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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
[Table view] |
Text
' C CELE RATED DIERIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8803150141 DOC-DATE-'8/03/11 NOTARIZED: NO DOCKET FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME AUTHOR AFFILIATION SHRIVER,T.D. Arizona Nuclear Power Project (formerly Arizona Public Serv HAYNES,J.G. Arizona Nuclear Power Project (formerly Arizona Public Serv, RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
ler 88-008-00:on 880212,reactor coolant sys leakage monitor inoperable due to personnel error.
W/8 ltr.
DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR i ENCL Letc.SIZE:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, . D NOTES:Standardized plant. 05000528 8 RECIPIENT COPIES COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL h PD5 LA 1 1 PD5 PD 1 1 LICITRA,E 1 1 DAVIS,M 1 1 INTERNAL: ACRS MICHELSON AEOD/DOA 1
1 1
1 1'ECIPIENT ACRS MOELLER AEOD/DSP/NAS 2
1 2
1 AEOD/DSP/ROAB 2 2 AEOD/ DS P/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 -
1
, NRR/DEST/ADS7E4 1 0 NRR/DEST/CEB8H7 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB7A 1 1 NRR/DEST/MEB9H3 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB8D1 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB10D 1 1 NRR/DLPQ/QAB10A 1 1 NRR/DOEA/EAB11E 1 1 NRR/DREP/RABlOA 1 1 NRR/DREP/RPB10A 2 2 N DRY/SIB9A1 1 1 NRR/PMAS/ILRB12 1 1 EG 02 1 1 RES TELFORD,J 1 1 RES/DE/EIB 1 1 RES/DRPS DIR 1 1 RGN5 FILE 01 1 1 EXTERNAL: EG&G GROH,M 5 5 FORD BLDG HOY,A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 NOTES: 1 S
j A
TOTAL NUMBER OF COPIES REQUIRED: LTTR 48 ENCL 47
II
~ NRC Fotm 355 U.S. NUCLEAR RECULATORY COMMISSION (5 53)
APPROVED 0MB NO, 3150410(,
LICENSEE EVENT REPORT ILERI EXPIRES: 5/31/55 FACILITY NAME 11) DOCKET NUMBER 12) PA E Palo Verde Unit 1 p s p p p 5 2 8 i oFD TITLE I ~ I Reactor Coolant System Leakage Monitor Inoperable Due to Personnel Error EVENT DATE 15l LER NUMBER ISI REPORT DATE (7) O'THER FACILITIES INVOLVED ( ~ I MONTH DAY YEAR YEAR "$(c SEQVEtertIL R E VISIOrt SS) NUMSER MONTH OAY YEAR FACILITYNAMES DOCKE'1 NUMBER(SI R UM 5 E R Palo Verde Unit 2 o s o o o529 0 2 1 2 8 8 8 8 0 0 8 0 0 03 11 8 8 Palo Verde Unit 3 p 5 p p p 5 3 0 THIS REPORT IS SUBMITTED PURSUANT T 0 THE REOUIREMENTS OF 10 CF R ('I: ICnrce one ot morr of tnr foiiowinf) (11)
OPERATINO ill(ii)
MODE ( ~ I 20A02(b) 20.e05(cl 60.73(el(2) lirl 73.71PFI POWER 20.C05 (~ Ill)(i) 50.35(cl(1) 50.734)(2)lvl 13.7((cl LEYEL 0 0 0 20.405( ~ ) 50.35(cl(2) 50.73(e I I 2) lviiI O'THER (Specify in Abttfrct below entf in Test, ffRC Form 20.405(vill))till 50.7 3(e I (2) Ill 50.73(el(2)(rill l)AI 36SAI 20A05 Ie) III (iv) 50.73le)(2)(E) 60.73(el(2)(rill IIBI Special Report
- Cop W~.;P...4NSFb:":. 20.e05 ( ~ ) II I (v) 50.7 3(e l(2) I I 5) 50.73(el(2) (el LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE Timothy D. Shriver, Compliance Manager 60 23 93 -2 52 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC.
TURER
'YSTEM COMPONENT MANUFAC TURER EPORTABLE TO NPRDS iIN>Y4iiF~~
EBL 55 SUPPLEMENTAL REPORT EXPECTED ((1) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)
YES Iif yrr, compirte EXPECTED $ (iBMISSION DATE) X tto ABSTRACT ILimit to tc00 coecn, I.r., rppfoeimrtrfy hftren tinfle corer typewritten finn) (15)
On February 12, 1988, ANPP was notified by the manufacturer of the PVNGS Units', 2, and 3 containment building radiation monitors (IJ)(MON) that pareiculate filter change-out frequencies in excess of 48 hours could adversely affect the performance of the monitors. ANPP was changing the particulate filters on a weekly basis; therefore, the monitors were declared inoperable in Units 2 and 3 on February 12, 1988. At the time of the notification, RU-1 was not required to be operable in Unit 1. The channels have potentially been periodically inoperable in Unies 1 monitors'articulate and 3 since June 1987 and in Unit 2 since May 1987 when ANPP started changing the filter media on a weekly basis. The monitors are required for RCS leakage deteceion in accordance with Technical Specifications 3.3.3.1 and 3.4.5.1.
The root cause of this event is a cognitive personnel 'error in that ehe original equipment manufacturer (OEM) did not recognize the effect that exeended filter change-out frequencies had on monitor operation.
As immediate corrective action, the filter change-out periodicity was revised to once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in Units 2 and 3. ANPP is conducting an extensive review and test of the radiation monitor software utilized at PVNGS as described herein.
A previous similar occurrence was reporeed in Unit 1 LER 86-046-00.
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This report also contains information for a special report.
NRC eorm 355 SS03150141 380311 PDR ADOCK 05000528 8 DCD
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LICENSEE EVENT REPORT {LERI TEXT CONTINUATION t U 8, NUCLEAR REOULATORV COMMISSiON APPROVFO OM8 NQ 3188 PIOt EXPIRES: 8/3'I/88 FACILITY NAME (I I OOCKET NUMSER Ill LER NUMSER ISI PAOE ISI YEAR . ~F1. SSOI/SNrt*L REVISION NUM SR NUMSS4 Palo Verde Unit 1 p p p p p 5 2 8 8 8 0 0 8 0 0 0 2 oF 0 6 TEXT llfmotP tPtct/t NRt/itetL tttP ate%'Ons/H/IC FOnn JRSA't/ IITI On, February 12, 1988 ANPP was advised by Kaman Instrumentation Corporation that the containment building radiation monitors'IJ)(MON) particulate channel may not be able to perform its intended function. The affected channel provides indication of potential reactor coolant pressure boundary (AB) leakage. These monitors are utilized in all three (3) units. At the time of the notification, Unit 1 was in Mode 6 (REFUELING), Unit 2 was in Mode 1 (POWER OPERATION) at approximately 98 percent power, and Unit 3 was in Mode 1 at approximately 100 percent power. As immediate corrective action, the Unit Shift Supervisors (utility, licensed) were notified and the channels were declared inoperable at approximately 1505 and 1450 monitors'articulate MST in Units 2 and 3 respectively. RU-1 was not required to be operable in Unit 1 pursuant to Technical Specifications at the time of notification. The appropriate ACTION requirements for Limiting Conditions for Operation (LCO) 3.4.5.1 and 3.3.3.1 were entered and required action taken.
The containment building atmosphere monitors (RU-1) are non-redundant monitors supplied by Kaman Instrumentation Corporation. The function of each monitor is to measure four containment (CTMT) atmosphere parameters that provide indication of reactor coolant pressure boundary (RCPB) leakage. These parameters are: particulate, iodine, and gaseous radioactivity, and dew point temperature. The particulate and gas channels provide two of the three means of detecting increased leakage from the RCPB in accordance with Regulatory Guide 1.45. The third method utilized is the containment sump level and flow monitoring-system (IJ). The dew point and iodine channels provide an additional supportive means of verifying potential leakage.
RU-1 is required to be OPERABLE in accordance with PVNGS Technical Specifications Section 3/4.3.3 and 3/4.4.5 as follows:
a ~ The RCS leakage detection systems shall be operable in modes 1, 2, 3, and 4: (a) containment air particulate monitoring system (RU-1), (b) containment sump level and flow monitoring system, and (c) containment gaseous monitoring system (RU-1). When the required gaseous or particulate radioactivity monitoring system (RU-1) is inoperable, plant operation may continue for 30 days provided grab samples of containment atmosphere are obtained and analyzed once every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The RCS leakage"" is limited to (a) one gpm unidentified leakage and (b) ten gpm identified leakage in modes 1, 2, 3 and 4. The operator determines whether the RCS leakages are within these limits by monitoring the containment atmosphere gaseous and particulate radioactivity at least once every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and by using the other leakage detection methods.
The particulate channel alarm/trip setpoint shall be less than or equal to 2.'3E-6 uCi/cc with a measurement range of 1.0E-9 to 1.0E-4 uCi/cc.
The gaseous channel alarm/trip setpoint shall be less than or equal to 6 'E-2 uCi/cc with a measurement range of 1.0E-6 to 1.0E-1 uCi/cc.
44C t04M 3994 19 83t
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NRC 19 +3 I form 3SSA
~ ~ V.S. NUCLEAR REGULATORY COMM/SS/ON LICENSEE EVENT REPORT ILERI TEXT CONTINUATION APPROYEO OMS NO 3/50M/04 EXPIRES: d/31/dd FACILITY NAME 111 DOCKET NUMRER 131 LER NVMSER ldl PACE 131 YEAR SSQVSNTIAL f>IO A t V IS IO Ic
~ IUMSTR I/VM TA Palo Verde Unit'.1 0 5 0 0 0 5 2 8 8 8 0 0 8 00 03 OF 0 6 TEXT /// moro tpoco it n/II/'/OIL vto o4REMO/ R//TC for/II3/NA'tl llll RU-1 calculates the containment particulate activity by utilizing a rate of change algorithm. Containment atmosphere is constantly drawn through RU-1 and passes first through the particulate channel where the particulate is deposited on a paper filter (FLT). A beta scintillation detector (DET) measures gross activity of the deposit. As the activity on the paper increases, the count rate from the detector also increases. The measurement is transmitted to a microprocessor which is pre-programmed with the flowrate and detector efficiency. The algorithm in the microprocessor of RU-1 calculates the slope of the increase in counts per unit time and uses this slope to calculate the containment particulate activity which is utilized for display and alarm functions.
RU-1 was supplied to PVNGS in late 1982. At that time, the particulate monitoring channel was provided with an adjustable automatic particulate filter stepping device. The default stepping time was set at 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The stepping interval was variable with no operational limits provided by the OEM. Operational problems were experienced with the automatic stepping device which adversely affected the reliability and availability of the particulate channel. In order to increase the reliability of the monitor, it was determined (in conjunction with the manufacturer) that the filter stepping device could be removed and the filter media manually changed on a periodic basis. It was determined that the removal of the automatic filter stepping device did not impact the calculation of particulate activity as there was no operational difference between adjusting the automatic stepping device to step at weekly intervals or manually changing the filter media weekly. The stepping device was removed and manual change-out of the filter media every week was implemented in May 1987 in Unit 2 and in June 1987 in Units 1 and 3.
It should be noted that RU-1 was not required to be October operable in Unit 3 prior to the initial entry into Mode 4 (HOT SHUTDOWN) on 1, 1987
'n early 1988 ANPP engineering personnel (contractor, non-licensed) were investigating the feasibility of changing the filter media monthly vice weekly. During this investigation, it was identified that extended filter change-out periods could potentially prevent the monitor from responding to radiation increases. The manufacturer was contacted on February 11, 1988 to review ANPP's findings. On February 12, 1988 the manufacturer contacted ANPP and identified that, based upon initial testing results, filter change-out periods in excess of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> could adversely affect the ability of the particulate channel to provide the required alarm function following increases in containment activity. As immediate corrective action, control room personnel (utility, licensed) were notified and the monitors'. particulate channels declared inoperable on February 12, 1988 at approximately 1505 MST, and 1450 MST in Units 2 and 3 respectively. The approximate elapsed time from the time of discovery until the monitoring systems were returned to service was 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> for Unit 2 and 44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br /> for Unit 3. In Units 2 and 3 the filter media was replaced and, after appropriate surveillance testing, the monitors were returned to service at approximately 1627 MST on February 12, 1988, and approximately 1100 MST on February 14, 1988, respectively. In Unit 1, the filter media will be replaced and the monitor returned to service prior to an operational mode for which RU-1 is required. The filter media change-out interval has been reduced to once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in all three units.
N/IC I 0/IM 3SOA IS dlr
'l NAC FRNR 844A U 4 NUCLEAR AEGULATOAYCOMMISSION 19M I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPAOVEO OM8 NO 4 ISO~)OS EXPIRES'IS)i88 FACILITY NAME 11) DOCKET NUMSEA I?I LEA NUMEEA 14) ~ AOE ISI YEAR Cij' SEQVENTIAL '.n REVISION NVM ER:NR NVMSER Palo Verde Unit 1 scen ie sp4MRNE vsp Assiicvel lYAC Foms 888A's) l)T) o s o o o 5 c) 8 8 0 0 8 00 04 OF 0 6 TE)CT IIT ssesp The root cause of this event has been determi'ned to be a cognitive personnel error on the part of the original equipment manufacturer (OEM). The OEM did not provide limitations or precautions for the filter stepping interval which would have forewarned ANPP that extended filter change-out intervals could have impacted the ability of the monitor to operate per design. Additionally, when the automatic stepping device was removed and weekly change-out of the filter media implemented, the OEM did not specify that extended filter change-out intervals would impact the ability of the monitor to operate per design.
As corrective action, the monitors were declared inoperable in Units 2 and 3 and a reduced filter change-out interval implemented. The filter change-out interval will be maintained at less than or equal to 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> in all three units until appropriate software modifications are made which would allow extended filter change-out intervals.
There were no unusual characteristics of the work location, which contributed to the event. ANPP procedures were evaluated and determined to be adequate.
There were no automatic or manually initiated safety responses and none were necessary. Other than discussed herein, there were no structures, systems, or components inoperable at the start of the event which contributed to the event. No safety limits were approached and no fission product barriers were challenged. During the period that the filter was being replaced on a weekly basis, the particulate channel of RU-1 was capable of detecting changes in containment activity levels, and thus providing indication of possible RCS leakage. The affect of the extended filter change-out intervals was to reduce particulate channel sensitivity such that it may not have alarmed per design requirements. However, control room personnel (utility, licensed) periodically monitor the activity levels detected by RU-1 and would have perceived unexplained increases in indicated activity as potential RCS leakage.
If the containment atmosphere particulate channel insufficiently indicated increases in containment radiation level as a result of increases in RCS leakage, then either (1) the gaseous channel would have responded to increasing radiation levels and alerted the operators of a potential problem and/or (2) the containment radwaste sump flow alarm would have been initiated in the main control room (NA) alerting control room personnel (utility, licensed) that the containment sump flow had increased by one gpm above normal flow for one hour. If indications occur that a potential leak exists, control room personnel are required to verify the rate and take the appropriate actions.
Based upon the above, there were no safety consequences resulting from this event.
NRC S I) RM )44A I9 8) I
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NRC FPN>> 355A U.5. NUCLEAR REGULATORY COMM>55>ON
>9431 LICENSEE EVENT REPORT {LERI TEXT CONTINUATION APPROVEO OMS NO 3(50 GIC4 EXPIRES: EI311(8 FACILITY NAME (11 OOCKET NUMEER (11 LER NUMEER (5) PAGE I31 YEAR g~i' 55GUENTIAL NUM 58 AEV >5>ON NUM55>l Pa 1 o Verde Uni t 1 0 5 0 0 0 5 P 8 8 0 0 800 05 0 6 TEXT IIP>>>>>>p solace >5 newed, I>5p CCkio'>el HPC F>>m> 3(((A3( (131 Palo Verde Unit 1 LER 86-046-00 reported a previous similar event wherein ANPP personnel (utility, non-licensed) discovered that software conversion constants supplied by Kaman for RU-1 were in error. This resulted in a reduced alarm capability due to the incorrect conversion of activity levels detected (i.e. counts) into displayed activity. This problem was also addressed in Deficiency Evaluation Report (DER) 86-25 and Notice of Violation (NOV) 528/86-28-01.
As a result of the previous software problem, ANPP implemented the following programmatic corrective actions to prevent recurrence:
- 1. A software control evaluation program for Kaman radiation monitors was initiated.
- 2. An independent validation and verification on Radiation Monitoring System (RMS) software in use was initiated.
- 3. A procedure was developed to require proper documentation and testing of software activities in the RMS system.
As previously discussed, the problem with the manner in which RU-1 calculates containment activity was discovered by ANPP personnel. This discovery was a result of the programs described above. ANPP believes that these programs are sufficient. However as an additional measure, ANPP had initiated a Reliability Improvement Project for the ANPP radiation monitoring system prior to this event. This is intended to evaluate methods for improving the operability and reliability of the radiation monitoring systems.
RU-1 INFORMATION:
Manufacturer: Kaman Instrumentation Corporation Model No: 952140-002 Tra s ortabilit The deficiency-.with the manner in which RU-1 calculates activity levels is also applicable to other radiation monitors utilized at PVNGS. The following monitors are affected:
RU-51, 52, 53 - Moveable Airborne Monitors (utilized as backups for RU-1)
RU-8 - Auxiliary Building (NF) Ventilation Exhaust Filter Inlet Monitor RU- 14 - Radwaste Building (NE) Ventilation Exhaust Filter Inlet Monitor RU-13A - Technical Support Center Monitor RU-13B - Emergency Operations Facility (NC) Monitor RU-143 - Plant'Vent (VL) Monitor N>IC IO>IM 555A IQ 53>
NRC Eorm 344A V.S. NUCLEAR REGULATORY COMM/SS/QN IS 831 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEQ OM8 NQ 3/EQW/84 EXP/RES; 8/31/88 FACILITY NAME 111 OOCKET NVMEER 131 LER NVMEER IS) PAGE 131 SEQUENTIAL YEAR NUM ER .'rr. REVISION NUMEER Pa1o Verde Unit 1 o s o o o 6 2 8 8 8 0 0 8 00 06 oF 0 6 tEXT l/lrnn/4 EPPce /I IPEIRRNE PSP 8//Pi'encl P/RC P4nn 38%4 3/ 1111 r Monitors RU-8, 13A, 13B, 14, 51, 52, and 53 are not required pursuant to Technical Specifications and are not considered reportable. When RU-51, 52, and 53 are utilized as replacements for RU-1, the corrective actions described herein will be implemented (i.e., reduced filter change-out intervals). The affected particulate channel in RU-143 is required by Technical Specification 3.3.3.1 only to collect particulate samples. Therefore RU-143's operability is not affected by the algorithm deficiency described herein. A corrective action plan for the other affected monitors is currently being developed. If additional information which could change the readers perception or understanding of the event is identified during the development of this corrective action plan, a supplement to this report will be provided.
Based upon the problem described herein, an evaluation for 10CFR Part 21 reportability is being conducted.
This report also contains information for a special report required pursuant to Units 1, 2, and 3 Technical Specifications 3.3.3.1 and 6.9.2 for RU-1 being periodically inoperable for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.
'IRC I ORM 3444 IS 83I
II
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Arizona Nuclear Power Project P.O. BOX 52034 ~ PHOENIX. ARIZONA 85072-2034 192-00352-JGH/TDS/DAJ March 11, 1988 NRC Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 1 Docket No. STN 50-528 (License No. NPF-41)
Licensee Event Report 88-008-00 File: 88-020-404 Attached please find Licensee Event Report (LER) No. 88-008-00 prepared and submitted pursuant to 10CFR 50.73. In accordance with 10CFR 50.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V office.
If you have any questions, please contact T. D. Shriver, Compliance Manager at (602) 393-2521.
Very truly yours, J. G. Haynes Vice President Nuclear Production JGH/TDS/DAJ/kj Attachment'c:
- 0. M. DeMichele (all w/a)
E. E. Van Brunt, Jr.
J. B. Martin T. J. Polich R. C. Sorenson E. A. Licitra A. C. Gehr INPO Records Center
/pS
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