Standby Liquid Control system subsystems were declared inoperable when control room personnel were notified of a through wall leak on the common discharge piping. Technical Specification (TS) 3.1.7, " Standby Liquid Control System," Condition B was entered. The pipe repair schedule projected that the work could not be completed within the allowed Completion Time of TS 3.1.7 and DNPS requested a Notice of Enforcement Discretion ( NOED) to allow Unit 3 to remain at power during the repair. The NRC granted the NOED on September 12, 2017, at 1746 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.64353e-4 months <br />. The system was restored to operable status by replacing the piping on September 12, 2017, at 2035 hours0.0236 days <br />0.565 hours <br />0.00336 weeks <br />7.743175e-4 months <br /> within the time allowed by the NOED. This event is reportable under 10 CFR 50.73(a)(2)(i)(B), as a condition prohibited by TS. The cause of the event was a manufacturing defect. Corrective actions include replacing the failed piping (completed) and performing extent of condition pipe inspections. |
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Category:Letter
MONTHYEARML24303A0712024-11-0404 November 2024 Letter to K. Meshigaud, Chairperson Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0692024-11-0101 November 2024 Letter to J.A. Crawford, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0302024-11-0101 November 2024 Letter to D.G. Lankford, Chief Request to Initiate Section 106 Consultation for SLR of DNP Station RS-24-104, Nuclear Radiological Emergency Plan Document Revision2024-11-0101 November 2024 Nuclear Radiological Emergency Plan Document Revision ML24303A0492024-11-0101 November 2024 Letter G. Kakkak, Chairwoman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0552024-11-0101 November 2024 Letter to J. Keys, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station IR 05000237/20254012024-11-0101 November 2024 Information Request for the Cyber Security Baseline Inspection, Notification to Perform Inspection 05000237/2025401 05000249/2025401 ML24303A1462024-11-0101 November 2024 Letter to W. Gravelle, Chairperson Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0992024-11-0101 November 2024 Lett to R. Carter, Principal Chief Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0242024-11-0101 November 2024 Letter to D. Kaskaske, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A1422024-11-0101 November 2024 Letter to V. Jefferson, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24291A0252024-11-0101 November 2024 Letter to R. Blanchard Tribal Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0272024-11-0101 November 2024 Letter to D. Rios, Chairperson Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0532024-11-0101 November 2024 Letter to J. Greendeer, President Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0432024-11-0101 November 2024 Letter to E. Elizondo, Sr. Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0512024-11-0101 November 2024 Letter to J. Barrett, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0472024-11-0101 November 2024 Letter to G. Cheatham, Chairwoman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0892024-11-0101 November 2024 Letter to M. J. Wesaw, Chair Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0152024-11-0101 November 2024 Letter to C. Harper, Chief Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A1442024-11-0101 November 2024 Letter to V. Kitcheyna, Chairwoman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A1342024-11-0101 November 2024 Letter to T. Carnes, Chairperson Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A1102024-11-0101 November 2024 Letter to R. Gasco, Chairperson Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0132024-11-0101 November 2024 Letter to B. Barnes, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0202024-11-0101 November 2024 Letter to C. Chavers, Chairwoman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0172024-11-0101 November 2024 Letter to B. Peters, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0642024-11-0101 November 2024 Letter to J. Rupnick, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A1352024-11-0101 November 2024 Letter to T. Rhodd, Chairperson Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A1172024-11-0101 November 2024 Letter to R. Yob, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24303A0602024-11-0101 November 2024 Letter to J. R. Shotton, Chairman Request to Initiate Section 106 Consultation for SLR of DNP Station ML24291A0202024-10-31031 October 2024 NRC Letter to J. Loichinger Achp Request for Comments Concerning the Environmental Review of DNPS Units 2 and 3 Subsequent License Renewal Application ML24291A0272024-10-31031 October 2024 NRC Letter to C. Mayer Illinois SHPO Request to Initiate Section 106 Consultation for Subsequent License Renewal of Units 2 and 3 IR 05000237/20240032024-10-29029 October 2024 Integrated Inspection Report 05000237/2024003 and 05000249/2024003 RS-24-102, Supplement to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b, and TSTF-5912024-10-21021 October 2024 Supplement to License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b, and TSTF-591 RS-24-103, Annual 10 CFR 50.46 Report of Emergency Core Cooling System Evaluation Model Changes and Errors2024-10-21021 October 2024 Annual 10 CFR 50.46 Report of Emergency Core Cooling System Evaluation Model Changes and Errors RS-24-080, Request to Replace Formerly Submitted Documents Available in the Agency Documents Access and Management System (ADAMS) with Documents Redacted in .2024-10-16016 October 2024 Request to Replace Formerly Submitted Documents Available in the Agency Documents Access and Management System (ADAMS) with Documents Redacted in . RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24225A2132024-09-26026 September 2024 Relief Request Regarding Examination Coverage for the Fifth Inservice Inspection Interval ML24253A0942024-09-23023 September 2024 License Renewal Regulatory Audit Regarding the Environmental Review of the License Renewal Application (EPID L-2024-Sle-0002) (Docket Numbers: 50-237 and 50-249) SVPLTR 24-0030, ISFSI Annual Effluent Release Report2024-09-20020 September 2024 ISFSI Annual Effluent Release Report ML24270A0332024-09-20020 September 2024 Independent Spent Fuel Storage Installation Annual Radioactive Effluent Release Report IR 05000237/20244022024-09-19019 September 2024 – Security Baseline Inspection Report 05000237/2024402 and 05000249/2024402 - (Public) ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24260A2152024-09-16016 September 2024 Confirmation of Initial License Examination ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24215A2912024-08-14014 August 2024 Request for Withholding Information from Public Disclosure Alternative Schedule to Complete Decommissioning Beyond 60-Years of Permanent Cessation of Operations IR 05000237/20240022024-08-14014 August 2024 Integrated Inspection Report 05000237/2024002 and 05000249/2024002 IR 05000237/20240102024-08-0909 August 2024 NRC Age-Related Degradation Inspection Report 05000237/2024010 and 05000249/2024010 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000237/LER-2023-001, HPCI Inoperable Due to Air Void Accumulation2024-01-19019 January 2024 HPCI Inoperable Due to Air Void Accumulation 05000237/LER-2022-001-01, Reactor Scram Due to Turbine Trip on High Reactor Water Level Caused by Feedwater Regulating Valve Failure2022-10-28028 October 2022 Reactor Scram Due to Turbine Trip on High Reactor Water Level Caused by Feedwater Regulating Valve Failure 05000237/LER-2022-002-01, Ultimate Heat Sink Declared Inoperable Due to River Grass Accumulation2022-10-28028 October 2022 Ultimate Heat Sink Declared Inoperable Due to River Grass Accumulation 05000237/LER-2022-002, Ultimate Heat Sink Declared Inoperable Due to River Grass Accumulation2022-09-27027 September 2022 Ultimate Heat Sink Declared Inoperable Due to River Grass Accumulation 05000237/LER-2022-001, Reactor Scram Due to Turbine Trip on High Reactor Water Level Caused by Feedwater Regulating Valve Failure2022-09-0909 September 2022 Reactor Scram Due to Turbine Trip on High Reactor Water Level Caused by Feedwater Regulating Valve Failure 05000249/LER-2021-001-01, Reactor Scram Due to Main Power Transformer Failure2022-06-14014 June 2022 Reactor Scram Due to Main Power Transformer Failure ML20135G7442020-05-14014 May 2020 Final ASP Analysis - Dresden 2 (LER 237-90-006) 05000249/LER-2017-0012017-12-27027 December 2017 Unit 3 Standby Liquid Control System Inoperable Due to a Manufacturing Defect Causing a Piping Leak, LER 17-001-01 for Dresden Nuclear Power Station, Unit 3 Regarding Unit 3 Standby Liquid Control System Inoperable Due to a Manufacturing Defect Causing a Piping Leak ML17252B5052017-11-0303 November 2017 LER 77-050/03L-0 for Dresden, Unit 2 Re Local Leak Rate Test of Drywell Personnel Air Lock During Refueling ML17252A3262017-10-21021 October 2017 LER 77-040/03L-0 for Dresden 3 Regarding the Circuit Breaker for Service Water Makeup Valve MO-3-4102 to the Isolation Condenser Found in Off Position ML17252B4922017-08-28028 August 2017 LER 78-028/01X-1 for Dresden, Units 2 and 3 Re NRC Request for Immediate Actions to Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suction 05000237/LER-2016-0032017-05-26026 May 2017 Control Room Emergency Ventilation System Charcoal Filter Bank Failure to meet the Methyl Iodide Penetration Acceptance Criteria, Dresden Nuclear Power Station, Units 2 and 3, Cancellation of Licensee Event Report 237/2016-003-00, Control Room Emergency Ventilation System Charcoal Filter Bank Failure to meet the Methyl Iodide Penetration Acceptance Criteria ML17153A0342017-05-26026 May 2017 Cancellation of Licensee Event Report 237/2016-003-00, Control Room Emergency Ventilation System Charcoal Filter Bank Failure to Meet the Methyl Iodide Penetration Acceptance Criteria 05000237/LER-2016-0042017-01-0909 January 2017 Reactor Building Differential Pressure Less than Technical Specification Requirement, LER 16-004-00 for Dresden Nuclear Power Station, Unit 2, Regarding Reactor Building Differential Pressure Less than Technical Specification Requirement 05000249/LER-2016-0012016-08-25025 August 2016 Alert Declared from Unit 3 HPCI Auxiliary Oil Pump Motor Fire, LER 16-001-00 for Dresden Nuclear Power Station Regarding Alert Declared from Unit 3 HPCI Auxiliary Oil Pump Motor Fire 05000237/LER-2016-0022016-07-15015 July 2016 Unit 2 HPCI Inlet Steam Drain Pot Piping Leak Resulting in HPCI Inoperability, LER 16-002-00 for Dresden Nuclear Power Station, Unit 2 Regarding HPCI Inlet Steam Drain Pot Piping Leak Resulting in HPCI Inoperability 05000237/LER-2016-0012016-04-0808 April 2016 Secondary Containment Differential Pressure Transient, LER 16-001-00 for Dresden Nuclear Power Station, Unit 2 and 3 Regarding Secondary Containment Differential Pressure Transient 05000249/LER-2015-0012016-01-22022 January 2016 Main Steam Line Flow Switches Found Outside Tech Spec Allowed Value, LER 15-001-01, Dresden, Unit 3 Main Steam Line Flow Switched Found Outside Tech Spec Allowed Value ML1015505692009-07-24024 July 2009 Letter LS-AA-1 25-1001, Elevated Tritium Values Identified in 2 Storm Drains Due to Through-Wall Leaks in Underground Piping for Dresden Units 2 and 3. ML0602404072004-05-0505 May 2004 Final Precursor Analysis - Dresden Unit 3 - Unit 3 Scram Due to Loss of Offsite Power and Subsequent Inoperability of the Standby Gas Treatment System for Units 2 and 3 ML0234501722002-12-0202 December 2002 LER 89-029-05, Dresden Unit 2, Elevated HPCI Discharge Piping Temperature Due to Reactor Feedwater System Back Leakage ML17252B5391981-06-10010 June 1981 LER 81-034/03L-0 for Dresden, Unit 2 Re J-3 CRD Was Tested for Overtravel. the Overtravel Alarm Came Up and Rod Position Indication Was Lost ML17252B5411981-06-0808 June 1981 LER 81-030/01T-0 for Dresden, Unit 2 Re Operator Noticed the HPCI Steam Line Was Cold and Filled with Water. the HPCI System Was Declared Inoperable ML17252B5401981-06-0505 June 1981 LER 81-024/03L-0 for Dresden, Unit 2 Re While Conducting Routine Review of Surveillance, It Was Found That the Monthly Surveillance Required by Tech. Spec. 4.4.c.1 for Standby Liquid Control Tank Sampling Was Three Days Overdue ML17252B5271981-06-0303 June 1981 LER 81-023/03L-0 for Dresden, Unit 2 Re While Running HPCI Pump Test, the Operator Observed Torus Wide Range Level Instrument Reading 0 Inches and Narrow Range Level Instrument Reading, About - 2 Inches and Oscillating ML17252B5281981-04-14014 April 1981 LER 81-015/03L-0 for Dresden, Unit 2 Re the Fire Marshall Discovered That the Heat Detectors Were Not Functionally Tested within the 6 Month Interval Required by Tech. Spec. 4.12.A.1 ML17252B5291981-03-23023 March 1981 LER 81-011-03L-0 for Dresden, Unit 2 Re Observed Inadequacies in the Implementation of Administrative or Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection Systems or Engineered Safe ML17252B5301981-02-20020 February 1981 LER 81-080/031-0 for Dresden, Unit 2 Re Abnormal Degradation of Systems Other than Those Specified in Item B.1.e Above Designed to Contain Radioactive Material Resulting from the Fission Process ML17252B5321981-02-17017 February 1981 LER 81-070/03L for Dresden, Unit 2 Re While Conducting Steam Line Area Temperature Switch Calibration Surveillance, Temperature Switch TS 2-261-180 Failed to Trip ML17252B5331981-02-0202 February 1981 LER 81-020/03L-0 for Dresden, Unit 2 Re During Refueling Outage LPCI Test Spray Valve Failed to Shut Electrically, One Set of Thermal Contacts Would Not Reset ML17252B5351981-01-23023 January 1981 LER 80-050/03L-0 for Dresden, Unit 2 Re the 1501-62D Pressure Switch Actuated at 44.2 Inches of Water Increasing, Tech. Spec. Limit Is Less than or Equal to 41.6 Inches of Water Increasing ML17252B5341981-01-23023 January 1981 LER 80-049/03L-0 for Dresden, Unit 2 Re at Completion of Secondary Containment Leak Rate Test the Reactor Building Ventilation Isolation Valve 2A-5742 Would Not Open ML17252B5371980-12-30030 December 1980 LER 80-046-00 for Dresden 2 Regarding a Failure to Receive CRD Volume During a Reactor Scram ML17252B5361980-12-29029 December 1980 LER 80-046/03L-0 for Dresden, Unit 2 Re Conditions Leading to on Operation in a Degraded Mode Permitted by a Limiting Condition for Operation or Plant Shutdown Required by a Limiting Condition for Operation ML17252B5381980-12-0303 December 1980 LER 80-043/03L-0 for Dresden, Unit 2 Re Surveillance Testing of the Condenser Low Vacuum Switches, Pressure Switch 2-503D Was Found to Have a Trip Point of 22.85 Inches Hg ML17252B5431980-11-12012 November 1980 LER 80-041/03L-0 for Dresden, Unit 2 Re Reactor Building Vent and Refueling Floor Rad Monitor Surveillance (DCP 2007-12) Was Performed ML17252B5421980-11-12012 November 1980 LER 80-042/03L-0 for Dresden, Units 2 and 3 Re That Technical Staff Personnel Revealed That the Ultrasonic Testing of the Scram Discharge Volume Was Not Performed During the 1500-2300 Shift ML17252B1841980-10-31031 October 1980 LER 80-40/01T-0 for Dresden Unit 3 Regarding Failure of the HPCI Inboard Steam Supply Valve to Open ML17252B5441980-10-29029 October 1980 LER 80-039/03X-1 for Dresden, Unit 2 Re HPCI Inboard Steam Supply Valve Opened and Had a Dual Light Indication ML17252B5451980-10-23023 October 1980 LER 79-017-01X2 for Dresden, Units 2 and 3 Re Inadequacies Observed in Implementation of Administrative Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection System or Engineered Safety ML17252B5461980-10-0808 October 1980 LER 80-016/01T-1 for Dresden, Unit 2 Re While Shutdown and Conducting 300 Psi Primary System Hydrostatic Leak Inspection, Water Discovered Dripping from LPCI Check Valve Up Stream Drain Line ML17252B5471980-10-0707 October 1980 LER 80-036/03L-0 for Dresden, Unit 2 Re Discovery That the Six Month Functional Test Required by Tech. Spec. 4.12.A.1 of the Cardox System Heat Detectors Was Not Performed within the Allowable Surveillance Interval ML17252B5481980-10-0101 October 1980 LER 80-033/03L-0 for Dresden, Unit 2 Re the Frequency of Water Addition to the Torus Increased. Leak Rate Tests Indicated a Leak in the 2B LPCI Heat Exchanger ML17252B1861980-08-22022 August 1980 LER 80-032/03L-0 for Dresden Unit 3 Regarding During Normal Operations While Performing APRM Rod Block and Scram Functional Tests, APRM 3 Failed to Initiate a Rod Block ML17252B5501980-08-19019 August 1980 LER 80-027/03L-0 for Dresden, Unit 2 Re Dropping Load in Preparation for I.E.B. 80-17 Scram Tests, Low Level of Diesel Generator Coolant Present in the Water Tank Was Noticed by Equipment Operator ML17252B5161980-08-14014 August 1980 LER 80-024/03L-0 for Dresden, Unit 2 Re Drywell Oxygen Concentration Indication Failed Downscale in Violation of Tech. Spec. 3.7.A.6.d ML17252B1881980-08-0404 August 1980 LER 80-030/03L-0 for Dresden Unit 3 Regarding While Reducing Power for Manual Scram Required by I.E. Bulletin 80-17, Routine Surveillance of MSIV Closure Times Showed That MSIVs 3-203-2B and 2D Closed in Less than 3 Seconds ML17252B1901980-06-13013 June 1980 LER 80-023/03L-0 for Dresden Unit 3 Regarding During Normal Operation with Reactor Level Instrument Surveillance in Progress, Level Switch LIS 3-263-58A Tripped at Less than Tech. Spec. Limit of 144 Inches ML17252B1911980-06-13013 June 1980 LER 80-024/03L-0 for Dresden Unit 3 Regarding During Normal Operation with Reactor Level Instrument Surveillance in Progress, Level Switch LIS 3-263-58AB Tripped at Less than Tech. Spec. Limit of 84 Inches ML17252B1921980-06-10010 June 1980 LER 80-025/03L-0 for Dresden Unit 3 Regarding During Normal Operation While Performing Main Steam Line High Flow Isolation Surveillance, Flow Switch DPIS 3-261-2A Was Out of Tech. Spec. Limits, Table 3.2.1 2024-01-19
[Table view] |
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3. LER NUMBER
17 - 01 001
PLANT AND SYSTEM IDENTIFICATION
Dresden Nuclear Power Station (DNPS), Unit 3, is a General Electric Company Boiling Water Reactor with a licensed maximum power level of 2957 megawatts thermal. The Energy Industry Identification System codes used in the text are identified as [XX].
A. Plant Conditions Prior to Event:
Unit: 03 Reactor Mode: 1 Event Date: 09/12/17 Event Time: 1131 CDT Mode Name: Power Operation Power Level: 100 percent
B. Description of Event:
On September 10, 2017, during Equipment Operator (EO) rounds, the EO found crystalized boron on Dresden, Unit 3 Standby Liquid Control System (SLC) [BR] discharge piping [PSF]. There was no active leak at the time of discovery and the source of the boron crystals was unknown. Work activities began to determine the source of the boron deposits.
On September 12, 2017, the Division 1 SLC pump [P] was started to pressurize the system to the normal In-Service Testing test pressure as directed by station procedures. With the system pressurized, a leak of approximately one drop per minute was identified on the common discharge line of the SLC pumps. The leak was characterized as a through wall leak from an American Society of Mechanical Engineers (ASME), Class 2 pressure boundary of the SLC system. This leak was treated as a structural integrity issue; therefore, the affected piping was isolated in accordance with station procedures. Isolating the failed piping resulted in both divisions of SLC being declared Inoperable. This action led to entering Technical Specification (TS) Limiting Condition for Operation (LCO) 3.1.7, "Standby Liquid Control (SLC) System," Condition B, "Two SLC subsystems inoperable," and Required Action B.1, "Restore one SLC subsystem to OPERABLE status," with a Completion Time of eight hours.
DNPS requested a Notice of Enforcement Discretion (NOED) to exceed the TS 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> Completion Time to complete the pipe repair and replace the pipe. The NRC verbally granted the NOED on September 12, 2017 at 1746 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.64353e-4 months <br />. At 2035 hours0.0236 days <br />0.565 hours <br />0.00336 weeks <br />7.743175e-4 months <br />, the failed piping was replaced in accordance with station work instructions, thereby restoring the Unit 3 SLC system to Operable status within the time allowed by the NOED.
The piping through-wall flaw did not meet ASME Code structural integrity requirements.
Therefore, Dresden determined that since there was boron buildup identified on September 10 and later confirmed leakage on September 12, the system was inoperable for longer than allowed by TS and is reportable under 10 CFR 50.73(a)(2)(i)(B) for a condition prohibited by TS.
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3. LER NUMBER
17 - 01 001 Subsequently, the pipe flaw was analyzed and an evaluation concluded that the leak flaw met the ASME Code,Section XI structural margin, considering Service Level D structural factor in the evaluation, as required by the NRC Inspection Manual. Even though the flaw was through- wall, which exceeded the ASME Code,Section XI allowable flaw depth of 75% of wall thickness, the safety function of the component was not compromised when the leak was identified. Based on meeting structural integrity criteria this condition is not reportable under 10 CFR 50.73(a)(2)(v)(A) and 10 CFR 50.73(a)(2)(v)(D) for an event or condition that could have prevented the fulfillment of a safety function.
C. Cause of Event:
The determined root cause is a manufacturing defect which evolved into a through wall leak.
Metallurgical evaluations show that the leak area coincided with a cluster of large, closely spaced inclusions from the manufacturing process. The through wall leakage occurred when the closely spaced inclusions connected due to service induced stresses to form a through wall leak path. There was no evidence that corrosion or stress corrosion cracking contributed to defect growth in the evaluated sample. Based on the qualitative chemistry evaluations of the inclusions, the defects were characterized as oxide inclusions with elevated levels of silicon, manganese and aluminum in comparison to the base metal composition.
D. Safety Analysis:
The SLC System is designed to provide the capability of bringing the reactor, at any time in a fuel cycle, from full power and minimum control rod inventory, which is at the peak of the xenon transient, to a subcritical condition with the reactor in the most reactive, xenon free state without taking credit for control rod movement. The SLC System is also used to maintain suppression pool pH at or above 7 following a Loss of Coolant Accident (LOCA) involving significant fission product releases. Maintaining suppression pool pH levels at or above 7 following an accident ensures that iodine will be retained in the suppression pool water.
The SLC System consists of a bordn solution storage tank, two positive displacement pumps, two explosive valves that are provided in parallel for redundancy, and associated piping and valves used to transfer borated water from the storage tank to the reactor pressure vessel.
The borated solution is discharged near the bottom of the core shroud, where it then mixes with the cooling water rising through the core.
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3. LER NUMBER
17 - 01 001 An engineering evaluation was performed on the pipe flaw. The evaluation determined that the safety function of the component was not compromised when the leak was identified. The pipe flaw would not have grown beyond the allowable flaw size during SLC System operation. The required flow rate for SLC System to inject into the Reactor Pressure Vessel is 40 gallons per minute minimum. The leakage through the flaw is relatively small (i.e., approximately 1 drop per minute) and would not jeopardize the SLC system from performing its safety function.
Therefore, the leaking component had adequate structural margin when the leak was identified and the resulting leakage would not have prevented the SLC system from performing its intended safety function.
Since the SLC subsystems were available to perform their safety functions, the overall safety significance of this event was minimal. Normal means of reactivity control were maintained during this event.
The engineering analysis demonstrates this event did not constitute a Safety System Functional Failure (SSFF) (Reference NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Section 2.2, "Mitigating Systems Cornerstone, Safety System Functional Failures, Clarifying Notes, Engineering Analyses"). As such, this event will not be reported in the NRC Performance Indicator (PI) for SSFF since an engineering analysis was performed which determined that the system could perform its safety function during this event.
E. Corrective Actions:
The failed piping was replaced in accordance with station procedures and work instructions on September 12, 2017. Additionally, corrective actions include performing extent of condition piping inspections with piping insulation removed.
F. Previous Occurrences:
A search of similar events from the past 15 years was performed. One event was identified:
On January 18, 2007, Dresden, Unit 2 identified a through wall linear crack at the SLC Tank temperature switch well. However, the degradation mechanism (i.e., transgranular stress corrosion cracking) is not the same as this event (i.e., latent forging defect).
G. Component Failure Data:
The piping with the leak was a 1-1/2 inch pipe tee, ASME A/SA-182-Grade stainless steel. The pipe was in service for over 50 years.