ML17252B480

From kanterella
Jump to navigation Jump to search
LER 76-060-00 for Dresden Units 2 and 3 Re Discovery of Water Leakage in Diesel Generator Room Led Identification of Small Hole in HPCI Test Return Line at Condensate Storage Tank
ML17252B480
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 10/05/1976
From: Stephenson B
Commonwealth Edison Co
To: James Keppler
NRC/RGN-III
References
BBS LTR 76-707 LER 76-060-00
Download: ML17252B480 (3)


Text

R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 Edison

. , Dresden Nuelear rower Station BBS Ltr. #76-707 October 5, 1976 Mr. James G. Keppler, Regional Director Director~te of Regulatory Operations-Region III U. S. Nuclear .Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137

REFERENCE:

Docket No. 50-237 and Docket No. 50-249 Enclosed please find Reportable Occurrence report number 50-237/1976-60.

This report is being submitted to your office in accord.ance with the Dresden Nuclear P6wer St~tion Te~hnical Specifications, Section,6.6.~.

~~*Station Superintendent Dresden Nuclear Power Station BBS :jo Enclosure cc: Director of .Inspection & Enforcement Director of ~nagement Information & Program Control File/NRG R£GUU\l0Rl DOClH FILE COPl 1*02G6

~ -~--h.__._:-:"7"-;**-

!i' .

I (j .-

  • ucEi\JSEE EVEj\JT RE~DRT.

..>!.** CONTRC3L. BLOCK:! 1 1 1 1. 1 6

r ** . .. [Pl.EASE PRINT Al.l. REQUIRED*INFORMAT.l_ON) 1

  • * .<
  • LICENSEE LICENSE EVENT ....

. NAME LICENSE. NUMBER TYPE TYPE

@El II IJ- ID IR Is I :21 10101-10101010101-10101 IJJ I I 11 , , I I I 10131 31 32 ..

  • 7 8 9 14 15 25 26 30 REPORT REPORT CATEGORY . TYPE. SOURCE DOCKET NUMBER EVENT DATE REPORT DATE

@IT]coN* I. I *I I~! LhJ IO IS-;j:D*l-1 OI J.J 3 l.71* 1019 10 I 5171 I <I f Io I o 15 74' 75. .

f71 (o80L..

7 8 57 58. 59 60 61 * *6a 69.

  • EVENT. DESCRIPTION jo(2J *I J)UR1l\JC.-. NO~MAL OPERAT16N1 TH Dl~CO\f£R.y OF WME:& L£/U<Bt;,,C IN THF .* *.

7 8 9. . . ' . 80

~B 9I UNIT 1'3. 1>1E~EL G-ENER.PiTof2.... RooM J...£D To IH£ IDENTrFrcf!TtON. OF A . I 7 , . . .. . . 80

. [£EJ*lsVYIALL HOJ-£ *1rJ HPCt T~s-r R.£1URN L1NG" 21a-:l341.-Al2 1' AT-:n1E.* 11 G CO/\/:f 7 B 9 . . . . . .BO folsl89ll?ENSATE 7

$T6.1<8G-E"" TANK t SVSTt;m 01'.JERABJL./Ty we~ NrJT AFFECTD BE"CAUS£1

. 80 (ol6l * £ J.,JN£d IS* ND~fYIALl-'/ !SOL,A.TE'P Tl-1£ HPC/ SYSIFIYI E'X.C£PT WHEN USED 7 8 9 PRME (<;EC PtTT;tl;(.HfJ) SW£E!T.

  • 80.

SYSTEM CAUSE

  • COMPON°ENT COMPONENT CODE *. COOE . : COMPONENT CODE SUPPLIER* MANUFACTURER VIOLATON

(§0 ls I i=- I ~J . I P. l 1 I P I£ .Jx Ix l. . l!{J , I Z I q I'1,*19 I .ll{I 7 8 .9 10 11 . 12 17' . 43 44 . 47 *. 48

. .CAUSE DESCRIPTION 7

~

8 9.

I Al som£ 1NPEiER.fY1#NAT£**'f1rn.~

1 THE. . 'PIPE *INS1JJ...AT1o_iJ WA~ APPAR£NTLY

. **. 80 I

. *. lolsl I WeFTETJ, CA.USING GHJ...ORID£S To LEACH .OUT OF TH£ LAGG.tNC'>4, */UIS £Vt -

  • J

.] 8 9. . 80

    • r
      ,~;l~}.~!~~;.'D.~N~U~Yi~~;.\J,l\0.0.,E{~**~LRi_IJ.$£~7;>~,~E
      X&-:Pi?i:*R:*!J:~';f!~~Wff ~;~[9}!!.:~;:~:;.;r!!_~:2?;/;e~~~~~~,'1,~:;:'f:,~~t:!J;~.,~~~\!
    • .. * . FACILITY . . ' . . METHOD OF .
  • aJ

. STATUS .  % POWER OTHER STATUS DISCOVERY . DISCOVERY DESCRIPTION

[1E] . . llJ . I01715 I NA l.E..J 1......--"M

__fl'-'------,--------__,

7 8 9. .. 10 12 13 44 45 46 80 FORM OF ACTIVITY CONTENT RELEASED . OF RELEASE.

  • AMOUNT OF ACTIVITY LOCATION .OF RELEASE riEl , 9.LZJ . . .
7. 8 .

l~J 10 .

l..__.__ __./0--:4_ ____.I 11 44 I

45 80 PERSONNEL EXPOSURES

  • NUMBER . TYPE , .. DESCRIPTION

[filJ IDl-ol.O.I..*. ~* ~-*--'AJ.~f1-*_ _ _ _ _ _ _ _ _ ____;___ _ _ _ _ __.____ ___,

7 8 9 . 11 . 12 13 80 PERS'ONNEL INJURIES.

  • IIEJ 10 ID 10 I ____N_tt_______________________

NUMBER DESCRIPTION

~

7 8 9 11 12 80 OFFSITE. COl\ISEQUENCES

{iliJ. .AiA .

7 8 9 . 80

. LOSS OR DAMAGE TO FACILITY TYPE ciesc~lPTION .

7 BE8 9lE..I. 10

.NA 80 PUBLICITY (fill . N'.

7 8 9 80 ADDITIONAL FACTORS

~ 80 7 8 9

~ 80 7 89 ffiDNf = _£._x.,....-r,

  • .-'-.~--.2:--'-~---

9

(,' **

c*

,( ..

EVENT DESCRIPTION (Continued) for flow testing. The line was subsequently taken out of service. A leak in the Unit-2 HPCI test return line was discovered on 9-15-76. (50-237/1976-60)

CAUSE DESCRIPTION (Continued) resulted in failure of the pipe wall. The affec~ed area, which was less than

~" in diameter, was temporarily. repaired. To prevent future corrosion, this section of line will be replaced and fitted with a different type of insul-ation as soon as practicable.