IR 05000498/2019004

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Integrated Inspection Report 05000498/2019004 and 05000499/2019004
ML20029F018
Person / Time
Site: South Texas  STP Nuclear Operating Company icon.png
Issue date: 01/29/2020
From: Jeffrey Josey
NRC/RGN-IV/DRP/RPB-A
To: Gerry Powell
South Texas
References
IR 2019004
Preceding documents:
Download: ML20029F018 (40)


Text

January 29, 2020

SUBJECT:

SOUTH TEXAS PROJECT ELECTRIC GENERATING STATION, UNITS 1 AND 2-INTEGRATED INSPECTION REPORT 05000498/2019004 AND 05000499/2019004

Dear Mr. Powell:

On December 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at South Texas Project Electric Generating Station, Units 1 and 2. On January 23, 2020, the NRC inspectors discussed the results of this inspection with Ms. K. Harshaw, Vice President Regulatory Affairs and General Counsel, and other members of your staff. The results of this inspection are documented in the enclosed report.

Four findings of very low safety significance (Green) are documented in this report. Four of these findings involved violations of NRC requirements. One Severity Level IV violation without an associated finding is documented in this report. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at South Texas Project Electric Generating Station, Units 1 and 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at South Texas Project Electric Generating Station, Units 1 and 2.

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000498 and 05000499

License Numbers:

NPF-76 and NPF-80

Report Numbers:

05000498/2019004 and 05000499/2019004

Enterprise Identifier: 1-2019-004-0004

Licensee:

Facility:

Location:

Inspection Dates:

Inspectors:

Approved By:

STP Nuclear Operating Company

South Texas Project Electric Generating Station, Units 1 and 2

Wadsworth, TX 77483

October 1, 2019, to December 31, 2019

B. Baca, Health Physicist

J. Choate, Resident Inspector

K. Clayton, Senior Operations Engineer

R. Kopriva, Senior Reactor Inspector

J. O'Donnell, Health Physicist

A. Sanchez, Senior Resident Inspector

Jeffrey E. Josey, Chief

Reactor Projects Branch A

Division of Reactor Projects

Enclosure This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, "Public

Inspections, Exemptions, Requests for Withholding."

Docket Nos. 05000498 and 05000499

License Nos. NPF-76 and NPF-80

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

Sincerely,

Jeffrey E. Josey, Chief

Reactor Projects Branch A

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensee's performance by conducting an integrated inspection at South Texas Project Electric Generating Station, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRC's program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Report a Chanqe in Medical Condition of a Licensed Operator Cornerstone Significance Cross-Cutting Report Aspect Section Not Applicable NCV 05000499,05000498/2019004-01 Not Applicable 71111.11 B Open/Closed The inspectors identified a Severity Level IV non-cited violation of 10 CFR 55.25,

"Incapacitation Because of Disability or Illness," for the licensee's failure to notify the NRC within 30 days of a chanqe in a licensed operator's medical condition.

Failure to Perform a Risk Assessment Prior to Performing Maintenance Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green

[H.5] -Work 71152 NCV 05000498/2019004-02 Management Open/Closed The inspectors identified a Green finding and associated non-cited violation of 10 CFR 50.65(a)(4) when the licensee failed to perform a risk assessment prior to performing maintenance. Specifically, inspectors identified breaker relay calibrations being performed on protected equipment in Unit 1 during the 345kV North bus outage.

Inadequate Work Instruction Results in Loss of Spent Fuel Pool Cooling Cornerstone Significance Cross-Cutting Report Aspect Section Barrier Integrity Green

[H.8] -

71152 NCV 05000499/2019004-03 Procedure Open/Closed Adherence A self-revealed Green finding and associated non-cited violation of Technical Specification 6.8.1.a, Regulatory Guide 1.33, Section 9, was identified for the failure to provide adequate work instruction for maintenance associated with an emergency diesel generator sequencer and resulted in a loss of spent fuel pool cooling. Specifically, the licensee failed to identify the correct replacement part for the train C sequencer and once installed, resulted in a loss of all train C electrical loads, including the operating train of spent fuel pool cooling.

Inadequate Work Instructions Result in Reactor Coolant System Leaks Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green

[H.5] -Work 71152 NCV 05000499,05000498/2019004-04 Management

I Open/Closed I

I A self-revealed Green finding and associated non-cited violation of Technical Specification 6.8.1.a was identified for the failure to provide adequate work instruction for compression fitting connections that resulted in reactor coolant system leakage. Specifically, the licensee failed to provide adequate work instructions for reconnecting high-pressure RCS instrument tubing compression fittings. This resulted in RCS leaks which required a temporary modification and a high-risk work activity to stop the leaks that threatened stable plant operations.

Failure to Follow Procedure Results in Two Inoperable Emergency Diesel Generators Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green

[H.11] -

71152 Systems NCV 05000499,05000498/2019004-05 Challenge the Open/Closed Unknown A self-revealed Green finding and associated non-cited violation of Technical Specification 6.8.1.a, Regulatory Guide 1.33, Section 3.s.2.a, was identified for the failure to follow an emergency diesel generator (EOG) testing procedure, which resulted in two EDGs becoming inoperable at the same time. Specifically, the licensee failed to follow Procedure OPOP02-DG-0001, "Emergency Diesel Generator 11 (21 ), " Checklist 1,

"DG Standby Operation Checklist," Revision 70, Step 29.2, such that the train B EOG became inoperable while the train A EOG was inoperable.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 operated at or near rated thermal power for the entire period.

Unit 2 began the inspection period at 98 percent thermal power due to coast down operations.

On October 4, 2019, Unit 2 commenced rector shutdown to being refueling outage 2RE20 and entered Mode 3. Unit 2 entered Mode 1 on November 4, 2019, and reached rated thermal power on November 7, 2019. Unit 2 operated at or near rated power for the rest of the period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, "Light-Water Reactor Inspection Program - Operations Phase." The inspectors performed plant status activities described in IMC 2515, Appendix D, "Plant Status," and conducted routine reviews using IP 71152, "Problem Identification and Resolution." The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated readiness to cope with external flooding for the following areas:
  • Units 1 and 2 flood panels for component cooling water heat exchangers
  • Unit 1 reactor containment building
  • Electrical auxiliary building flood doors
  • Essential cooling water intake structure

71111.040 - Equipment Alignment Partial Walkdown Sample (IP Section 03.01 )

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1, train B essential chilled water system while train C was out of service for planned maintenance on December 16, 2019
(2) Unit 1, condenser air removal pumps 11 and 13 while condenser air removal pump 12 was out of service due to emergent maintenance on December 17, 2019
(3) Unit 2, train A component cooling water while train B was out of service for planned maintenance on December 18, 2019

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Unit 2, train C component cooling water, with train B out of service, while train C was relied upon for decay heat removal during the refueling outage on October 17, 2019.

71111.050 - Fire Protection Quarterly Inspection (IP Section 03.01 )

The inspectors evaluated fire protection program implementation in the following selected areas:

(1)

(2)

(3}

(4}

(5}

Unit 2, reactor containment building, Fire Area 63, on October 18, 2019 Unit 2, train A essential cooling water intake structure, Fire Area 58, on December 30, 2019 I

Unit 1, train A component cooling water, Fire Area 02 and 20, on December 30, 2019 Unit 1, train A essential cooling water intake structure, Fire Area 58, on December 31, 2019 Unit 2, train A component cooling water, Fire Area 02 and 20, on December 31, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) The inspectors evaluated internal flooding mitigation protections in Unit 2, train 8, 4160 volt switchgear room on November 20, 2019

71111.08P - lnservice Inspection Activities (PWR) PWR lnservice Inspection Activities Sample (IP Section 03.01 )

(1}

The inspectors verified that the reactor coolant system boundary, steam generator tubes, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing the following activities from October 15 to 28, 2019:

03.01.a - Nondestructive Examination and Welding Activities.

  • 1 - Magnetic Particle Examination
  • 2 - Dye Penetrant Examinations
  • 6 - Ultrasonic Examinations
  • 1 - Visual Examination r

On October 16, 2019, during Unit 2 refueling outage 2RE20, inservice inspections of the pressurizer 2A upper head safety nozzle N4C (nozzle designation per ISi Figure A-PRZ-1; see Attachment B) to shell weld discovered one ultrasonic testing (UT) indication. The subject indication was processed in accordance with Addendum 2 of Procedure OPGP04-ZE-0304 "lnservice Inspection Program for Welds and Component Supports." The indication was determined to be a

'

subsurface flaw and subsequently characterized within Ultrasonic Examination Reports UT-2019-031 and UT-2019-032. Article IWB-3000 of Section XI contains the criteria for the acceptance of flaws or other relevant conditions found during examination with the Acceptance Standards summarized within Table IWB-3410-1 "Acceptance Standards." For this particular location, this weld falls into Examination Category B-D (full penetration and welded nozzles in vessels); therefore, IWB-3512 acceptance standards apply. Using the flaw dimensions summarized above, and the Allowable Flaws given in Table IWB-3512-1, the flaw does not meet the acceptance standards for the aspect ratio calculated. Given this, the indication requires the use of IWB-3132.3 requiring an analytical evaluation per IWB-3600. Indications that are rejectable based on IWB-3500 can be evaluated per a detailed fracture mechanics evaluation based on IWB-3600 to demonstrate flaw acceptability.

By Letter LTR-SDA-19-095-P, Westinghouse has performed a detailed fracture mechanics evaluation in accordance with IWB-3612 and Non-Mandatory Appendix A, "Analysis of Flaws," and has shown that the indication found during 2RE20 inservice inspections is acceptable for at least 36 months (two full fuel cycles).

One gas tungsten arc welding activity was observed (control volume and chemical control system valve replacement under Work Orders 96017307 and 598944 for Weld Nos. RW0027 and FW0028).

03.01.b - Pressurized-Water Reactor Vessel Upper Head Penetration Examination Activities.

  • The bare metal visual inspection of the reactor vessel upper head penetrations was required to be performed during this outage, 2RE20. The inspector reviewed the following reactor head penetration visual examinations: penetration nozzles 1-9, 14-23, 25-27, 29-61, 66, 68, 70, 72, 75-78, including vent pipe and general head area. Also, a direct visual was performed in those areas that had limitations for the crawler. No concerns were identified.
  • The bare metal visual inspection of the bottom mounted instrumentation nozzles was performed during this outage, 2RE20. The inspector reviewed the following reactor head penetration visual examinations: Penetration nozzles 1-58. No concerns were identified.

03.01.c - Pressurized-Water Reactor Boric Acid Corrosion Control Activities.

  • The inspector reviewed the following documents associated with boric acid leaks and evaluations:
  • Evaluations: 17-18419-2, 18-11258-2, 18-6471, 19-7578-3, 19-7950
  • Corrective Actions: 19-10796, 19-10798, 19-11061, 19-11062, 19-11065, 19-11066, 19-11067, 19-11072, 19-11074, 19-11075, 19-11076, 19-11111, 19-11112, 19-11113, 19-11114, 19-11160, 19-11161, 19-11163, 19-11202, 19-11219, 19-11220, 19-11221, 19-11222, 19-11223,19-11224, 19-11225 03.01.d - Mechanical Stress Improvement Process used on Reactor Vessel Hot and Cold Leg Nozzle to Safe-End Welds.
  • During the 2019 Refueling Outage for Unit 2, 2RE20, the inspector witnessed the license's performance of mechanical stress improvement on the reactor vessel hot and cold leg nozzle to safe-end, dissimilar metal welds. This mechanical process helps prevent and mitigate primary water stress corrosion cracking in piping by minimally contracting the pipe on one side of the weldment, replacing residual tensile stresses with compressive stresses.

This removal of as-welded tensile stresses is an effective and permanent means to prevent or mitigate primary water stress corrosion cracking.

71111.11 B - Licensed Operator Requalification Program and Licensed Operator Performance Licensed Operator Requalification Program (IP Section 03.04)

(1) Biennial Requalification Written Examinations The inspectors evaluated the quality of the licensed operator biennial requalification written examination administered on August 5, 2019.

Annual Requalification Operating Tests The inspectors evaluated the adequacy of the facility licensee's annual requalification operating test.

Administration of an Annual Requalification Operating Test The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives.

Requalification Examination Security The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.

Remedial Training and Re-examinations The inspectors evaluated the effectiveness of remedial training conducted by the licensee, and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.

Operator License Conditions The inspectors evaluated the licensee's program for ensuring that licensed operators meet the conditions of their licenses.

Control Room Simulator The inspectors evaluated the adequacy of the facility licensee's control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.

Problem Identification and Resolution The inspectors evaluated the licensee's ability to identify and resolve problems associated with licensed operator performance.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated an operating crew annual exam on November 26, 2019.

===71111.11 Q - Licensed Operator Requalification Program and Licensed Operator Performance Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01 )

=

( 1 )

The inspectors observed a evaluated the performance of a Unit 1 operating crew while in an alternate 13.BkV bus alignment due to an emergent issue with the main generator output breaker preventing automatic trip of that breaker on December 11, 2019.

The inspectors observed and evaluated the performance of a Unit 1 operating crew during a high risk evolution to replace two power supplies in the train R solid state protection system on December 18, 2019.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01 } (3 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Units 1 and 2, essential cooling water systems on November 30, 2019
(2) Units 1 and 2, component cooling water system on December 30, 2019
(3) Units 1 and 2, emergency safeguards sequencer on December 30, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01 ) (4 Samples}

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 2, planned risk due to train C essential cooling water, essential chilled water, emergency core cooling, containment spray, and emergency diesel generator maintenance the week of October 1, 2019
(2) Unit 2, emergent risk due to train C engineered safety feature load sequencer requiring a card replacement on October 28, 2019
(3) Unit 2, emergent risk due to train A engineered safety feature load sequencer failure during a large train B work week and resulted in the use of the Configuration Risk Management Program on November 20, 2019
(4) Units 1 and 2, planned risk due to the maintenance on the 345kV south bus and Unit 2, standby transformer and use of the Configuration Risk Management Program the week of December 4, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (6 Samples}

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2, turbine-driven auxiliary feedwater governor stem nut missing on October 21, 2019
(2) Unit 1, train A essential chilled water due to a degraded temperature control module that failed to keep the output temperature less than 48 degrees Fahrenheit on November 8, 2019
(3) Unit 2, damaged control room envelope door on November 11, 2019
(4) Unit 2, train B emergency diesel generator jacket water leak on November 14, 2019
(5) Unit 1, train A essential cooling water due to a through wall indication on flange EW-1006 due to aluminum bronze dealloying phenomenon on November 20, 2019
(6) Unit 2, train C high head safety injection pump bearing oil level indicator installed upside down following motor replacement on November 27, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(3 Samples}

The inspectors evaluated the following temporary or permanent modifications:

(1) Units 1 and 2, temporary diesel-driven fire pump during repair and replacement of diesel-driven fire pump components on April 15, 2019
(2) Unit 2, temporary modification to power spent fuel pool cooling pump 2A during refueling outage 2RE20 on October 18, 2019
(3) Units 1 and 2, permanent modification to install a quick exhaust valve to reduce the time required to close the valve on a main steam actuation signal on December 31, 2019

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01 ) (4 Samples)

The inspectors evaluated the following post maintenance tests:

( 1)

Unit 2, local leak rate test of the auxiliary containment airlock following maintenance on the sealing surfaces on October 24, 2019

.

(2) Unit 2, local leak rate test of the normal containment purge exhaust isolation damper, 2-HC-9, following emergent maintenance following a failed local leak rate test on October 27, 2019
(3) Unit 2, nuclear instrumentation Nl-35 following the replacement of the log amplifier module on November 3, 2019
(4) Unit 1, reactor coolant system leak check and flow transmitter FT-0419 following the replacement of the reactor coolant system instrument tubing due to an increasing leak on December 6, 2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample {IP Section 03.01 ) (1 Sample)

( 1)

The inspectors evaluated refueling outage 2RE20 activities from October 4 through November 5, 2019.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01 )

(1) Unit 1, train C essential cooling water pump surveillance test on December 14, 2019
(2) Unit 1, train C emergency diesel generator monthly surveillance test on December 17, 2019
(3) Unit 1, train C auxiliary feedwater pump surveillance test on December 18, 2019

FLEX Testing (IP Section 03.02) (1 Sample)

(1) Unit 1, FLEX diesel generator surveillance test on December 12, 2019

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample}

(1) The licensee submitted "South Texas Project Emergency Plan," Revision ICN 20-21, as well as a copy of Revision ICN 20-22, to the NRC on August 8, 2019. The inspectors conducted an in-office review of the changes from November 13 to November 25, 2019. This evaluation does not constitute NRC approval.

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 02.01 ) (1 Sample)

The inspectors evaluated radiological hazards assessments and controls.

(1}

The inspectors reviewed the following:

Radiological Surveys

  • Spent Fuel Pool Cell Inventory
  • Concentrate Transfer Pump 1 B
  • Fuel Transfer Tube Access
  • Radwaste Truck Bay
  • Reactor Cavity Walkway Risk Significant Radiological Work Activities
  • In-Core (Thimble Tube)
  • Head Lift

===22373

  • 21434
  • 21441
  • 21468
  • 21505 Instructions to Workers (IP Section 02.02)===

The inspectors evaluated instructions to workers including radiation work permits used to access high radiation areas.

(1) The inspectors reviewed the following:

Radiation Work Packages

  • 2019-2-0165, 2RE20 - Maintenance and Support Work - Room 307 (LHRA)
  • 2019-2-0173, 2RE20 - Maintenance on N2CVPSV3100 (LHRA)
  • 2019-2-0158, 2RE20 - Reactor Head Lift Activities (LHRA)

Electronic Alarming Dosimeter Alarms

  • Dose Rate Alarm - 18-04050
  • Dose Rate Alarm -18-04757
  • Dose Rate Alarm - 18-11562
  • Dose Rate Alarm -18-12585 Labeling of Containers
  • Box 300437
  • Radwaste Bags
  • 55 Gallon Barrel
  • Box #20-2466
  • OSSC#26

Contamination and Radioactive Material Control (IP Section 02.03) (1 Sample)

The inspectors evaluated licensee processes for monitoring and controlling contamination and radioactive material.

(1) The inspectors verified the following sealed sources are accounted for and are intact:
  • MS-0042
  • MS-0132
  • NAM-1335
  • NCF-0604
  • NCS-0008

Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)

The inspectors evaluated in-plant radiological conditions during facility walkdowns and observation of radiological work activities.

(1) The inspectors also reviewed the following radiological work package for areas with airborne radioactivity:
  • Unanticipated airborne radioactivity during 2RE20 flood-up o

RWP 2019-2-0158, 2RE20- Reactor Head Lift Activities (LHRA)o ALARA Review Package 19-3165-7, 2RE20 Non-Rapid Refuel o

DAC-hr Assessment for Condition Report 19-11442 High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample)

(1) The inspectors evaluated risk-significant high radiation area and very high radiation area controls.

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP

Section 02.06) (1 Sample)

(1) The inspectors evaluated radiation worker performance and radiation protection technician proficiency.

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Engineering Controls (IP Section 02.01 ) (1 Sample)

The inspectors evaluated airborne controls and radioactive monitoring.

( 1 )

The inspectors reviewed the following :

Installed Ventilation Systems

  • Radwaste sorting vent hoods and associated HEPA units
  • Reactor head HEPA units Portable or Installed Monitoring Systems
  • Room specific AMS-4 units: Radwaste sorting room and seal table (thimble)room
  • General containment monitoring with AMS-4
  • Low volume filter air samples covering reactor head, cavity, and thimble work

Use of Respiratory Protection Devices (IP Section 02.02) (1 Sample)

The inspectors evaluated the licensee's use of respiratory protection devices by:

( 1)

Observing in-field applications; verifying the licensee validated the level of protection provided by the devices; inspecting the material condition of devices, reviewing records and certification of devices issued for use; reviewing the qualifications of workers that use the devices; and observing workers' donning, doffing and testing devices.

Self-Contained Breathing Apparatus for Emergency Use (IP Section 02.03) (1 Sample)

The inspectors evaluated self-contained breathing apparatus program implementation.

(1) The inspectors reviewed the following:

Status and Surveillance Records for Self-Contained Breathing Apparatus

  • SCBA kit #551 Self-Contained Breathing Apparatus Fit for On-Shift Operators The inspectors selected two on-shift Unit 2 reactor operators for verification of fit testing, medical approval, donning/doffing practical, and bottle change out protocol.

Self-Contained Breathing Apparatus Maintenance Check

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS09: Residual Heat Removal Systems (IP Section 02.08)===

(1) Unit 1, October 1, 2018, through September 30, 2019
(2) Unit 2, October 1, 2018, through September 30, 2019

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1, October 1, 2018, through September 30, 2019
(2) Unit 2, October 1, 2018, through September 30, 2019

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) January 1, 2018, through September 30, 2019 PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)
(1) January 1, 2018, through September 30, 2019

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

( 1)

The inspectors reviewed the licensee's corrective action program for potential adverse trends that might be indicative of a more significant safety issue.

Annual Follow-up of Selected Issues (IP Section 02.03) (4 Samples)

The inspectors reviewed the licensee's implementation of its corrective action program related to the following issues:

(1) The increase in the number of reactor coolant system leaks for high pressure compression fitting leading to reactor coolant system loop flow transmitters in Units 1 and 2
(2) The failure to assess risk prior to performing maintenance on protected 13.8kV supply breaker to the train B 4.16kV switchgear while the 345kV North bus and the Unit 1 standby transformer were out of service for planned maintenance
(3) Inadequate work instruction on Unit 2, train C engineered safety feature load sequencer results in the loss of spent fuel pool cooling
(4) The Unit 1, train B emergency diesel generator was rendered inoperable by a human performance error

INSPECTION RESULTS

Failure to Report a Change in Medical Condition of a Licensed Operator Cornerstone Severity Cross-Cutting Not Applicable Severity Level IV NCV 05000499,05000498/2019004-01 Open/Closed Aspect Not Applicable Report Section 71111.11 B The inspectors identified a Severity Level IV non-cited violation of 10 CFR 55.25, "Incapacitation Because of Disability or Illness," for the licensee's failure to notify the NRC within 30 days of a change in a licensed operator's medical condition.

Description:

On June 19, 2014, a senior reactor operator self-reported to the site medical department the diagnosis of a new medical condition. The licensee recorded the new medical condition in the operator's site medical record and drafted a new NRC Form 396 to report a "no solo". condition was being added on the license. The new Form 396 was lost in the review and approval process on site, and at the time there was not a tracking mechanism in place to ensure the review and approval process was completed. As a result, the new Form 396 was never provided to the NRC.

While reviewing a license renewal application, an inspector identified that a "no solo" restriction that had not previously been reported to the NRC was included on the NRC Form 396 that was submitted with the license renewal application. The NRC notified the licensee of the discrepancy on October 8, 2019. The licensee confirmed that site records reflected a "no solo" condition had been added for the individual. The licensee determined that the senior reactor operator had not been on shift since the condition was reported in 2014.

Corrective Actions: On October 17, 2019, the South Texas Project Nuclear Operating Company submitted a letter to the NRC with a revised NRC Form 396, "Certification of Medical Examination by Facility Licensee," that prohibited solo operation of the controls. The "no solo" condition was required for fitness-for-duty reasons in accordance with the American National Standards Institute (ANSl)-3.4-1983, "Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants,"

Corrective Action References: Condition Report 2019-11414

Performance Assessment:

The inspectors determined this violation was associated with a minor performance deficiency.

Enforcement:

The ROP's significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation which impedes the NRC's ability to regulate using traditional enforcement to adequ~tely deter non-compliance.

Severity: The inspectors determined the violation to be a Severity Level IV violation, similar to Example 6.4.d.1.b in the NRC Enforcement Policy because it was a nonwillful compromise of an examination required by 10 CFR Part 55. Specifically, the licensee nonwillfully failed to inform the NRC of a change in an operator's medical condition. The individual did not perform the functions of a senior reactor operation while having a disqualifying medical condition.

Violation: Title 10 CFR 55.25 requires, in part, that if a licensed senior reactor operator develops a permanent physical condition that causes the licensee to fail to meet the requirements of 10 CFR 55.21, the facility shall notify the Commission within 30 days of learning of the diagnosis. For conditions where a license condition is required, the facility licensee must provide medical certification on NRC Form 396, "Certification of Medical Examination by Facility Licensee." Contrary to the above from June 9, 2014, to October 17, 2019, the licensee failed to notify the Commission, within 30 days of learning the diagnosis of a change in medical condition of a licensed senior reactor operator that developed a permanent physical condition that caused the licensed senior reactor operator to fail to meet the requirements of 10 CFR 55.21. Specifically, on June 9, 2014, a senior reactor operator self-reported a new medical condition, the medical department determined that the individual required a "no solo" condition on his license, but the NRC did not receive the revised NRC Form 396 until October 17, 2019.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Perform a Risk Assessment Prior to Performinq Maintenance Cornerstone Significance Cross-Cutting Initiating Events Green NCV 05000498/2019004-02 Open/Closed Aspect

[H.5]-Work Management The inspectors identified a Green finding and associated non-cited violation Report Section 71152 of 10 CFR 50.65(a)(4) when the licensee failed to perform a risk assessment prior to performing maintenance. Specifically, inspectors identified breaker relay calibrations being performed on protected equipment in Unit 1 during the 345kV North bus and Unit 1 standby transformer planned maintenance.

Description:

The South Texas Project 345kV switchyard consists of two 345kV buses, North and South. Each of the buses in the switchyard supplies offsite power to the Units 1 and 2 standby transformers. These transformers constitute an offsite power source. On April 30, 2018, while the North bus and the Unit 1 standby transformer were out of service for planned maintenance activities, which placed the station in the configuration risk management program, the inspectors performed a walkdown of the protected equipment due to the maintenance. Specifically, the inspectors walked down all protected electrical power supplies, including the 13.8kV Standby bus in Unit 1. There, inspectors discovered two electricians performing relay calibrations on the 13.8kV standby bus 1 G to the 4.16kV Aux EAB XFMR E 1 B breaker. The inspectors determined that the work could have resulted in a trip of the breaker and would present a loss of offsite power to the train B 4.

16kV switchgear which would result in an auto start signal to the train B emergency diesel generator. The inspectors observed the work activity for a while to ensure the activity was being performed with quality before heading to the work start desk to inquire why the work was allowed to take place.

The inspector asked if the work start personnel were aware of the current plant condition and the heightened level of awareness for protected equipment due to the maintenance and why the observed relay work was approved. The work start personnel stated that it was in the approved work schedule, so permission was granted. The inspector then spoke with the work week coordinator and presented the situation observed. The work week coordinator stated that the work should not have been given permission to start and that the work activity should not be on the schedule. It had somehow been missed in the work schedule scrub for the work week for the given plant condition. The work week coordinator initiated Condition Report 2018-6019.

The licensee determined that the relay calibration for the supply breaker should not have been allowed and should not have been on the schedule. The work planning schedule reviews (multiple reviews) by maintenance, engineering, planning, and operations failed to identify and remove the activity from the schedule.

Corrective Actions: The licensee held discussions with work control specifically to inform them of the condition report, the NRC observation, and stressed the need to thoroughly review work during the work planning process.

Corrective Action References: Condition Report 2018-6019

Performance Assessment:

Performance Deficiency: The failure to perform a risk assessment prior to performing maintenance activities was a performance deficiency. Specifically, the licensee failed to perform a risk assessment prior to allowing relay work on the Unit 1 13.8kV standby bus 1 G to 4.16kV Aux EAB XFMR E1 B (train B 4.16kV switchgear) while these components were protected for 345kV North bus and Unit 1 standby transformer planned maintenance.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the human performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the failure to perform a risk assessment on the relay calibration activity prevented proper controls to be implemented if the work activity was deemed necessary, as such the licensee unknowingly increased the likelihood of upsetting the stability of the plant.

Significance: The inspectors assessed the significance of the finding using Appendix K, "Maintenance Risk Assessment and Risk Management SDP." In accordance with Step 4.1.1, "Licensee Evaluation of Risk," the inspectors reviewed the licensee's risk evaluation that indicated no additional numerical risk as a result of the additional maintenance activity because the activity was not intended to open the associated breaker. The licensee's risk assessment tools do not include an increase in the probability that equipment being worked on will be lost from a postulated maintenance error. Given this notable limitation with the licensee's configuration risk assessment tool, the inspectors requested the regional senior reactor analyst to independently evaluate the risk. The analyst evaluated the bounding risk related to a loss of offsite power to Bus E1 B. The analyst determined this failure would not result in a plant transient and would not affect the other two Unit 1 trains being supplied by offsite power. The analysis indicated that the availability of other redundant trains, emergency onsite power, and the short period of time that offsite power would have been unavailable given a maintenance error, resulted in a very low risk deficit (incremental core damage probability). Therefore, this finding is of very low safety significance (Green).

Cross-Cutting Aspect: H.5 - Work Management: The organization implements a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. Specifically, the licensee failed to implement the process of planning, controlling and executing work activities such that nuclear safety is the overriding priority. The work control process did not identify and manage the risk for the 13.8kV standby bus 1 G breaker to the 4.16kV Aux EAB XFMR EIB relay work activity.

Enforcement:

Violation: Title 10 CFR 50.65 (a)(4) states, in part, "before performing maintenance activities, the licensee shall assess and manage the increase in risk that may result from the proposed maintenance activiti~s... " Contrary to the above, on April 30, 2018, before performing maintenance, the licensee failed to assess and manage the increase in risk that may result from proposed maintenance activities. Specifically, the inspectors discovered that the licensee performed relay calibration maintenance activities on the Unit 1, 13.8kV standby bus 1 G to 4.16kV Aux EAB XFM R E 1 B (train B 4.16kV switchgear) without a risk assessment as required by 10 CFR 50.65(a)(4).

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Inadequate Work Instruction Results in Loss of Soent Fuel Pool Cooling Cornerstone Significance Cross-Cutting Aspect Barrier Integrity Green

[H

.8 ] -

NCV 05000499/2019004-03 Procedure Ooen/Closed Adherence,

Report Section 71152 A self-revealed Green finding and associated non-cited violation of Technical Specification 6.8.1.a, Regulatory Guide 1.33, Section 9, was identified for the failure to provide adequate work instruction for maintenance associated with an engineered safety feature load sequencer and resulted in a loss of spent fuel pool cooling. Specifically, the licensee failed to identify the correct replacement part for the train C engineered safety feature load sequencer, and once installed resulted in a loss of all train C electrical loads, includinq the operatinq train of spent fuel pool coolinq.

Description:

On October 24, 2019, Unit 2 was in Mode 6 coming out of the refueling outage with the core reloaded and one of two trains of spent fuel pool cooling in service when an annunciator in the control room indicated an issue with the train C engineered safety feature load sequencer. Work Planning developed a work order to remove and replace opto-isolators in the sequencer as part of troubleshooting. Work Planning wrote the work order procedure and ordered the parts from the warehouse to be delivered to the craft in their shop but used the wrong stock code. Per the vendor drawings, opto-isolator model 0DC-24A was supposed to be used (stock code 596-849). Instead, the work order and parts order referenced stock code 596-775 which is for opto-isolator model ODC-24. While the two models appear very similar, 0DC-24A allows an output of 125VDC while the ODC-24 allows only 24VDC.

Instrumentation and control technicians went to the sequencer to replace the opto-isolators as part of troubleshooting. When they removed the original opto-isolators (0DC-24A), the technicians noted the "A" on the original components which were not present on their replacements (ODC-24). Neither of the technicians could recall what the "A" represented, and the work order did not explicitly provide the opto-isolator model (0DC-24A vs. ODC-24),only the stock code which is not printed on the actual parts. The technicians installed the replacement opto-isolator into the enqineered safety feature load sequencer and the sequencer immediately shed all electrical loads from the train C electrical bus. With the train C EDG in pull-to-stop for the sequencer troubleshooting, all train C electrical loads were lost including the single train of spent fuel pool cooling that was in operation at the time.

Annunciators in the control room alerted operators the loads on the train C electrical bus were lost, and one of those loads was spent fuel pool cooling. Operators restored spent fuel pool cooling within 30 minutes with no rise in spent fuel pool water temperature. Operators took the train C EDG out of pull-to-stop the EDG automatically started and loaded the bus without issue. The core never lost residual heat removal as trains A and B were in service at this time. The licensee made an 8-hour report to the NRG on October 25, 2019, at 3:24 a.m. for a valid engineered safety feature actuation signal (Event Notification 54351 ).

The licensee initiated Condition Report 2019-12401 to investigate the event. The apparent cause determined that work control failed to provide adequate work instruction by identifying the wrong part to be installed jn the Unit 2, train C engineered safety feature load sequencer.

The licensee determined that the planners failed to use a reference Procedure, WCG-0003, "Planner's Guide," Revision 39, that would have required this issue to be elevated to an emergent issue requiring multiple stakeholders to meet to review the planned work.

Furthermore, the cause evaluation determined that maintenance technicians failed to follow the maintenance conduct of operations procedure and compare parts and stop work if there are any discrepancies.

Corrective Actions: The licensee counseled the technicians and work planners involved and a lessons learned document was written and discussed with planning and maintenance. The licensee has also included this event as a case study for their mechanical maintenance training with an emphasis on verifying like-for-like parts.

Corrective Action References: Condition Reports 2019-12372 and 2019-12401

Performance Assessment:

Performance Deficiency: The failure to provide adequate work instruction for maintenance associated with an engineered safety feature load sequencer, which resulted in a loss of spent fuel pool cooling, was a performance deficiency. Specifically, the licensee failed to identify and incorporate accurate component information when planning work on the train C engineered safety feature load sequencer.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the SSC performance attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, the failure to properly pre-plan and perform maintenance on the train C engineered safety feature load sequencer caused a loss of all electrical loads associated with the train C electrical bus. As a result, the single operating train of spent fuel pool cooling was lost.

Significance: The inspectors assessed the significance of the finding using Appendix A, "The Significance Determination Process (SDP) for Findings At-Power." Specifically, the finding did not cause the spent fuel pool (SFP) temperature to exceed its maximum analyzed temperature limit, did not result in a detectible release of radionuclides, did not result in a loss of SFP water inventory below the SFP's minimum analvzed level limit, and did not affect the SFP neutron absorber, fuel bundle loading pattern, or soluble boron concentration; therefore, the findings were determined to be of very low safety significance, Green.

Cross-Cutting Aspect: H.8 - Procedure Adherence: Individuals follow processes, procedures, and work instructions. Specifically, work planning failed to follow appropriate procedures to ensure multi-discipline participation to determine a proper plan of action and in assembling adequate work instructions to repair the Unit 2, train C engineered safety feature load sequencer without challenqing the plant equipment.

Enforcement:

Violation: Technical Specification 6.8.1.a, requires, in part, that written procedures shall be established, implemented, and maintained in accordance with Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Section 9 of Appendix A to Regulatory Guide 1.33, Revision 2, requires that "maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances."

Contrary to the above on October 24, 2019, the licensee failed to properly pre-plan maintenance that can affect the performance of safety-related equipment. Specifically, the licensee failed to identify and request the correct replacement parts for the Unit 2, train C engineered safety feature load sequencer. As a result, Unit 2, lost all train C electrical loads, including the single operating train of spent fuel pool cooling.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Inadequate Work Instructions Result in Reactor Coolant System Leaks Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green

[H.5] -Work 71152 NCV 05000499,05000498/2019004-04 Management Open/Closed A self-revealed Green finding and associated non-cited violation of Technical Specification 6.8.1.a was identified for the failure to provide adequate work instruction for compression fitting connections that resulted in reactor coolant system (RCS) leakage. Specifically, the licensee failed to provide adequate work instructions for reconnecting high-pressure RCS instrument tubing compression fittings. This resulted in RCS leaks which required a temporary modification and a high-risk work activity to stop the leaks that threatened stable plant operations.

Description:

At South Texas Project, each RCS primary loop has three independent flow transmitters that would input into the reactor protection system to trip the reactor if 2 out of 3 flow transmitters in a single loop were to read less than 92 percent. Per Technical Specification 3.3.1, each channel could be bypassed for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> then the channel would have to be restored or placed into a "Trip" condition.

On August 29, 2018, Unit 2, field operators inside containment identified an active RCS leak at RCS flow transmitter RC-FT-0428 (loop B flow transmitter). Specifically, the leak was almost a steady stream of fluid, apparently emanating from a tubing fitting. Condition Report 2018-10183 was written to note the deficiency. Later that year, a temporary modification was installed to encapsulate the leaking tube fitting and injected with leak stop until the leak was arrested. Operations installed a camera to periodically monitor the leak for degradation. The modification was planned to be removed, and tubing and fittings replaced during the next Unit 2, refueling outage in October 2019.

On November 14, 2018, Unit 1 field operators inside containment identified an active RCS leak at RCS flow transmitter RC-FT-0419 (loop A flow transmitter). Specifically, the leak was approximately a two-foot steam plume. Condition Report 2018-13993 was written to note the deficiency. The licensee gained alignment to tighten the tubing connection, which was a high-risk work activity. The tubing connection was successfully tightened, which reduced the steam plume to several milliliters per minute leak. Operations installed a camera to periodically monitor the leak for degradation. In addition, operations collected actual leak rates from this tube connection. Due to the tubing configuration, a temporary modification to install an encapsulating box as was done for the loop B flow transmitter was not feasible and would have to be repaired in the next Unit 1, refueling outage in March 2020. However, prior to the refueling outage, the leak began to get worse and engineering was tasked with developing a repair solution. On December 6, 2019 the licensee successfully replaced the leaking connection and tubing while at 100 percent power without perturbating the Unit. This was a high-risk evolution that could have resulted in a reactor trip.

On November 24, 2018, Unit 1 operators identified that RCS flow transmitter RC-FT-0449 (loop D flow transmitter) would periodically exceed its three percent channel checks with the other two loop D flow transmitters, RC-FT-0447 and RC-FT-0448. Condition Report 2018-14266 was written to document the deficiency. It was determined that the flow transmitter RC-FT-0449 was over ranged following a repair of a fitting leak identified at the end of the refueling outage, while in Mode 3. This issue would have to be addressed in the next Unit 1, refueling outage in March 2020.

The licensee initiated Condition Report 2018-14369 to evaluate the current trend of RCS tubing compression fitting leaks as well as search for tubing leaks for the last four refueling outages. The licensee's evaluation identified approximately 44 compression fitting issues dating back to 2015. The common cause concluded that the leaks were a result of improper assembly of Parker CPI compression fittings due to inadequate guidance in procedure OPGP03-ZE-0056, "Instrumentation Installation," Addendum 7, "Installation Instructions for Compression Fittings." In addition, the licensee determined that there was inconsistent work instruction rigor for re-making these fittings in maintenance packages and some relied on skill of the craft. It was also determined that the procedure did not incorporate vendor recommendations on reassembly and did not use proper gages and other reassembly tools.

Corrective Actions: The licensee enhanced procedure OPGP03-ZE-0056, 'Tubing and Instrumentation" to reflect vendor recommendations for reassembly and the use of proper tools. Training was identified and implemented to those maintenance workers who have this certification. Lastly, the licensee revised portions of the procedure to "in-hand" use to ensure compliance.

Corrective Action References: Condition Reports 2018-10183, 2018-13993, 2018-14266, and 2018-14369.

Performance Assessment:

Performance Deficiency: The failure to provide adequate work instruction for reassembly of tubing compression fittings was a performance deficiency. Specifically, maintenance activities of installing and reinstalling Parker tubing compression fittings without adequate guidance resulted in repetitive RCS tubing leaks, which challenged stable plant operations.

Screening: The performance deficiency was determined to be more than minor because it was associated with the equipment performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.

Specifically, the failure to provide adequate work instructions to repair, remake, replace Parker tubing compression fittings, resulted in RCS tubing leaks and instrument inaccuracies that unduly challenged stable plant operations and high risk work evolutions to mitigate and repair during the operational cycle.

Significance: The inspectors assessed the significance of the finding using Appendix A, "The Significance Determination Process (SOP) for Findings At-Power." Specifically, the finding (1 )could not result in exceeding RCS leak rate for a small LOCA;

(2) could not have affected other systems used to mitigate a LOCA (LOCA Initiator); and
(3) did not cause a reactor trip and the loss of mitigating equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition (Transient Initiators), therefore, the finding was determined to be of very low safety significance, Green.

Cross-Cutting Aspect: H.5 - Work Management: The organization implements a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. Specifically, the work planning organization failed to ensure that quality work instruction products were provided to the workforce to execute activities such that nuclear safety was the overriding priority.

Enforcement:

Violation: Technical Specification 6.8.1.a, requires in part, that written procedures shall be established, implemented, and maintained in accordance with Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Section 9, "Procedures for Performing Maintenance,"

of Appendix A to Regulatory Guide 1.33, Revision 2, requires, in part, that maintenance that can affect the performance of safety-related equipment should be properly pre planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. The licensee established procedure OPGP03-ZE-0056, "Instrumentation Installation," Addendum 7, "Installation Instructions for Compression Fittings," to meet that requirement for installing compression fitting on safety-related, reactor coolant system tubing connections. Contrary to the above, from March 23, 2015 to August 14, 2019, the licensee failed provide adequate work instructions to properly install compression fittings on safety-related reactor coolant system tubing connections. As a result, multiple leaks were discovered on both units which challenged stable plant operations.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Follow Procedure Results in Two Inoperable Emerqencv Diesel Generators Cornerstone Significance Cross-Cutting Report Mitigating Systems Aspect Section Green

[H.11]-

71152 NCV 05000499,05000498/2019004-05 Challenge the Open/Closed Unknown A self-revealed Green finding and associated non-cited violation of Technical Specification 6.8.1.a, Regulatory Guide 1.33, Section 3.s.2.a, was identified for the failure to follow an emergency diesel generator (EOG) testing procedure, which resulted in two EDGs becoming inoperable at the same time. Specifically, the licensee failed to follow procedure OPOP02-DG-0001, "Emergency Diesel Generator 11(21)," Checklist 1, "DG Standby Operation Checklist," Revision 70, Step 29.2, such that the train B EOG became inoperable while the train A, EOG was inoperable.

Description:

Unit 1 at South Texas Project has three trains of EDGs. On May 23, 2019, operations personnel began restoring the train A, EDG following planned maintenance using OPOP02-DG-0001, "Emergency Diesel Generator 11 (21 )," Checklist 1, "DG Standby Operation Checklist," Revision 70. A non-licensed operator was sent to the train A, EOG local panel to perform step 29.2, which states "DEPRESS both 'EMERGENCY STOP CIRCUIT' RESET pushbuttons." However, the non-licensed operator inadvertently went to the train B, EOG local panel, depressed the "STOP" pushbuttons after depressing the "RESET" pushbuttons, and did not receive an expected response. The control room immediately received unexpected alarms indicating a malfunction with the starting circuit for the train B, EDG and causing the EOG to become inoperable. With both the trains A and B, EDGs inoperable, Unit 1 entered Technical Specification 3.8.1.1.e with a 24-hour LCO action statement to restore at least one inoperable EOG to operable status, or apply the requirements of the Configuration Risk Management Program, or be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

The control room staff immediately investigated the unexpected alarms and identified that the issue with the starting circuit for the train B EOG was the result of human error. Another non-licensed operator restored the starting circuit for the train B EOG. The control room declared the train operable within 30 minutes of the train being made inoperable, exiting the 24-hour LCO action statement.

Corrective Actions: Operations counseled the non-licensed operator and issued a site wide Lessons Learned emphasizing the importance of taking the correct action on the correct train.

Corrective Action References: Condition Report 2019-5842

Performance Assessment:

Performance Deficiency: The failure to implement maintenance procedures involving safety-related equipment was a performance deficiency. Specifically, a non-licensed operator failed to implement procedure OPOP02-DG-0001, "Emergency Diesel Generator 11 (21 )," on the correct EOG train and failed to manipulate the correct pushbuttons on the EOG local panel.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable conseauences. Specificallv, the failure to implement maintenance procedures involving the emergency diesel generators caused a second train of EOG to be made inoperable. As a result, on May 23, 2019, Unit 1 entered into an unplanned 24-hour shutdown action statement for both train A and B emergency diesel generators being inoperable.

Significance: The inspectors assessed the significance of the finding using Appendix A, "The Significance Determination Process (SOP) for Findings At-Power." Specifically, the finding did not cause an actual loss of function of at least a single train for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The train B emergency diesel generator was restored to operable within 30 minutes.

Cross-Cutting Aspect: H.11 - Challenge the Unknown: Individuals stop when faced with uncertain conditions. Risks are evaluated and managed before proceeding. Specifically, the non-licensed operator failed to stop after depressing the "RESET pushbuttons on the emergency diesel generator local panel and not receiving an expected response. Operations also failed to evaluate and manage the risk of sending a newly qualified non-licensed operator to perform a first-time evolution without supervision or assistance.

Enforcement:

Violation: Technical Specification 6.8.1.a, requires, in part, that written procedures shall be established, implemented, and maintained in accordance with Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Section 3.s.2.a of Appendix A to Regulatory Guide 1.33, Revision 2, requires, in part, that instructions for energizing, startup, shutdown, and changing modes of operation should be prepared for emergency power sources (e.g.,

diesel generators). The licensee established OPOP02-DG-0001, "Emergency Diesel Generator 11 (21 }," Revision 70, to meet the Regulatory Guide 1.33 requirement. Checklist 1, "DG Standby Operation Checklist," step 29.2 of the OPOP02-DG-0001 procedure states, "DEPRESS both 'EMERGENCY STOP CIRCUIT' RESET pushbuttons." Contrary to the above, on May 23, 2019, a non-licensed operator depressed both "EMERGENCY STOP CIRCUIT" RESET pushbuttons for the incorrect EOG train and depressed an additional set of pushbuttons after not receiving the expected response from the RESET pushbuttons.

Specifically, the licensee depressed the RESET and STOP pushbuttons for the Unit 1, train B EOG. As a result, the train B, EOG was made inoperable during a time period where train A, EOG was inoperable for maintenance, and operations made an unplanned entry into Technical Specification 3.8.1.1.e, a 24-hour shutdown action statement.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Observation: Semi-annual Trend Review I 71152 The inspectors reviewed the licensee's corrective action program entries, maintenance activities, emergent maintenance issues, plant health reports, outage performance reviews, NRC generated condition reports, and NRC inspector walk downs.

The inspectors noted and documented the following issues and trends:

  • There are site wide issues with procedure use and adherence. Inspectors have identified numerous issues while performing inspections (minor violations). Some of these include signing work order steps complete before the step was complete, equipment for risk significant work requiring entry into the Configuration Risk Management Program were not properly protected, inadequate independent verification of procedure steps, and failure to construct scaffolding in accordance with orocedural quidance. In addition to these observations, the licensee identified similar issues as illustrated in the South Texas Project 2019 mid-cycle review. The licensee completed a common cause evaluation and is in the process of implementing corrective actions.
  • There have been several nuclear instrumentation issues and challenges, especially during the last few outages. These issues have resulted in issuance of a Licensee Event Report; an NRG-identified technical specification violation; and several emergent issues that have challenged operations (making technical specification calls), maintenance resources, and outage schedule delays and changes. The licensee has entered the issues into the corrective action program to perform an analysis and prescribe corrective actions, which is scheduled for completion in February 2020.
  • The licensee has recently experienced several issues involving engineered safety feature load sequencers. A13art from one self-revealed technical specification violation

( documented in this report in Section 71152), the licensee.handled each issue appropriately and without issue. In conjunction with the inspector observations, the licensee had also identified a possible trend and entered the issue into the corrective action program for analysis. The analysis is scheduled for completion in February

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 24, 2019, the inspectors presented the Occupational Radiation Safety inspection results to Ms. K. Harshaw, Vice President Regulatory Affairs and General Counsel, and other members of the licensee staff.
  • On October 28, 2019, the inspectors presented the in service inspection results to Mr. J. Connolly, Executive Vice President and Chief Nuclear Officer, and other members of the licensee staff.
  • On November 25, 2019, the inspectors presented the Emergency Plan In-Office Review inspection results to Mr. J. Enoch, Manager, Emergency Response, and other members of the licensee staff.
  • On December 17, 2019, the inspectors presented the failure to report a change in medical condition of a licensed operator inspection results to Mr. L. Sterling, Regulatory Affairs Manager, and other members of the licensee staff.
  • On December 19, 2019, the inspectors presented the biennial operator requalification inspection results to Mr. D. Breland, Supervisor, Operations Training, and other members of the licensee staff.
  • On January 23, 2020, the inspectors presented the integrated inspection results to Ms. K. Harshaw, Vice President Regulatory Affairs and General Counsel, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

71111.040 Drawings

5R209F05017#2

Piping and Instrumentation Diagram Component Colling

Water System

5R289F05038#1

Piping and Instrumentation Diagram Essential Cooling Water 20

System Train 1 B

5V119V10001#1

Piping and Instrumentation Diagram Essential Chilled Water

System

8T219F00031#1

Piping and Instrumentation Diagram Condenser Air Removal

Procedures

OPOP02-CC-OOO 1 Component CoolinQ Water

OPOP02-CH-OOO 1 Essential Chilled Water System

OPOP02-CR-OOO 1 Main Condenser Air Removal

71111.04S

Corrective Action

CR-YYYY-NNNN

2019-11970

2019-12022

2019-11969

2019-12023

Documents

Drawings

5R209F05019#2

Piping and Instrumentation Diagram Component Cooling

Water System

5R209F05020#2

Piping and Instrumentation Diagram Component Cooling

Water System

71111.05A

Procedures

OMAB02-FP-0128

Fire Preplan Mechanical Auxiliary Building CCW Pump and

Chiller, Train A

OMAB20-FP-0129

Fire Preplan Mechanical Auxiliary Building Non-Radioactive

Pipe Chase

OMAB27-FP-0142

Fire Preplan Mechanical Auxiliary Building CCW Heat

Exchangers

1ECW53-FP-

Fire Preplan Essential Cooling Water Intake Structure Pump

0600

Room Train A

71111.050 Procedures

OMAB02-FP-O 128

Fire Preplan Mechanical Auxiliary Building CCW Pump and

Chiller, Train A

OMAB20-FP-O 129

Fire Preplan Mechanical Auxiliary Building Non-Radioactive

Pipe Class

ORCB63-FP-0211

Fire Preplan Reactor Containment Building SW Peripheral

Area

ORCB63-FP-0212

Fire Preplan Reactor Containment Building NW Peripheral

Area

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

ORCB63-FP-0213

Fire Preplan Reactor Containment Building NE Peripheral

Area

2ECW58-FP-

Fire Preplan Essential Cooling Water Intake Structure Pump

0605

Room Train A

71111.06

Calculations

NC9701

Flooding Analysis: Electrical Auxiliary Building

Drawings

6M-18-9-N-5039

Mechanical & Electrical Auxiliary Building Section C-C Area

H

6M18-9-N-5023

Mechanical Electrical Auxiliary Building Plan @ EL. 35'-0"

Area H

6M189N05024

Mechanical Electrical Auxiliary Building Plan@ E

L. 35'-0",

Area J

9M-06-9-B-0155

Plumbing - M.E.A.B. Floor Plan EL. 35'-0" Area 18 & 19

9M131A01030

Mechanical and Electrical Auxiliary Floor Plan EL. 1 O' -0" Unit 17

9M131A01033

Mechanical and Electrical Auxiliary Building Floor Plan at

Elev. 35'-0" and 41'-0

71111.08P

Corrective Action

CR -YYYY-NNNN

2015-20733, 2017-13869, 2017-18341, 2018-6845,

Documents

2019-6008,

2019-7950,

2019-11368, 2019-11675,

2019-11865, 2019-12194, 2019-12243, 2019-12291,

2019-12444

Drawings

E10025E58

South Texas Units 1 & 2 Closure Head General Assembly

Interface Inf. for RRVCH

SB-9406-HL5007

Snubber and Mountinc::i Supports

Miscellaneous

South Texas Project, Units 1 AND 2 -Request for Relief RR-

04/05/2011

ENG-3-02 from ASME Code Requirements for Reactor

Pressure Vessel Insert Non-Destructive Examination {TAC

NOS. ME4764 AND ME4765)

South Texas Project, Unit 2 - Request for Relief NO. RR-

06/30/2016

ENG-3-20 for Extension of the Inspection Frequency of the

Reactor Vessel Cold-Leg Nozzle to Safe-End Welds with

Flaw Analysis (CAC NO. MF7428)

AE-NOC-

South Texas Project, Units 1 and 2 - Request for Relief RR-

09/10/2012

2002347

ENG-3-04 to Apply Alternative to the American Society of

Mechanical Engineers Boiler and Pressure Vessel Code

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

Section XI Requirements for Examination of Class 1 and

Class 2 Piping Welds (TAC NOS. ME70SS AND ME70S6)

MRP-058

Materials Reliability Program: Boric Acid Corrosion

Guidebook, Revision 2: Managing Boric Acid Corrosion

Issues at PWR Power Stations

PQR-003

Procedure Qualification Record

PQR-016

Procedure Qualification Record. P8-T-Ag-1

PQR-035

Procedure Qualification Record for P8-T-Aq.

PQR-037

Procedure Qualification Record for WPS P8-T-Ag, P8-A, P8-

09/05/1989

AT-Aq

PQR-040

Procedure Qualification Record for WPS P1-A/P1 -A-LLh/P1-

11/17/1989

AT-Lh

PQR-046

Procedure Qualification Record for WPS P8-T-Ag and P8-

01/24/1990

AT-Ag

PQR-087A

Procedure Qualification Record for WPS P1-AT-Lh (CVN)

10/28/1991

PQR-126

Procedure Qualification Record for WPS P1-T (CVN)

03/16/1995

PQR-127

Procedure Qualification Record for WPS P1-T (CVN)

03/16/1995

PQR-197

Procedure Qualification Record for WPS P8-T-Ao

04/10/2003

PQR-199

Procedure Qualification Record for WPS P1-A-Lh

10/14/2003

WPS P1-A-Lh

ASME Welding Procedure Specification (WPS). Single and

Revision 8

Double Welded Groove, Fillet Welds Socket Welds, and

other joint designs specified

In WPS WJD (Weld Joint Desiqn).

WPS P1-T

ASME Welding Procedure Specification (WPS). Single and

Revision 9

Double Welded Groove, Fillet Welds, Socket Welds, and

other joint designs specified

In WPS WJD (Weld Joint Desiqn).

NOE Reports

MT-2019-030

Closure Head Bolting/ Closure Stud 1 B through 368

10/18/2019

through MT-2019-

PT-2019-049

eves Low Pressure Letdown ORC Isolation Test Valve.

10/16/2019

FW0027 (Pipe to VLV CV0391 ).

PT-2019-052

eves Low Pressure Letdown ORC Isolation Test Valve.

10/16/2019

FW0028 (Pipe to Elbow)

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

PT-2019-054

CVCS Low Pressure Letdown ORC Isolation Valve CV-

10/18/2019

0391. FW0009.

PT-2019-057

Flange to Upper Case I SIAPLH-2AOPCW1 / Pump 2A

10/21/2019

PT-2019-059

Upper Case to Lower Case I SIAPLH-2A-PCW2 / Pump 2

10/20/2019

PT-2019-060

Lower Case Seam Weld / SIAPLH-2A-PCW5 / Pump 2A

10/20/2019

PT-2019-061

Nozzle to Upper Case I SIAPLH-2A-PCW4 / Pump 2A

10/21/2019

UT-2019-031

PRZ-2-N4C/Safety Nozzle to Shell

10/16/2019

UT-2019-042

PRZ-2-N4A/Relief Nozzle to Shell

10/19/2019

UT-2019-043

PRZ-2-N2/Spray Nozzle to Shell

10/19/2019

UT ~2019-044

PRZ-2-N3/Safety Nozzle to Shell

10/19/2019

UT-2019-048

RSG-2A-T1 / Tube plate to Lower Shell Barrel A

10/22/2019

VCT-2019-041

EW-2188-HL5001 / U-Strap Support

10/24/2019

VE-2019-001

BMI Penetration/ No. 1-58

10/07/2019

VE-2019-002

Reactor Vessel Closure Head/Bare Metal Visual Penetration

10/15/2019

Nozzles, 1-9, 14-23, 25-27, 29-61, 66, 68, 70, 72, 75-78,

including vent pipe and general head area.

VE-2019-003

Reactor Vessel Closure Head/Bare Metal Visual Penetration

10/16/2019

Nozzles, 1-9, 14-23, 25-27, 29-61, 66, 68, 70, 72, 75-78,

including vent pipe and general head area.

VE-2019-004

Reactor Vessel Closure Head/Bare Metal Visual Penetration

10/17/2019

Nozzles, 1-9, 14-23, 25-27, 29-61, 66, 68, 70, 72, 75-78,

including vent pipe and general head area.

VE-2019-005

Reactor Vessel Closure Head/Bare Metal Visual Penetration

10/18/2019

Nozzles, 1-9, 14-23, 25-27, 29-61, 66, 68, 70, 72, 75-78,

including vent pipe and general head area.

VT1/3-2019-094

Lower Case to Bottom Head/ SIAPLH-2A-PCW3 / Pump 2A

10/21/2019

Procedures

OPEP1 O-ZA-0004

General Ultrasonic Examination

OPEP10-ZA-0010

Liquid Penetrant Examination (Color Contrast Solvent

Removable)

OPEP1 O-ZA-0019

Wet Fluorescent Magnetic Particle Examination For ASME

Section XI PSI/ISi

OPEP1 O-ZA-0024

ASME XI Examination for VT-1 and VT-3

OPEP1 O-ZA-0054

ASME Section XI VE Visual Examinations

OPGP03-ZE-0033

RCS Pressure Boundary Inspection for Boric Acid Leaks

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

OPGP03-ZE-0133

Boric Acid Corrosion Control Program

OPM02-ZW-0005

Control of Postweld Heat Treat

OPMP02-0001 C

AWS-HVAC Weldinq Re.quirements

OPMP02-ZW-

General Welding Requirements

0001

OPMP02-ZW-

ASME Repair Replacement Welding Requirements

0001A

OPMP02-ZW-

ASME-ANSI B31.1 Welding Requirements

0001B

OPMP02-ZW-

Welding Documentation Requirements

0001D

OPMP02-ZW-

Welding procedure Specification Preparation and

0002

Qualification

OPMP02-ZW-

Welder Qualification and Certification

0003

OPMP02-ZW-

Control of Filler Materials

0004

OPMP02-ZW-

Arc Wire Thermal Spray Coatings

0006

Self-Assessments

CR 14-10410

Risk-Informed ISi Periodic Evaluation for South Texas

06/24/2014

Project Electric

Generating Station Units 1 & 2 in Conjunction with End of

the Third Interval, First Period.

Work Orders

w.o. 96011721

(1MB) LOOP 2 RCS Flow Transmitter FT-0429 ISOL VLV

w.o. 96011791

eves Letdown Orifice Header Isolation Valve

W.O. 96013680

Main Steam Isolation Valve 2D Above Seat Drain Isolation

W.0.576310

CentrifuQal Charqinq Pump 2A DischarQe Vent Valve

71111.118

Corrective Action

2019-10407

MSIV Operability Surveillance Procedure not followed

09/20/2019

Documents

2019-10562

Totalizer Event on 9/22/2019

09/24/2019

2019-4962

Train A CRE/HVAC Inoperable

05/02/2019

2019-8301

Inoperable Reactor Head Vent Valves

08/01/2019

2019-9357

Inadequate Control Room Loq entries

08/29/2019

Miscellaneous

None

Simulator Differences List

09/10/2019

None

2019 Biennial NRC Written Exams weeks 1 and 3

11/18/2019

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

None

NRC Annual Operatinq Tests Weeks 1 and 3

11/18/2019

TT01

Simulator Transient Test 01 Manual Reactor Trip

11/04/2019

TT02

Simulator Transient Test 2 Trip of all Main Feed Pumps

11/04/2019

Procedures

OPOP01-ZA-0014

Licensed Operator License Maintenance

Revision 30

OPGP03-ZA-

Medical Exams-NRG Regulated

Revision 0

28A

OPGP03-ZT-0132

Licensed Operator Requalification

Revision 13

OPNT01-TQ-1001

Examination Security

Revision 1

OPNT01-ZA-0037

Simulator Confiquration Control

Revision 13

LOR-GL-0001

LOR Training Program Guidelines

Revision 35

LOR-GL-0002

Licensed Operator Requal Annual/Biennial Evaluation

Revision 28

Guidelines

LOR-GL-0006

LOR Conduct of Simulator Training Guidelines

Revision 32

71111.110 Corrective Action

CR-YYYY-NNNN

2019-14056

2014-12615

1995-13955

2004-4336

Documents

Miscellaneous

Maintenance Rule Expert Panel Meeting Minutes, March,

May, June, July, August, Se,ptember November 2019

17-YU-003, 2017

Essential Cooling Pond (ECP) Seepage Calculations

MC-6498

Essential Coolinq Pond Thermal Performance Analysis

VTD-R 165-0029

Instruction Manual for Essential Cooling Water Pump Motor

VTD-STP1-0001

Rotating Equipment Oil Level Limits and Labels

VTD-W 120-0108

Lame AC Motors - Lice Line D Vertical Induction Motors

Procedures

OPMP04-EW-

Essential Cooling Water Pump Maintenance

0001A

OPMP05-EW-

Essential Cooling Water Pump Motor Inspection

0001

OPSP04-ZE-0313

Maintenance Rule Proqram

SEG-0009

Maintenance Rule Basis Document Guideline

Work Orders

Work

574254

2053

585021

2238

Authorization

Numbers

71111.12

Corrective Action

CR-YYYY-NNNN

2019-1762,

2019-2357, 2019-2393,

2019-4652,

Documents

2019-9269,

2019-8512, 2019-13994, 2019-4359,

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

2019-13709, 2019-8052

71111.13

Calculations

RA RICTCal

3505

Corrective Action

CR-YYYY-NNNN

2019-14338

Documents

Procedures

OPGP03-Z0-0055

Protected Components

OPOP01-Z0-0006

Risk Management Actions (RMAs)

71111.15

Corrective Action

CR-YYYY-NNNN

2019-12034, 2019-13137, 2019-13079, 2009-18939

Documents

2019-8731,

2014-8012,

2019-7580,

2019-5498

2019-13150, 2018-6459,

2019-13477

Drawings

50159F22540#2

Piping and Instrumentation Diagram Standby Diesel Jacket

Water

Miscellaneous

VTD-T147-0001

Terry Steam Turbine Manual

VTD-T147-0008

Terry Turbine Maintenance Guide, Auxiliary Feedwater AFW

Application

VTD-W290-0029

Installation and Operation Manual Overspeed Trip Test

Device for PG Governors

Procedures

OPGP03-AZ-0133

Fluid Leak Management Program

OPGP03-ZA-0514

Controlled System or Barrier Impairment

OPGP03-ZE-0030

Control Room Envelope Habitability Program

OPGP03-Z0-0046

RCS Leakage Monitoring

OPMP04-AF-0002

Auxiliary Feedwater Pump Turbine and Governor Valve

~

Maintenance

OPOP02-HE-0001

Electrical Auxiliary Buildinq HVAC System

Work Orders

Work

556056

489463

Authorization

Numbers

71111.18

Corrective Action

CR-YYYY-NNNN

2019-11901

2019-4165

2019-11971

Documents

Drawinqs

5R219F05028#2

Spent Fuel Pool Coolinq and Cleanup System

Procedures

OPMP09-PM-

Temporary Configuration Changes to Support Class 1 E

OOOB

Train B MCC Outages

71111.19

Corrective Action

CR-YYYY-NNNN

2019-11348, 2019-11348

Documents

Procedures

OPEP07-ZE-0002

LLRT Rig Operation

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

OPEP07-ZE-0003

Normal/Suoolementarv Purge Valve Failure/Troubleshooting

OPEP07-ZE-0003

Normal/Suoolementarv Purae Valve Failure/Troubleshooting

OPMP04-ZG-0093

Fisher Butterfly 12 and 48 in. Valve Maintenance

OPSP05-RC-

RCS Flow Transmitter Calibration

0417T

OPSP11-HC-0001

LLRT M-41 Normal Containment Purge Exhaust

OPSP11-HC-0001

LLRT M-41 Normal Containment Purge Exhaust

OPSP11-XC-0004

LLRT Penetration: M-91 Auxiliary Airlock Door Seals

Work Orders

Work

23127, 550267, 548433, 601368, 548433

Authorization

Numbers

71111.20

Miscellaneous

2RE20 Shutdown Risk Assessment Report

08/27/2019

Procedures

OPOP02-RC-0003

Filling and Ventina the Reactor Coolant System

OPOP03-ZG-0006

Plant Shutdown from 100% to Hot Standby

OPOP03-ZG-0007

Plant Cooldown

OPOP03-ZG-0007

Plant Cooldown

OPOP03-ZG-0010

Refuelinci Operations

OPOP08-FH-0001

Refueling Machine Operating Instruction

OPOP08-FH-0009

Core Refuelina

71111.22

Corrective Action

CR-YYYY-NNNN

2019-9708

2019-14780

2019-3044

Documents

Drawings

00009EODJM#1

Single Line Diagram 125VDC Class IE Distribution SWBD.

E1A11 (Channel 1) (E.A.B.) Sheet 01

Procedures

OPOP07-FR-0006

FLEX Diesel Generator Performance Test

OPOP07-FR-0006

FLEX Diesel Generator Performance Test

OPSP03-AF-0003

Auxiliarv Feedwater Pump 13(23) lnservice Test

OPSP03-DG-0003

Standbv Diesel 13(23) Ooerability Test

OPSP03-EW-

Essential Cooling Water System Train C Testing

0019

71114.04

Corrective Action

CR-YYYY-NNNN

2019-14047

Documents

Miscellaneous

NOC-AE-

South Texas Project, Units 1 and 2; Docket Nos. STN 50-

8/8/2019

19003676

498; STN 50-499; Supplement to Changes to the South

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

Texas Project Emergency Plan

NOC-AE-

South Texas Project, Units 1 and 2; Docket Nos. STN 50-

8/8/2019

19003678

498; STN 50-499; Changes to the South Texas Project

Emergency Plan

Procedures

OERP01-ZV-IN10

Administration of Potassium Iodide

71124.01

Corrective Action

CR-YYYY-NNNN

2018-03911, 2018-03912, 2018-04050, 2018-04527,

Documents

2018-04528, 2018-04757, 2018-04761, 2018-04933,

2018-06016, 2018-08247, 2018-09871, 2018-11562,

2018-11664, 2018-12157, 2018-12381, 2018-12559,

2018-12585, 2018-13229, 2018-14735, 2019-01215,

2019-03426, 2019-03573, 2019-07939, 2019-11659,

2019-12327

Miscellaneous

Stand Fast WB Count Report -.(reportinQ in nCi)

10/23/2019

18-12339

Ag-110 in CVCS during 1RE21

10/16/2018

19-11442-1

DAC-hr Assessment for Condition Report 19-11442

10/18/2019

19-3165-7

ALARA Review Package - 2RE20 Non-Rapid Refuel

10/01/2019

19-3165-9

ALARA Review Package - 2RE20 Room 003 Activities

10/01/2019

Procedures

OPEP02-ZM-0009

Spent Fuel Pool Storage and Work

OPGP03-ZR-0048

Personnel Dosimetry Program

OPGP03-ZR-0050

Radiation Protection Program

OPGP03-ZR-0051

Radiological Access Controls/Standards

OPRP01-ZA-0010

Radiation Protection Task Schedule

OPRP01-ZA-0042

Job Coverage

OPRP04-ZR-OO 13

Radiological Survey Program

OPRP04-ZR-0015

Radiological Postings and Warning Devices

OPRP04-ZR-0019

High Radiation Area Access Controls

OPRP07-ZR-0016

Lockdown and Posting for Transfer of Spent Fuel/Irradiated

Material ThrouQh Transfer Tube

Radiation

21434

Air Sample Data Sheet - Room 4 B/C Enclosure - Change

04/06/2018

Surveys

Out Filter

21441

Air Sample Data Sheet - B/C HEPA Enclosure Pre-Filter

04/07/2018

ChanQe Out

21468

Air Sample Data Sheet - Reactor Cavity Decontamination

04/14/2018

21498

Air Sample Data Sheet - "B" S/G Platform - Job CoveraQe of 04/19/2018

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

Nozzle Dams

21505

Air Sample Data Sheet - "B" SIG Platform - Job Coverage of 04/19/2018

Nozzle Dams

2373

Air Sample Data Sheet - Near S. Stairwell - Verify

10/01/2019

Conditions

Survey#

97442, 98130, 99286, 99321, 102863, 104598, 105041,

105049, 105646, 105785, 105796, 105992, 106223,

106234, 106258, 106397, 106565, 106797, 106801,

106824, 106862

Radiation Work

2019-2-0145

2RE20 - Maintenance Support for Work In and Around

Permits (RWPs)

Reactor Cavity, Spent Fuel Pool, and Transfer Canal (HRA)

2019-2-0158

2RE20 - Reactor Head Lift Activities (LHRA)

2019-2-0164

2RE20 - Retract/ Re-Insert Thimble Tubes (LHRA)

2019"'.2-0165

2RE20 - Maintenance and Support Work - Room 307

(LHRA)

2019-2-0167

2RE20 - Mechanical Stress Improvement Process (MSIP)

Work Activities (HRA)

2019-2-0173

2RE20 - Maintenance on N2CVPSV3100 (LHRA}

Self-Assessments

18-10431

Self-Assessment: FT-0428 Radiological Surveys

10/07/2018

18-11300-1

Self-Assessment: 1 RE21 Survey Snapshot

10/18/2018

19-02643

RP ProQram Formal Self-Assessment

06/06/2019

71124.03

Corrective Action

CR-YYYY-NNNN

2017-13657, 2017-13733, 2017-15060, 2017-16403,

Documents

2017-16501, 2017-17137, 2017-17894, 2017-19406,

2017-20490, 2017-24212, 2017-24235, 2018-01438,

2018-01607, 2018-01824, 2018-01837, 2018-04227,

2018-06620, 2018-08647, 2018-10747, 2019-05126,

2019-11442

Corrective Action

CR-YYYY-NNNN

2019-12240, 2019-12368

Documents

Resulting from

Inspection

Miscellaneous

AirHawk SCBA Personnel Fit Test, Medical, and Respiratory

Training dates for cost centers 87, 840, 841, 842, and 843

MSA CARE Certification for Darryl Malone (Vallen Freeport)

06/08/2018

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

000107

Vallen Freeport: Bauer Compressor Air Quality from

February 1, 2018-October 23, 2019

2019, 03

Department of Transoortation Audit: Vallen Freeport

09/23/2019

Respirator

453,

537,

569,

574, 606,

Review

210, 3709, 3715, 3716, 3718,

21, 3725, 3727, 3733, 3736

Procedures

OPEP05-ZH-0005

Non-Safety Related Filter Airflow Test

OPEP05-ZH-0008

MAB, TSC and RCB HV AC In-Place* HEPA Filter Leak Test

OPG03-ZE-0004

Plant Surveillance Program

OPGP-ZR-0050

Radiation Protection Proaram

OPGP03-Zl-0015

Control and Use of Industrial Compressed Air and Gases

OPGP03-ZR-0054

Respiratorv Protection Proaram

OPRP04-ZR-OO 16

Radioloaical Air Samplina and Analysis

OPRP05-RA-0007

Grab Sample Collection of the (PIG) Continuous

Atmospheric Monitors

OPRP05-ZR-0030

Portable Air Monitor Instruments (AMS-4)

OPRP06-ZR-0002

Respiratorv Protection Eauipment Issue and Return

OPRP06-ZR-0004

Cleanina and Sanitizina of Respiratory Protection Equipment 9

OPRP06-ZR-0005

Maintenance, Inspection, and Storage of Respiratory

Protection Eauioment

OPRP06-ZR-0008

Air Quality Evaluation for Compressors or Pressurized Gas

Cylinders

OPRP06-ZR-0013

Resoirator Fit Testina

OPRP06-ZR-0016

Charginq Breathinq Air Cylinders

OPSP11-HE-0001

Control Room Envelop Filter Airflow Capacity Test

OPSP11-HF-0001

FHB Exhaust Filter Airflow Capacity Test

OPSP11-ZH-0008

CRE and FHB HVAC In-Place HEPA Falter Leak Test

Radiation

21434

Air Sample Data Sheet: Chanqe Out of HEPA Pre-filter

04/11/2018

Surveys

21441

Air Samele Data Sheet - Pre-filter Chanqe Out

04/11/2018

21468

Air Sample Data Sheet - Cavitv Decontamination

04/14/2018

21498

Air Samele Data Sheet - Nozzle Dam Job Coverage

04/22/2018

21505

Air Sample Data Sheet - Nozzle Dam Job Coverage

05/03/2018

21669

Air Sample Data Sheet - Routine Unit 1 Radwaste Truck Bav 08/28/2018

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

(RWTB)

21882

Air Sample Data Sheet-Unit 1 Reactor Cavity

11/01/2018

21884

Air Sample Data Sheet-Unit 1 Reactor Cavity

11/01/2018

2338

Air Sample Data Sheet-RT-8011 Particulate Channel Alarm

09/23/2019

2373

Air Sample Data Sheet - FT-0419 Leaking Transmitter

10/02/2019

2476

Air Sample Data Sheet - Unit 2 Reactor Building 68' Grab

10/10/2019

Sample

2482

Air Sample Data Sheet - Unit 2 Reactor Building 68' Grab

10/10/2019

Sample

Radiation Work

2018-0-0159

Preventative Maintenance and Repair of Equipment in the

Permits *(RWPs)

FHB Fuel Transfer Canal including RP Surveys and

Decontamination

2019-2-0115

2RE20 - Mini Decontamination of Reactor Cavity and Initial

LISA and Tilt Pit Decontamination (LHRA)

2019-2-0117

2RE20 - Major Decontamination of Reactor Cavity and LISA

(LHRA)

2019-2-0151

2RE20 - Perform Maintenance and Inspection in RCB/FHB

Fuel Transfer Canals (LHRA)

2019-2-0155

2RE20 - Refuel - Inspect/Clean/Measure Upper/Lower 0-

rina Gro_oves (LHRA)

2019-2-0158

2RE20 - Reactor Head Lift Activities (LHRA)

2019-2-0163

2RE20 - Disconnect/Reconnect Seal Table (LHRA)

2019-2-0171

2RE20 - Remove/Reinstall Reactor Cavity Stairwell (HRA)

Self-Assessments

Assessment/Benchmark Report: Respiratory Program 2018

08/29/2018

MN-17-1-105942

Quality Monitoring Report: Radiological

04/02/2017

Instrumentation/Protective Equipment

MN-18-1-107276

Quality Monitoring Report: Radiological Surveys

10/23/2018

Work Orders

WAN 546352

EAB and FHB HVAC In-Place Adsorber Leak Test: Unit 2 -

09/24/2019

CRE TRN "A" Clean Up Filter 21A/ 3V112VXV001

WAN 546353

EAB and FHB HVAC In-Place Adsorber Leak Test: Unit 2

09/24/2019

CRE TRN "A" Clean Up Filter 21A / 3V112VXV001

71151

Procedures

OPGP05-ZN-0007

Preparation and Submittal of NRC Performance Indicators

Chaptijr 23

Conduct of Operations for Radiation Protection: Radiation

Protection Performance Improvement Guideline

Inspection

Type

Designation

Description or Title

Revision or

Procedure

Date

71152

Corrective Action

CR-YYYY-NNNN

2010-13994, 2019-13709, 2019-8052,

2019-4359,

Documents

2017-1786,

2017-17817, 2018-1529,

2018-3276,

2018-14380, 2019-9018,

2019-9019,

2019-7971,

2019-7483,

2019-12401, 2019-6155,

2019-5150,

2019-376,

2019-13709, 2019-8062,

2019-8052,

2019-4359,

2019-14697, 2019-13386, 2019-13436,

2019-14208, 2019-14736, 2019-14208, 2019-14743,

2019-13614, 2019-13950, 2019-14279, 2019-12597,

2019-9119,

2019-10504, 2019-11054, 2018-11855,

2018-3518,

2018-3559,

2019-7508,

2015-18703,

2017-15034, 2019-10837, 2019-2558,

2019-4575

38