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Category:SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
MONTHYEARIR 05000382/19980991998-04-24024 April 1998 SALP Rept 50-382/98-99 for 961201-980321 IR 05000382/19960991997-03-17017 March 1997 Revised Plant Support Section of SALP Rept 50-382/96-99 ML20133D2071997-01-0606 January 1997 SALP Rept 50-382/96-99 for 950429-961130 IR 05000382/19930991993-12-10010 December 1993 SALP Rept 50-382/93-99 for 920802-931030 IR 05000382/19870321988-07-31031 July 1988 SALP Rept 50-382/87-32 for Period Feb 1987 - Jul 1988 ML20209H7771987-04-30030 April 1987 SALP Rept 50-382/87-03 for Jan 1986 - Jan 1987 IR 05000382/19850301986-03-20020 March 1986 SALP Board Rept 50-382/85-30 for 841218-851231 ML20154S0311986-03-20020 March 1986 SALP Board Rept 50-382/85-30 for 841218-851231 ML20058D0491982-07-0101 July 1982 Notifies That Systematic Assessment of Licensee Board Performance Rept Issued Even Though Comments Requested from Util on 820520 Not Received ML20058D0751982-05-20020 May 1982 Requests Comments Re Systematic Assessment of Licensee Board Performance Rept Evaluation of Facility within 20 Days of Ltr Date 1998-04-24
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000382/19990201999-10-21021 October 1999 Insp Rept 50-382/99-20 on 990815-0925.Non-cited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support Activities IR 05000382/19990141999-10-19019 October 1999 Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Major Areas Inspected:Operator Requalification Training Program PNO-IV-99-038A, on 990929,restart of Waterford 3 Occurred. Cause Identified as Failed Seal Water Heat Exchanger Baffle. New Battle & Seal Assembled Were Installed & Reactor Coolant Pump 2B Was Returned to Svc Satisfactorily1999-10-0101 October 1999 PNO-IV-99-038A:on 990929,restart of Waterford 3 Occurred. Cause Identified as Failed Seal Water Heat Exchanger Baffle. New Battle & Seal Assembled Were Installed & Reactor Coolant Pump 2B Was Returned to Svc Satisfactorily IR 05000382/19990181999-09-29029 September 1999 Insp Rept 50-382/99-18 on 990830-0902.Violations Noted.Major Areas Inspected:Implementation of NRC-approved Fire Protection Program IR 05000382/19990191999-09-27027 September 1999 Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted. Major Areas Inspected:Plant Support PNO-IV-99-038, on 990910,operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.New Baffle & Seal Assembly Were Installed & Plant Was Returned to Power Operations on 9908101999-09-15015 September 1999 PNO-IV-99-038:on 990910,operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.New Baffle & Seal Assembly Were Installed & Plant Was Returned to Power Operations on 990810 IR 05000382/19990151999-09-14014 September 1999 Insp Rept 50-382/99-15 on 990719-23 with in Ofc Insp Until 0819.No Violations Noted.Major Areas Inspected:Assessment of 10CFR50.59 Safety Evaluation Program & Review of Previous Insp Findings Involving Tornado Missile Protection IR 05000382/19990071999-09-0808 September 1999 Insp Rept 50-382/99-07 on 990601-11.Noncited Violations Identified.Major Areas Inspected:Operations IR 05000382/19990161999-09-0101 September 1999 Insp Rept 50-382/99-16 on 990704-0814.Noncited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support PNO-IV-99-032A, on 990801,Waterford 3 Operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.Pump Was Secured Immediately Following Plant Sd.New Baffle & Seal Assembly Was Installed1999-08-12012 August 1999 PNO-IV-99-032A:on 990801,Waterford 3 Operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.Pump Was Secured Immediately Following Plant Sd.New Baffle & Seal Assembly Was Installed IR 05000382/19990101999-08-11011 August 1999 Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Major Areas Inspected:Solid Radioactive Waste Mgt & Radioactive Matl Transportation Programs PNO-IV-99-032, on 990801,Waterford 3 Operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.Pump Was Secured Immediately Following Plan Shutdown.Resident Inspectors Will Monitor1999-08-0303 August 1999 PNO-IV-99-032:on 990801,Waterford 3 Operators Manually Tripped Reactor from 100% Power in Response to Indications of Failure of RCP 2B Seal.Pump Was Secured Immediately Following Plan Shutdown.Resident Inspectors Will Monitor IR 05000382/19990131999-07-15015 July 1999 Insp Rept 50-382/99-13 on 990523-0703.Noncited Violations Noted.Major Areas Inspected:Aspects of Operations,Maint, Engineering & Plant Support Activities IR 05000382/19990121999-06-21021 June 1999 Insp Rept 50-382/99-12 on 990524-27.No Violations Noted. Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program IR 05000382/19990111999-06-18018 June 1999 Insp Rept 50-382/99-11 on 990524-28.No Violations Noted. Major Areas Inspected:Implementation of Liquid & Gaseous Radwaste Effluent Mgt Program,Status of Effluent Radiation Monitors & Counting Room Instruments ML20196C9461999-06-15015 June 1999 Notice of Violation from Insp Completed on 990422.Violation Noted:Licensee Failed to Consider Info Contained During Background Investigation Before Granting Temporary Unescorted Access to Contractor Employee IR 05000382/19990091999-06-0303 June 1999 Insp Rept 50-382/99-09 on 990411-0522.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20209B8581999-05-25025 May 1999 EN-98-046A:on 990524,staff Withdrew Proposed Civil Penalty in Amount of $110,000 Issued to Licensee.Action Based on Severity Level III Problems Associated with ECCS & Afws IR 05000382/19990061999-05-18018 May 1999 Insp Rept 50-382/99-06 on 990405-09.Non-cited Violations Identified.Major Areas Inspected:Issue Previously Identified During Architect Engineering Insp Which Documented NRC Insp Rept 50-382/98-201 IR 05000382/19990051999-05-10010 May 1999 Insp Rept 50-382/99-05 on 990228-0410.Non-cited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support ML20206F4801999-05-0303 May 1999 Insp Rept 50-382/99-08 on 990405-07.One Apparent Violation Noted & Being Considered for Escalated Eas.Major Areas Inspected:Plant Support Including Licensee Access Authorization Program IR 05000382/19990041999-04-0909 April 1999 Insp Rept 50-382/99-04 on 990301-19.One Violation Occurred & Being Treated as Noncited Violation.Major Areas Inspected: Review of Licensee Implementation of Facility ISI Program & Followup Review of Reactor Trip Breaker Performance IR 05000382/19990021999-04-0505 April 1999 Insp Rept 50-382/99-02 on 990117-0227.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support Activities IR 05000382/19990031999-03-26026 March 1999 Insp Rept 50-382/99-03 on 990308-12.Violations Noted.Major Areas Inspected:Radiation Protection Program Focusing on RF09 Refueling Outage Activities IR 05000382/19990011999-03-0303 March 1999 Partially Deleted Insp Rept 50-382/99-01 on 990125-29 & 0208-12 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Plant Support ML20207F1581999-03-0303 March 1999 Notice of Violation from Insp on 990125-29 & 0208-12. Violation Noted:Inspector Determined That Waterford Audits SA-98-025.1 & SA-98-036.1,dtd 980916,were Conducted by Individuals Not Independent of Program Mgt Being Audited IR 05000382/19980181998-12-21021 December 1998 Insp Rept 50-382/98-18 on 981018-1128.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000382/19980151998-11-24024 November 1998 Insp Rept 50-382/98-15 on 980906-1017.No Violations Noted. Major Areas Inspected:Aspects of Operations,Maint, Engineering & Plant Support Activities PNO-IV-98-054, on 981117,plant Shutdown Greater than 72 H Due to Unidentified Leak.Investigations by Licensee Verified That Leakage Occurred from RCP 2b Seal Area1998-11-19019 November 1998 PNO-IV-98-054:on 981117,plant Shutdown Greater than 72 H Due to Unidentified Leak.Investigations by Licensee Verified That Leakage Occurred from RCP 2b Seal Area IR 05000382/19980131998-11-17017 November 1998 Insp Rept 50-382/98-13 on 980831-0901 & 981005-08.No Violations Noted.Major Areas Inspected:Maint Using Guidance of Temp Instruction 2515/137, Insp of Medium-Voltage & Low-Voltage Power Circuit Breakers ML20155D0561998-10-29029 October 1998 Insp Rept 50-382/98-17 on 981005-08.Violations Noted. Major Areas Inspected:Routine Review of Radiation Protection Program Activities ML20155D0411998-10-29029 October 1998 Notice of Violation from Insp on 981005-08.Violation Noted: Inspectors Identified That Radiation Surveys to Evaluate Extent of Radiation Levels Had Not Been Performed Prior to Operations Personnel Entering Area ML20155D5111998-10-27027 October 1998 Partially Withheld Insp Rept 50-382/98-16 on 980914-18. Violations Noted.Major Areas Inspected:Licensee Physical Security Program.Portions Withheld (Ref 10CFR2.790) ML20155D5021998-10-27027 October 1998 Notice of Violation from Insp on 980914-18.Violation Noted: Performance Tests of Protected Area Detection Sys Identified That Two Detection Zones Did Not Meet Design Criteria to Detect Test Individuals ML20154L0831998-10-0909 October 1998 Notice of Violation from Insp on 980726-0905.Violation Noted:On 980721,NRC Inspectors Found Door 206,vital Area Portal,Unlocked & Not in Alarm at Central Alarm Station ML20154L1281998-10-0909 October 1998 Insp Rept 50-382/98-14 on 980726-0905.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support PNO-IV-98-045, on 980926,Unit 3 Declared Unusual Event of Hurricane Warning in St Charles Parish.River Bend Station Continued to Operate at Full Power Since Hurricane Force Winds Were Not Predicted in Vicinity of Site1998-09-28028 September 1998 PNO-IV-98-045:on 980926,Unit 3 Declared Unusual Event of Hurricane Warning in St Charles Parish.River Bend Station Continued to Operate at Full Power Since Hurricane Force Winds Were Not Predicted in Vicinity of Site PNO-IV-98-040, on 980917,licensee Commenced Shutdown of Reactor in Order to Replace Pressurizer Code Safety Valve That Had Been Experiencing Increased Leakage.Licensee Plans to Restart Facility on 9809231998-09-18018 September 1998 PNO-IV-98-040:on 980917,licensee Commenced Shutdown of Reactor in Order to Replace Pressurizer Code Safety Valve That Had Been Experiencing Increased Leakage.Licensee Plans to Restart Facility on 980923 IR 05000382/19980121998-08-21021 August 1998 Insp Rept 50-382/98-12 on 980614-0725.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000382/19992011998-07-27027 July 1998 Insp Rept 50-382/99-201 on 990511-0619.No Violations Noted Major Areas Inspected:Engineering IR 05000382/19980101998-07-20020 July 1998 Insp Rept 50-382/98-10 on 980622-26.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program Including Access Authorization,Alarm Stations,Protected Area Access Control of Personnel & Packages & Vehicles ML20236P2431998-07-10010 July 1998 Notice of Violation from Insp on 980503-0613.Violation Noted:On 980521,AP UNT-005-013 Was Not Implemented in That Impairment to Fire Door D150 Was Not Controlled IR 05000382/19980091998-07-10010 July 1998 Insp Rept 50-382/98-09 on 980503-0613.Violations Noted.Major Areas Inspected:Aspects of Operations,Maint,Engineering & Plant Support Activities.Fire Door in Reactor Auxiliary Bldg Was Observed to Be Open W/No Controls in Place ML20249A9611998-06-16016 June 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $100,000.Violation Noted:Licensee Identified That Calculated Peak Fuel Cladding Temp Would Have Exceeded 2200 F Using Licensing Basis Analysis & HPSI Flow ML20151R9131998-06-0909 June 1998 EN-98-046:on 980616,notice of Proposed Imposition of Civil Penalty in Amount of $110,000 Issued to Licensee.Action Based on Level III Problem Involving HPSI Flow Issues at Waterford-3 Facility IR 05000382/19980081998-05-29029 May 1998 Insp Rept 50-382/98-08 on 980322-0502.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support ML20248F6801998-05-29029 May 1998 Notice of Violation from Insp on 980322-0502.Violation Noted:Licensee Failed to Establish Adequate Procedures for Operation of EDG When in No or Low Electrical Loading Condition in That No Specific Guidance Provided IR 05000382/19980991998-04-24024 April 1998 SALP Rept 50-382/98-99 for 961201-980321 ML20217B6731998-04-21021 April 1998 Notice of Violation from Insp on 980201-0321.Violation Noted:On Past Occasions,Engineer Operated Governor Valve on Emergency Feedwater Turbine W/O Direction or Concurrence of Shift Superintendent or Control Room Supervisor ML20217B6981998-04-21021 April 1998 Insp Rept 50-382/98-06 on 980201-0321.Violations Noted.Major Areas Inspected:Operations,Maint & Engineering 1999-09-08
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l PLANT SUPPORT Overall safety performance in the plant support area during this assessment period was determined to be good. While the licensee maintained an appropriate focus on safety-related issues, performance declined in the radiological controls and security areas, and inconsistencies were identified with the implementation of otherwise strong programs for emergency preparedness and fire protection. A number of corrective actions have been initiated to re-establish the performance standards of the past, but their effectiveness had yet to be determine l i
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Generally, good performance was noted in the radiological controls area. An appropriately trained and qualified staff was maintained. The radiation protection program remained sound, but declined from the previous performance level. Problems were noted with material and contamination controls and worker adherence to radiological control 1 requirements. The goals for skin and clothing contamination events were not met during the 1995 refueling outage. Nevertheless, the 3-year average exposure at the site was better than the national average for pressurized water reactors. The effectiveness of the l ALARA program was good but inconsistent and did not meet management expectations in j several cases. Conversely, quality assurance audits were performance-based, included l specialists from outside the site, and were part of the licensee's self-improvement effort The emergency preparedness program continued to be an overall strength. Actual events were correctly classified and offsite agency notifications were timely. Quality assurance audits, management controls, and self-critiques were effective. However, there were several exceptions to the superior indicators typical of past performance. Although good performance was observed in all response facilities during the biennial exercise, an exercise weakness associated with communications problems was identified and two poor emergency planning practices at the emergency operations facility were noted. Finally, during the annual program review, declaration of a General Emergency was delayed because two operating crews had difficulty diagnosing fuel integrity statu Performance in the security area was good but inconsistent. As a result of the preparations for the Operational Safeguards Response Evaluation, coordination between the security and operations organizations improved. Significant changes were made within the management structure of the security organization, partly in response to daily operational and morale issues, such as those associated with the conduct of fire watches and the differentiation of duties between armed and unarmed officers. Deficiencies were also noted in the implementation of the access authorization program, the identification of degraded lighting conditions, and the establishment of compensatory measures. White, overall, there was a decline in security during this assessment period, there was evidence of improvement in the latter part of this assessment perio The fire protection program was found to be effective. The transition to the updated fire protection system went well; however, examples of inconsistent and questionable conduct ]
of fire watch rounds detracted from the overall performance. Housekeeping remained at an acceptable level. While several problems were noted early in the assessment period and ;
during outage conditions, performance improved and was considered very good during .
normal plant operating condition )
i The performance rating in the plant support area is Category l
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l 9703240183 970317 I PDR ADOCK 05000382 G PDR
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- Q W3F1-97-0012 A4.05 PR February 21,1997 .. m:
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U.S. Nuclear Regulatory Commission pg 2 4997 ATTN: Document Control Desk Washington, D.C. 20555 b -
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M Offl Subject: Waterford 3 SES Docket No. 50-382 License No. NPF-38 Reply to Systematic Assessment Licensee Performarice (SALP)
Report 50-382/96-99 Gentlemen:
By letter dated January 6,1997, the Nuclear Regulatory Commission (NRC)
requested that Entergy Operations, Inc. provide written comments to address weaknesses in the Engineering functional area. The weaknesses are documented in the NRC's SALP report that covers Waterford 3 performance for the period April 30, 1995, through November 30,1996. Enclosed (see Attachment 1) is Waterford 3's response to that reques Your assessment of Waterford 3 reflects both a decline in our performance and a rebaselining of performance criteria. Although the issues identified by Waterford 3 and the NRC during the SALP period are well understood and addressed, we recognize that the plant's overall performance was unacceptable. That performance
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did not reflect the expectations of Entergy or the NRC.
Waterford 3 is committed to continuous improvement. To that end, we will continue to identify, correct and preclude the recurrence of adverse conditions. We will vigorously pursue improvements in all functiona! area For example, in the Operations area, we have taken aggessive steps to address identified weaknesses such as procedural adherence. Operations is committed to enhancing their role as leaders and owners of the plant. Training continues to be ha b r 7 - O'T ~7 l
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W3F1-97-0012 Page 2 February 21,1997 l
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a strong point for Operations. Organizational changes are being implemented to l improve functionality and responsiveness. Furthermore, Operations will better utilize I self assessments to assist in the discovery of plant problems and in the bounding of plant issue l l
In the Maintenance area, we have developed a well-trained and competent staf That staff is aggressively taking action to address weaknesses in human i performance and procedural compliance on a broad scale. Maintenance will utilize !
INPO training in Human Performance and implement a task force to determine the )
root cause(s) of procedural compliance issues. We agree that our Maintenance !
backlogs are high but well controlled. However, we intend to use additional resources and overtime to reduce those backlogs. Design Engineering now has the responsibility for the IST plan. A comprehensive review of ASME class 1,2, and 3 '
pumps and valves has been performed to ensure appropriate valves are in the pla l In addition, procedural controls have been implemented to ensure consistency between the IST and basis document In the Plant Support Area, Waterford concurs with the assessment of its performance with the exception of your characterization that the 3-year average radiation i exposure was at the national average. Waterford's three year average radiation exposure is better than approximately 70% of other operating domestic PWR plant l
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Your staff acknowledged that fact during the SALP public meeting. Waterford 3 has taken aggressive steps to address weaknesses identified in the SALP report and to continuously improve performance in this area. Enhancements in training, organization and processes have been made to strengthen personnel and department performance Currently, Waterford 3 has an aggressive self assessment schedule. These assessments will be more critical and intrusive and will better assist all functional areas in reaching higher performance levels. Finally, we believe that although our performance has improved, we hold people to higher standards of performance. The.-
Timeless Principles and "True North" goals that have been set at Waterford 3 are the foundr. tion upon which continuous improvement will be mad .
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Reply to SALP Report 96-99 W3F1-97-0012 Page 3
. February 21,1997 If you have any questions concerning this letter or the attached response, please j contact Tim Gaudet at (504) 739-6666.
! Very truly yours, t
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T.J. Gaudet Acting - Director i Nuclear Safety & Regulatory Affairs TJG/GCS/WDM/tjs Attachment
cc: zLJ Callan (NRC Region IV)
C.P. Patel (NRC-NRR)
- R.B. McGehee
> N.S. Reynolds NRC Resident inspectors Office i
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Attachment 1 to >
W3F1-97-0012 b' Pcge 1 of 2 b
j Waterford 3 accepts the finding of the NRC in the Engineering section of the SALP
! report and acknowledges that significant work is ahead of us. Action plans, l j organizational changes, resource additions, and budgets are being developed to 1
- ensure that the implementation is appropriately integrated to achieve the expected results. Our immediate challenge is to further develop and sustain the high level of
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questioning attitude, work down the backlogs (focusing on the highest priority items ,
first), and simultaneously embark on some major engineering program i improvements.
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Waterford 3 Engineering recognizes the need to aggressively identify problems, to l thoroughly bound them, and to solve them the first time. As a result of initiatives implemented in early 1996, Engineering directly initiated, or indirectly participated in, 11 major assessments. Engineering is actively striving to minimize operator workarounds, long standing or repetitive temporary alterations, and compensatory actions. A prioritized modification list has resulted in approximately 40 planned modifications for RF0 Waterford 3 is committed to licensing and design basis fidelity. It should be emphasized that Waterford's basic design is sound and provides opportunities to increase our confidence in its overall safety and reliability. Major programs are planned for the FSAR and design basis documents that will focus on retrieval, confirming assumptions, eliminating inconsistencies, preserving margin, and recapturing original design margin where required. Improved Technical Specification and IST programs are in progress. The challenge is to integrate these various actions, including FSAR review, improved Tech Specs, and 50.54(f) commitments, to get prompt result Another result of recent initiatives is changes that have been implemented to improve the quality of information provided to the control room. Engineering interface with the control room is more rigorous and formal. Engineering inputs are independently reviewed and treated within the design control progra Rigor in the control and use of assumptions and inputs has been tightened so that engineering outputs have appropriate documented bases. The technical review process has been improved and supervisors have been charged with the responsibility to maintain standards for quality, rigor, and bases of engineering ,
evaluations. Refresher training has been given to all engineering staff qualified to '
perform 10CFR50.59 evaluations. The Design Review Committee has been implemented to provide ongoing oversight and assessment to ensure standards for performance are being met and to identify areas of additional improvement in a multi-discipline settin .
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