IR 05000498/2019001

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NRC Integrated Inspection Report 05000498/2019001; 05000499/2019001, and Independent Spent Fuel Storage Inspection 07201041/2019001
ML19128A334
Person / Time
Site: South Texas, 07201041  STP Nuclear Operating Company icon.png
Issue date: 05/08/2019
From: Nick Taylor
NRC/RGN-IV/DRP/RPB-B
To: Gerry Powell
South Texas
References
IR 2019001
Download: ML19128A334 (33)


Text

May 8, 2019

SUBJECT:

SOUTH TEXAS PROJECT ELECTRIC GENERATING STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000498/2019001; 05000499/2019001, AND INDEPENDENT SPENT FUEL STORAGE INSPECTION 07201041/2019001

Dear Mr. Powell:

On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your South Texas Project Electric Generating Station, Units 1 and 2. On April 11, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

One of these findings involved a violation of NRC requirements.

The inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at South Texas Project Electric Generating Station, Units 1 and 2.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at South Texas Project. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Nicholas H. Taylor, Branch Chief Project Branch B Division of Reactor Projects

Docket Nos. 05000498; 05000499 and 07201041 License Nos. NPF-76 and NPF-80

Enclosure:

Inspection Report 05000498/2019001; 05000499/2019001 and 07201041/2019001 w/attachment: NRC Request for Information

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number(s):

05000498; 05000499 and 07201041

License Number(s):

NPF-76 and NPF-80

Report Number(s):

05000498/2019001; 05000499/2019001, and 07201041/2019001

Enterprise Identifier: I-2019-001-0004 and 1-2019-001-0082

Licensee:

STP Nuclear Operating Co.

Facility:

South Texas Project Electric Generating Station, Units 1 and 2

Location:

Wadsworth, TX 77483

Inspection Dates:

January 1, 2019, to March 31, 2019

Inspectors:

B. Baca, Health Physicist

J. Choate, Resident Inspector

A. Sanchez, Senior Resident Inspector

L. Brookhart, Senior ISFSI Inspector, FCDB

C. Smith, Reactor Inspector, DRS, EB1

O. Masnyk Bailey, Health Physicist, RI, DIRHB

M. Learn, Reactor Engineer, RIII, MCID

R. Edwards, Senior Health Physicist, RIII, MCID

Approved By:

Nicholas H. Taylor

Chief, Project Branch B

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a quarterly inspection at South Texas Project Electric Generating Station, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC and self-revealed findings, violations, and additional items are summarized in the table below. Licensee-identified non-cited violations are documented in report sections:

7115

List of Findings and Violations

Failure to Implement the Procedure for Equipment Failures Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green FIN 05000499/2019-01 Closed

[H.12] - Avoid Complacency 71152 Problem Identification and Resolution The inspectors identified a Green finding for the licensees failure to implement the procedure for the failure of a plant generation risk high risk component. Specifically, the licensee failed to implement and follow Procedure WCG-0008, Preventing Recurring Equipment Problems (PREP), Revision 7, following the failure of the Unit 2 steam generator 2C normal feedwater regulating control valve, FCV-553.

Failure to Provide Adequate Procedural Guidance for a Surveillance Test Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000499/2019-02 Closed

[H.12] - Avoid Complacency 71152 Problem Identification and Resolution The inspectors documented a Green self-revealed NCV for the failure to provide an adequate procedure for a Unit 2 qualified display processing system (QDPS) surveillance procedure that resulted in unnecessary troubleshooting, unnecessary replacement of properly operating circuit cards, and placing the loop 2 over-temperature delta-T, over-pressure delta-T, and low Tavg feedwater isolation bistables into a TRIPPED condition, a half-trip condition for the reactor. Following an investigation, the licensee discovered that incorrect biases were inputted into the QDPS surveillance procedure.

Additional Tracking Items

Type Issue number Title Inspection Procedure Status LER 05000498/2017-002-00 Unit 1 Condition Prohibited by Technical Specifications due to Inoperable Control Room Envelope Makeup Filtration System Heating Coil 71153 Follow-up of Events Closed LER 05000498/2018-001-00 Unit 1 Main Steam Safety Valve As Left Settings Outside of Required Range Contrary to Technical Specifications due to Inadequate Procedure 71153 Follow-up of Events Closed

PLANT STATUS

Unit 1 operated at rated thermal power for the entire inspection period.

Unit 2 began the inspection period at rated thermal power. On March 2, 2019, while performing main turbine governor valve testing at 90 percent power, a procedural error resulted in an unexpected decrease in reactor power to 86 percent power. The reactor was returned back to rated thermal power on March 3, 2019, and remained there for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown (IP Section 02.01) (5 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1, train B chemical and volume control system during train A centrifugal charging pump maintenance on January 2, 2019
(2) Unit 2, turbine driven auxiliary feedwater system with elevated unit trip risk during north bus outage on March 1, 2019
(3) Unit 2, train C emergency core cooling system during train B emergency diesel generator maintenance on March 13, 2019
(4) Unit 2, train A essential chilled water system during train B essential chilled water system maintenance on March 16, 2019
(5) Unit 2, train A essential cooling water system during train C essential cooling water maintenance on March 22, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 2, safety injection pump cubicles, Fire Area 35 on February 2, 2019
(2) Units 1 and 2, balance of plant diesel generator rooms and turbine generator building switchgear rooms, Fire Areas 78 and 90 on February 26, 2019
(3) Unit 1, auxiliary feedwater pump cubicles, Fire Areas 48, 49, 50, and 51 on February 27, 2019
(4) Unit 1, train C essential cooling water intake structure, Fire Area 55 on March 22, 2019
(5) Unit 1, train C vital switchgear room, battery room, 125 vdc distribution room, and motor generator room, Fire Areas 52 through 54 on March 26, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the Unit 1, train B essential cooling water pump room on March 26, 2019.

71111.07A - Heat Sink Performance

Annual Review (IP Section 02.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) Unit 1, train C emergency diesel generator jacket water and lube oil heat exchangers the week of January 14, 2019
(2) Unit 2, train B essential chilled water cooler the week of March 12, 2019

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

The inspectors observed and evaluated licensed operator performance in the Unit 1 control room during a secondary side electro-hydraulic leak which resulted in the closure of the 13 west reheat stop valve to the low pressure turbine on January 9, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

The inspectors observed and evaluated Unit 1 operations in the simulator during a loss of coolant accident followed by a loss of offsite power on February 27, 2019.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Unit 1, turbine driven auxiliary feedwater pump low governor oil level that resulted in inoperability of the train on January 3, 2019
(2) Unit 1, electro-hydraulic control system leak that resulted in the closure of reheat stop valve 13 on January 9, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Units 1 and 2, planned north bus outage that resulted in entering the Configuration Risk Management Program on February 26, 2019
(2) Unit 2, planned turbine driven auxiliary feedwater pump extent of condition maintenance for connecting rod engagement on January 31, 2019
(3) Unit 1, train B essential cooling water unplanned pump replacement February 13 through 19, 2019
(4) Unit 1, elevated risk due to unplanned entry into the Configuration Risk Management Program for exceeding the train B essential chilled water system 7 day limiting condition for operation due to maintenance activities on March 10, 2019

71111.15 - Operability Determinations and Functionality Assessments

Sample Selection (IP Section 02.01) (5 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 1, turbine driven auxiliary feedwater pump following the identification of a degraded conduit for the remote trip solenoid on January 16, 2019
(2) Unit 1, train B control room envelope heating, ventilation, and air conditioning damper controller on February 6, 2019
(3) Unit 2, cask loading pool leakage on February 12, 2019
(4) Unit 1, train B emergency diesel generator shutdown when taken out of emergency mode on March 11, 2019
(5) Unit 2, turbine driven auxiliary feedwater pump experiencing high main oil pump discharge pressure on March 15, 2019

71111.19 - Post Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Unit 1, train C emergency diesel generator following fuel oil storage tank level transmitter replacement on January 31, 2019
(2) Unit 2, turbine driven auxiliary feedwater pump following failure of connecting rod on January 31, 2019
(3) Unit 1, train B essential cooling water pump following pump replacement on March 4, 2019
(4) Unit 1, train B emergency diesel generator following replacement of shutdown air solenoid valve on March 13, 2019
(5) Units 1 and 2, diesel fire pump number 3 following replacement of the pump impeller, diesel starter solenoid, and pump packing on March 18, 2019
(6) Unit 2, train C residual heat removal pump following control room handswitch replacement on March 19, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

In Service Testing (IST) (IP Section 03.01)

(1) Unit 1, turbine driven auxiliary feedwater pump surveillance test on January 24, 2019
(2) Unit 1, train B essential cooling water system surveillance test on February 14, 2019

Surveillance Testing (IP Section 03.01) (4 Samples)

(1) Unit 2, train B emergency diesel generator surveillance test on February 12, 2019
(2) Unit 2, train A auxiliary feedwater regulating valve dynamic pressure test on March 4, 2019
(3) Unit 1, train B emergency diesel generator fast start surveillance on March 13, 2019
(4) Unit 1, train C emergency diesel generator fast start surveillance on March 15,

RADIATION SAFETY

71124.02 - Occupational ALARA Planning and Controls

Radiological Work Planning (IP Section 02.01) (1 Sample)

The inspectors evaluated the licensees radiological work planning by reviewing the following activities:

  • 1RE21 - Reactor Cavity and Head Activities
  • 1RE21 - Fuel Transfer Canal Activities
  • 2RE19 - Reactor Cavity and Head Activities

Verification of Dose Estimates and Exposure Tracking Systems (IP Section 02.02) (1 Sample)

The inspectors evaluated dose estimates and exposure tracking. The inspectors reviewed the following ALARA planning documents:

  • 18-276-7 ALARA Review Package: 2RE19 Non-Rapid Refuel, Revision 1
  • 18-7926-4 ALARA Review Package: 1RE21 Non-Rapid Refuel

Additionally, the inspectors reviewed the following radiological outcome evaluations:

  • 18-276-7 ALARA Close Out Review Package: 2RE19 Non-Rapid Refuel, Revision 1
  • 18-7926-4 ALARA Close Out Review Package: 1RE21 Non-Rapid Refuel
  • 18-7926-4 ALARA Close Out Review Package Supplement 1: 1RE21 Non-Rapid Refuel

71124.04 - Occupational Dose Assessment

External Dosimetry (IP Section 02.02) (1 Sample)

The inspectors evaluated the external dosimetry program implementation.

Internal Dosimetry (IP Section 02.03) (1 Sample)

The inspectors evaluated the internal dosimetry program implementation.

Three contaminated workers' whole body counts were reviewed for potential uptakes. The licensee had no positive whole body counts indicating an internal uptake of radioactive material.

The licensee had no occurrences to observe or review in-vitro internal monitoring or dose assessments performed using air sampling and DAC-hr. monitoring.

Source Term Categorization (IP Section 02.01) (1 Sample)

The inspectors evaluated the licensees characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity.

Special Dosimetric Situations (IP Section 02.04) (1 Sample)

The inspectors evaluated special dosimetric situations, as detailed below.

  • The inspectors reviewed approximately five declared pregnant workers' documentation from January 1, 2017, to March 21, 2019.
  • The licensee did not perform any EDEX assessments from July 31, 2017, to March 21, 2019.
  • The inspectors reviewed one shallow dose equivalent assessment (Condition Report 2019-1215).
  • The inspectors reviewed the licensee's use of Mirion neutron thermoluminescent dosimetry and electronic alarming dose meters (Model EPDN2) for neutron dosimetry. The inspector compared radiological surveys, RWP and WAN assignments, and worker exposures to confirm the licensee is appropriately assigning neutron dose to occupational workers.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below.

=

(1) IE01: Unplanned Scrams per 7000 Critical Hours Sample (Units 1 and 2, January - December 2018
(2) IE03: Unplanned Power Changes per 7000 Critical Hours Sample (Units 1 and 2, January - December 2018
(3) IE04: Unplanned Scrams with Complications Sample (Units 1 and 2, January - December 2018)

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (4 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Unit 2, pressurizer master controller card failure, Condition Report 2017-658.

Inspectors reviewed the plant response to the event, operator actions, corrective actions, and interviewed licensee personnel.

(2) Unit 1, low head safety injection breaker failure, Condition Report 2017-20444.

Inspectors reviewed the apparent cause investigation, operability evaluation, and corrective actions.

(3) Unit 2, train C steam generator main control valve failed low in automatic mode, Condition Report 2017-17659. Inspectors reviewed the plant response to the event, operator actions, maintenance and engineering troubleshooting repair of the issue, interviewed licensee personnel and corrective actions.
(4) Unit 2, train D qualified display processing system calibration procedure that resulted in exceeding the Technical Specification allowed outage time and placed the bistables into a trip condition, Condition Reports 2016-11346 and 2016-11257. The inspectors reviewed the prompt investigation, interviewed maintenance and engineering personnel, and evaluated the corrective actions.

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000498/2017-002-00, "Unit 1 Condition Prohibited by Technical Specifications due to Inoperable Control Room Envelope Makeup Filtration System Heating Coil,"

on January 22, 2018:

(2) LER 05000498/2018-001-00, "Unit 1 Main Steam Safety Valve As Left Settings Outside of Required Range Contrary to Technical Specifications due to Inadequate Procedure," on December 4, 2018:

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

60854 - Preoperational Testing of an Independent Spent Fuel Storage Inspection (ISFSI)60855 - Operation of an ISFSI at Operating Plants 60857 - Review of 10 CFR 72.48 Evaluations

Inspections of dry cask storage operations were conducted at STP on January 21-25 and on January 28 through February 2, 2019, by inspectors from NRC Regions I, III, and IV. The STP ISFSI was licensed as a general 10 CFR Part 72 license and utilized the Holtec HI-STORM FW Certificate of Compliance (COC) 1032 Amendment 2 and HI-STORM FW Final Safety Analysis Report (FSAR) Revision 5.

In prior NRC ISFSI inspections at STP (ADAMS Accession Nos. ML18221A385 and ML19032A079), the NRC staff documented the observations and evaluations of many of the required pre-operational demonstrations from License Condition No. 9 of the COC performed by STP. Those inspections included an in-depth review of the licensees dry cask storage program implementation into existing 10 CFR Part 50 programs to support ISFSI operations at the site. The purpose of the NRC inspections in January and February 2019 were to:

(1) observe and evaluate the remaining pre-operational demonstrations and training exercises which STP was required to complete prior to commencing loading operations, and
(2) observe and evaluate the licensees first loading operations. On January 21-25, 2019, the NRC staff observed STP complete the remaining demonstrations listed in License Condition No. 9 of the COC to allow use of the Holtec HI-STORM FW storage system. South Texas Project had successfully completed all the required pre-operations activities and fully demonstrated that the procedures, programs, and training related to those dry cask storage operations had been successfully integrated into its site operations. The subsequent week, from January 28 to February 2, 2019, NRC staff observed the licensees first canister loading operations.

The ISFSI activities specifically reviewed during the on-site inspections and during in-office review included:

1. Evaluated and observed dry run demonstrations from License Condition No. 9 of the

COC, which included: preparation of the canister storage system for fuel loading; loading a dummy fuel assembly into the canister with appropriate independent verification; selection and verification of the specific fuel assemblies to ensure type conformance; remote installation of the canister lid; removal of the canister from the spent fuel pool; and unloading operations that included remotely removing a lid from the canister to support fuel unloading.

2. Reviewed the licensees structural and seismic calculations for dry cask storage

operations which included: over-head spent fuel building crane with loaded Transfer Cask (TC); loaded TC in the spent fuel pools loading area; loaded TC in the canister wash-down area for processing operations; loaded TC in the stack-up configuration to support downloading of a canister into the concrete over-pack; loaded over-pack on low-profile transporter; and loaded over-pack being carried by the vertical cask transporter to the ISFSI pad.

3. Reviewed two 10 CFR 72.48 safety evaluations performed by the licensee for changes

made to the ISFSI program since the previous NRC ISFSI inspection per Inspection Procedure 60857.

4. Reviewed spent fuel documentation for the first canister to verify the fuel met all

Appendix B Technical Specifications requirements for storage.

5. Evaluated and observed fuel selection and fuel loading operations associated with dry

fuel storage canister No. 1.

6. Evaluated and observed welding of the canister, non-destructive testing of the welds,

forced helium drying, helium backfill, and heavy load movements from the spent fuel pool to the sites vertical cask transporter.

7. Reviewed the licensee's loading, processing, and heavy load procedures associated

with their current dry fuel storage campaign.

8. Reviewed the licensees corrective action programs condition reports of issues identified

for resolution since the previous NRC ISFSI inspection performed in November 2018.

9. Evaluated and observed the licensees radiation protection implementation during the

dry run and loading operations.

10. Evaluated and observed the licensees implementation of foreign material exclusion process during the dry run and loading operations.

The inspectors did not identify any issues of concerns requiring documentation.

INSPECTION RESULTS

Failure to Implement the Procedure for Equipment Failures Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events

Green FIN 05000499/2019-01 Closed

[H.12] - Avoid Complacency 71152 Problem Identification and Resolution The inspectors identified a Green finding for the licensees failure to implement the procedure for the failure of a plant generation risk (PGR) high risk component. Specifically, the licensee failed to implement and follow Procedure WCG-0008, Preventing Recurring Equipment Problems (PREP), Revision 7, following the failure of the Unit 2 steam generator 2C normal feedwater regulating control valve FCV-553.

Description:

On June 19, 2017, Unit 2 reactor operators responded to control room alarms and indications for steam flow/ feed flow mismatch for steam generator 2C. Operators identified that the steam generator 2C main feedwater regulating valve had failed closed and that steam generator level was decreasing for that steam generator. Operators entered the appropriate off-normal procedure and within 28 seconds regained control of steam generator levels by manually controlling feedwater flow through the main feedwater regulating valve. As a result of the failure, reactor power lowered to approximately 97 percent, average reactor coolant system temperature (Tavg) reached a maximum valve of 592.9 degrees F (normally Tavg is 592.0), and steam generator 2C narrow range level lowered to 52.8 percent (normally 70 percent).

Following the failure, engineering and maintenance discussed and implemented changing out a suspected nuclear tracker-driver (NTD) circuit card. This type of activity in the 7300 control cabinets is a high risk evolution and required a work activity risk review to help ensure no mistakes were made and that operations prepared for the worst case outcome. South Texas Project (STP) has site specific operating experience where card calibration and card replacement activities have resulted in reactor trips. Engineering was confident that the NTD circuit card was the problem. Maintenance personnel suggested measuring voltage readings at various locations inside the panel to ensure the faulty card was identified, however these measurements were not taken due to engineerings position that the NTD card was faulty.

The inspectors attended the pre-job brief and observed the field work. Maintenance performed the card replacement successfully, but the issue remained. Maintenance and engineering regrouped and decided to take voltage measurements to identify the circuit card failure. Maintenance identified the nuclear control board (NCB) as the problem and replaced the NCB without issue. STP performed the high-risk evolution twice due to inadequate troubleshooting and over-reliance on engineering assumptions.

The licensee evaluated the operators response to the main feedwater regulating valve failure and engineering and maintenances response to troubleshooting and repair of the failed circuit card. The inspectors interviewed engineering and maintenance and determined that the licensee should have entered and implemented Procedure WCG-0008 following the failure of the Unit 2 steam generator 2C normal feedwater regulating control valve, FCV-553.

The procedure would have ensured the appropriate degree of rigor was applied when pursuing resolution of high risk equipment issues. Specifically, Step 1.3 states, in part, The PREP process entry criteria are: Loss of Key Equipment function/ Critical Attribute.

The failure of the main feedwater regulating valve was a loss of key equipment function. The PREP process would have engaged more management oversight, directed the gathering of facts through Addendum 3, Preventing Recurring Equipment Problems (PREP) checklist, and may have led to the development of a troubleshooting plan.

Corrective Actions: The licensee replaced the failed card and developed a lessons-learned presentation for engineering to use human performance tools, validate assumptions, and challenge recommendations (use technical conscience).

Corrective Action References: Condition Reports 2017-17659 and 2019-4368

Performance Assessment:

Performance Deficiency: The failure to enter and use station Procedure WCG-0008, Preventing Recurring Equipment Problems (PREP), Revision 7, following the failure of the Unit 2 steam generator 2C normal feedwater regulating control valve, FCV-553, was a performance deficiency. Specifically, the licensee failed to enter WCG-0008 upon the failure of the main feedwater regulating valve, a loss of key equipment function due to the component being classified as a high PGR. The result of not implementing this procedure was an increased probability of tripping the reactor due to possible human error while in the 7300 control cabinet.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the human performance attribute and adversely affected the Initiating Events Cornerstone objective to limit the likelihood of events that can upset plant stability during power operations and is therefore a finding. Specifically, engineering relied on past experience and did not consider entering and implementing the PREP process procedure, which would have applied more rigor to troubleshooting and resolving the issue.

Significance: The inspectors used IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, issued June 19, 2012, to determine the finding was of very low safety significance, Green. Specifically, one finding did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

Failure to Provide Adequate Procedural Guidance for a Surveillance Test Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events

Green NCV 05000499/2019-02 Closed

[H.12] - Avoid Complacency 71152 Problem Identification and Resolution The inspectors documented a Green self-revealed NCV for the failure to provide an adequate procedure for a Unit 2 qualified display processing system (QDPS) surveillance procedure that resulted in unnecessary troubleshooting, unnecessary replacement of properly operating circuit cards, and placing the loop 2 over-temperature delta-T (OTDT), over-pressure delta-T (OPDT), and low Tavg feedwater isolation bistables into a TRIPPED condition, a half-trip condition for the reactor. Following an investigation, the licensee discovered that incorrect biases were inputted into the QDPS surveillance procedure.

Description:

On September 15, 2016, operations declared the loop 2 OTDT, OPDT, and the low Tavg feedwater isolation inoperable for loop calibration surveillance testing and bypassed the channel per Technical Specifications 3.3.1, items 8 and 9, action 6, and 3.3.2, item 5F, action 20. If not restored within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, the channel must be placed into a TRIPPED condition. During the performance of Surveillance Procedure 0PSP05-RC-0420, Delta T and T average loop 2 Set Calibration (T-0420), Revision 53, maintenance identified an out-of-tolerance condition. Engineering recommended maintenance perform a QDPS output calibration using Procedure 0PMP08-AM-APCD2, QDPS Train D SGWLCS/TAS Input/Output Calibration, Revision 10. During this calibration, the licensee again identified an out-of-tolerance condition which could not be resolved. The licensee performed troubleshooting and began to replace circuit boards in the train D QDPS cabinet without success. On September 18, 2016, the bistables for the OTDT, OPDT, and Low Tavg feedwater isolation were placed into a TRIPPED condition as required by technical specifications.

The licensee subsequently discovered that an engineering error resulted in incorrect biases being placed into the Calibration Procedures 0PSP05-RC-0420 and 0PMP08-AM-APCD2.

The two procedures were corrected with the proper biases and completed satisfactorily. The manual substitution of the resistance temperature detector (RTD) biases in the two calibration procedures had never been performed before and, due to the complex nature of the QDPS system, only three people on site could perform and peer check these biases. The licensee performed a prompt investigation and a review for organizational learnings. The licensee determined that the engineer made changes to the procedure to account for the two RTD operation, but failed to get the values peer checked for accuracy. This failure led to excessive out-of-service time, unnecessary QDPS maintenance, and having to place the loop 2 protection bistables into a TRIPPED condition, i.e. half reactor trip.

Corrective Actions: The licensee immediately corrected the procedures and re-performed the calibrations and satisfactorily performed analog channel operational testing. The licensee also developed a lessons-learned document and has an outstanding action to develop an engineering guideline when either unit is in two RTD operation.

Corrective Action References: Condition Reports 2016-11346, 2016-11257, 2019-4367

Performance Assessment:

Performance Deficiency: The failure to provide adequate procedures for maintenance on safety-related equipment was a performance deficiency. Specifically, engineering supplied inaccurate information to calibration procedures for the Unit 2 loop 2 and train D QDPS that resulted in unnecessary maintenance in QDPS and TRIPPED bistables associated with OTDT, OPDT, and low Tavg feedwater isolation which caused Unit 2 to be in a half reactor trip.

Screening: The inspectors determined the performance deficiency was more than minor because it is associated with the Procedure Quality attribute and adversely affected the Initiating Event Cornerstone objective to limit the likelihood of events that can upset plant stability during power operations and is therefore a finding. Specifically, the loop 2 bistables associated with OTDT, OPDT, and low Tavg were placed into a TRIPPED condition which placed Unit 2 one spurious reactor trip signal away from a true reactor trip due to the performance deficiency.

Significance: The inspectors used IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, issued June 19, 2012, to determine the finding was of very low safety significance, Green. Specifically, one finding did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. The inspectors determined that the finding had a crosscutting aspect in the area of human performance associated with avoiding complacency. Specifically, engineering provided inaccurate biases for the procedure changes without utilizing appropriate error reduction tools [H.12].

Enforcement:

Violation: Technical Specification 6.8.1.a requires, in part, that written procedures shall be established, implemented, and maintained in accordance with Appendix A of Regulatory Guide 1.33, Revision 2, February 1978, Section 8.b.(L) reactor protection system tests and calibrations. The licensee established Procedure 0PSP05-RC-0420, Delta T and T average loop 2 Set Calibration (T-0420), Revision 53 to meet the Regulatory Guide 1.33 requirement.

The Unit 2 data package loop 2 set 2 (T-0420) provides appropriate biases to be used to test and calibrate the loop.

Contrary to the above, on September 15, 2016, the licensee failed to ensure that the Unit 2 data package loop 2 set 2 (T-0420) provided the appropriate biases to be used to test and calibrate the loop. Specifically, engineering failed to provide accurate biases for procedures used for surveillance and calibration of the OTDT, OPDT, and low Tavg feedwater isolation trip setpoints.

Enforcement Action: This violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the Enforcement Policy.

Minor Violation 71153 Follow-up of Events Minor Violation: Technical Specification 3.7.7, Control Room Makeup and Cleanup Filtration System, states, in part, that if one Control Room Makeup and Cleanup Filtration System is inoperable, it must be restored to operable in Modes 1, 2, 3, and 4 within 7 days, or be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

Contrary to the above, between September 27 and November 24, 2017, the licensee failed to restore one control room makeup and cleanup filtration system to operable. Specifically, the licensee failed to properly jumper a circuit board for the control room makeup and cleanup filtration system heating coil.

Screening: The inspectors determined the performance deficiency was minor. The inspectors found this violation to be minor in accordance with IMC 0612 Appendix B, Issue Screening, issued December 13, 2017, because the violation did not satisfy any of the four More-than-Minor screening questions.

Enforcement:

This failure to comply with Technical Specification 3.7.7 constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Licensee-Identified Non-Cited Violation 71153 Follow-up of Events This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Technical Specification 3.7.1.1, Safety Valves, states, in part, that if one or more main steam line code safety valves are inoperable, they must be restored to operable status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or reduce the Power Range Neutron Flux High Trip Setpoint or be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Contrary to the above, between October 2 and 6, 2018, the licensee failed to restore two of the Unit 1 steam generator B main steam safety valves to operable status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, failed to reduce the Power Range Neutron Flux High Trip Setpoint, and failed to be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Specifically, the licensee failed to identify that two of the Unit 1 Steam Generator B main steam safety valves were left outside of their Technical Specification required lift settings following testing.

Significance: Green.

The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the mitigating systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors assessed the significance of the finding using Exhibit 2, Mitigating Systems Screening Questions, of IMC 0609, Appendix A, Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012, and determined this finding did not represent an actual loss of function. Therefore, the inspectors determined the finding was of very low safety significance (Green).

Corrective Action References: Condition Reports 2018-11811 and 2019-4374

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 11, 2019, the inspector presented the quarterly resident inspector inspection results to Mr. G. T. Powell, President and Chief Executive Officer, and other members of the licensee staff.
  • On March 21, 2019, the inspector presented the baseline radiation safety inspection to Mr. J. Connolly, Executive Vice President and Chief Nuclear Officer, and other members of the licensee staff.
  • On March 21, 2019, the inspector presented the pre-operational dry run and first loading inspection to Mr. J. Connolly, Executive Vice President and Chief Nuclear Officer, and members of the licensee staff.

DOCUMENTS REVIEWED

71111.01-Adverse Weather

Procedures

Number

Title

Revision

0PGP03-ZV-0001

Severe Weather Plan

71111.04-Partial Equipment Alignment

Condition Reports

CR-2018-2825

Procedures

Number

Title

Revision

0POP02-AF-0001

Auxiliary Feedwater

0POP02-SI-0002

Safety Injection System Initial Lineup

0PSP03-CH-0001

Essential Chilled Water Pump 11A(21A) Inservice Test

0POP02-EW-0001

Essential Cooling Water Operations

Drawings

Number

Title

Revision

5R179F05007#1

Chemical and Volume Control System

5S142F00024#1

Auxiliary Feedwater

5N129F05015#2

Safety Injection System

5V119V10001#2

HVAC Essential Chilled Water System

5R289F05038#2

Essential Cooling Water System Train 2B

71111.05-Fire Protection

Procedures

Number

Title

Revision

0FHB35-FP-0306

Fire Preplan Fuel Handling Building Train B SI/CSS Cubicle 2

0FHB35-FP-0307

Fire Preplan Fuel Handling Building Train A SI/CSS Cubicle 2

0PGP03-ZF-0011

STPEGS Fire Brigade

0DMB99-FP-0920

Fire Preplan for Make-Up Demineralizer Building

0TGB78-FP-0703

Fire Preplan Turbine Generator Building BOP Diesel

Generator Building

0TGB90-FP-0702

Fire Preplan for Turbine Generator Building 4.16 KV and

Electrical Equipment Rooms

Procedures

Number

Title

Revision

0TGB90-FP-0710

Fire Preplan Turbine Generator Building 13.8 KV Switchgear

Room and Cable Vault

0IVC48-FP-0403

Fire Preplan Isolation Valve Cubicle Pump Room Train C

0IVC49-FP-0402

Fire Preplan Isolation Valve Cubicle Pump Room Train B

0IVC50-FP-0401

Fire Preplan Isolation Valve Cubicle, Pump Room Train A

0IVC51-FP-0400

Fire Preplan Isolation Valve Cubicle, Pump Room Train D

0EAB-FP-0052

Fire Preplan Electrical Auxiliary Building ESF Switchgear

Room Train C

0EAB-FP-0053

Fire Preplan Electrical Auxiliary Building, Channel IV Battery

and Distribution Room

0EAB-FP-0054

Fire Preplan Electrical Auxiliary Building, Motor Generator

Room

1ECW55-FP-0602

Fire Preplan Essential Cooling Water Intake Structure Pump

Room Train C

71111.07A - Annual Heat Sink

Procedures

Number

Title

Revision

0PMP05-CH-0003

York Chiller Inspection & Maintenance 300 Tons

0PGP03-ZE-0080

Essential Cooling Water System Reliability Program

Work Authorization Numbers

443062

71111.11-Simulator/Control Room Observation

Condition Reports

CR-2019-364

CR-2019-423

Procedures

Number

Title

Revision

0POP02-EH-0001

Main Turbine EHCS

0POP07-MS-0003

Main Turbine Steam Inlet Valve Test

P&ID

Number

Title

Revision

6S109F00017#1

P&ID Main Steam

P&ID

Number

Title

Revision

7T089F10001#1

P&ID EH Fluid System

71111.12-Maintenance Effectiveness

Condition Reports

CR-2015-18885

CR-2017-15182

CR-2017-23544

CR-2018-995

CR-2018-8533

CR-2018-1108

CR-2018-12813

CR-2018-15270

CR-2018-15273

Work Authorization Numbers

499003

519391

21829

2330

540499

548908

568084

603714

Procedures

Number

Title

Revision

0PMP04-AF-0002

Auxiliary Feedwater Pump Turbine Maintenance

0PMP04-AF-0003

Auxiliary Feedwater Turbine Trip Throttle Valve Maintenance 36

0PSP03-AF-0007

Auxiliary Feedwater Pump 14(24) Inservice Test

Drawings

Number

Title

Revision

6S109F00017#1

Piping and Instrumentation Diagram Main Steam

7T089F10001#1

Piping and Instrumentation Diagram Electro Hydraulic Fluid

System

71111.13-Maintenance Risk and Emergent Work

Procedures

Number

Title

Revision

0PGP03-ZA-0091

Configuration Risk Management Program

0POP01-ZO-0006

Risk Management Actions (RMAs)

Work Activity Risk (WAR)

2804

RasCal Sequences

3331

3336

3337

71111.15-Operability Determinations and Functionality Assessments

Condition Reports

CR-2019-47

CR-2019-347

CR-2019-1377

19-2777

19-637

Drawings

STI. Number

Title

Date

31390502

Cabinet-Control (Assembly Engine Control)

2/27/1978

298485

Control Schematic (Starting Sequence Control)

09/29/1977

71111.19-Post Maintenance Testing

Condition Reports

CR-2018-7676

CR-2018-9443

CR-2018-14727

CR-2019-111

CR-2019-893

CR-2019-1762

CR-2019-2357

CR-2019-2435

CR-2019-2777

CR-2019-1020

Work Authorization Numbers

545649

565703

571744

571827

2175

576480

2665

604208

604273

606453

573948

605423

Procedures

Number

Title

Revision

0PSP04-DG-0004

Standby Diesel Generator Fuel Oil Storage Tank Inspection 9

0PMP08-DO-9109

ESF Diesel Generator Fuel Oil Storage Tank Level

Calibration

0PSP03-EW-0011

Essential Cooling Water Pump 1B(2B) Reference Values

Measurement

0PSP03-AF-0007

Auxiliary Feedwater Pump 14(24) Inservice Test

0POP07-FP-0001

Diesel Fire Pump Test

0PTP03-FP-0106

Fire Protection Water System Functional Test

0PSP03-DG-0002

Standby Diesel 12(22) Operability Test

Miscellaneous

Documents

Number

Title

Revision

VTD-T343-0001

Installation and Service Instructions for Tuthill Cartridge

Pumps

VTD-P104-0011

Patterson Operation and Maintenance Manual for Double

Suction Split Case Pumps

71111.22-Surveillances

Condition Reports

CR-2019-975

CR-2019-1762

Procedures

Number

Title

Revision

0POP02-AF-0001

Auxiliary Feedwater

0PSP03-AF-0007

Auxiliary Feedwater Pump 14(24) Inservice Test

0PMP05-ZE-0425

MOV Diagnostic Testing (VOTES) - Rising Stem Valves

0PEP07-AF-0003

Dynamic Stroke Testing of Train A Auxiliary Feed Motor

Operated Feed Regulating Valve

0PSP03-DG-0003

Standby Diesel 13(23) Operability Test

0PMP07-DG-0001

Standby Diesel Recording M&TE Installation

0PSP03-DG-0002

Standby Diesel 12(22) Operability Test

0PSP03-EW-0018

Essential Cooling Water System Train B Testing

71124.02 - Occupational ALARA Planning and Controls

Condition Reports

CR-2018-3840

CR-2018-3991

CR-2018-4050

CR-2018-4125

CR-2018-4555

CR-2018-4860

CR-2018-5849

CR-2018-6071

CR-2018-8097

CR-2018-9179

CR-2018-9284

CR-2018-11217

CR-2018-12339

CR-2018-13572

CR-2019-234

CR-2018-1066

Procedures

Number

Title

Revision

0PGP03-ZR-0050

Radiation Protection Program

0PGP03-ZR-0052

ALARA Program

0PRP07-ZR-0001

ALARA Engineering and Procedure Review

0PRP07-ZR-0010

Radiation Work Permits/Radiological Work ALARA Reviews 38

Procedures

Number

Title

Revision

0PRP07-ZR-0033

Radiological Briefings

0PRP07-ZR-0034

Radiological Risk Management

Conduct of Operations for Radiation Protection, Chapter 18:

ALARA Planning

Audits and Self-Assessments

Number

Title

Date

18-15289-1

Snapshot Self-Assessment using NRC 71124, Att. 2

2/28/2019

MN-19-0-107465

Radiation Protection Department Annual Evaluation

2/26/2019

SOER 85-3/ SOER 01-1

Excessive Personnel Radiation Exposures; Unplanned

Radiation Exposures

2/05/2018

Radiation Work Permits

Number

Title

Revision

2018-1-296

1RE21 - Transfer Cart Repair in the FHB / RCB Fuel Transfer Canals

including RP Surveys and Decontamination

2018-1-296

1RE21 - Transfer Cart Repair in the FHB / RCB Fuel Transfer Canals

including RP Surveys and Decontamination

2018-2-129

2RE19 - Steam Generator-Primary Side Support and Equipment

Setup/Tear Down (HRA) - Medium Radiological Risk

2018-2-130

2RE19 - Steam Generator-Primary Side Manway/Inserts Removal

(LHRA) - High Radiological Risk

2018-2-131

2RE19 - Steam Generator-Primary Side Nozzle Dams (LHRA) - High

Radiological Risk

2018-2-131

2RE19 - Steam Generator-Primary Side Nozzle Dams (LHRA) - High

Radiological Risk

2018-2-132

2RE19 - Steam Generator-Eddy Current Testing (LHRA) - High

Radiological Risk

2018-2-133

2RE19 - Steam Generator-Re-Install Primary Side Manway (HRA) -

Medium Radiological Risk

2018-2-135

2RE19 - Steam Generator-Secondary Side Inspections (HRA)

ALARA In-Progress Reviews

Review

Number

Title

Date

249

Stud Detensioning

10/11/2018

250

HP Job Coverage

10/12/2018

ALARA In-Progress Reviews

Review

Number

Title

Date

254

HP Job Coverage in High Radiation Areas

10/21/2018

255

Request PMPI to provide craft support for the removal and

installation of mechanical snubbers per 0PMP04-SN-0001 in support

of snubber testing

10/22/2018

257

Contingency for Repairs to Unit 1 Fuel Handling Building Side Fuel

Transfer System

10/25/2018

259

Fuel Movement/Reactor Containment Building (RCB)

10/28/2018

ALARA Reviews

Number

Title

Date

18-276-4

ALARA Review: 2RE19 Snubber Inspections

03/02/2018

18-276-4

ALARA Close Out Review: 2RE19 Snubber Inspections

05/24/2018

18-276-8

ALARA Review: 2RE19 Steam Generator Inspections, Revision 1 04/04/2018

18-276-8

ALARA Close Out Review: 2RE19 Steam Generator Inspections

05/24/2018

18-7926-4

ALARA Review: 1RE21 Non-Rapid Refuel

10/02/2018

18-7926-5

ALARA Review: 1RE21 Flow Accelerated Corrosion Inspections -

In Service Inspections

09/12/2018

18-7926-6

ALARA Review: 1RE21 Room 003 Activities

09/26/218

19-234

ALARA Review: Dry Cask Storage

01/16/2019

19-234

ALARA Review: Initial DCS Campaign - Dry Cask Storage

Supplement 1

01/25/2019

Miscellaneous

Documents

Number

Title

Date

Refuel Outage 1RE20: ALARA Report

09/06/2017

Refuel Outage 2RE18: ALARA Report

05/18/2017

Refuel Outage 2RE19: ALARA Report

07/18/2018

71124.04Occupational Dose Assessment

Condition Reports

CR-2017-21141

CR-2018-2745

CR-2018-3052

CR-2018-4574

CR-2018-6875

CR-2018-8097

CR-2018-8247

CR-2018-10111

CR-2018-10591

CR-2018-10771

CR-2018-14460

CR-2018-14735

CR-2018-15144

CR-2019-1215

CR-2019-1254

Procedures

Number

Title

Revision

0PGP03-ZR-0048

Personnel Dosimetry Program

0PGP03-ZR-0050

Radiation Protection Program

0PRP02-ZR-0007

Evaluation of Intakes

0PRP02-ZR-0010

Personnel Exposure Investigation

0PRP02-ZR-0013

Determination of Skin Dose

0PRP02-ZR-0017

Dose to the Embryo/Fetus

0PRP02-ZX-0022

Non-Routine Dosimetry Issue and Control

0PTP04-ZC-0047

Calibration of the Siemens Environmental Systems Limited /

Thermo Electron Corporation Electronic Personal Dosimeter

Audits and Self-Assessments

Number

Title

Date

100555-0

Mirion Technologies (GDS), Inc. Onsite NVLAP Assessment Report 01/09/2018

Snapshot Assessment: Dosimetry Program 2018

2/04/2018

Snapshot Self-Assessment using NRC Inspection

Procedure 71124.04 Occupational Dose Assessment Criteria

2/19/2019

Personnel Exposure Records

2017-07

2017-28

2017-29

2017-30

2017-49

2018-08

2018-09

2018-10

2018-11

2018-23

2018-24

2018-35

2018-40

2018-41

2018-42

2018-43

2018-44

2018-45

71152-Issue Follow-up

Condition Reports

CR-2008-9639

CR-2019-893

CR-2019-1762

CR-2019-1954

CR-2019-2357

Work Authorization Numbers

335148

2175

576480

604273

606453

607307

Procedures

Number

Title

Revision

0PMP04-EW-0001A

Essential Cooling Water Pump Maintenance (Product-

Lubricated Bearing Design)

0POP02-EW-0001

Essential Cooling Water Operations

Miscellaneous

Documents

Number

Title

Revision

or Date

VTD-H127-0006

VSN Centrifugal Pump Installation and Operation

Manual

DCP 06-15147-45

Replace Essential Cooling Water Pump 2B

2/26/2009

4OA5.1 Other Activities (IP 60854, IP 60855, IP 60857)

Condition Reports

CR-2018-14418

CR-2018-14718

CR-201814770

CR-2019-540

CR-2019-630

CR-2019-631

CR-2019-665

CR-2019-706

CR-2019-816

Procedures

Number

Title

Revision

0PEP02-ZM-0012

Fuel Selection for Dry Cask Storage

0DCS03-ZO-0002

HI-STORM and MPC Pre-Use Inspections

0DCS03-ZO-0003

MPC Loading Operations

0DCS03-ZO-0004

MPC Closure Operations

0DCS03-ZO-0005

MPC Transfer Operations

0DCS03-ZO-0007

MPC Unloading Operations

0DCS03-ZO-0001

HI-STORM Transport Operations

0DCS03-ZO-0008

DCS Abnormal Response

PI-OP-HLTC-H-01

PCI Closure Welding of MPC Procedure

GQP - 9.2

PCI Liquid Penetrant Procedure

GQP - 9.6

PCI Visual Examination of Welds Procedure

0PGP03-ZX-0002

Condition Reporting Process

0PQP01-ZA-0003

Vendor Overview Activities (numerous)

0PRP07-ZR-0036

Radiological Controls for Dry Cask Storage

N/A

ALARA Review Package

0DCS01-ZA-0001

Dry Cask Storage Program Implementation

Procedures

Number

Title

Revision

0DCS02-ZN-0002

10CFR72.48 Screening and Evaluations

WPS 8 MN-GTAW

ASME Section XI Welding Procedure Specification

WPS 8 MC-GTAW

ASME Section XI Welding Procedure Specification

PI-CNSTER-OP-

HLTC-H-01

Closure Welding of Holtec Multi-Purpose Canisters

0PEP02-ZM-012

Fuel Selection for Dry Cask Storage

Design Basis

Documents

Number

Title

Revision

HI-2114830

Final Safety Analysis Report on the HI-STORM FW MPC

Storage System

N/A

Certificate of Compliance No. 1032

2.212

STP ISFSI 10 CFR 72.212 Report

Miscellaneous

Documents

Number

Title

Revision

or Date

2.48 Screen

Initial Issue of STP ISFSI 10 CFR 72.212 Report

2.48 Eval

Initial Issue of STP ISFSI 10 CFR 72.212 Report

2.48 Eval

Non-Mechanistic Tipover Analysis for STP

VTI B056404

Design Report Stainless Steel Gate Cask Channel

58171-14-107

Whiting Corp Seismic Analysis Derived Values for 150 ton

Crane

04/13/2015

5817-14-050

Seismic Analysis for STP 150 ton Crane

CC09978

FHB Crane Seismic Analysis Decoupling Evaluation

B05315-0005

Seismic Stability HI-STORM/HI-TRAC Stack-up at STP

B05315-0003

STP Low Profile Transporter Analysis

B05315-00062

Time History Generation for STP

B05315-00066

Dynamic Analysis of HI-TRAC in Cask Wash-down area

B05315-00068

Dynamic Analysis of HI-TRAC in Cask Loading Pool

B05315-00069

Structural evaluation of Cask Loading and wash-down

areas

B05315-00071

Structural evaluation of Cask Loading Pool Pedestal

B05315-00073

Structural analysis of FHB Truck Bay Slab

B05315-00076

Safety Analysis of VCT Stability and Structural Evaluation

Miscellaneous

Documents

Number

Title

Revision

or Date

N/A

CK0001 - Fuel Selection for Dry Cask Storage

08/30/2018

N/A

CK0002 - Fuel Selection for Dry Cask Storage

08/30/2018

N/A

CK0003 - Fuel Selection for Dry Cask Storage

08/30/2018

N/A

CK0004 - Fuel Selection for Dry Cask Storage

08/30/2018

N/A

CK0005 - Fuel Selection for Dry Cask Storage

08/30/2018

RRTI 2319-11R0

Response to Request for Technical Information

2/12/2019

50.59 Screen 13-

6991-1 Supp 5 & 13-

6991-2 Supp 6

Fuel Handling Building Cask Loading Pool (CLP) and

Cask Connecting Channel (CCC) Gate and Liner

Modification

2/27/2018

DCP 13-6991-1

Supp. 0

Design Report Stainless Steel Gate Cask Connecting

Channel

10/08/2015

WO No. 96009469

HI Storm Overpack #6

01/15/2019

G. Powell

The following items are requested for the

Occupational Radiation Safety Inspection

at South Texas Project

Dates of Inspection: 03/18/2019 to 03/22/2019

Integrated Report 2019001

Inspection areas are listed in the attachments below.

Please provide the requested information on or before Monday, March 04, 2019.

Please submit this information using the same lettering system as below. For example, all

contacts and phone numbers for Inspection Procedure 71124.02 should be in a file/folder titled

2-A, applicable organization charts in file/folder 2-B, etc.

The information should be provided in electronic format or a secure document management

service. If information is placed on a secured document management system, please ensure

the inspection exit date entered is at least 30 days later than the onsite inspection dates, so the

inspectors will have access to the information while writing the report.

In addition to the corrective action document lists provided for each inspection procedure listed

below, please provide updated lists of corrective action documents at the entrance meeting.

The dates for these lists should range from the end dates of the original lists to the day of the

entrance meeting.

If more than one inspection procedure is to be conducted and the information requests appear

to be redundant, there is no need to provide duplicate copies. Enter a note explaining in which

file the information can be found.

If you have any questions or comments, please contact Bernadette Baca at 817-200-1235 or via

e-mail at Bernadette.Baca@nrc.gov.

PAPERWORK REDUCTION ACT STATEMENT

This letter does not contain new or amended information collection requirements subject

to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.). Existing information

collection requirements were approved by the Office of Management and Budget,

control number 3150-0011.

2.

Occupational ALARA Planning and Controls (71124.02)

Date of Last Inspection:

March 26, 2018

A.

List of contacts and telephone numbers for ALARA program personnel, as well as the

Licensing/Regulatory Affairs staff. Please include area code and prefix. If work cell

numbers are appropriate, then please include them as well.

B.

Applicable organization charts including position or job titles. Please include as

appropriate for your site, Site Management, RP, Chemistry, Maintenance (I&C),

Engineering, and Emergency Protection. (Recent pictures are appreciated.)

C.

Copies of audits, self-assessments, LARs, and LERs, written since the date of last

inspection, focusing on ALARA

D.

Procedure index for ALARA Program procedures and other related disciplines.

E.

Please provide specific procedures related to the following areas noted below.

Additional Specific Procedures may be requested by number after the inspector reviews

the procedure indexes.

1. ALARA Program

2. ALARA Planning

3. ALARA Reviews

4. ALARA Committee

5. Radiation Work Permit Preparation

F.

Please provide a list of NRC Regulatory Guides and NUREGs that you are currently

committed to relative to this program. Please include the revision and/or date for the

commitment and where this may be located in your current licensing basis documents.

G.

Please provide a summary list of corrective action documents (including corporate and

sub-tiered systems) written since the date of last inspection, related to the ALARA

program, including exceeding RWP Dose Estimates.

NOTE: These lists should include a description of the condition that provides

sufficient detail that the inspectors can ascertain the regulatory impact, the

significance level assigned to the condition, the status of the action (e.g., open,

working, closed, etc.) and the search criteria used. Please provide in document

formats which are sortable and searchable so that inspectors can quickly and

efficiently determine appropriate sampling and perform word searches, as

needed. (Excel spreadsheets are the preferred format.) If codes are used,

please provide a legend for each column where a code is used.

H.

List of work activities (RWPs) greater than 1 rem, since date of last inspection,

including the original dose estimates and actual doses accrued. (Excel format

preferred). Please provide all revisions/changes, as well as any related RWPs that

support the work activity.

ML19128A334

SUNSI Review

ADAMS:

Non-Publicly Available

Non-Sensitive

Keyword:

By: NTaylor

Yes No

Publicly Available

Sensitive

NRC-002

OFFICE

SRI:DRP/B

RI:DRP/B

C:DRS/OB

C:DRS/IPAT

C:DRS/EB1

C:DRS/EB2

NAME

ASanchez

JChoate

GWerner

RKellar

VGaddy

JDrake

SIGNATURE

AAS

JMC

GEW

RLK

VGG

JFD

DATE

05/08/19

05/03/2019

04/30/2019

04/30/2019

04/30/2019

04/29/2019

OFFICE

C:DNMS/CHP

C:DRS/RCB

BC:DRP/B

NAME

GWarnick

NMakris

NTaylor

SIGNATURE

GXW

NJM

NHT

DATE

05/06/2019

4/29/19

5/8/19