IR 05000397/1989005

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Forwards Mgt Meeting Rept 50-397/89-05 on 890105 Re Items of Interest Pertaining to Activities Authorized by License NPF-21.Addl Responsiveness or Attention to Safety & QA Issues Needed
ML17285A254
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 01/24/1989
From: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Mazur D
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
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ML17285A255 List:
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NUDOCS 8902220274
Download: ML17285A254 (44)


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ACCESSION NBR:8902220274 DOC.DATE: 89/01/24 NOTARIZED: NO DOCKET N

FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH.NAME AUTHOR AFFILIATION MARTIN,Z.B.

Region 5, Ofc of the Director RECIP.NAME RECIPIENT AFFILIATION MAZUR,D.W.

Washington Public Power Supply System SUEGECT: Forwards Mgt Meeting Rept 50-397/89-05 on 890105 re items of interest pertaining to activities authorized by license.

DISTRIBUTION CODE:

IE01D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation esponse NOTES:

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Docket No. 50-397 Washington Public Power Supply System

.P.O.

Box 968 3000 George Washington Way Richland, Washington 99352 Attention:

Mr. D.

W. Mazur Managing Director Gentlemen:

Subject:

Management Meeting This refers to the Management Meeting held with members of the Supply System staff at Supply System Headquarters in Richland, Washington, on January 5, 1989.

The purpose of this meeting was to discuss items of interest pertaining to activities authorized by NRC License NPF-21.

Subjects discussed during the meeting are summarized in the enclosed meeting report 50-397/89-05.

You stressed during thi. meeting, as on previous occasions, that the Supply System will not be satisfied with average performance, but is determined to perform in the top 10Ã of the nuclear industry.

It is apparent that progress is being made in improving overall performance, especially in reducing scrams, safety system actuations, and personnel errors.

We also note that program improvements have been and continue to be made in the Operations, Engineering, and guality Oversight areas.

As discussed during our meeting, however, we also have observed that addi-tional responsiveness or attention to safety and gA issues is needed.

Examples discussed were:

Some recent problems have beer dealt with by line management only after encouragement hy safety= oversight group: or the NRC.

Ci recent example was the observed leakage of nitrogen into containmert from the contain-ment instrument air system, requiring frequent venting for containment pressure control.

  • In addition to increased attention by line organizations, it appears that your engineering groups must become more involved in the resolution of technical proble'ms such as the one discussed above.

To sustain the improvement observed in recent months, your senior management should become more visible in various areas of the plant to continually convey to the plant staff their interest in good performance.

These examples appear to reflect average performance, and represent weaknesses which must be overcome if the Supply System is to achieve its goal of being a

top 10Ã performe JAM 2< ]gag We appreciated the opportunity to meet with the chairman of your Executive Board's Operations Committee and the members of your Corporate Nuclear Safety Review Board, during this meeting.

We believe that meetings such as this one are of significant benefit in maintaining effective communications'between the Supply System and the NRC.

In accordance with 10,CFR 2.790(a),

a copy of this letter and the enclosure will be placed in the NRC Public Document Room.

Should you have any questions concerning this meeting, we will be pleased to discuss them with you.

Sincerely, W'

~

t,

}P($ ~ 1 Q gY)Zl E }I J.

B. Martin Regional Administrator Enclosure:

Meeting Report No. 50-397/89-05 cc w/enclosure:

A. L. Oxsen, WPPSS Director, Operations G.

D. Bouchey, WPPSS Director, Assurance 8 Licensing C.

M. Powers, WNP-2 Plant Manager A. G. Hosier, WNP-2 Licensing Manager G.

E. Doupe, Esq.

N. S. Reynolds, Debevois, Cook, Purcell 8 Reynolds State of Washington bcc w/copy of enclosure:

Docket File Project Inspector Resident Inspector G.

Cook B. Faulkenberry J. Martin A. Johnson T. Fol}ep, KRR bcc w/o erclosure:

M.

S)it,h LFMB ~RECVEE .N5 Y I/&/89 P hnson I/23/89 p.P4 RZimmerman AChaffee I/~ 5 /89 I/3989 Martin I/Pt/89 g~UE P PEQ S P YES '/ NO /YES ' NO~~YE / NO U ES / NO YES / NO DJ TO PDR YES / NO

U.S.

NUCLEAR REGULATORY COMMISSION REGION V Report No: Docket No: Licensee: 50-397/89-05 50-397 Washington Public Power Supply System P. 0.

Box 968 Richland, WA 99352 Facility Name: Washington Nuclear Project No.

2 (WNP-2) .Meeting at: Supply System Headquarters, Richland, Washington Meeting Conducted: January 5, 1989 Prepared by: 'pproved by: Summary: 7 / orensen, Res i ent Inspector /i o nson, ie Reacto Projects Section

'I I<< ate agne (/~ ate igne Mana ement Meetin on Januar 5, 1989 Re ort No. 50-397/89-05 A Management Meeting was held on January 5, 1989 at the Supply System Headquarters to discuss issues of current and recent irterest to the NRC and the Supply System.

Supply System representatives made presentations on actions in progress to provide for improved performance in identified weak areas.

Recent plant and licensee staff performance was also discusse DETAILS l.

Mana ement Meetin Partici ants Nuclear Re ulator Commission J.

A.

G.

G.

J.

P.

C.

R.

R.

B. Martin, Regional Administrator E. Chaffee, Deputy Director, Division of Reactor Safety and Projects W. Knighton, Director, Project Directorate V, NRR P.

Yuhas, Chief, Radiation Safety Branch L. Crews, Senior Reactor Engineer H. Johnson, Chief, Reactor Projects Section

J. Bosted, Senior Resident Inspector B.. Samworth, Project Manager C. Sorensen, Resident Inspector Washin ton Public Power Su

S stem Parker D.

A.

J.

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J.

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L.

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D.

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J.

Knight, Chairman, Operations Committee, Board of Directors Mazur, Managino Director Oxsen, Assistant Managing Director for Operations Shannon, Deputy Managing Director Bouchey, Director, Licensing and Assurance Burn, Director, Engineering Sorensen, Manager, Regulatory Programs Powers, Plant Manager Garvin, Manager, Programs and Audits McGilton, Manager, Operational Assurance Programs Baker, Assistant Plant Manager Harrold, Manager, Generation Engineering McKay, Operations Manager Dyekman, Manager, WNP-I Engineering Harmon, Maintenance Manager Koenigs, Technical Manager Waddel, Manager, Planning and Scheduling Pisarcik, Health Physics Support Supervisor Cor orate Nuclear Safet Review Board J.

R.

L.

W.

D.

D.

P.

B.

R.

C.

L.

W.

Chasse, Senior Environmental Licensing Engineer, WPPSS Glasscock, Management Specialist,, WPPSS Eliason, General Manager, Nuclear Plants, Northern States Power Co.

Jones, Senior Vice President, Nuclear Functions, Omaha Public Power District Larkin, Manager, Engineering Analysis and Nuclear Fuels, WPPSS Simpson,'ice President and Manager, Safety, (juality Assurance, and Security, Westinghouse Hanford Company Roberts, Ph.D., Manager, Materials, Science and Technology, Battelle Northwest Westinghouse Hanford C State of Washin ton Ener Facilit Site Evaluation Council EFSEC C.

R.

Mal 1 is, Vice Chairman M. L. Fitch, Executive Secretary Bonneville Power Administration R.

F. Nazurkiewicz, Chief, Operations Branch D. L. Williams, Nuclear Engineer 2.

~Back round'n August 18, 1988, a meeting was held with various members of Supply System senior management to discuss the findings of the NRC SALP Board for the period ending Nay 31, 1988.

This meeting, held on January 5, 1989, was intended to follow, up on those topics and discuss other actions being taken by the Supply System in response to the findings of the SALP Board.

Other areas discussed included actions in progress to provide improved performance by guality Assurance and other safety oversioht groups.

NRC representatives also discussed issues of current NRC interest.

Selected slides from the licensee's presentations are included as an enclosure to this report.

3.

The meeting convened at 8:00 a.m.

The Regional Administrator opened the meeting by stating that the purpose was to discuss topics of mutual interest in an effort to avoid missed signals of mutual expectations.

Nr. Martin stated that the meeting was also needed to determine how the action plan developed by the Supply System as a result of the last meeting was progressing.

Finally, he noted that it provided an opportunity to discuss perceptions regarding Supply System performance at a point roughly half-way through the SALP period.

Nr. Nazur then introduced various dignitaries in attendance from the State of Washington, the Supply System Board of Directors, and the Corporate Nuclear Safety Review Board (CNSRB).

He explained the Supply System's strategic gian through 1995, which includes a commitment to improved performance.

He then discussed the Supply System's current emphasis on management training.

Nr. Oxsen then reviewed the meeting agenda, noting that plant performance had improved and that the Supply System had taken some positive steps which included: Completion of the first system SSFI Conduct of management training Ordering of a new simulator

Organizational improvements involving the movement of 54 people to different positions Nr. Oxsen stated that the backlog of resolutions to identified problems appeared to exceed the capacity of the Supply System staff, and that the Supply System was evaluating the need to obtain additional resources on a te'mporary basis to assist with disposition of the problems.

He concluded his opening remarks by expressing his belief that the performance of the Supply System and the WNP-2 plant had improved over the past six months, although additional improvement was needed.

Nr. Powers then discussed plant performance in the light of recent achievements and shortcomings.

He also discussed performance indicators and stated that he believed plant performance had turned in a positive direction.

Mr. Powers went on to discuss recent operating events e.g., degraded'oltage relays and containment purge valves.

Regarding the November 21, 1988, issue involving the degraded voltage relays, he stated that he recognized Plant Management had made a non-conservative decision regarding the applicability of Technical Specification 3.0.3 and the requirement to initiate a plant shutdown.

He also discussed responsiveness to gA findings and other operational concerns.

Nr. Hartin noted the plant's improved performance during the last half of 1988, and stated that it may be based on solid progress in focusing attention on important areas, or may be a period of good luck -- time will tell.

He noted in particular that performance was good in the area of scrams and safety system actuations, and encouraged the Supply System to continue its efforts in this area.

However, he admonished the licensee for a perceived lack of responsiveness to safety and gA issues, noting that some issues were dealt with only after encouragement by safety oversight groups or the NRC.

For example, nitrogen leakage into the containment (from the containment instrument air system) had not been dealt with, with the result that frequent venting was necessary for pressure control.

Nr. Hartin alluded to the Supply System's goal of performing in the top 10/ of the nuclear industry, and stated that this is not the way a top 10'. perfoimer reacts to such problems.

He noted that the Supply System has for a long v.ime had ~he capacity to excel, and that there is opportunity for continued improvement.

He expressed his impression that engineering needs to be more involved in the resolution of such technical problems.

Nr. Mazur stated that-the Supply System's goal is still to be a top 10% performer or better.

He stated that their plate was full and that he wasn't making any excuses, but was pleased with their progress so far and that he felt their sights were set in the right direction, Nr. Bosted pointed out the virtues of proactive initiatives vice reactive responses.

This was acknowledged by Mr. Mazur.

Mr. Pisarcik then presented a health physics performance assessment which involved conclusions and corrective actions from a review that was conducted of 1988 Radiological Occurrence Reports.

Nr. Yuhas pointed out the various prot )er ~ exeter'r r~r ec bv argy} pr licer ~@~~> with ncstjr~ pf'igh i.-.0ir~, lAn area~. r.<<~~ei v~u aiiaa wIi~-2 nas nao some s>ms lar prooiems and shou!o renew efforts to provide improvement in this are Mr. I,'addel then made a presentation concerning the schedule and scope of the April 1989 refueling outage.

Mr. Harrold reviewed the status of the Supply System's Engineering Improvement Plan.

He noted that the plan had been issued on December 16, 1988, and was well on its way to implementation.

This in'eluded the adoption of a Program Leader concept and improvements in span of control brought about by the establishment of 12 new engineering supervisor positions.

He stated that planning and scheduling improvements had been implemented in October 1988 for refueling outage items and in December for non-outage items, and that by February 1989 he would have the capability to provide work schedules for individual design engineers.

He also noted that schedules allow an extra 50K manhour allowance for checking and verification of the design engineering work.

Mr. Harrold also described the benefits being realized from the recently established Modification Review Committee and Design Review Board.

The Modification Review Committee, which had held 90 meetings so far, is composed of plant, engineering, and design oversight representatives, and provides improved communication (including plant walkdowns) on the best ways to implement a desired design change.

The Design Review Board provides an overview of the design process, including criteria, review of'udit results, and consideration of training effectiveness.

Mr. Harrold also discussed, other engineering p'rocess enhancements and the status of engineering work for the 1989 refueling outage.

Additional detail is provided in the enclosure.

Mr. Bouchey then discussed recent Licensing and Assurance initiatives and changes.

These included completion of the revised staffing plan discussed during the previous management meeting, relocation of the operational assurance manager to the plant site, establishment of an Engineering Assurance group and a dedicated Root Cause Assessment group, and additional emphasis on followup to ensure appropriate corrective actions for identified problems, He stated that gA audits had been changed to a performance-based approach and were producing meaningful findings.

He also noted that the Supply System's first SSFI, on the Low Pressure Core Spray System, had been completed, and would be discussed by Mr. Dyekman.

After this presentation, Mr. Martin commented that he was encouraged by the developments in Engineering and gA, and stated that the NRC would look at the substance of the design engineering work and safety oversight group activities in the months ahead, along with the aggressiveness of the line organizations in correcting identified weaknesses.

He noted that big problems develop from numerous small problems which accumulate over a period of time, and that it is gA's responsibility to identify and encourage correction of small problems before they become big ones.

Mr. Dyekman then discussed the recent SSFI the Supply System had com-pleted on the Low Pressure Core Spray (LPCS) system.

He noted that this had resulted in 183 observations, including 16 nonconformance reports (NCRs), which would provide for more reliable system operation.

In

- response to a question from Nr. Johnson, he and other licensee represen-tatives stated that the SSFI had not accomplished one of the initial goals, which was to, verify the adequacy of the process used to update the design data base on the LPCS system.

Nr. Bouchey stated that he would take action to ensure proper validation of this process.

Mr. McKay then made a presentation on Operations Department initiatives and commitments.

Nr. Harmon followed by discussing recent Maintenance Department initiatives.

Mr. Powers concluded the Supply System's presentation by stating that he had heard the various messages from the NRC and was taking them to heart.

He believed actions being taken would be effective in turning performance around.

He stated that the Supply System staff was looking forward to the months ahead with confidence, but with the, attitude that further improvements need to be made.

Nr. Martin stated that this was the proper attitude to distinguish them between an average performer and a top 10K performer.

4.

Closinc Remarks Nr. Martin concluded the meeting by asking licensee representatives which of them believed they spend enough time in the plant.

He noted that to sustain the improvement observed, more management presence was needed in the plant, based upon security access data he had reviewed.

He encouraged the licensee to keep up the good work, get more aggressive in dealing with technical problems, and get into the plant more often.

Nr. Mazur agreed with these concluding assessments.

The meeting adjourned at 12:35 p.m.. Enclosure: Selected slides from the licensee's presentations

ENCLOSURE TO YiEETING REPORT SELECTED SLIDES FROh'I THE SUPPLY SYSTBI'S PRESENTATIONS

~ ~ SUPPLY SYSTEM PERFORMANCE WALKLEY CONFERENCE ROOM January 5, 1989 8:00 a.m.

hgENDA A.

Opening Remarks ~ Strategi c Pl an ~ Management Training B.

Agenda Introducti on I.

Overall Plant Performance ~ Operating Events Relay Surveillance Containment Valve Sea't Material ~ Organizational Responsiveness ~ Health Physics Performance, ~ R-4 Modification Planning II.

Engineering Improvement Initiati ves ~ Previous Commitments ~ PMR Improvements III.

Licensing and Assurance ~ Previous Commitments ~ Activities/Accomplishments ~ Commitment Tracking I LPCS SSFI IV.

Operations Experience ~ Previous Commitments o Performance e Attention to Detail ~ PPM 1.3.1 V.

Maintenance Experience ~ Previous Commitments ~ Backlog Reduction e Organization ~ Field Supervision of Work Activities VI.

Overall Performance Summary v~r.

'iopics of interest to NR4 JB Martin DW Mazur AL Oxsen

CM Powers

DJ Pisarcik

WW Waddel

LT Harrold

GD Bouchey

GK Dyekman

SL McKay

JD Harmon

CM Powers

/ STRATEGIC PLAN FOR THE SUPPLY SYSTEM ~ Effort Began for the First Time in August 1987 o Planning Completed in September 1988 Reviews, Approval and Printing Complete in December 1988 ~ Purpose Define the Intended Future Through 1995 Express the Vision and Action to Reach It ~ Points of Emphasis A Statement of Values, Shared by Employees Highest Priority to Safe, Reliable, Economic Operation of Plant

Commitment to Improved Plant and Employee Performance

MANAGEMENT TRAINING IN THE SUPPLY SYSTEM ~ An Old Subject o New Commi tments Fl owing from Strategi c Plan and Concerns Expressed by INPO and NRC ~ Management and Personnel Manual Issued November

~ 'hrust of Program Assurance of Acceptable Level of Skills Stimulate a New Culture of Participative Management and Employee Involvement Methods and Stimulus to Practice Teamwork Leading to an Inner-Driven Accountability for Work ~ Highlights Management Development Track Established Covers All Managers and Supervisors Established Mandatory Training Required Core For All Levels of Management Required - Varies by Level of Position Elective To Suit Job and Individual Needs Action Plans will Become a Contract o Old Process Offered Some of. the Right Training to Some Managers ~ New Process is Comprehensive, with Purpose and "Teeth" ~ From November Through January, Managers are Being Trained in equality Management Skills ~ Not a One-Shot or a One Year Program A Long-Term Process of Continuous Improvement

OVERALL PLANT PERFORMANCE ~ Successful Refueling Outage (R-3)/Solid Recovery ~ Three (3) Forced Outages to Cold Shutdown High Drywell Leakage (RCIC Steam Supply Valve Packing) Main Steam Line Drain Cracked Weld . CSP-V-9 Seat Leakage ~ Generation Higher Than Budgeted ~ Personnel Performance Improved ~ Management Initiatives Paying-Dividends Personnel Accountability/Procedural Compliance Management Involvement/Problem Resolution Root Cause Analysis and Plant Problem Process ~ Selected Performance Indicators

RESPONSIVENESS TO SAFETY/OA ISSUES ~ Safety Sensitivity Measured by Response to Challenges ~ 'ecent Challenges High 'Drywell Leakage RHR Check Valves Control Room Ventilation Design Issue Containment Inerting Control Problem Main Steam Drain Line Cracked Weld Containment Isolation Valve Seat.

Leakage D/G-3 Speed Sensor Failure

RESPONSIYENESS TO SAFETY/QA ISSUES (CONTINUED) ~ Operati onal Concerns MSIV Binding Acousti cal Monitor Rel i ab'i 1 ity CEP/CSP Valve Seats Turbine Valve Vibration MSRV Seat Leakage Significant R-4 Activity Planned on These Issues ~ New Restart Process ~ Monthly gA/OPS Directorate Issues Meeting ~ Improved Process for Resolution of Plant gA Deficiencies ~ Increased Accountability for Open Items e General Downward Trend in Open gA Surveillance Deficiencies

RECENT. OPERATING EYENTS ~ Degraded Undervoltage Relay Surveillance Identified Through Supply System SSFI Technical Meeting with NRC on Surveillance Intervals Tech Spec Change Submitted More Conservative Posture on LCO 3.0.3 Applicability Until Tech Spec Change Approved (GL 87-09) Plant Problem Report Process More Rigorous Operability Reviews ~ Containment Valve Seat Material Recent Monthly Stroking and LLRTs Successful Root Cause Batch Material Defect Viton Properties Inappropriate for Service Application Replace Valve Seats on Affected Valves in R-4 Industry/New Vendor Experience

R4 OUTAGE SCOPE MAJOR DESIGN CHANGE/MAINTENANCE TASKS ~ SM 75/85 Logic ~ SW A/B Discharge X Hi ~ Leak Detection Instrument Replacement ~ D/W Hot Spot Removal ~ RHR 53A Valve Replacement ~ Feedwater Heater Level Control Change-Out ~ IN-1 Inverter Replacement ~ Turbine Supervisory Instrument Replacement ~ MSIV Overhaul ~ RFW Turbine Inspection ~ Turbine Valve Overhaul ~ MSRV Actuator Rebuild ~ MSRV Replacement/Seat Rework ~ Acoustical Monitor Cable Replacement o

CRD Rebuild ~ RRC Discharge Valve Inspection/Modification o MS SRV Vacuum Breaker Rework

ENGINEERING PREVIOUS COMMITMENTS ~ Engineering Improvement Program Status Implementation Plan Issued Program Leader Designated 12 Supervisors Selected Planning/Scheduling R-4 Outage Non-Outage Individual Engineer Schedules 12/16/88 11/22/88 9/17/88 10/13/88 12/15/88* (2/28/89) ~ Modification Review Committee 8/11/88

ENGINEERING PREVIOUS COMMITMENTS (CONTINUED) . ~ Configuration Management Program Status Design Bases Document Program LPCS Pilot Program Onsite AC Power.Pilot Program . Begin Long Term Program Corporate Standard for Configuration Management Program Integrated Data Base Program 6/30/88-(7/30/89) (7/89) (7/89) 11/88 ~ Expansion of Cable and Raceway Schedule Program Added Combustible Loading Added Voltage Drop Calculation 7/1/88 7/1/ss

'ENGINEERING PREVIOUS COMMITMENTS (CONTINUED) o Electrical Mi-ring Diagrams ~a~tu gC-1 MOV Electrical Miring Diagrams Non gC-1 MOV Electrical Miring Diagrams Schedule for System Level EMD Penetration Seal Tracking System Tech Spec Fire Rated Penetrations 'Design Control Procedures 10/3/88: (2/1/89) 12/30/88 9/30/88 9/1/88

ENGINEERING PMR IMPROVEMENTS SPAN-OF-CONTROL EMPLOYEE SUPERVISOR RATIO ~ Electrical/I8C Systems Department 3 Discipline Engineering Supervisors 1 Design Group Supervisor 5/1 '9/1 o Mechanical Systems 'Department 3 Disci pl ine Engineering Supervi sors 1 Design Group Supervisor 5/1 4/1 ~ Nucl.ear Systems E Analysis Department 2 Discipline Engineering Supervisors ~ Equipment Engineering Department 2 Discipline Engineering Supervisors 5/1 6/1

ENGINEERING PMR IMPROVEMENTS (CONTINUED) PLANNING AND SCHEDULING ~ Established Common Scheduling Tool ~ Augmented Planning Staff with Outside Resources Schedules Include 50K Manhour Allowance for Checking and Verification ~ Reduced Number of Design Changes to Match Resource ~ Provide Planning Support to Each Manager ~ Specific Work Prioritization for Engineers

ENGINEERING PMR-IMPROVEMENTS (CONTINUED) M~DDIFICATI N. IIEET EII CITMMITTEE ~ Improve Communication and Teamwork ~ Includes Malkdowns ~ Better Understanding of Problem to be Solved ~ Establish the Preferred Approach to Problem Resolution ~ 90 Meetings So Far ~ Results Beneficial to equality and Technical Merit

ENGINEERING PNR IMPROVEMENTS (CONTINUED) OE!~I REL~IM QQARD ~ Approval of Criteria Level Document Changes ~ Overview of Engineering Design Process ~ Approval of Standards o Technical Advisor to Manager, Generation Engineering ~ Review Results of Audits and Ensure Proper Corrective Action ~ Assess Effectiveness of Training Error Trends Overview Function o Review Results of Field Feedback Problems/Trends Needing Improvement

ENGINEERING PMR IMPROVEMENTS (CONTINUED) ~PROCES ENHANCEMENTS ~ Design Safety Evaluations o Minor Modifications Process e System Design Engineer Approval on Changes ~ Document Change Only Process

ENGINEERING PMR IMPROYEMENTS (CONTINUED) R-4 DESIGN QUALITY ENHANCEMENTS ~ Formal Design Review of Three Recently Issued Changes ~ Re-Review Design Issued Prior to May, 1988 ~ Improved Checking and Verification ~ Improved Design Safety Evaluations ~ Modification Review Committee ~ Management Emphasis on equality Improvements

ENGINEERING R-4 SCHEDULE PERFORMANCE INTEGRATED OUTAGE PLAN AUGUST 1988 ~ 83 Plant Modifications Initially Planned for R-4 ~ 51 Engineering Complete ~ 32 Engineerig To Go ENGI NEER ING STATUS 1/5/89 ~ 9 Design Changes To Go 1 Complete by January 25, 1989 3 Complete by February 10, 1989 5 Complete Past February 1 Late Add 4 Procurement Cycle/Vendor Information

STATUS OF QA/SAFETY ACTION PLAN PRESENTED AT NRC MANAGEMENT MEETING DATE 6/88 7/88 8/88 ACTION Engineering Assurance group formed Procurement QA Consolidation Relocate at Site Split gA/gC Fewer layers of management Strengthen Safety.Focus/ Involvement in Safety Decision Making Relocate Manager Operational Assurance at Site Dedicated Root Cause Group formed Add Statistics, Analytical, and Trending Capability New Policy Statement on gA More Clearly Defined Goals and Planning Line Yerification Assessment (Corrective Maintenance) Dedicate Root Cause Staffing Improve Coordination of Licensing 8 Compliance Group Improved Engineering Capabili-ties Performance Monitoring Training by SAIC Program Plan for Engineering Assurance STATUS Complete 6/20/88 Complete 6/20/88 'Complete=6/20/88 Complete 6/88 Complete 7/1/88 Complete 6/20/88 Complete 7/1/88 Complete ll/7/88 Complete 7/27/88 Rescheduled for 1/89 Complete 8/5/88 Ongoing Complete 8/88, Complete 8/25/88 Complete 8/88

STATUS OF OA/SAFETY ACTION PLAN PRESENTED AT NRC MANAGEMENT MEETING (comxwveD) DATE 9/88 10/88 12/88 1/89 ACTION QA Consultant (FY89) Contract in Place for Organization Assessment Staffing Level Adequacy Procurement QA Initiatives QC Staffing Study Publish Improved Trend Reports uality Management Systems ~ ~ raining Improved GET Module Root Cause Program Fully Implemented STATUS Contract with OAC 9/88 in Progress In progress several goa(s scheduled through FY89 (see goals) Complete 12/88 Complete 10/88 Complete for all Managers and Supervisors 1/89 Rescheduled 6/89 'omplete 12/21/88

LICENSING AND ASSURANCE SUMMARY OF MAJOR ACCOMPLISHMENTS (1) Reorgani zati on to Focus on Key Issues (2) Clear Goals and Improved Planning (3) Staff Improvements (Engineering, Operations, Statistics) (4) Strengthen Licensing Organization's Role and Staff (5) Engineering Assurance Program Implementation (6) Pilot SSFI Completed (7) Operating Experience Review Backlog Reduction (8) Root Cause Assessment Program Implementation (9) Trending and Reporting Improvements (10) Standardized Quality Finding (11) Performance-Based QA Surveillances and Audits (12) Improved Corrective Action Follow-up and Effectiveness'valuation

MNP-2 LICENSING IMPROVEMENTS ~ Stronger Technical and Safety Emphasis ~ Monitoring Plant Licensing Basis and FSAR Commitments Operations Procedures LER Reviews NOV Response Reviews ~ Improved Technical Capability of Staff ~ High Level of Professionalism in Dealing With NRC Staff

ENGINEERING ASSURANCE ACCOMPLISHMENT ~ Assessments Performed (32 deficiencies) ATMS Rule Diesel Generator Slow Idle Modification Nonconformance Report Process Management Commitment Tracking 10CFR50.59 Compliance Drawing Control System ~ SSFI on Low Pressure Core Spray e Programmatic Recommendations FUTURE ACTIONS Formal Independent Design Reviews (R-4 Modifications) ~ Review of Design Products ~ 10CFR50.59 Safety Evaluation Reviews ~ Development of Performance Indicators ~ Component Reliability Assessment (Feedback to Plant and QA/QC)

OPERATIONAL EXPERIENCE REVIEW PROGRAMS GOAL Prevent Repeat Events From Occurring at MNP-2 IR-ROIIEE 0 PE RATE RO ~RIPER IIX E -- ROOT OAOEE ARRI Y TIE ~ Established Dedicated Group ~ Implemented Interim Program 8/88 9/1/88 ~ Training Completed

RCA Course by EG8G 100+ HPES Training

Management Overview Other miscellaneous training including INPO, Ontario Hydro, DOE MORT/Accident Investigation ~ Implemented State-Of-The-Art Program 12/21/88

II ~ ~ I OPERATING EXPERIENCE REVIEW PROGRAMS (GONTINUED) ~RO T ~AUSE ~ANALY I 192 Problem Reports Screened (since 9/1/88)

Require RCA

RCA Complete

Recommendations from RCA ANALYSES COMPLETED EXAMPLES Pipe Crack From Nitrogen Inerting RWCU Pump Trip High Unidentified Drywell Leakage Three 1/2-Scrams During Surveillance Unanalyzed Control Room Ventilation Bypass Flow Paths Feedwater Heater Water Hammer RRC Pump Trip During Surveillance ANALYSES IN ~PROGRE S EXAMPLES RWCU Pump Failure Problems Degraded Voltage Relay Testing Problems Cracked Welds on Steam Line Drain Piping Violations of MWR Work Instructions Missed IRM.Surveillance During Startup

~ ~ ~ EFFECTIVENESS ASSESSMENT 1) ALL SALP, INPO and Major Management Initiatives Scheduled and Tracked o Reviewed Monthly by Directors (exceptions) ~ Review quarterly by Executive Board 1) Independent Effectiveness Assessment ~ Commitments Grouped by Major Problem Area o Verification that Commitments are met ~ Asses'sment of Effectiveness at Resolving Major Problems 3) Responsiveness o Formalized Escalation Process e Routine Rating and Feedback on all gFRs ~ Trending ~ Monthly Reporting and Senior Management Meetings

SAFETY SYSTEM FUNCTIONAL INSPECTION (SSFI) I OBJECTIVES: o Perform pilot self-initiated inspection similar in approach and thoroughness to NRC SSFIs ~ Assess operational readiness of the Low Pressure Core Spray (LPCS) System ~ Use technical personnel that have been reasonably free from involvement in LPCS system design, modification, testing, maintenance and operation.

~ Provide feedback to assist in validation of the Design Bases Document (DBD) ~ Develop experience for planning future SSFIs

INSPECTION CONCLUSIONS ~ LPCS System Mill Perform Its Intended Design Function ~ . Methodology outlined in SSFI Program Manual is sound, we have confidence in our approach, process, and results.

~ Structured DBD Verification is Necessary ~ DBD is Valuable Source Reference ~ Programmatic, Procedures, and Configuration Control Observations Collectively Represent an Area of Concern not Limited to LPCS ~ Plant Staff Participation Extremely Valuable

INSPECTION RECOMMENDATIONS ~ Develop a Plan to Address Disposition of Observations ~ Integrate Observations Disposition Into Current Impr ovement Programs ~ Apply Root Cause Analysis for Identification of.

Root Problem ~ Commit Full-time Participant from Plant Technical Staff for Future SSFIs ~ Do Not Perform SSFIs During Refueling Outages

OPERATIONS DEPARTMENT COMMITMENTS ~ Personnel'hanges ~ Communication and Management Involvement ~ Procedure Upgrade (A equality Process) ~ Department Ownership in Training ~ Define Expectations and Set Standards ~ Clearance Order Safety

OPERATIONAL PERFORMANCE AND ATTENTION TO DETAIL e Improvement in Operational Performance I ~ Personnel Error Reduction ~ Per formance Feedback

CONDUCT OF OPERATIONS H SET OPERATIONAL STANDARDS AND ESTABLISH POLICY Personnel Accountability and Authority EOP Execution

- Individual Accountability Tech.

Spec.

Compliance ~ Standards for Plant Safety (Nuclear and Non-Nuclear) Health Physics Practices ~ Professionalism Attire Eti quette Communication ~ Procedural Compliance Heat Up Event Vessel Level Control ~ Problem Solving Containment Spray Valve. Failure Containment Nitrogen Valve/Line Failure Roof Event o Attention to Detail REA Sampling Reactor Drain Down Rod Manipulation Errors

TOTAL OPEN MWRs 1.60 1.50 1.40 1513 I f63 TOTAL MWRs 1391 19.5% REDUCTION 1.30 Fi N p, g I.20 0 1 1.10 gA K 0.90 0.00 1167 NON-OUTAGE MWRs 1030 970 1263 006 1217 34% REDUCTION 0.70 AUG SEP OCT MONTFI 1900 NOV DEC

DEPARTMEN.T SUP ERVISOR WORK CONTROL SUP ERVISOR PLANNER & SCHEDULER ENGINEERING SU P E RVISOR CRAFT SUP ER.

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