt on the instrument root valve have been replaced.
B. Action to Prevent Recurrence:
As action to prevent recurrence, additional instructions have been included in operating procedures to ensure that operations personnel take the appropriate measures for maintaining adequate main feedwater pump speed during low power operations.
An engineering evaluation of Unit 2's automatic feedwater control system operation will be performed. As an initial result of the Engineering Evaluation, an enhancement to the preventive maintenance task for the feedpump governor is being implemented.
A Human Performance Evaluation is being performed to address factors which contributed to the operations personnel performance concern. Additionally, this event will be reviewed by the appropriate operations department personnel from Units I, 2, and 3 during normally scheduled periodic training. If additional corrective action is identifie'd as a result of the Human Performance Evaluation which significantly alter impact the perception of this event, a supplement to this report will be issued.
As discussed in Section I. I, the appropriate procedure changes did not get implemented as a result of the site modification. As a corrective action, the current site modification administrative controls will be evaluated and improved where appropriate. The system engineer program and the system engineer/Plant Standards and Control interface will be evaluated to determine can be implemented to ensure that necessary procedure changes are if improvements incorporated following plant modifications. A representative sample of cur'rent site modifications will be reviewed to determine if additional procedure revisions are necessary.
VIIC I 0AM $ 44A IS 43>>
0
'f
NRC Perm 3SSAr (0431 U.S. NUCLEAR REOULATORY COMM/SS/ON LICENSEE EVENT REPORT (LER) TEXT CONTINUATIQN, APPRQYED DMS No 3150wl/N EXP/RES: d/31/SS FACILI'TY NAME 11> DOCKET NUMSER Ql LER NUM@ER N1 ~ AOE 131 ScaVENT/AL ~?~ +E Y+/Vrr
~ rvM E/I NUMSEA Pal o Verde Uni TEXT llfmore /eeoc /I rl/I/'red.
t 2 o s o o o 5 2 9 8 8 0 1 4 '00, 08 or- 0 8 oee edd/dorM/A/RC form 3//SA'e/1171 Concerning the bolt failures discussed in Section I.B, the problem with boric acid causing premature failures had been previously identified. An engineering evaluation had been performed and as corrective action, a new bolting material was specified (ASTH A564 TP 630). The bolting is being changed out on an "as-needed" basis.
Concerning the cracks in the incore instrument chase concrete wall, a procedure for sealing the cracks is being developed. The cracks will be sealed during Unit 2's next refueling outage. It should be noted that this is a long-term solution for corrosion protection.
A design or structural repair is not required.
IV. PREVIOUS SIHILAR EVENTS:
There have been no previous similar .events reported pursuant to IOCFR50.73. It should be noted that other reactor trips have been reported which resulted from feedwater flow problems; however, none involve the sequence of events or root cause described in this LER.
'I/IC ~ 0/IM 34oo 10 SSI
0 0 P Arizona Nuclear Power Project P.O. BOX 52034 ~ PNOENIX. ARIZONA85072-2034
,192-00437-JGH/TDS/DAJ December 14,, 1988 U. S. Nuclear Regulatory Commission NRC Document Control Desk Washington, D.C. 20555
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 2 Docket No. STN 50-529 (License No. NPF-51.)
Licensee Event Report 88-014-00 File: 88-020-404 Attached please find Licensee Event Report (LER) No. 88-014-00 prepared and submitted pursuant to 10CFR 50.73. I'n accordance with 10CFR 50.73(d)., we are herewith forwardi'ng a copy of the LER to the Regional Administrator of the Region V office.
If you have any questions, please contact T. D. Shriver, Compl-iance Hanager at (602) 393-2521.
Very tru y yours, I/g J'. G. Haynes Vice President Nuclear Production JGH/TDS/DAJ/kj Attachment CC: D. B. Karner (all w/a)
E. E. Van Brunt, Jr.
J. B. Hartin T. J. Polich H. J. Davis A. C. Gehr INPO Records Center
4! 4 l'