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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
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AC CELERATED ÃSXRIBUTJON DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8801140122 DOC.DATE: 88/01/07 NOTARIZED: NO DOCKET FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH. NAME , AUTHOR AFFILIATION MALIK,J.E. Arizona Nuclear Power Project (formerly Arizona Public Serv HAYNES,J.G. Arizona Nuclear Power Project (formerly Arizona Public Serv RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 87-016-01:on 870609,both trains of ESF pump room air exhaust cleanup sys inoperable due to personnel error.
W/8 ltr.
DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc. D plant. 05000528'OTES:Standardized RECIPIENT ID CODE/NAME PD5 LA COPIES LTTR ENCL 1 1 ID RECIPIENT PD5 PD CODE/NAME COPIES LTTR ENCL 1 1 j
A LICITRA,E 1 1 DAVIS,M 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 AEOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DEST/ADS 1 0 NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 1 NRR/DEST/ICSB 1 1 NRR/DEST/MEB 1 1 NRR/DEST/MTB 1 1 NRR/DEST/PS B 1 1 NRR/DEST/RSB 1 1 NRR/DEST/SGB 1 1 NRR/DLPQ/HFB 1 1 NRR/DLPQ/QAB 1 1 NRR/DOEA/EAB 1 1 NRR/DREP/RAB 1 1 NRR/DREP/RPB 2 2 RID)(5 IB 1 1 NRR/PMAS/ILRB 1 1 02 1 1 RES DEPY GI 1 1 RES TELFORD,J 1 1 RES/DE/EIB 1 1 RGN5 FILE 01 1 1 EXTERNAL: EG&G GROH,M 5 5 FORD BLDG HOY,A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 NOTES 1 1 S
A TOTAL NUMBER OF COPIES REQUIRED: LTTR 48 ENCL 47
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Arizona Nuclear Power Project P.O. BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00325-JGH/JEM January 7, 1988 NRC Document Control Desk Nuclear Regulatory Commission Washington, D.C. 20555
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 1 Docket No. STN 50-528 Licensee Event Report 1-87-016-00 File: 87-020-404 Attached please find Supplement No. 1 to Licensee Event Report (LER No.
87-016-00 prepared and submitted pursuant to the requirements of 10CFR 50.73(d). .We are herewith forwarding a copy of this report to the Regional Administrator of the Region V Office.
If you have any questions; please contact J. E. Halik, (Acting) Compliance Lead at (602) 393-3531.
Very truly yours, Vice President Nuclear Production JGH/JEH/kj Attachment CC: 0. H. DeHichele (all w/a)
E. E. Van Brunt, Jr.
J. B. Hartin J. R. Ball R. C. Sorensen E. A. Licitra A. C. Gehr INPO Records Center
NRC Fertn 344 U.S. NUCLEAR REOULATORY COMMISSION (94)3)
APPROVED OMS NO. 31504104 LICENSEE EVENT REPORT {LER) EXPIRES) Si31iSS FACILITY NAME (II DOCKET NUMSER (2) PA 05000528ioF04 3
Palo Verde Unit 1
"'" "'oth Trains of ESF Pump Room Air Exhaust Cleanup System Inoperable Due to P ersonnel Error in Schedulin Maintenance Activities EVENT DATE(5) LEA NUMBER IS) REPORT DATE 17I OTHER FACILITIES INVOLVED (SI MONTH DAY YEAR YEAR SeQVENTIAL ICCe RCVtOKP MON'TH DAY YEAR FACILITYNAMES DOCKET NUMSERISI NVMOEtl NUMo e II N/A 0 S 0 0 0 0 6 0 9 8 7 8 7 01 6 0 1 0 1 0 7 8 8 N/A 0 5 0 0 0 OPERATINO THIS REPORT IS SUEMITTED PURSUANT TO THE REDUIREMENTs DF 10 cF R ()) (cnectr one or morr oi tne ioiiowinoi 1111 MODE ( ~ I 20.402(o) 1 20.405(c) 50.73(e I (2) I lv) 73.71(O)
POWE R 20.405( ~ I II I I II 50.35(cl(1) 50.73(el(2) H) 73.7)(c)
LEYEL 1 0 0 20.405(c)(1)(4) 50.35(cl(2) 50.73(e H2)(v4) OTHER ISpeciry in Apttrrct Oeiow met in Trot, HIIC form 20.405( ~ l(1)()ill 50.73(c) (2) ll) 50.73(e) (2)(vill)(A) 366AI 20.405(e) (1)(lv) 50.73(e) (2)(ll) 50,73(el(2) (vill l(S) 20.405(el()i(v) 50.73(el(2)(llll 50.73(e l(2) (el LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NVMSER AREA CODE J. E. Ma 1 i k, (Acting) Compl i ance Lead 60 23 93 -3 52 7 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRISED IN THIS REPORT (13)
MANUFAC. EPORTASLE MANUFAC.
CAUSE SYSTEM COMPONENT 'TO NPADS CAUSE SYSTEM COMPONENT TVRER TURER Ke.-:EYING>>
SUPPLEMEN'TAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUSMISSION DATE 05)
YES ill'eL compietr EXPECTED SV64tiSSiOH DATEI NO AssTRAcT i(.imit to (400 coerce. I ~ ., rpproepnetely iiiteen einorr.opere typewritrrn iinrti (15)
On June 11, 1987 it was discovered that between 1700 and 2330 MST on June 9, 1987, with Palo Verde Unit 1 in Mode 1 (POWER OPERATION) operating at 100 percent power, both trains of the Engineered Safety Feature (ESF) Pump Room Air Exhaust Cleanup System (PRAECS) were rendered inoperable at the same time.
While reviewing the work completed during a recent Fuel Building Essential Ventilation Train HBH online outage, the on-shift Shift Supervisor discovered that the combination of two separate maintenance activities may have rendered both trains of the ESF PRAECS inoperable. Based on further evaluation, if the operable Train HAH of the ESF PRAECS had been started following a Safety Injection Actuation Signal, the ability to exhaust the Technical Specification required flowrate from the Auxiliary Building below the 100'levation would have been impaired.
The root cause of the event was a cognitive personnel error by the Work Control Shift Supervisor who did not recognize that concurrent maintenance activities such as these would render the system inoperable.
As corrective action to prevent recurrence, a report of the event has been issued to the appropriate Operations, Maintenance and Work Control personnel, warning tags have been placed on the appropriate equipment to help prevent cross ties between ventilation systems, and a procedure will be developed to provide guidance for the preparation of Online Outages. z 880ii40i22 880107 PDR ADOCK 05000528 S DCD
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NRC form 388A U.S, NUCLEAR REOUEATORV COMMISSION
/9431 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED OM8 NO 3150 OICS EXPIRES; 8/31/88 DOCKET NUMSER 11l LER NUMSER 18) yEA II u<H<< SEOVENT/AV rl8 v rs Io 4 NVMSTR NVMSSA Palo Verde Unit 1 o o o o o 5 28 87 01 6 0 1 02oF0 4 TEXT /// /rroro I//oso is osl/wor/, I/so PM/oraoo/ HRC for//I 3//EA'sl Ill l On June 22, 1987, it was discovered that between 1700 and 2330 IIST on June 9, 1987, with Palo Verde Unit I in t1ode I (POWER OPERATION) operating at 100 percent power, both trains of the Engineered Safety Feature (ESF) Pump Room Air Exhaust Cleanup System (PRAECS)(VF) were rendered inoperable. With both trains of ESF PRAECS inoperable, the ACTION Statement for Technical Specification 3.7.8 was exceeded and Limiting Condition for Operation 3.0.3 should have been entered.
During ESF PRAECS operation following the receipt of a Safety Injection Actuation Signal (SIAS)(JE), the levels below the 100'levation of the Auxiliary Building (NF) are isolated from the upper levels by the automatic closure of essential isolation dampers (BDt<P). Air is then exhausted from the lower levels of the Auxiliary Building via a common connecting tunnel to the Fuel Building (ND) Air Filtration Units (AFU)(HFA-JOI and HFB-JOI) and then to the atmosphere. Technical Specification Surveillance Requirement 4.7.8.b.3 requires that an ESF PRAECS flowrate of 6000 cubic feet per minute (cfm) +/-
10 percent be maintained from the Auxiliary Building.
While reviewing the work completed during a recent Fuel Building Essentia I Ventilation System (FBEVCS) (VG) Train UBU online outage, the onshift Shift Supervisor (utility-licensed) identified that the combination of having the Train UB" essential AFU (HFB-JOI) door(s) open and the Train UB" essential isolation damper (HFB-f106)(BDI1P) open may have rendered both trains of ESF PRAECS inoperable. AFU HFB-JOI door(s) were open for door seal replacement and damper HFB-f106 (which is located inside of HFB-JOI) was intentionally opened to rework the damper's actuator (HCU). If the operable Train UAU of the ESF PRAECS had to be started following a SIAS, the ability to exhaust the Technical Specification required flowrate from the Auxiliary Building below the 100'levation would have been impaired. Subsequent testing conducted under an approved work order in Palo Verde Unit 3 on June 16, 1987 confirmed that approximately 3000 cfm could be exhausted from the Auxiliary Building under worst case system configuration vice the required 6000 cfm.
The original June Online Outage Schedule identified a work order to replace damper HFB-N06, at that time there was no work order for HFB-JOI door seal replacement listed. On June 9, 1987, the damper work order was amended to rework the damper actuator. During this time parts became available for the HFB-JOI door seal replacement and it was added to the outage schedule. The clearance was hung and the damper was de-energized (fails open) at approximately 0540 on June 9, 1987 and remained this way until 2212 on June 10, 1987. The work order for the seal replacement was initiated at 1700 on June 9, 1987 and the seals replaced by 2330 on June 9, 1987. Therefore, both trains of ESF PRAECS could have been inoperable for up to 6 I/2 hours. The root cause of the event was determined to be a cognitive personnel error by the Work Control Shift Supervisor (utility-licensed) who did not recognize that concurrent maintenance activities such as these would render the system inoperable. There were no specific procedural guidelines governing the development and approval of the Online Outage Schedule.
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NRC FMM 388A I9 83 I 0 U,S, NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT ILERI TEXT CONTINUATION APPROVED OMS NO 3I50 010l EXPIRES; SI31I88 FACILITY NAME ill OOCKET NUMSER Ill LER NUMSER (SI YE*A:N'SEOVENTIAL NVM SA ASVISION 4oE NVMSSA Palo Verde Unit 1 o s o o o 5 2 8 7 0 1 60 1 03oFO 4 TEXT IN ANNO u>>oo M newed, Moo NFIooAOI NIIC FoAA ~'Pl IIT)
At the time the event was discovered, the system configuration, as previously described, no longer existed since the AFU door(s) had been closed and the isolation damper had been shut. As corrective action to prevent recurrence, )
the following actions will/have been taken for Palo Verde Units 1, 2, and 3.
- 1) An Operations Department Experience Report and several Night Orders have been developed and issued to all Shift Supervisors to discuss this event with their crews. In addition, a copy of one of the Night Orders has been distributed to Work Control and Maintenance Control Center (HVAC) personnel for their information.
- 2) Warning tags have been placed on the doors of the Fuel Building essential AFUs, the Fuel Building Suction Dampers, and the large plugs which could cross tie the Fuel Building and Auxiliary Building as well as cross tie the Auxiliary Building above and below the 100'levation.
- 3) Operation's Procedure "FUEL BUILDING HVAC (HF)U has been revised to include specific guidelines for allowing certain Fuel Building doors/inspection panels to be opened.
- 4) Engineering is conducting a design study to determine the allowable size of penetration openings within the system in order to ensure ESF PRAECS operability. The study will also include a review of the basis for Technical Specification flow requirements since the Unit 3 testing indicated that system operability is more dependent upon the relative pressures in the area than upon the amount of flow being exhausted from the Auxiliary Building.
- 5) The Plant Hanager has issued a letter to onsite flanagers and Supervisors discussing the precautions being implemented to ensure ESF PRAECS operability until the Engineering design study is completed and requesting that all personnel are made aware of the'information.
- 6) The Day Shift Supervisor (utility-licensed) has discussed the event with the responsible Work Control Supervisor.
- 7) An administrative control procedure will be developed to provide guidance for the preparation-of Online Outages. This procedure will address the concern regarding maintenance activities being conducted on one train of safety related equipment potentially rendering the other train of equipment inoperable.
The ESF PRAECS is required to control the release of airborne" activity caused by leakage from below the 100'levation in the Auxiliary Building (including the ESF pumps in the ESF equipment rooms) fol lowing a Loss of Coolant Accident (LOCA). Control of airborne radioactivity includes filtering releases from below the 100'levation of the Auxiliary Building to the atmosphere as well as limiting releases to above the 100'levation.
4AC IGAM SSSA (9 83>
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NRC Po>>> 999A U.S. NUCLEAR REOOLATORS COMMISSION
>99ll UCENSEE EVENT REPORT tLER) TEXT CONTINUATION APPROVED OMS NO liM~IOo EXPlllES Sll(ISS DOCKET NVMSER tll LER NVMSER (9) PACE LEI SEOMENT>AL 9 4i AEV>O>04 Wr!> NUM E>>:.-'> >>OMOEA Palo Verde Unit 1 o s o o o 528 01 6 01 04 oFO 4 TExT (ifo>o>o aoo(o N o>>>i>o>E o>> >ddloooo HJtc form lssAEI ((Tl Testing was performed in Palo Verde Unit 3 to measure the actual air flow from the Auxiliary Building and differential pressure between the ESF pump room area and the atmosphere under worst case conditions. The results indicate that 3000 cfm was being evacuated to the essential AFU (consisting of both High Efficiency Particulate Air and Charcoal Filters [FLT]) obtaining a subatmospheric pressure of -0. 120" (water gauge). Based on a review of the test results and the Final Safety Analysis Report LOCA analysis, the releases to the atmosphere would still be within the allowable 10 CFR Part 100 limits and therefore would not adversely affect the health and safety of the public.
Engineering Evaluation 87-HA-020 has been dispositioned and it has been determined that dose contributions to PASS habitability from the area below the 100 foot level are negligible.
Tracer gas testing was performed with both the normal and essential ventilation in service simulating a SIAS without a loss of power in order to determine transport from below the 100 foot level to above the 100 foot level of the Auxiliary Building. On August 22, 1987 gas was injected into the "A" High Pressure Safety. Injection (HPSI)(Bg), "A" Low Pressure Safety Injection (LPSI)(BP), and "A" Containment Spray (CS)(BE) pump, rooms. Samples were then taken on the 100 foot and above levels. No tracer gas was detected above the 100 foot level. The test was repeated on August 23, 1987 with the injection gasses in the "B" HPSI, "B" LPSI, and "B" CS pump rooms. Again, no tracer gas was detected above the .100 foot elevation.
Based upon the sensitivity of the chromatographs used and the injection concentrations, isolation of better than 50,000 to one was achieved.
Therefore, dose contributions to PASS habitability from the area below the 100 foot level are negligible.
There were no structures, components, or systems that were inoperable at the start of the event, other than those previously described, that contributed to the event. There were no unusual characteristics of the work location which contributed to the event. There were no automatic or manually initiated safety system responses.
There have been no previous similar events reported regarding the inoperability of two independent trains of a.safety related system due to the inappropriate scheduling of maintenance activities.
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