ML17223A887

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LER 90-003-00:900726,determined That Main Steam Line Radiation Monitor Returned to Svc Following Power Supply Replacement W/O Performing Required Tech Spec Surveillance. Caused by Personnel Error.Personnel counseled.W/900816 Ltr
ML17223A887
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 08/16/1990
From: Neely L, Sager D
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-90-300, LER-90-003-03, LER-90-3-3, NUDOCS 9008240144
Download: ML17223A887 (6)


Text

ACCELERATED DIRIBUTION DEMONST]+TION SYSTEM REGULATORY INFORMATION DXSTRI BUTION SYSTEM (RI DS )

ACCESSXON NBR:9008240144 DOC.DATE: 90/08/16 NOTARIZED: NO DOCKET FACIL:50-389 St. Lucie Plant, Unit 2, Florida Power 6 Light Co. 05000389 AUTH. NAME AUTHOR AFFXLIATION NEELY, L. W. Florida Power 6 Light Florida Power 6 Light Co.,

Co.'AGER,D.A.

RECIP.NAME RECIPXENT AFFILIATION

SUBJECT:

LER 90-003-00:900726,missed surveillance on radiation monitor returned to svc due to personnel error.

W/9 DISTRIBUTION CODE: IE22T COPIES RECEIVED'LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES RECIPIENT COPIES RECIPXENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 1 PD2-2 PD 1 1 NORRIS,J 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DS P/TPAB 1 1 AEOD/ROAB/DS P 2 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DLPQ/LHFB11 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB 7E 1 1 DSZf SPLB8D1 1 1 NRR/DST/SRXB 8E 1 1 02 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL EGGG BRYCE i J H 3 3 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSXC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOi>1 Pl-37 (EXT. 20079) TO ELliV!INATE YOUR MAIE FROiv! DISTRIBUTION LISTS FOR DOCUik!ENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 34 ENCL 34

P.O. Box14000, Juno Beach, FL 33408-0420 August 16, 1990 L-90-300 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:

Re: St. Lucie Unit 2 Docket No. 50-389 Reportable Event: 90-03 Date of Event: July 26, 1990 Missed Surveillance on Radiation Monitor Returned to Service Due to Personnel Error The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.

Very truly yours, D. A. ager Vice P esident St. ie Plant DAS/GRM Attachment cc: Stewart D. Ebneter, Regional Administrator, USNRC Region Senior Resident Inspector, USNRC, St. Lucie Plant II 0r,~82<r.) g 44 900 .2r

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/ ~ 4$) APPROVEO OMS NO. 3150.0104 LICENSEE EVENT REPORT (LER) EXPIRES 8/31/85 FACILITYNAME (1) DOCKET NUMBER (2 PAGE 3 St. Lucie Unit 2 0 5000 3891OF0 3 MISSED SURVEILLANCE ON RADIATIONMONITOR RETURNED TO SERVICE DUE TO PERSONNEL ERROR EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)

MONTH DAY YEAR YEAR S QU N IAL MONTH FACILITYNAMES DOCKET NUMBER(S)

NUMBER NUMB R DAY YEAR NIA 0 5000 0 7 2 9 0 9 0" 0 3 00081690 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR OPERATING Check one or more of the followin 11 MODE (9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)

POWER LEVEL 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)

(10) 1 0 0 20.405(a)(1 )(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a)(1 )(III) (Specifyin Abstract X 50.73(a)(2)(I) 50.73(a)(2)(vlli)(A) below.andin Text 20.405(a)(1)(lv) 50.73(a)(2)(ii) 50.73(a)(2)(vlii)(B) NRC Form 366A) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER (12)

NAME H N NUMB L. W. Neely, Shift Technical Advisor AREA CODE COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 4 0 7 465-3 550 CAUSE SYSTEM COMPONENT MANUFAC REPORTABLE CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE TO NPRDS TURER TO NPRDS SUPPLEMENTAL REPORT EXPECTED 14 EXPECTFD ONTH AY Y AR SUBMISSION YES (lfyes, complete EXPECTED SUBMISSION DATE) NO DATE (15)

ABSTRACT (Limit to 1400 spaces. i.e. approximately lifteen single-space typewritten lines)(16)

On July 26, with Unit 2 in Mode 1 at 100% power, it was determined that the "B" Main Steam Line Radiation Monitor was returned to service following a power supply replacement on July 14, 1990 without performing required Technical Specification Surveillances. Unit 2 Technical Specification 4.3.3.1 required that the Channel Calibration and the Channel Functional Test be performed.

The root cause of this event was personnel error such that non-licensed utilily maintenance personnel failed to follow a procedure.

Corrective actions: Chemistry Department personnel satisfactorily performed the required surveillances. The individuals involved were counseled. Instrumentation and Control Department will revise the Instrumentation and Control Test Control procedure such that a note is added to inform Chemistry or Health Physics, as necessary, before returning Technical Specification required radiation monitoring instrumentation back into service.

U.S. NUCLEAR REGULATORY COMMISSCN LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO 0MB NO. 3150-0104 EXPIRES 8/31/85 FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR N SEQUENTIAL g~.

NUMBER REVISION NUMBER St. Lucie Unit 2 0500038990 TEXT (ifmore spaceis required, use additional NRC Form 366A's)(17) 0 0 3 0 0' OF 0 3 DE RIP N E On July 14, 1990, Unit 2 was in Mode 1 at 100% power, with the "B" Main Steam Line Radiation Monitor (EIIS:IL) out of service for the repair of a failed power supply. The "B" Main Steam Line Radiation Monitor was placed in the Equipment Out of Service Log. Non-licensed utility Instrumentation and Control (l8 C) personnel replaced the 700 volt power supply for the "B" Main Steam Line Radiation Monitor. Upon completion of the repair, a utility licensed operator reviewed and approved the Nuclear Plant Work Order, authorized the return of service of the "B" Main Steam Line Radiation Monitor, and removed the item from the Equipment Out of Service Log.

On July 25, 1990, review of the Nuclear Plant Work Order was performed by utility maintenance supervisory personnel. It was determined that the proper retest requirements for returning to service of the "B" Main Steam Line Radiation Monitor was not given to utility Chemistry Department personnel, who normally perform the surveillances. On July 25, 1990, Chemistry Department non-licensed personnel satisfactorily performed a Channel Calibration and Channel Functional Test.

On July 26, 1990, it was determined by utility Technical Staff personnel that the the "B" Main Steam Line Radiation Monitor was returned to service on July 14, 1990 without a Channel Calibration and a Channel Functional Test performed as required in accordance with Surveillance Requirement 4.3.3.1 of the Unit 2 Technical Specifications.

EE The root cause of this event is that there was failure of utility non-licensed maintenance personnel to properly follow an l8C procedure, Instrumentation 8 Control Test Control. This procedure was stated to be used on the Nuclear Plant Work Order. Since I8C personnel do not perform either the Channel Calibration or the Channel Functional Test of the Main Steam Line Radiation Monitors, they normally contact Chemistry or Health Physics personnel to perform those surveillances. However, Appendix A.0.12, "Maintenance Test Sheets Power Supply Form", was not used and therefore not attached to the Nuclear Plant Work Order. Proper annotation of the form and attachment to the Nuclear Plant Work Order would have brought to the attention of the licensed utility operator the need for performance of the Channel Calibration and Channel Functional Test prior to returning the the "B" Main Steam Line Radiation Monitor to service.

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~ i'I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO 0MB NO. 31QM104 EXPIRES B/31/BS FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR,," SEQUFhNTIAL j'EVISION a NUMBER St. Lucie Unit 2 05000389 0 0 0 3 OF 0 3 TEXT (If more spaceis required, use additional NRC Form 366A's)(17)

F THE EV This event is reportable under the requirements of 10 CFR 50.73.a.2.i.B, as an operation or condition prohibited by the St. Lucie Unit 2 Technical Specifications.

Technical Specification 3.3.3.1 requires that the "B" Main Steam Line Radiation Monitor be operable in Modes 1, 2, 3, and 4. Other instrumentation for radiation monitoring of the secondary system, the Steam Generator Blowdown Monitor and the Steam Jet Air Ejector Monitor, were operable during the time frame of July 14 through July 25, 1990. No indications of abnormal trends or alarm conditions in the secondary systems occurred during this period. A regularly scheduled surveillance of the "B" Main Steam Line Radiation Monitor performed July 25, 1990 was satisfactory and demonstrated that the monitor was operable while it was in service.

Improper use of St. Lucie Plant procedure, Instrumentation and Control Test Control, QI11-PR/PSL-4, by non-licensed utility maintenance personnel resulted in the inability of a licensed reactor operator to properly assess that the testing requirements were not completed.

There were no unusual characteristics of the work location that contributed to the error.

Thus, the health and safety of the public were not at risk during this event.

t

1. Chemistry non-licensed utility personnel satisfactorily performed a Channel Calibration and a Channel Functional Test of the "B" Main Steam Line Radiation Monitor.
2. I8C personnel were counseled on the need to follow procedures.
3. IBC Department will revise the Instrumentation and Control Test Control procedure such that a note is added to inform Chemistry or Health Physics, as necessary, before returning Technical Specification required radiation monitoring instrumentation back into service.

NT FAI NONE IMI A The most recent similar event is LER 335-89-006, which describes a radiation effluent monitor being out of service due to having electric leads reversed.

Another similar event is LER 335-87-009, which describes a fuel handling building ventilation radiation monitor being out of service due to cognitive personnel error on the part of utility licensed personnel.

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